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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
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ACCELERATED DISTRIBUTION DEMONSTRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9401110017 DOC.DATE: 93/12/22 NOTARIZED: NO DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH.'AME AUTHOR AFFILIATION MARTIN,J.T. Rochester Gas & Electric Corp.
MECREDY,R.C., Rochester Gas & Electric Corp.
RECIP.NAME RECIPIENT AFFILIATION Project Directorate I-3 R'OHNSON,A.R.
I
SUBJECT:
LER 93-007-00:on 931122,RT occurred due to high source range D',
flux level during reactor startup.Caused by failure of personnel focusing on RT setpoint.Replaced status lights &
corrected PPCS alarm message.W/931222 ltr. $
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
A NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 D
RECIPIENT COPIES RECIPIENT COPIES D, ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD1-3 LA 1 1 PD1-3 PD 1 1 JOHNSON,A 1 1 INTERNAL: AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DORS/OEAB 1 1 NRR/DRCH/HHFB, 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRIL/RPEB 1 1 NRR/DRSS/PRPB 2 2 QB~RDSSQ/D PLB 1 1 NRR/DSSA/SRXB 1 1 1 1 RES/DSIR/EIB 1 1 1 1 EXTERNAL EG&G BRYCE g J ~ H 2 2 L ST LOBBY WARD 1 1 NRC PDR .1 1 NSIC MURPHYgG A ~ 1 1 NSIC POORE,W. 1 1 NUDOCS FULL TXT 1 1 D
D D
NOTE TO ALL "RIDS" RECIPIENTS:
S PLEASE HELP US TO REDUCE lVASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOibl PI-37 (EXT. 20079) TO ELIiVIINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
-FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 28 ENCL 28
r ion K .
ssssr ROCHESTER GAS AND ELECTRIC CORPORATION e 89 EAST AVENUE, ROCHESTER N. Y. 14649-0001 R6BERT C, MEGREOY TELEPHONE Vice Presiden< AsrEA CODE 716 546 2700 Cinna Nuclear Produriion December 22, 1993 U.S. Nuclear Regulatory Commission Attn: Allen R. Johnson Project Directorate I-3 Document Control Desk Washington, DC 20555
Subject:
LER 93-007, High Source Range Flux Level During Reactor Startup Causes a Reactor Trip R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73 I Licensee Ev en t R epor t System,
~
item (a ) (2 ) iv who.ch requires a report of, "any event or (zv),
condition that resulted in a manual or automatic ct e y feature (ESF), including the reactor protection t'a system (RPS)", the attached Licensee Event Report LER 93-007 07 1s hereby submitted.
Thxs event has in no way affected the public's health and safety.
Very truly yours, Robert C. Mecredy XC U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector 0 60053.
9401>~OOX7 93>~~>
PDR ADQCK 050002 POR
NRC FORH 366 U.S. II)CLEAR REGULATORY C<NNIISSION APPROVED BY QGI NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY lllTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
LICENSEE EVENT REPORT (LER) FORHARD COMMENTS REGARDIHG BURDEN ESTIMATE TO THE IHFORHATIOH AND RECORDS MANAGEHENT BRANCH (HNBB 7714), U.S. NUCLEAR REGULATORY COMHISSIOH, (See reverse for required number of digits/characters for each block) NASHINGTOH, DC 20555-0001 AND TO THE PAPERUORK REDUCTION PROJECT (31/0-0104), OFFICE OF MAHAGEHENT AND BUDGET NASHINGTON DC 20503-FAclLITY lQ% (1) R. E ~ Ginna Nuclear Power Plant DOCKET NQIBER (2) PAGE (3)
