IR 05000266/2003003
| ML032110177 | |
| Person / Time | |
|---|---|
| Site: | Point Beach |
| Issue date: | 07/28/2003 |
| From: | Grant G Division of Reactor Safety II |
| To: | Cayia A Nuclear Management Co |
| References | |
| FOIA/PA-2006-0113 IR-03-003 | |
| Download: ML032110177 (77) | |
Text
July 28, 2003
SUBJECT:
POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT 50-266/03-03; 50-301/03-03
Dear Mr. Cayia:
On June 30, 2003, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Point Beach Nuclear Plant, Units 1 and 2. The enclosed integrated inspection report documents the inspection findings, which were discussed on July 1, 2003, with you and members of your staff.
The inspection examined activities conducted under your licenses as they relate to safety and to compliance with the Commissions rules and regulations and with the conditions of your licenses. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
This report documents three NRC-identified findings of very low safety significance (Green),
each of which was determined to involve a violation of NRC requirements. However, because of the very low safety significance and because they were entered into your corrective action program, the NRC is treating these issues as Non-Cited Violations consistent with Section VI.A of the NRC Enforcement Policy. Additionally, licensee-identified violations which were determined to be of very low safety significance are listed in this report.
If you contest the subject or severity of a Non-Cited Violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 801 Warrenville Road, Lisle, IL 60532-4351; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Point Beach Nuclear Plant facility.
In addition to the routine NRC inspection and assessment activities, Point Beach performance is being evaluated quarterly as described in the May 9, 2003, Annual Assessment Follow-Up Letter - Point Beach Nuclear Plant. Consistent with Inspection Manual Chapter (IMC) 0305, plants in the multiple/repetitive degraded cornerstone column of the Action Matrix are given consideration at each quarterly performance assessment review for (1) declaring plant performance to be unacceptable in accordance with the guidance in IMC 0305; (2) transferring to the IMC 0350 Oversight of Operating Reactor Facilities in a Shutdown Condition with Performance Problems process; and (3) taking additional regulatory actions, as appropriate.
On May 22 and July 22, 2003, the NRC reviewed Point Beach operational performance, inspection findings, and performance indicators for the first and second quarters of 2003, respectively. During the July 22nd review of Point Beach performance, we also reviewed recent 3rd quarter events, including the Unit 2 automatic trip due to a main feed pump failure on July 10, the manual safety injection signal and reactor trip on July 11, and the Unit 1 automatic trip on July 15 due to failure of a control rod drive power supply voltage regulator. From our review of these recent operational challenges and their apparent causes, we concluded that Point Beach performance, while not good, did not represent either significant degradation or unsafe operations. We determined that the plant continues to be operated in a safe manner and that no additional regulatory actions are currently warranted. The NRC will continue to closely monitor Point Beach performance consistent with the guidance in IMC 0305.
Since the terrorist attacks on September 11, 2001, NRC has issued five Orders and several threat advisories to licensees of commercial power reactors to strengthen licensee capabilities, improve security force readiness, and enhance controls over access authorization. In addition to applicable baseline inspections, the NRC issued Temporary Instruction 2515/148, "Inspection of Nuclear Reactor Safeguards Interim Compensatory Measures," and its subsequent revision, to audit and inspect licensee implementation of the interim compensatory measures required by order. Phase 1 of TI 2515/148 was completed at all commercial nuclear power plants during calender year 2002 and the remaining inspection activities for Point Beach Nuclear Plant are scheduled for completion in August 2003. The NRC will continue to monitor overall safeguards and security controls at the Point Beach Nuclear Plant.
In accordance with 10 CFR 2.790 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and any response you choose to submit will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/ RA /
Geoffrey Grant, Director Division of Reactor Projects Docket Nos. 50-266; 50-301 License Nos. DPR-24; DPR-27
Enclosure:
Inspection Report 50-266/03-03; 50-301/03-03 w/Attachment: Supplemental Information See Attached Distribution
DOCUMENT NAME: C:\\ORPCheckout\\FileNET\\ML032110177.wpd To receive a copy of this document, indicate in the box:"C" = Copy without enclosure "E"= Copy with enclosure"N"= No copy OFFICE RIII E
RIII E RIII NAME MKunowski/trn AVegel GGrant DATE 07/25/03 07/25/03 07/28/03 OFFICIAL RECORD COPY
REGION III==
Docket Nos:
50-266, 50-301 License Nos:
50-266/03-03; 50-301/03-03 Licensee:
Nuclear Management Company, LLC Facility:
Point Beach Nuclear Plant, Units 1 and 2 Location:
6610 Nuclear Road Two Rivers, WI 54241 Dates:
April 1 through June 30, 2003 Inspectors:
P. Krohn, Senior Resident Inspector M. Morris, Resident Inspector M. Kunowski, Project Engineer M. Holmberg, Reactor Inspector T. Madeda, Physical Security Inspector T. Ploski, Senior Emergency Preparedness Inspector R. Schmitt, Radiation Specialist D. Schrum, Reactor Inspector R. Winter, Reactor Inspector A. Klett, Nuclear Safety Intern F. Ramirez, Nuclear Safety Intern Approved by:
Anton Vegel, Chief Branch 7 Division of Reactor Projects
SUMMARY OF FINDINGS
IR 05000266/2003-003, 05000301/2003-003; Nuclear Management Company, LLC; 04/01/03 - 06/30/03; Point Beach Nuclear Plant, Units 1 and 2; Maintenance Risk Assessment and Emergent Work Evaluation, Temporary Modifications, Radiological Environmental Monitoring and Radioactive Material Control Programs.
