IR 05000443/2025001

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Integrated Inspection Report 05000443/2025001
ML25125A230
Person / Time
Site: Seabrook NextEra Energy icon.png
Issue date: 05/05/2025
From: Matt Young
Division of Operating Reactors
To: Coffey B
Florida Power & Light Co
References
IR 2025001
Download: ML25125A230 (1)


Text

May 5, 2025

SUBJECT:

SEABROOK STATION - INTEGRATED INSPECTION REPORT 05000443/2025001

Dear Bob Coffey:

On March 31, 2025, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Seabrook Station. On April 8, 2025, the NRC inspectors discussed the results of this inspection with Chris Robinson, Site Operations Director, and other members of your staff. The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding did not involve a violation of NRC requirements.

If you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; and the NRC Resident Inspector at Seabrook Station. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Matt R. Young, Chief Projects Branch 2 Division of Operating Reactor Safety

Docket No. 05000443 License No. NPF-86

Enclosure:

As stated

Inspection Report

Docket Number:

05000443

License Number:

NPF-86

Report Number:

05000443/2025001

Enterprise Identifier: I-2025-001-0055

Licensee:

NextEra Energy Seabrook, LLC

Facility:

Seabrook Station

Location:

Seabrook, New Hampshire

Inspection Dates:

January 1, 2025 to March 31, 2025

Inspectors:

T. Daun, Senior Resident Inspector

S. Flanagan, Resident Inspector

N. Floyd, Senior Reactor Inspector

P. Koch, Civil Engineer

G. Thomas, Senior Civil Engineer

Approved By:

Matt R. Young, Chief

Projects Branch 2

Division of Operating Reactor Safety

SUMMARY

The NRC continued monitoring the licensees performance by conducting an integrated inspection at Seabrook Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Incorrect Work Activity Risk Management Leads to Loss of 'B' Feedwater Pump and Manual Reactor Trip Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green FIN 05000443/2025001-01 Open/Closed

[H.12] - Avoid Complacency 71153 A self-revealed Green Finding was identified for Seabrooks failure to adequately evaluate the impact of performing maintenance for the 'B' main feedwater pump turbine control system in accordance with WM-AA-100-1000, "Work Activity Risk Management," and MA-AA-100,

"Conduct of Maintenance." During the maintenance, an incorrect setting in the turbine control system was selected resulting in the trip of the 'B' main feedwater pump resulting in partial loss of feedwater flow. Control room operators recognized that the loss would result in low steam generator water levels with the plant at full power so a manual reactor trip was inserted.

Additional Tracking Items

Type Issue Number Title Report Section Status LER 05000443/2024-002-00 Licensee Event Report (LER) 2024-002-00 for Seabrook Station, Manual Reactor Trip Due to 'B' MFP Trip 71153 Closed

PLANT STATUS

Seabrook Station began the inspection period operating at or near 100 percent rated thermal power. On February 13, 2025, the plant commenced down power to 48 percent rated thermal power in preparation for replacement of a loop 4 reactor coolant system flow transmitter.

Following the flow transmitter replacement on February 14, 2025, Seabrook Station returned to 100 percent rated thermal power on February 15, 2025, where it remained for the duration of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1)

'B' safety injection system during 'A' safety injection system valve maintenance and motor inspection on March 17, 2025 (2)

'B' emergency diesel generator during 'A' emergency diesel generator maintenance on March 18, 2025

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1)

'A' residual heat removal (RHR) vault (RHR-F-1B,1D,4B-Z) on February 24, 2025 (2)

'B' RHR vault (RHR-F-1A,1C,4A-Z) on February 24, 2025 (3)

'A' and 'B' electrical tunnels (ET-F-1A,1B,1C,1D) on March 11, 2025

(4) Service water pump house (SW-F-1B,1C,1D,1E-Z) on March 27, 2025
(5) Service water cooling tower (CT-F-1C,1D,2B-A) on March 27, 2025

Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the on-site fire brigade training and performance during an unannounced fire drill on February 20, 2025.