=05000244 1 OF 7 TITLE (4) High Source Range Flux Level During Reactor Startup Causes a Reactor Trip EVENT DATE 5 LER INNBER 6 REPORT DATE 7 OTHER FACILITIES INVOLVED 8 SEQUENTIAL REVISION FACILITY NAHE DOCKET NUMBER MONTH DAY YEAR YEAR MOHTH DAY YEAR HUHBER NUMBER 11 22 93 93 --007-- 00 12, 22 FACILITY HAME DOCKET NUMBER STRAYING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR : Check one or more 11 INXIE,(9) N 20.402(b) 20.405(c) 50.73(a)(2)(iv) 73.71(b)
POUER 20.405(a )(1)(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c) 000 50.73(a)(2)(vii)
LEVEL (10) 20.405(a)(1)(ii) 50.36(c)(2) OTHER 20.405(a)(1)(iii) 50.73(a)(2)(i) 50.73(a)(2)(viii)(A) (Specify in 20.405<a)(1)(iv) 50.73(a)(2)(ii) 50.73(a)(2)(viii)(B) Abstract beioM and in Text, 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)<2)(x) HRC Form 366A LICENSEE CONTACT FOR THIS LER 12 HAME John T~ St. Hartin - Director, Operating Experience TELEPHONE NUMBER (Include Area Code)
(315) 524-4446 C<NPLETE ONE LINE FOR EACH C<NPONENT FAILURE DESCRIBED IN THIS REPORT 13 REPORTABLE %%)3%@i4 REPORTABLE CAUSE SYSTEH COHPOHEHT HANUFACTURER CAUSE SYSTEH COMPOHEHT HANUFACTURER TO NPRDS TO NPRDS jgc0pQWp:
SUPPLEMENTAL REPORT EXPECTED 14 EXPECTED MONTH DAY YEAR YES SUBMISSION (If yes, complete EXPECTED SUBHISSIOH DATE). X DATE (15)
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten tines) (16)
The plant was at hot shutdown condition, with a reactor startup- in progress. At 0644 EST the reactor tripped on High Source Range Flux Level (>/= lE5 counts per second).
The underlying cause was determined to be a Control Room operator not adeguately focused on approaching the reactor trip setpoint. With two status lights burned out and a misleading PPCS alarm message, the operator was focused on Permissive P-6 setpoint instead of the reactor trip setpoint. (This event is NUREG-1220 (A) cause code.)
Corrective actions were to replace the status lights, correct the PPCS alarm message, and apprise the Control Room operators of the need to focus on reactor trip setpoints. Corrective action to preclude repetition is outlined in Section V (B).
NRC FORH 366 (5-92)
I NRC FORH 366A U.S IN)CLEAR REGULATORY COIIISSIQI APPROVED BY QQ NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO CONPLY llITH THIS IHFORNATIOH COLLECTIOH REQUEST: 50.0 HRS.
FORlIARD CONNEHTS REGARDIHG BURDEN ESTIHATE TO LICENSEE EVENT REPORT (LER) THE INFORHATION AND RECORDS HANAGEHENT BRANCH TEXT CONTINUATION (NHBB 7714), U.S. NUCLEAR REGULATORY COHHISSIOHg llASHIHGTON, DC 20555-0001 AND TO THE PAPERlSRK REDUCTIOH PROJECT (3140-0104), OFFICE OF HANAGENENT AND BUDGET MASHINGTON DC 20503.
FACILITY NAHE 1 DOCKET N(NBER 2 LER NIMBER 6 PAGE 3 SEOUEHTIAL REVISION YEAR R.E. Ginna Nuclear Power Plant 05000244'3 2 OF 7
-- 007 00 TEXT (If more space is required, use additional copies of HRC Form 366A) (17)
PRE-EVENT PLANT CONDITIONS The plant was stable in the hot shutdown condition, and the reactor was subcritical with a reactor startup in progress, using procedure 0-1.2 (Plant Startup From Hot Shutdown to Full Load).
II. DESCRIPTION OF EVENT A. DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:
o November 22, 1993, 0644 EST: Event date and time.
o November 22, 1993, 0644 EST: Discovery date and t'ime.
o November 22, 1993, 0644 EST: Control Room operators verify both reactor trip breakers open, and all control and shutdown rods inserted.
o November 22, 1993, 0650 EST: Plant stabilized at hot shutdown condition.