The report covered a 3-month period of inspection by resident inspectors, and announced baseline inspections by regional health physics, emergency preparedness, reactor, and physical security inspectors. Three Green Non-Cited Violations (NCVs) were identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
A.
Inspector-Identified and Self-Revealing Findings
Cornerstone: Mitigating Systems
- Green.
Units 1 and 2. The inspectors identified a Non-Cited Violation of 10 CFR 50.65(a)(4) for failure to implement required risk management actions during calibration of volume control tank level transmitters during September 2002 and January 2003. The primary cause of this finding was related to the cross-cutting area of human performance in that probabilistic risk assessment, production planning, and on-shift personnel had not utilized the full capabilities of the risk assessment tool to recognize the unavailability of components associated with pre-planned work activities.
The finding is greater than minor because, if left uncorrected, it would become a more significant safety concern if risk assessments that had not considered the impact of equipment and components rendered unavailable by pre-planned activities resulted in high risk levels without compensatory risk management analyses in place. The finding is of very low significance because it was not a design or qualification deficiency, did not represent an actual loss of the safety function, and did not involve internal or external initiating events.
(Section 1R13.1)
Cornerstone: Barrier Integrity
- Green.
Unit 2. The inspectors identified a Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, for not taking appropriate and timely corrective actions to fully assess and correct degraded conditions associated with the safety-related Unit 2 containment cooling fan backdraft damper, 2W-1D2-A, during thermal performance testing activities on March 20, 2003. The primary cause of this finding was related to the cross-cutting area of human performance. Despite the involvement of the test coordinator, control room operating supervisor, and system engineer, incomplete communications and coordination resulted in damper parts on the cooling fan plenum floor not being fully identified as components affecting operation of the safety-related damper. The condition adverse to quality was identified 13 days later when, on April 2, 2003, a mechanic passing through a radiologically controlled machine shop, identified the damper counterweight amongst other controlled material.
The finding was more than minor because: 1) it affected the reactor safety barrier integrity cornerstone objective of maintaining the functionality of primary containment, in that the reliability and availability of the Unit 2, D containment cooling fan, a risk significant large-early-release component, was affected, and 2) if left uncorrected, would become a more significant safety concern if components relied upon to perform safety-related functions were returned to service prior to fully assessing and correcting degraded conditions. The finding was determined to be of very low risk significance since the degraded backdraft damper did not represent a degradation of the radiological barrier function of the control room, auxiliary building, or spent fuel pool; did not represent degradation of the barrier function of the control room against smoke or a toxic atmosphere; and did not represent an actual open pathway in the physical integrity of reactor containment or an actual reduction of the atmospheric pressure control function of the reactor containment. (Section 1R23.1)
Cornerstone: Radiation Safety
- Green.
The licensee identified a self-revealing violation of 10 CFR 20.1802, involving the failure to maintain control and constant surveillance of licensed radioactive material in an unrestricted area (an instrument and calibration training laboratory) that was not in storage. The material was an unaccounted for, 1.0 microcurie strontium-90/yttrium-90 check source, installed in an area radiation monitor.
The finding was more than minor because it was associated with the Program and Process attribute of the Public Radiation Safety Cornerstone and affected the cornerstone objective of ensuring adequate protection of public health and safety from exposure to radioactive materials released into the public domain.
This was a legacy issue, for which the apparent cause occurred prior to implementation of an effective radioactive material source control program in 1998. However, this finding was of very low safety significance in that public radiation exposure was not greater than 0.005 rem and the licensee did not have more than five radioactive material control occurrences (in the previous eight quarters). Thus, this finding will be documented as a Non-Cited Violation of 10 CFR 20.1802, for the licensees failure to maintain control of licensed radioactive material in an unrestricted area that was not in storage.
(Section 2PS3).
Licensee-Identified Violations
Violations of very low safety significance, which were identified by the licensee have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. These violations and corrective actions are listed in Section 4OA7 of this report.
REPORT DETAILS
Summary of Plant Status
Unit 1 began the inspection period at full power and remained there except for brief periods when power was reduced for routine testing. On June 25, 2003, power was reduced to 95 percent due to a minor fish intrusion. The Unit was returned to full power later that evening and remained there until June 30, when power was lowered to 95 percent due to a second minor fish intrusion.
