IR 05000443/2019001
| ML19133A222 | |
| Person / Time | |
|---|---|
| Site: | Seabrook |
| Issue date: | 05/13/2019 |
| From: | Brice Bickett Reactor Projects Branch 3 |
| To: | Nazar M NextEra Energy Seabrook |
| Brice Bickett | |
| References | |
| IR 2019001 | |
| Download: ML19133A222 (14) | |
Text
May 13, 2019
SUBJECT:
SEABROOK STATION, UNIT NO. 1 - INTEGRATED INSPECTION REPORT 05000443/2019001
Dear Mr. Nazar:
On March 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Seabrook Unit 1. On April 18, 2019 the NRC inspectors discussed the results of this inspection with Mr. Eric McCartney, Site Vice President and other members of your staff. The results of this inspection are documented in the enclosed report.
NRC inspectors documented two self-revealing Severity Level IV violations with no associated finding. The NRC is treating these violations as a non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.
If you contest the violations or significance or severity of the violations documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC resident inspector at Seabrook. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Brice A. Bickett, Chief Reactor Projects Branch 3 Division of Reactor Projects
Docket No.: 50-443 License No.: NPF-86
Enclosure:
Inspection Report 05000443/2019001
Inspection Report
Docket Number:
05000443
License Number:
Report Number:
Enterprise Identifier: I-2019-001-0041
Licensee:
NextEra Energy Seabrook, LLC (NextEra)
Facility:
Seabrook Station, Unit No. 1 (Seabrook)
Location:
Seabrook, NH
Inspection Dates:
January 1, 2019, to March 31, 2019
Inspectors:
P. Cataldo, Senior Resident Inspector
E. Allen, Resident Inspector
J. Furia, Senior Health Physicist
Approved By:
Brice A. Bickett, Chief
Reactor Projects Branch 3
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring NextEras performance
at Seabrook by conducting the baseline inspections described in this report in accordance with
the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for
overseeing the safe operation of commercial nuclear power reactors. Refer to
https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC-identified and
self-revealing findings, violations, and additional items are summarized in the table below.
List of Findings and Violations
Reactor Coolant Loop 4 Overpower Delta Temperature Instrument Setpoint Exceeded
Allowable Value Resulting in a Condition Prohibited by Technical Specifications
Cornerstone
Significance
Cross-cutting
Aspect
Report
Section
Not Applicable
Open/Closed
Not Applicable
The inspectors identified a self-revealing, Severity Level IV, non-cited violation of Technical Specification 2.2.1, Reactor Trip System Instrumentation Setpoints, following the likely
intermittent failure of a printed circuit card in the Westinghouse 7300 portion of the reactor
protection system. This failure resulted in a calculated setpoint value greater than the
Technical Specification allowable valve for approximately 38 hours4.398148e-4 days <br />0.0106 hours <br />6.283069e-5 weeks <br />1.4459e-5 months <br /> in September 2018.
Inoperable Charging System Valve Resulting in a Condition Prohibited by Technical
Specifications
Cornerstone
Significance
Cross-cutting
Aspect
Report
Section
Not Applicable
Open/Closed
Not Applicable
The inspectors identified a self-revealing, Severity Level IV, non-cited violation of Technical Specification 3.5.2, Emergency Core Cooling Systems, which occurred when two centrifugal
charging pump emergency core cooling system subsystems were inoperable. Specifically,
the 'B' centrifugal charging pump had been out of service for more than 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> for
maintenance when it was discovered that the 'A' centrifugal charging pump's minimum flow
isolation valve would not automatically close.
Additional Tracking Items
Type
Issue number
Title
Report
Section
Status
LER 05000443/2018-002-00 Automatic Valve in Emergency Core
Cooling System Inoperable
Closed
LER 05000443/2018-003-00 Overpower Delta T Setpoint
Exceeded Allowable Value for Time
Longer than Permitted by the
Technical Specifications
Closed
PLANT STATUS
Seabrook Station began the inspection period operating at 100 percent rated thermal power.