71111.06 - Flood Protection Measures

Flooding Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated internal flooding mitigation protections in the primary auxiliary building on March 26, 2025.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control room during a plant power reduction to 48 percent for replacement of a loop 4 reactor coolant system flow transmitter on February 14, 2025.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated licensed operator training conducted in the plant reference simulator on February 10, 2025.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (1 Sample)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components remain capable of performing their intended function:

(1) Main feedwater system action plan on March 27, 2025

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Risk management actions associated with emergent work on 'B' emergency diesel generator on January 30, 2025
(2) Risk management actions associated with emergent work on 'A' emergency diesel generator on March 20, 2025

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Loop 4 reactor coolant system flow transmitter drift (Action Request (AR)02505963)on January 20, 2025 (2)

'B' emergency diesel generator scavenging air header o-ring leak (AR02506824) on January 30, 2025 (3)

'A' service water pump (AR02507884) on February 15, 2025

(4) Containment fire detection deficiencies (AR02509821) on March 14, 2025
(5) RHR vault building rebar strain testing results and revised operability determination limits for alkali-silica reaction (ASR) expansion monitoring on March 25, 2025

71111.24 - Testing and Maintenance of Equipment Important to Risk

The inspectors evaluated the following testing and maintenance activities to verify system operability and/or functionality:

Post-Maintenance Testing (IP Section 03.01) (6 Samples)

(1)

'B' emergency diesel generator post-maintenance testing following air intake manifold gasket repairs on February 4, 2025

(2) Reactor coolant flow loop 4 protection channel III post-maintenance testing following replacement on February 14, 2025
(3) Rod control post-maintenance testing following replacement of failed power supply to rod control cabinet on February 25, 2025 (4)

'A' atmospheric steam dump valve post-maintenance testing following solenoid valve replacement on March 10, 2025 (5)

'A' safety injection pump post-maintenance testing following valve maintenance and motor inspection on March 18, 2025 (6)

'A' emergency diesel generator post-maintenance testing following repairs to address engine idle speed overshoot on March 21, 2025

Surveillance Testing (IP Section 03.01) (2 Samples)

(1) Supplemental emergency power supply system monthly surveillance testing on February 5, 2025 (2)

'B' emergency diesel generator operability demonstration (common mode)surveillance on March 19, 2025

Inservice Testing (IP Section 03.01) (1 Sample)

(1)

'A' RHR quarterly inservice testing and 18-month valve position verification on January 15, 2025

Diverse and Flexible Coping Strategies (FLEX) Testing (IP Section 03.02) (1 Sample)

(1) Periodic testing of FLEX fuel transfer pump on January 17, 2025

71114.06 - Drill Evaluation

Required Emergency Preparedness Drill (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated the conduct of a routine full participation emergency planning drill on January 22,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01)===

(1) For the period January 1, 2024 through December 31, 2024

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) (1 Sample)

(1) For the period January 1, 2024 through December 31, 2024

IE04: Unplanned Scrams with Complications Sample (IP Section 02.03) (1 Sample)

(1) For the period January 1, 2024 through December 31, 2024

===71152A - Annual Follow-up Problem Identification and Resolution

Annual Follow-up of Selected Issues (IP Section 03.03)===

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Review of NextEras evaluations and corrective actions of safety-related structures affected by ASR and activities required by license conditions
(2) Review of 'A' emergency diesel generator oil and glycol leaks from floating tube sheet on lube oil heat exchanger
(3) Review of fire detection deficiencies inside primary containment building

71153 - Follow-up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)

The inspectors evaluated the following LER:

(1) LER 05000443/2024-002-00, Manual Reactor Trip Due to 'B' MFP Trip, (Agencywide Documents Access and Management System (ADAMS) Accession No. ML25013A036). The inspection conclusions associated with this LER are documented in this report under Inspection Results Section 71153. This LER is Closed.

INSPECTION RESULTS

Observation: Review of NextEras Evaluations and Corrective Actions of Safety-Related Structures Affected by ASR and Activities Required by License Conditions 71152A An NRC inspector, accompanied by two civil engineers (structural) from the NRC Office of Nuclear Reactor Regulation, completed an on-site inspection at the Seabrook Station from March 24 to March 28, 2025 to review NextEras performance to monitor reinforced concrete structures affected by ASR. Activities included addressing applicable license conditions and providing corrective actions for those structures in accordance with the structures monitoring program, NRC-approved license amendment methodology document, and corrective action program procedures. Specifically, the inspectors reviewed NextEras evaluations and corrective actions associated with:

(1) corroboration study for concrete modulus-expansion correlation to address ASR license condition,
(2) results of reinforcement bar strain testing inside the RHR vaults to address ASR license condition, and
(3) temperature data collected from the containment internals structure (CIS) reactor pit area during fall 2024 refueling outage to verify thermal load assumptions used in the CIS structural evaluations.