B. EVENT:
At approximately 0643 EST, the Control Room operators were conducting the final approach to criticality, in accordance with procedure 0-1.2. The operator performing the reactor startup was moving control rods out to establish a positive startup rate (SUR) prior to declaring the reactor critical. At this time, the two Nuclear Instrument System (NIS) Source Range (SR) instruments were indicating reactor power. at approximately 5E4 counts per second (CPS). The Control Room operator was anticipating that Permissive P-6 status lights would illuminate at this time, prior to exceeding the reactor trip setpoint of 1E5 CPS.
Permissive P-6 setpoint is generated from NIS Intermediate Range (IR) channels, when 1 of 2 channels is above 1E-10 amps. This is normally equivalent to approximately 1E4 CPS indication on the SR 'instruments. Permissive P-6 allows the Control Room, operator to manually block the High Source Range Flux Level reactor trip and de-energize the SR detectors.
NRC FORM 366A (5-92)
NRC FORH 366A U.S. NUCLEAR REGULATORY CNHIISSION APPROVED BY (NB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COHPLY WiTH THIS INFORHATION COLLECTIOH REQUEST: 50.0 HRS ~
FORWARD CONHENTS REGARDIHG BURDEN ESTIHATE TO LICENSEE EVENT REPORT (LER) THE INFORMATION AHD RECORDS HANAGEHEHT BRANCH TEXT CONTINUATION (HHBB 7714), U.S. NUCLEAR REGULATORY COHHISSIOH, WASHINGTON, DC 20555 0001 AHD TO THE PAPERWORK REDUCTION PROJECt (3150-0104), OFFICE OF HANAGEHENT AHD BUDGET WASHINGTON DC 20503.
FACILITY NAHE 1 DOCKET NNBER. 2 LER NNBER 6 PAGE 3 SEQUEHT IAL REVISION YEAR R.E. Ginna Nuclear Power Plant 05000244 93 007-- 00 3 OF 7 TEXT (If more space is required, use additionat copies of HRC Form 366A) (17)
Prior to the P-6 status lights illuminating, at approximately 0644 EST, the reactor tripped on High Source Range Flux Level
()/= 1E5 CPS). The Control Room operators performed the appropriate actions of Emergency Operating Procedure E-0 (Reactor Trip or Safety Injection), and verified that safety injection was not actuated or required. They then transitioned to Emergency Operating Procedure ES-0.1 (Reactor Trip Response).
The- plant was subsequently stabilized in hot shutdown, using procedure 0-2.1 (Normal Shutdown'to Hot Shutdown).
C~ INOPERABLE STRUCTURES g COMPONENTS / OR SYSTEMS THAT CONTRI BUTED TO THE EVENT:
o The light bulbs for the status lights that provide indication that reactor power is above Permissive P-6 were both burned out.
o Plant Process Computer System (PPCS) alarm message to indicate reactor power is above Permissive P-6 was misleading. With reactor power above the P-6 setpoint, the PPCS alarm message indicated that power was still below the setpoint.
D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None E. METHOD OF DISCOVERY:
This event was immediately apparent due to Main Control Board Annunciator D-26 (Source Range Hi Flux Level Reactor Trip lE5 CPS) and other alarms and indications in the Control Room.
HRC FORH 366A (5 92)
I I
NRC FORH 366A U.S. INCLEAR REGULATORY CONI SSION APPROVED BY (NQ NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPOHSE TO COHPLY MITH THIS INFORHATION COLLECTIOH REOUEST: 50.0 HRS.
FORMARD COHHEH'IS REGARDING BURDEN ESTIHATE TO LICENSEE EVENT REPORT (LER) THE IHFORHATIOH AND RECORDS HANAGEHEHT BRANCH TEXT CONTINUATION (HNBB 7714), U.S. NUCLEAR REGULATORY,COHHISSION, MASHINGTOH, DC 20555-0001 AND TO THE PAPERNNK REDUCTION PROJECT (3'I40-0104), OFFICE OF HANAGEHENT AND BUDGET MASHINGTON DC 20503.
FACILITY lOWE 1 DOCKET NNIBER 2 LER NINBER 6 PAGE 3 SEOUENTIAL REVISION YEAR R.E. Ginna Nuclear Power Plant 05000244 93 007-- 00 4 OF 7 TEXT (If more space is required, use additional copies of HRC Form 366A) (17)
F. OPERATOR ACTION:
After the reactor trip, the Control Room operators performed the appropriate actions of Emergency Operating Procedures E-0 (Reactor Trip or Safety Injection) and ES-0.1 (Reactor Trip Response). The plant was stabilized at hot shutdown.