There were no operational power changes of regulatory significance for the remainder of the
inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in
effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with
their attached revision histories are located on the public website at http://www.nrc.gov/reading-
rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared
complete when the IP requirements most appropriate to the inspection activity were met
consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection
Program - Operations Phase. The inspectors performed plant status activities described in
IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem
Identification and Resolution. The inspectors reviewed selected procedures and records,
observed activities, and interviewed personnel to assess licensee performance and compliance
with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Impending Severe Weather Sample (IP Section 03.03) (1 Sample)
(1)
The inspectors evaluated readiness for impending adverse weather conditions
for winter storm preparations on January 19-20
71111.04 - Equipment Alignment
Partial Walkdown (IP Section 03.01) (4 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following
systems/trains:
(1)
Service water vacuum breaker monthly exercise on January 7
(2)
'A' residual heat removal testing on January 16
(3)
1D battery replacement on January 31
(4)
'B' service water ocean and cooling tower return-to-service on March 1
71111.05A - Fire Protection (Annual)
Annual Inspection (IP Section 03.02) (1 Sample)
(1) The inspectors evaluated fire brigade performance on February 7
71111.05Q - Fire Protection
Quarterly Inspection (IP Section 03.01) (5 Samples)
The inspectors evaluated fire protection program implementation in the following selected
areas:
(1)
Circulating water pump room (SW-F-1A-Z) on March 25
(2)
'A' train MCC room (SW-F-1B-A) on March 25
(3)
'B' train MCC room (SW-F-1C-A) on March 25
(4)
HVAC room (SW-F-1D-A) on March 25
(5)
Service water pump room (SW-F-1E-Z) on March 25
71111.06 - Flood Protection Measures
Inspection Activities - Internal Flooding (IP Section 02.02a.) (1 Sample)
The inspectors evaluated internal flooding mitigation protections in the following area:
(1) Turbine building sump in March 2019
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
The inspectors observed and evaluated the following performance activities in the main
control room:
(1) 'B' emergency diesel generator fast start on January 28
(2) Turbine control valve testing on February 8
(3) Ocean/cooling tower service water alignment on February 28
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
The inspectors observed and evaluated a licensed operator requalification examination in
the simulator on January 28, 2019. This examination involved simulated multiple failures
and events, including: loss of a charging pump, turbine building flooding, a reactor trip
complicated by safety valve failures on the 'D' steam generator that required demonstration
of faulted steam generator emergency operating procedure actions, coupled with recovery
from a loss of all electrical power.
71111.12 - Maintenance Effectiveness
Routine Maintenance Effectiveness Inspection (IP Section 02.01) (2 Samples)
The inspectors evaluated the effectiveness of routine maintenance activities associated with
the following equipment and/or safety significant functions:
(1)
Fire seal maintenance and inspections in January 2019
(2)
Recurrent radiation monitoring instrumentation deficiencies on March 26
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated the risk assessments for the following planned and emergent work
activities:
(1)
Service water system alignment during transfer from the cooling tower to the
ocean on January 17
(2)
Safety-related 'D' battery replacement on February 13
(3)
Service water alignment and switchyard maintenance on March 8
(4)
'A' emergency diesel generator surveillance and switchyard maintenance on
March 11
(5)
Switchyard activities including breaker 294 and emergency feedwater pump testing
on March 20
71111.15 - Operability Determinations and Functionality Assessments
Sample Selection (IP Section 02.02) (4 Samples)
The inspectors evaluated the following operability determinations and functionality
assessments:
(1)
Corrosion of service water temperature element flange bolts on January 29