Modulus-Expansion Correlation Corroboration Study NextEra completed the initial study required by ASR license condition

(b) in the Seabrook Station operating license to corroborate the concrete modulus-expansion correlation used to determine pre-instrument through-thickness expansion of ASR-affected concrete. As required by the license condition, NextEra notified the NRC of completion of the study by letter dated March 14, 2025 (ML25073A082). The inspectors reviewed the corroboration study report and supporting documents, including ARs 02491393, 02510025, and 02510271, to verify the study was conducted in accordance with Appendix C of MPR-4273, Revision 1, and covered at least 20 percent of installed extensometer locations at the time frame of the study. The inspectors performed independent walkdowns of a sample of accessible portions of the 14 selected extensometer sampling locations for the study to assess consistency with the sampling plan and study results. The inspectors observed that except for one location, the normalized modulus of elasticity tested at the time of the study were within or above (i.e.,

conservative) the acceptance range defined using the approach in report MPR-4273. The inspectors noted that the overall scatter of the data from the corroboration study with respect to the correlation curves appeared generally consistent with the original data set from the large-scale testing program used to develop the modulus-expansion correlation. For the one location below the acceptance range (i.e., non-conservative), NextEra plans to install an additional extensometer near that location to supplement the existing through-wall expansion monitoring and to provide for trend comparison. The NRC inspectors determined that the corroboration study met ASR license condition

(b) requirements for the initial study.

In addition, to satisfy ASR license condition (f), NextEra performed petrographic examinations of cores removed from the vicinity of extensometer locations sampled in the corroboration study. NextEra performed the petrography in accordance with ASTM C856. The inspectors reviewed NextEras report of the petrographic examination results to verify NextEra met the requirements of the license condition. The inspectors observed that the concrete specimens contained ASR and fine cracking typical of ASR-affected reinforced concrete. The inspectors also observed the petrographic examinations did not indicate formation of large mid-plane cracking or delamination resulting from ASR.

Reinforcing Bar Strain Testing in RHR Vaults NextEra performed in-situ tests on a sample of horizontal and vertical reinforcing bars (i.e.,

rebar) inside the RHR vault concrete walls and completed an evaluation of the vertical rebar stress to increase the established operability limits in the prompt operability determination for the RHR vault structure. The inspectors reviewed NextEras prompt operability determination and supporting documents to verify that operability was justified and that the structure remains capable of performing its specified safety function.

The evaluation focused on the vertical reinforcing bars and concluded that these bars remain below the nominal yield stress of the material. As part of the evaluation, NextEra performed several tests on the reinforcing bars in the B RHR vault using a hole-drilling method and a stress-relieving method to measure the strain and estimate the in-situ stress. NextEra established a new operability limit for vertical expansion based on the ASR loads estimated from the in-situ rebar stress. The inspectors noted the new operability limits for vertical expansion (as measured by the invar wires under the structures monitoring program)corresponded to the vertical reinforcement bars reaching their yield stress in the controlling load combination. NextEra did not re-evaluate the horizontal reinforcement bars since the measured expansions are lower than the established limits. The NRC inspectors determined that NextEra developed a monitoring program to detect potential rebar yield or failure due to ASR (along with other in-situ loads) as required by ASR license condition (d). The inspectors further determined the updated prompt operability determination for the RHR vault structure provided reasonable assurance that the structure remains capable of performing its intended function.

CIS Reactor Pit Temperature Data The inspectors reviewed NextEras evaluation associated with the temperature data collected from the CIS reactor pit area during the fall 2024 refueling outage (actual data captured from May 2023 - October 2024 operating cycle). The inspectors also reviewed NextEras field walkdowns of the reactor pit area in the fall 2024 refueling outage. This data was necessary to verify the thermal load assumptions used in the revised CIS structural evaluations. The inspectors noted that there were no significant changes observed in the recent fall 2024 refueling outage walkdowns compared to the previously documented distressed conditions from prior refueling outages. The recorded data for the measured ambient temperature in the reactor pit area was slightly lower than the temperature used in the structural evaluation. The inspectors observed that NextEra evaluated the lower recorded temperature using a higher and more realistic temperature boundary condition at the bedrock than was previously used, which indicated the overall thermal load is likely not reduced and the previous evaluation remains valid. The inspectors also observed that NextEra planned to monitor temperatures for an additional cycle and continue field walkdowns of the reactor pit area for the next two refueling outages to obtain additional trending data to confirm the causes of the observed distress and to confirm no additional ASR expansion needs to be evaluated. The NRC inspectors determined NextEra appropriately evaluated the recorded temperature data and planned further confirmatory actions to determine whether the revised CIS structural evaluations need to be updated.

