IR 05000341/1980018
| ML19340D635 | |
| Person / Time | |
|---|---|
| Site: | Fermi |
| Issue date: | 11/19/1980 |
| From: | Byron P, Little B, Little W NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | |
| Shared Package | |
| ML19340D632 | List: |
| References | |
| 50-341-80-18, NUDOCS 8012310511 | |
| Download: ML19340D635 (3) | |
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U.S. NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCMENT
REGION III
Report No. 50-341/80-18 Docket No. 50-341 License No. CPPR-87 Licensee: Detroit Edison Company 2000 Second Avenue Detroit, MI 48226 Facility Name: Enrico Fermi Nuclear Station, Unit 2
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Inspection At: Fermi Site, Monroe, MI Inspection Conducted: October 1-31, 1980
< J.%1L Inspectors:,B. H. Little
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[}P.M. Byron
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W. S. Little, Chief
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Projects Section 2 Inspection Summary Inspection on October 1-31,1980 (Report No. 50-341/80-18)
Areas Inspected: Routine resident inspector, pre-operational inspection consisting of a review of licensee action on previous inspection findings, IE Bulletin and Circular followup, licensee event followup, review of safety related pipe support systems, review of instrumentation (cables & terminations)
work activities, and plant tours. The inspection involved a total of 82 inspector-hours onsite by two NRC inspectors including four inspector-hours onsite during offshifts.
Results:
No items of noncompliance or deviations were identified.
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DETAILS
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1.
Persons Contacted
- T. Alessi, Project QA Director
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H. Arora, Acting Start Up Engineer
- W. Everett, Project Superintendent W. Fahrner, Manager Fermi 2 Project J. Gressner, Assistant Project QA Director S. Noetzel, Assistant Project Manager
- J. Nyquist, Acting Plant Superintendent H. Walker, Project QA Section Superivsor
- Denotes those attending weekly management meeting.
2.
Licensee Action on Previous Inspection Findings (Closed) Unresolved item (341/80-10-02) Control and sL. cage of electrical measuring and test equipment.
The inspector has completed review of licensee's 10 CFR 50.55(e) final report, and of the corrective actions identified therein. These actions have been completed or are being applied, and appear adequate to prevent recurrence. Corrective actions include; change of instrument calibration lab (QA verified), procedures developed for the re-testing of those in-struments completed prior to test suspension, procedures revised to include additional test " controls", and procedural training for start-up technicians.
No items of noncompliance or deviations were identified.
3.
IE Bulletin and Circular Followup No IE Bulletins were received during this period which require licensee action.
Licensee action on previous IE Bulletins include:
IE Bulletin 79-03A, (0 pen)
IE Bulletin 80-02, (0 pen)
Licensee reports issued on these bulletins are pending inspector review.
Followup and close out of these items will be documented in a subsequent construction report.
No items of noncompliance or deviations were identified.
4.
Licensee Event Followup Damage to EF-2 equipment; the licensee notified NRC Region III of apparent deliberate damage to an instrument tube (approximately 1/8" cut) for RHR-2-l l
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Flow Transmitter "E11-FXE-N015B".
Investigation by Edison is in progress.
Inspector followup and close out will be documented in a subsequent resident monthly Inspection Report. This matter is assigned open item
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number (341/80-18-01)
No items of noncompliance or deviation were identified.
5.
Observation of Work and Work Activities (Construction)
Safety Related Pipe Support Systems; the inspector observed completed pipe supports for the emergency equipment cooling water system.
No deformation, deterioration, or corrosion was evident. The.as-built configuration prohibits pipe contact with other pipe, equipment or components.
The inspector compared actual installation to approved drawings. The inspector verified that one of the selected supports had a modification pending. This in process change had received review and approval, and was properly documented.
Instrument Cables and Terminations; the inspector observed on going activities in cable pulling, crimping, and terminations. The inspector verified that performance and QC procedures were being followed. The inspector verified cable identifications and wireway loadings were as specified.
No items of noncompliance or deviations were identified.
6.
Plant Tours The inspector conducted tours of the reactor, auxiliary, and turbine, and RHR buildings. Specific inspection effort was devoted to licensee's maintenance of fire prevention, housekeeping and safety system integrity.
Conditions noted in all the above areas, were found to be adequate.
No items of noncompliance or deviations were identified.
7.
Exit Interview The inspector met with licensee representatives (denoted in paragraph 1)
at the conclusion of the inspection period.
The inspector summarized
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the scope of the inspection findings.
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