(2)
'B' emergency diesel generator cumulative oil leaks in March 2019
(3)
Corrosion evaluation for emergency diesel generator fuel oil transfer piping in
March 2019
(4)
'B' service water pressure transmitter corrosion on March 22
71111.18 - Plant Modifications
Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1
Sample)
The inspectors evaluated the following permanent modification:
(1) Service water discharge flow transmitter replacement (EC 292323) on March 1
71111.19 - Post Maintenance Testing
Post Maintenance Test Sample (IP Section 03.01) (6 Samples)
The inspectors evaluated the following post maintenance tests:
(1)
'B' main steam radiation monitor replacement on January 2
(2)
Battery charger 2P relay replacement on January 9
(3)
Fire pump 20B annual maintenance on January 14
(4)
'B' emergency diesel generator air start compressor swap out on February 1
(5)
Enclosure air handling fan 5A maintenance on February 19
(6)
Primary component cooling water flange fastener corrosion repair on March 4
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
In Service Testing (IST) (IP Section 03.01) (1 Sample)
(1)
Turbine-driven emergency feedwater pump and associated main steam valve timing
tests on March 20
Surveillance Testing (IP Section 03.01) (4 Samples)
(1)
'A' atmospheric steam dump valve operability test on January 4
(2)
'C' steam generator FW-P-535 channel calibration on January 24
(3)
Quarterly control rod operability surveillance on February 1
(4)
Reactor coolant system sampling activities on March 5
71114.06 - Drill Evaluation
Drill and/or Simulator-Based Licensed Operator Requalification Training (IP Section 02.01) (1 Sample)
The inspectors evaluated the emergency planning aspects of a licensed operator annual
simulator evaluation conducted in the Unit 1 plant-reference simulator on January 28. This
evaluation included the initiation conditions and reporting requirements that resulted in
associated emergency classification and notifications in accordance with prescribed
procedures of the NextEra emergency plan.
Emergency Preparedness (EP) Drill (IP Section 02.01) (1 Sample)
The inspectors evaluated the conduct of a routine, full participation emergency planning drill
No. 19-01 on March 13.
RADIATION SAFETY
71124.06 - Radioactive Gaseous and Liquid Effluent Treatment
Calibration and Testing Program (Process & Effluent Monitors) (IP Section 02.02) (1 Sample)
The inspectors reviewed gaseous and liquid effluent monitor instrument calibration,
functional test results, and alarm set-points based on National Institute of Standards and
Technology calibration traceability and offsite dose calculation manual specifications.
Dose Calculations (IP Section 02.05) (1 Sample)
The inspectors reviewed changes in reported dose values from the previous annual
radioactive effluent release reports, several liquid and gaseous radioactive waste discharge
permits, the scaling method for hard-to-detect radionuclides, offsite dose calculation
manual changes, land use census changes, public dose calculations (monthly, quarterly,
annual), and records of abnormal gaseous or liquid radioactive releases.
Instrumentation and Equipment (IP Section 02.04) (1 Sample)
The inspectors reviewed the methodology used to determine the radioactive effluent stack
and vent flow rates to verify that the flow rates were consistent with Technical Specifications,
Offsite Dose Calculation Manual and Updated Final Safety Analysis Report values. The
inspectors reviewed radioactive effluent discharge system surveillance test results based on
technical specification acceptance criteria.
Sampling and Analysis (IP Section 02.03) (1 Sample)
The inspectors reviewed radioactive effluent sampling activities, representative sampling
requirements, compensatory measures taken during effluent discharges with inoperable
effluent radiation monitoring instrumentation, the use of compensatory radioactive effluent
sampling, and the results of the inter-laboratory and intra-laboratory comparison program
including scaling of hard-to-detect isotopes.
Walk Downs and Observations (IP Section 02.01) (1 Sample)
The inspectors walked down the gaseous and liquid radioactive effluent monitoring and
filtered ventilation systems to assess the material condition and verify proper alignment
according to plant design.