Observation: Review of 'A' Emergency Diesel Generator Oil and Glycol Leaks from Floating Tube Sheet on Lube Oil Heat Exchanger 71152A Inspectors completed a review of the licensees corrective actions associated with lube oil and glycol leaks from the floating tube sheet area of the lube oil heat exchanger on the 'A' emergency diesel generator. Recent industry operating experience was used to determine if Seabrook was susceptible to similar failure mechanisms. While Seabrook has the same engines with essentially the same heat exchangers, inspectors reviewed packing ring replacement strategies, lube oil sampling methods, and vendor recommendations.

Inspectors reviewed the diesel engine crankcase and supply header oil sampling procedures (preventive maintenance work activity DG-SKD-A-L4) and noted appropriate sample locations and prerequisites to ensure representative samples as recommended by the vendor.

Inspectors reviewed the most recent 'A' emergency diesel generator lube oil sampling and noted normal parameters and no adverse trends (Work Order (WO)40988387-01).

Inspectors noted Seabrook engineering initiated corrective action program actions based on a recent industry operating experience failure (AR2508957-2) with a recommendation to proactively replace the packing rings and initiated actions to evaluate the preventive maintenance strategy for the packing rings (AR02509678-3).

Observation: Review of Fire Detection Deficiencies Inside Primary Containment Building 71152A Inspectors completed a review of the licensees corrective actions associated with multiple zones of containment fire detection being disabled due to material issues with containment building ionization detectors.

Inspectors noted an increasing number of fire detection zone deficiencies following the fall 2024 refueling outage. All five zones on the lower level of containment building were out of service for a period of time and required extensive maintenance efforts to restore a single zone to service. The detection system replacement was scheduled for the fall 2021 refueling outage and has been deferred until the spring 2026 refueling outage.

Inspectors noted that while the station has maintained the requirements of their fire protection program by monitoring bulk average containment temperature as required by the technical requirements manual, this has placed a burdened on the control room operators with the large number of spurious alarms that have occurred on the containment building fire detection system.

Incorrect Work Activity Risk Management Leads to Loss of 'B' Feedwater Pump and Manual Reactor Trip Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events

Green FIN 05000443/2025001-01 Open/Closed

[H.12] - Avoid Complacency 71153 A self-revealed Green Finding was identified for Seabrooks failure to adequately evaluate the impact of performing maintenance for the 'B' main feedwater pump turbine control system in accordance with WM-AA-100-1000, "Work Activity Risk Management," and MA-AA-100, "Conduct of Maintenance." During the maintenance, an incorrect setting in the turbine control system was selected resulting in the trip of the 'B' main feedwater pump resulting in partial loss of feedwater flow. Control room operators recognized that the loss would result in low steam generator water levels with the plant at full power so a manual reactor trip was inserted.

Description:

On November 19, 2024, at approximately 1:50 p.m., Seabrook operators inserted a manual reactor trip from 100 percent rated thermal power in response to a loss of the 'B' main feedwater pump turbine. Prior to the trip of the 'B' main feedwater pump, maintenance technicians were performing a replacement of one of the turbine specific primary trip packs associated with the 'B' main feedwater pump to address alarms that had occurred on the turbine control system the previous shift. There are three turbine specific primary trip packs with a trip logic of two out of three required for a turbine trip. Above 45 percent rated thermal power, typically two main feedwater pumps are in operation to maintain steam generator water level. On a low steam generator water level in any steam generator an automatic reactor trip will occur.

On the morning of November 19, 2024, the control room received main feedwater pump 'B' major alarms from the turbine control system multiple times. After initial troubleshooting by maintenance and engineering personnel, a failed turbine specific primary pack and emergency turbine protection pack was suspected. WO41000171 was generated for maintenance technicians to replace the failed packs for the 'B' main feedwater pump. WM-AA-100-1000, "Work Activity Risk Management," Section 3.8 requires the work activity owner, who is generally a department first line supervisor, to complete the risk classification and complete the mandatory actions to manage the risk associated with the work activity. Section 4.0 provides the instructions for the risk classification and specifies all aspects of the work activities shall be evaluated for risk. Attachment 1, Work Activity Risk Classification, provides a list of activities that shall be high risk which includes: 1) single point vulnerability that can cause a trip or plant transient; and 2) online work resulting in loss of component redundancy such that failure of an additional component would result in a unit trip. For each adverse consequence, Attachment 2, Risk Severity, Attachment 3, Probability of Occurrence, and 4, Risk Level Determination, are used to classify the activity risk. Based on the activity risk classification, WM-AA-100-1000 then directs actions to manage work activity risk.