Subsequently, the Control Room operators notified higher supervision. The Nuclear Regulatory Commission was notified per 10CFR50.72, Non-Emergency, 4 Hour Notification at approximately 1022 EST.
G. SAFETY SYSTEM RESPONSES:
None III. CAUSE OF EVENT A. IMMEDIATE CAUSE:
The reactor trip was due to NIS SR high flux level above the SR reactor trip setpoint of 1E5 CPS.
B. INTERMEDIATE CAUSE:
The high flux level was caused by failure to block the SR reactor trip, after establishing a SUR of approximately 0.5 to 1 decades per minute (DPM) during the final approach to criticality, with power approaching the SR reactor trip setpoint.
NRC FORH 366A (5-92)
NRC FORM 366A U.S. NUCLEAR REGULATORY COHISSION APPROVED BY 0$ NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEH PER RESPOHSE TO COMPLY MITH THIS IHFORHATIOH COLLECT ION REQUEST: 50.0" HRS.
FORMARD COMMENTS REGARD IHG BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER) THE INFORHATION AND RECORDS MANAGEHEHT BRANCH TEXT CONTINUATION (HHBB 7714), U.S. NUCLEAR REGULATORY CDMHISSIOH ~
MASHINGTOH, DC 20555-0001 AHD TO THE PAPERNORK REDUCTION PROJECT (31i0-0104), OFF ICE OF MANAGEMENT AND BUDGET MASHINGTON DC 20503.
FACILITY NAME 1 DOCKET IRHIBER 2 LER MINBER 6 PAGE 3 SEQUENT I AL REVISION YEAR R.E. Ginna Nuclear Power Plant 05000244 93 007-- 00 5 OF 7 TEXT (If more space is required, use additional copies of HRC Form 366A) (17)
C. ROOT CAUSE:
The underlying cause of the failure to block the SR reactor trip with power increasing at a 0.5 to 1 DPM SUR, was cognitive personnel error by a Control Room operator. The Control Room operator was not adequately focused on approaching the SR.
reactor trip setpoint.
The Control Room operator was anticipating that the status lights indicating reactor power above Permissive P-6 setpoint would be illuminated, allowing block of the SR-reactor trip, prior to reaching the trip setpoint. His attention was focused on these status lights instead of on the approach to the reactor trip setpoint. The statusout.lights did not illuminate due to the light bulbs being burned The PPCS alarm message provided incorrect reinforcement that reactor power was still below the P-6 setpoint. The actions of the operator performing the reactor startup were not contrary to procedures established for this evolution. (This event is NUREG-1220 (A) cause code, Personnel Error.)
IV. ANALYSIS OF EVENT This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (iv), which requires a report of, "any event or condition that resulted in manual or automatic actuation of any engineered safety feature (ESF) including the reactor protection system (RPS)". The reactor trip was an automatic actuation of the RPS.
An assessment was performed considering both the safety consequences and implications of this event with the following
~ results and conclusions:
There were no safety consequences or implications attributed to the reactor trip because:
o The two reactor trip breakers opened as required.
o All control and shutdown rods inserted as=- designed.
/
o The plant was stabilized at hot shutdown.
HRC FORM 366A (5-92)
NRC FORH 366A U.S. IR)CLEAR REGULATORY CQIIISS ION APPROVED BY QGI NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEH PER RESPONSE TO COHPLY MITH THIS IHFORHATIOH COLLECTIOH REQUEST: 50.0 HRS.
FORllARD COHHEHTS REGARDIHG BURDEN ESTIHATE TO LICENSEE EVENT REPORT (LER) THE IHFORHATIOH AND RECORDS HANAGEHEHT BRANCH TEXT CONTINUATION (HHBB 7714), U.S. NUCLEAR REGULATORY COHHISSIOH,
'WASHINGTON, DC 20555-0001 AHD TO THE PAPERIQRK REDUCTION PROJECT (3140-0104), OFFICE OF HAHAGEHEHT AHD BUDGET NASHIHGTOH DC 20503.