OTHER ACTIVITIES - BASELINE
71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
IE01: Unplanned Scrams per 7000 Critical Hours (IP Section 02.01) (1 Sample)
For the period January 1, 2018, through December 31, 2018
IE03: Unplanned Power Changes per 7000 Critical Hours (IP Section 02.02) (1 Sample)
For the period January 1, 2018, through December 31, 2018
IE04: Unplanned Scrams with Complications (IP Section 02.03) (1 Sample)
For the period January 1, 2018, through December 31, 2018
71153 - Follow-up of Events and Notices of Enforcement Discretion
Event Report (IP Section 03.02) (2 Samples)
The inspectors evaluated the following licensee event reports which can be accessed at
https://lersearch.inl.gov/LERSearchCriteria.aspx:
(1)
Licensee Event Report 05000443/2018-002-00, Automatic Valve in Emergency Core
Cooling System Inoperable (ADAMS accession: ML18262A408). The circumstances
surrounding this licensee event report are documented in the Inspection Results
section of the report.
(2)
Licensee Event Report 05000443/2018-003-00, Overpower Delta T Setpoint
Exceeded Allowable Value for Time Longer than Permitted by the Technical
Specifications (ADAMS accession: ML18330A208). The circumstances surrounding
this licensee event report are documented in the Inspection Results section of the
report.
INSPECTION RESULTS
Reactor Coolant Loop 4 Overpower Delta Temperature Instrument Setpoint Exceeded
Allowable Value Resulting in a Condition Prohibited by Technical Specifications
Cornerstone
Severity
Cross-cutting
Aspect
Report
Section
Not Applicable
Open/Closed
Not
Applicable
The inspectors identified a self-revealing, Severity Level IV, non-cited violation of Technical Specification 2.2.1, Reactor Trip System Instrumentation Setpoints, following the likely
intermittent failure of a printed circuit card in the Westinghouse 7300 portion of the reactor
protection system. This failure resulted in a calculated setpoint value greater than the
Technical Specification allowable valve for approximately 38 hours4.398148e-4 days <br />0.0106 hours <br />6.283069e-5 weeks <br />1.4459e-5 months <br /> in September 2018.
Description: During a parameter trend review on September 27, 2018, control room
operators discovered elevated readings associated with the loop 4 overpower delta
temperature instrument setpoint values for approximately 38 hours4.398148e-4 days <br />0.0106 hours <br />6.283069e-5 weeks <br />1.4459e-5 months <br /> between September 25
and September 26. Troubleshooting activities narrowed the cause of the elevated setpoint
value to four printed circuit boards within the Westinghouse 7300 portion of the reactor
protection system. The licensee reported this to the NRC via Licensee Event Report 2018-
003-0 on November 26, 2018, in accordance with 10 CFR 50.73 requirements.
Inspectors reviewed the printed circuit board failure history for the types associated with the
setpoint vales, which included internal Seabrook Station histories, as well as applicable
industry failure rates for those circuit board types installed at several nuclear plants currently
in operation. The inspectors did not identify any trend of circuit board failures for the types
attributable to the setpoint exceedance that would be indicative of a performance-based trend
that would have been reasonably within the licensees ability to foresee and predict.
The inspectors also reviewed the licensee's implementation of the 7300 system printed circuit
board replacement program. This program is risk-ranked and applies reasonable priorities on
highly risk-significant and single-point vulnerabilities associated with safety-related aspects of
plant operation and reactor protection. The replacement program is well underway and the
inspectors determined the prioritization of the cards in the system to reasonable.
The inspectors also noted that the initial troubleshooting performed as a result of the elevated
readings, were isolated to four, specific printed circuit boards, based on their unique function
within the circuit loop. Moreover, these circuit cards were tested under the normal analog
channel operational testing procedures, and the source of the elevated readings could not be
identified as the boards test results were satisfactory.