MA-AA-100, "Conduct of Maintenance," provides consistent standards and expectations on the conduct of maintenance across the NextEra nuclear fleet and applies to all maintenance at all NextEra nuclear fleet sites. Section 5.5, "Field Work Preparation," states planners and/or supervisors shall determine whether an activity is a single-person task in accordance with Attachment 1. Attachment 1 states "Examples of Task that MAY NOT qualify as Single-Person-Tasks: Procedure steps that have the potential to impact plant reliability."

WO41000171 was classified as low risk because it was not recognized by Seabrook that a technician would have the capability to select the active modules in the turbine control system. It was assumed by the organization that only the replaced pack module would be able to be selected and the two inservice redundant modules would be unaffected. The first precaution in Section 3 of WO41000171 states "TRIP AVOIDANCE."

Maintenance technicians replaced the turbine specific primary trip pack using performer-verifier practices as directed by WO section 4.15. Following replacement of the turbine specific primary trip pack, a single maintenance technician continued performing the software download to the replaced pack from the turbine control system, as directed by the WO. This maintenance technician was the only technician involved with the WO that was qualified to perform actions on the turbine control system. When the maintenance technician went to download the backup file, an error message was received stating the pack required rebooting. The technician then selected the options to reboot the pack believing that only the replaced pack was selected. When the technician executed the reboot, a status window appeared showing that all three packs were being rebooted. When the three packs rebooted, a trip of the 'B' main feedwater pump turbine occurred. The control room received multiple alarms indicating the trip of the 'B' main feedwater pump and an automatic main turbine runback to 55 percent. With the unit at 100 percent power, the unit supervisor directed the reactor operator to manually trip the reactor.

Corrective Actions: With the plant shutdown, all three turbine specific primary packs and all three emergency turbine protection packs were replaced. An issue investigation was performed in accordance with Seabrook's corrective action program which resulted in modifications to the maintenance simulator to allow for technicians to gain proficiency with the turbine control system with the plant in an online status.

Corrective Action References: 2502022, 2501328, 2501443, 2501968, 2502587, 2502944

Performance Assessment:

Performance Deficiency: Inspectors determined that not performing an adequate work activity risk classification for replacement of the 'B' main feedwater pump turbine control system components was a performance deficiency. Specifically, Seabrook screened the work activity as low risk and allowed for a single-person task to perform the software download, which did not follow the requirements outlined in WM-AA-100-1000 or MA-AA-100.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, by not implementing appropriate risk reviews for the work, a single technician made a critical error that caused the trip of the 'B' main feedwater pump resulting in an unplanned manual reactor trip.

Significance: The inspectors assessed the significance of the finding using IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power. The inspectors assessed significance using Question B, Transient Initiators, of Exhibit 1, Initiating Events Screening Questions, and determined that while the finding did contribute to a reactor trip, there was not a loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. Therefore, the inspectors determined the finding to be of very low safety significance (Green).

Cross-Cutting Aspect: H.12 - Avoid Complacency: Individuals recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Individuals implement appropriate error reduction tools. Specifically, based on the recent successful performance of similar tasks on the feedwater pump turbine control system, a risk assessment was not fully vetted through the organization to understand the potential consequences or inherent risk of performing this work as would be expected for emergent maintenance that can cause a trip or plant transient.

Enforcement:

Inspectors did not identify a violation of regulatory requirements associated with this finding.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On March 28, 2025, the inspectors presented the ASR inspection results to David Sluszka, Site Vice President, and other members of the licensee staff.
  • On April 8, 2025, the inspectors presented the integrated inspection results to Chris Robinson, Site Operations Director, and other members of the licensee staff.

THIRD PARTY REVIEWS

Inspectors reviewed the June 2024 Institute of Nuclear Power Operations evaluation report that that was issued during the inspection period.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.04