FACILITY NAHE 1 DOCKET NIMBER 2 LER NLSIBER 6 PAGE 3 SEQUENTIAL REVI SIOH R.E. Ginna Nuclear Power Plant '5000244 93 "
007-- 00 ' OF 7 TEXT (lf more space is required, use additional copies of HRC Form 366A) (Tl)
The reactor trip did not cause any reactor coolant system (RCS) transient, as the re'actor was not at the point of adding heat. All reactor protection circuitry actuated as designed to place the reactor in a tripped mode at hot shutdown.
Based on the above and a review of post trip data and past plant transients, it can be concluded that the plant operated as designed and that *there were no unreviewed safety questions and that the public's health and safety was assured at all times.
V. CORRECTIVE ACTION A. ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:
o The light bulbs for the status lights that indicate reactor power is above P-6 were replaced, and a surveillance procedure was performed to verify their functionality.
o The PPCS alarm message for P-6 was corrected to ensure a clear understanding of the status of Permissive P-6.
0 Operations Management reevaluated their expectations for an appropriate approach to criticality at flux levels near the SR reactor trip setpoint, and communicated these revised expectations to the personnel on the Operating Shift scheduled to perform the subsequent reactor startup.
B. ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
,0 Procedure 0-1.2 was revised to incorporate the revised management expectations. These included procedural guidance for (1) a conservative power level (below the SR reactor trip setpoint), where the power increase should be stopped if P-6 status lights have not to evaluate the status of P-6, illuminated, (2) a conservative SUR when the SR reactor trip setpoint is not defeated, (3) a formalized shift briefing conducted by the Shift Supervisor, prior to commencing a reactor startup.
NRC FORH 366A (5-92)
NRC FORH 366A U.S NICLEAR REGULATORY COHISSIOH APPROVED BY QHI NO. 3150-0104 (5-92) EXPIRES 5/31/95 EST IHATED BURDEN PER RESPONSE TO CONPLY illTH THIS INFORHAT ION COLLECT ION REQUEST: 50.0 HRS ~
FORllARD CONHENTS REGARD IHG BURDEN EST INATE TO LICENSEE EVENT REPORT (LER) THE INFORHAT ION AHD RECORDS HANAGEHEHT BRAHCH TEXT CONTINUATION (HHBB 7714), U.S. NUCLEAR REGULATORY CONHISSIOHg MASHIHGTOH, DC 20555-0001 AHD TO THE PAPERMORK N
REDUCTION PROJECT (3140-0104), OFF ICE OF HANAGENENT AND BUDGET NASHIHGTON DC 20503.
FACILITY l6WE 1 DOCKET Nl(BER 2 LER NNBER 6 PAGE 3 SEQUENTIAL REVISION YEAR R.E. Ginna Nuclear Power Plant 05000244 93 007-- 00 7 OF 7 TEXT (lf more space is required, use additional copies of HRC Form 366A) (17) 0 Personnel on the Operating Shift scheduled to perform the subsequent reactor startup were trained on the revisions to procedure 0-1.2 prior to commencing the startup.
0 A Human Performance Enhancement System (HPES) evaluation was performed to determine causal factors for this event. The
.results of the HPES evaluation were used to identify the root cause and appropriate corrective actions.
0 The two Control Room operators directly involved in this.
reactor trip were removed from shift until they had completed additional simulator training on reactor startups, and had been apprised of the revised management expectations contained in the revision to procedure 0-1.2.
0 All.licensed reactor operators, as part of normal training, will be trained on the revisions to procedure 0-1.2.
0 Appropriate lesson plans for the Licensed Operator Training programs will be revised to ensure management expectations contained in procedure 0-1.2 are continually reinforced during simulator training.
VI. ADDITIONAL INFORMATION A. FAILED COMPONENTS:
None B. PREVIOUS LERs ON SIMILAR EVENTS:
A similar LER event historical .search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Nuclear Power Plant could be identified.
C. SPECIAL COMMENTS:
None HRC FORN 366A (5-92)
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