Corrective Actions: The licensee performed an operational test of the affected channel on
September 27, 2018, and identified no issues. Subsequently, during the refueling outage on
October 21, 2018, the licensee proactively replaced the four printed circuit boards that were
considered relevant to the setpoint value exceedance that existed for those
approximate 38 hours4.398148e-4 days <br />0.0106 hours <br />6.283069e-5 weeks <br />1.4459e-5 months <br /> in September.
In addition, the licensee enhanced the instrument trend review to ensure timely identification
of this potential silent failure to ensure future failures or erratic operation of circuit boards
can be addressed appropriately, for these important technical specification and reactor
protection systems.
Corrective Action Reference: Action Request 02282344
Performance Assessment: The NRC determined this violation was not reasonably
foreseeable and preventable by the licensee and therefore is not a performance deficiency.
Specifically, the inspectors noted that there were no significant failures or intermittent failures
in the industry of the specific type of printed circuit boards that would have warranted
replacement prior to the occurrence in September 2018. Moreover, the inspectors also noted
the licensee had established a circuit card replacement program, which contained reasonable
single point vulnerability and risk prioritization attributes to drive decision-making on card
status.
Enforcement: The ROPs significance determination process does not specifically consider a
violation without a finding in its assessment of licensee performance. Therefore, it is
necessary to address this violation using traditional enforcement to adequately deter non-
compliance.
Severity: The inspectors determined that the violation was a condition prohibited by
Technical Specifications of very low safety significance, and consistent with Enforcement
Policy Section 2.2.2.d, a Severity Level IV violation.
Violation: Technical Specification 2.2.1, Reactor Trip System Instrumentation Setpoints,
requires that reactor trip system instrumentation and interlock setpoints shall be consistent
with the trip setpoint values shown in Technical Specification 2.2.1. In addition, Table 2.2-1,
item 8, notes 3 and 4, refer to calculations and values that also reference allowable values
contained in the cycle dependent Core Operating Limits Report. Technical Specification 2.2.1.b further states that with setpoints less conservative than the values shown in TS Table
2.2-1, either adjust the setpoint consistent with the setpoint value in Table 2.2-1, or declare
the channel inoperable until the channel is restored to operable status.
Contrary to the above, the applicable channel of overpower delta temperature exceeded the
technical specification allowable value for approximately 38 hours4.398148e-4 days <br />0.0106 hours <br />6.283069e-5 weeks <br />1.4459e-5 months <br /> between September 25
and September 26, without taking the applicable actions to place the channel in the tripped
condition in 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> consistent with Technical Specification 2.2.1.b.2.
Enforcement Action: This violation is being treated as a non-cited violation, consistent with
Section 2.3.2 of the Enforcement Policy.
The disposition of this violation closes Licensee Event Report 2018-003-00.
Inoperable Charging System Valve Resulting in a Condition Prohibited by Technical
Specifications
Cornerstone
Severity
Cross-cutting
Aspect
Report
Section
Not Applicable
Open/Closed
Not
Applicable
The inspectors identified a self-revealing, Severity Level IV, non-cited violation of Technical Specification 3.5.2, Emergency Core Cooling Systems, which occurred when two centrifugal
charging pump emergency core cooling system subsystems were inoperable. Specifically,
the 'B' centrifugal charging pump had been out of service for more than 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> for
maintenance when it was discovered that the 'A' centrifugal charging pump's minimum flow
isolation valve would not automatically close.
Description: On July 25, 2018, 'B' train centrifugal charging pump was tagged out of service
for maintenance in accordance with Charging Pump A & B Quarterly Flow and Valve Stroke
Test. The 'B' charging pump had been out of service for more than 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> when it was
discovered that the 'A' centrifugal charging pump minimum flow isolation valve would not
automatically close.
The purpose of the minimum flow bypass line is to recirculate discharge flow from the
centrifugal charging pump to the pump suction after cooling via the seal water heat
exchanger. In the event of an accident, the centrifugal charging pump's minimum flow
isolation valve is designed to automatically close. When the minimum flow isolation valve
closes, the centrifugal charging pump's total flow is directed to the emergency core cooling
system.