Drawings

1-SI-B20446

Safety Injection System Intermediate Head Injection System

Detail

Revision 18

Procedures

ON1090.12

Equipment Long Term Layup

Revision 5

Work Orders

40894278

71111.05

Miscellaneous

Fire Protection Pre-Fire Strategies

Revision 21

CMP-25-5051

Transient Combustible Permit

Fire Protection Pre-Fire Strategies

Revision 31

Procedures

FP 2.2

Control of Combustible Materials

Revision 24

FP 6.1

Fire Protection Inspections and Logs

Revision 4

FP-AA-104-1003

Fire Response

Revision 3

MX0599.06

6-month Surveillance and Post-Maintenance Inspection of

Technical Requirements Fire-Rated Doors

Revision 13

OA1200.00

Response to Fire or Fire Alarm Actuation

Revision 28

OS0443.61

Fire Prevention Weekly Inspection Safety-Related Areas

Revision 10

Work Orders

40975472

40976282

40996812

40996968

71111.06

Miscellaneous

Report TP-7

Moderate Energy Line Break Study

Revision 5

Procedures

MA5.7

Station Barriers, Penetration Seals, and Fire Barrier Wrap

Revision 20

71111.11Q Procedures

OP-AA-100-1000

Conduct of Operations

Revision 42

OS1000.05

Power Increase

Revision 44

OS1000.06

Power Decrease

Revision 30

TR-AA-220-1002

NRC Licensed Operator Exam Security

Revision 6

TR-AA-220-1004

Licensed Operator Continuing Training Annual Operating

and Biennial Written Exams

Revision 9

TR-AA-230-1007

Conduct of Simulator Training and Evaluation

Revision 19

71111.12

Corrective Action

Documents

2502022

Procedures

ER-AA-100-2002

Maintenance Rule Program Administration

Revision 16

71111.13

Corrective Action

2506824

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

2507195

2508215

Work Orders

41002958

71111.15

Corrective Action

Documents

2497807

2498041

2499803

2500387

2500543

2505963

2506060

2507056

2507178

2507195

2507884

2508215

2508473

2508930

2508933

2509051

2509324

2509525

2509592

2510256

Work Orders

40081732

40997106

41002958

270257

71111.24

Corrective Action

Documents

2506824

2506934

2507178

2507195

2507404

2507432

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

2508100

2508750

Drawings

1-NHY-310944

Rod Control System Schematic Diagram

1-NHY-505231

Flow Instrument with Test Tee

Revision 3

1-NHY-509004

Reactor Coolant Flow Protection Set III Process Control

Block Diagram

Revision 2

9763-F-500163

Instrument Piping Containment Loop 4

Revision 13

FP58440

Rod Control System Corrective Maintenance Guide

Procedures

IS0603.005

Equipment Qualification For ASCO Solenoid Valves

Revision 15

IS0603.902

Installation/Repair of Instrument Tubing/Fittings/Clamps

Revision 8

IX1605.073

RC-F-446 Reactor Coolant Flow Loop 4 Protection Channel

III Time Response Test

Revision 6

IX1662.143

RC-F-446 Reactor Coolant Flow Loop 4 Protection Channel

III Calibration

Revision 11

LS0565.01

Fuse Control

Revision 5

OX1405.07

Safety Injection Quarterly and 18 Month Pump Flow and

Valve Test

Revision 15

OX1413.01

'A' RHR quarterly flow and 18 month valve test

Revision 33

OX1426.17

DG 1B Tech Spec Action Statement Surveillance

Revision 19

OX1461.04

SEPS Monthly availability surveillance

Revision 17

OX1462.05

FLEX Fuel Transfer Pump Periodic Testing

Revision 6

Work Orders

40081732

40756050

40812230

40858172

40881765

40889707

40894027

40894278

40894333

40971735

41002591

41002958

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

41003681

41003966

41003997

41012159

271078

71114.06

Miscellaneous

CFD 24-01

Seabrook Emergency Preparedness

01/31/2024

Procedures

EPDP-03

Emergency Preparedness Performance Indicators

Revision 27

71152A

Corrective Action

Documents

2497807

2498041

2499803

2500387

2500543

2508930

2508933

2508957

2509051

2509324

2509525

2509592

2509678

276197

Corrective Action

Documents

Resulting from

Inspection

2511473

Miscellaneous

26-0120-RPT-

001

ASR Corroboration Study Plan at Seabrook Station

03/19/2024

FP101510

Re-evaluation of Residual Heat Removal Equipment Vault

(RHR) Vertical Rebar Stress at East Interior Wall at EL (-) 45

ft

2/04/2024

FP101568

Summary and Interpretations of CIS Reactor Pit

Temperature and Field Inspection Findings

01/31/2025

FP101569

Corroboration Study for Correlation of Concrete Elastic

2/04/2025

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Modulus to ASR Expansion

FP101570

Transmittal of Petrography Examination Reports for Cores

from Seabrook Station

2/04/2025

SMPM

Seabrook Station Structures Monitoring Program Manual

Revision 18

Work Orders

00W002423

40962014

40988387

271162