The licensee identified that a Westinghouse 7300 printed circuit board responsible for
providing signals to the 'A' minimum flow isolation valve had experienced a silent failure.
Although the board was energized, the nature of the failure prevented both an output signal to
reposition the valve and indication of failure. Technical Specification 3.5.2 requires two
independent emergency core cooling systems with one operable centrifugal charging pump
and its operable flow path. The combination of the inoperable valve and inoperable charging
pump caused a condition prohibited by technical specifications, because the A' train did not
have an operable flow path and 'B' train did not have an operable charging pump. The
licensee reported this to the NRC via Licensee Event Report 2018-002-00 on September 19,
2018, in accordance with 10 CFR 50.73 requirements.
Corrective Actions: The licensee identified the faulty printed circuit board, replaced it, and
performed a successful retest on July 26, 2018. The licensee investigated the cause of
failure and determined the valve had failed open on July 8, 2018, and had been inoperable for
17 days. The licensee entered the issue into the corrective action program, and performed a
past operability/functionality review that determined the 'A' charging pump would perform its
emergency core cooling system safety function with the inoperable valve in the open position.
Corrective Action Reference: Action Request 02273539
Performance Assessment: The NRC determined this violation was not reasonably
foreseeable and preventable by the licensee and therefore is not a performance deficiency.
Specifically, the inspectors noted that there were no significant failures or intermittent failures
in the industry of the specific type of printed circuit boards that would have warranted
replacement prior to the occurrence in July 2018. Moreover, the inspectors also noted the
licensee had established a printed circuit board replacement program, which contained
reasonable single point vulnerability and risk prioritization attributes to drive decision-making
on card status. While these circuit boards have been known to fail on occasion, the
inspectors determined, because this was a random circuit board failure, the large population
of circuit boards in various protection and control systems, the existence of the proactive
replacement program, and that the board in question experienced a silent failure that was not
readily identifiable, it was reasonable to conclude the issue was not foreseeable and
preventable, and therefore, there is no performance deficiency.
Enforcement: The ROPs significance determination process does not specifically consider a
violation without a finding in its assessment of licensee performance. Therefore, it is
necessary to address this violation using traditional enforcement to adequately deter non-
compliance.
Severity: The inspectors determined that the violation was a condition prohibited by
Technical Specifications of very low safety significance, and consistent with Enforcement
Policy Section 2.2.2.d, a Severity Level IV violation.
Violation: Technical Specification 3.5.2 Emergency Core Cooling Systems, requires two
independent emergency core cooling system subsystems to be operable, which includes one
operable centrifugal charging pump, and an operable flow path capable of taking suction from
the refueling water storage tank on a safety injection signal and automatically transferring
suction to the containment sump during the recirculation phase of operation. The associated
action requirement (a) allows a single system to be inoperable for 7 days or be in at least
HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in HOT SHUTDOWN within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.
TS 3.0.3 requires that when an LCO is not met, within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> action shall be initiated to place
in the unit in a MODE in which the specification does not apply. It further requires that the
unit be placed in hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.
Contrary to the above, on July 25, 2018, the licensee was in Mode 1 Power Operation while
the 'A' flow path had been inoperable for 17 days. This exceeded the 7 day allowed outage
time by approximately 10 days for TS 3.5.2. Further, the inoperability of both emergency core
cooling system subsystems for over 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> exceeded the allowable timeframe in TS 3.0.3.
Enforcement Action: This violation is being treated as a non-cited violation, consistent with
Section 2.3.2 of the Enforcement Policy.
The disposition of this violation closes Licensee Event Report 2018-002-00.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
On April 18, 2019, the inspector presented the quarterly resident inspector inspection
results inspection results to Mr. Eric McCartney, Site Vice President and other members
of the licensee staff.
On January 31, 2019, the inspector presented the radiation safety inspection results to
Ms. Teri Smith and other members of the licensee staff.