Unit 2 began the inspection period at full power and remained there until April 5, when power was reduced to 53 percent due to a stuck open condensate pump discharge check valve that resulted in low condenser vacuum. Initially, the main turbine was manually tripped while maintaining the reactor critical. However, as a result of control rod bank overlap limits not being met, operators initiated a Technical Specification-required shutdown later the same day. Unit 2 was made critical on April 8, and returned to full power operations on April 10. The Unit remained at full power until May 2, when power was reduced to 85 percent as a condenser fouling contingency action, during starting of the Units second circulating water pump. Unit 2 returned to full power operations on May 3, and remained there until May 23, when power was reduced to 52 percent for 2P-28A main feedwater pump repairs. The Unit returned to full power operations on May 27, and remained there for most of the remainder of the reporting period.
On June 30, power was reduced to 90 percent because of a minor fish intrusion. At the end of the reporting period, reactor power was at 90 percent.
SAFETY Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
==1R01 Adverse Weather Protection
==
.1 High Wind/Tornado Preparations
a. Inspection Scope
During the week of April 26, 2003, the inspectors reviewed the facility design and the licensees procedures to evaluate the facilitys susceptibility to high winds and tornado conditions. Additionally, the inspectors walked down selected areas to evaluate plant buildings, switchyard, and equipment susceptible to high winds and tornados. The inspectors also reviewed Abnormal Operating Procedure, AOP-136, "Severe Weather Conditions," dated February 27, 2003, which prescribed station actions for severe weather conditions and several corrective action program documents (CAPs)associated with recent high wind conditions.
b. Findings
No findings of significance were identified.
.2 Hot Weather Preparations
a. Inspection Scope
During the week of June 28, 2003, the inspectors reviewed the facility design and the licensees procedures to evaluate preparations for summertime high temperatures.
Additionally, the inspectors walked down selected areas to evaluate plant equipment susceptible to high temperatures. The inspectors discussed with licensee personnel the changes that were being made to the methodology used to perform hot weather preparations as compared to the changes being made from the lessons learned during cold weather preparations.
b. Findings
No findings of significance were identified.
==1R04 Equipment Alignment
==
.1 Instrument Air System
a. Inspection Scope
During the week of April 19, 2003, the inspectors walked down the instrument air system to verify a proper return to service following the replacement of both after filters in response to the identification of desiccant fines in air filters. The inspectors observed the in-line filters for the condenser steam dumps and verified the valve lineup.
The inspectors reviewed the engineering evaluations for the failure of the after filters for the instrument air dryer.
b. Findings
No findings of significance were identified.
.2 Control Room and Cable Spreading Room Ventilation
a. Inspection Scope
During the week of June 20, 2003, the inspectors walked down the control room and cable spreading room ventilation and air conditioning system to ensure proper lineup and operation following control room envelope modifications. The inspectors reviewed the design bases, system drawings, and testing procedures. The inspectors discussed with licensee personnel the effects of cable pulls that disrupted the control room envelope and the compensatory measures taken during the modification.
b. Findings
No findings of significance were identified.
.3 Water Treatment System
a. Inspection Scope
During the week of June 20, 2003, the inspectors walked down the water treatment system to ensure proper lineup and operations following discussions of use of the water treatment system to supply the condensate storage tank during accident conditions. The inspectors walked down the system with the system engineer and discussed modifications that the licensee plans to implement during the next refueling outage, and reviewed the design basis, system drawings, and testing procedures. The inspectors reviewed the means of providing water to the auxiliary feedwater (AFW)system during an emergency.
b. Findings
No findings of significance were identified.
.4 Emergency Diesel Generator (EDG) Ventilation Systems
a. Inspection Scope
During the week of June 28, 2003, the inspectors walked down the ventilation systems for the EDGs to verify the adequacy of cooling capabilities for hot weather. The inspectors interviewed engineering staff regarding the effects on the motor starting currents of the backwards rotation of the fans for emergency diesels G03 and G04.
The licensee generated CAP033706, Potential for G-03/4 Radiator Fans to Trip Breaker When Freewheeling Backwards, and Operability Determination OPR000066, Potential for G-03/4 Radiator Fans to Trip Breaker When Freewheeling Backwards.
b. Findings
No findings of significance were identified.
==1R05 Fire Protection
==
.1 Walkdown of Selected Fire Zones
a. Inspection Scope
The inspectors walked down the following areas to assess the overall readiness of fire protection equipment and barriers:
- Fire Zone 140, Area A01-A, Valve Gallery - Unit 1;
- Fire Zone 155, Area A08, Valve Gallery - Pipeway 1;
- Fire Zone 246, Area A01-E, Electrical Equipment Room - Unit 2;
- Fire Zone 304, Area A23, AFW Pump Room Area Over the Tunnel;
- Fire Zone 308, Area A27, Diesel Room - G01;
- Fire Zone 309, Area A28, Diesel Room - G02;
- Fire Zone 700, Area A52, North Service Building; and
- Fire Zone 773, Area A71, G03 Switchgear Room.
The inspectors verified the adequacy of control of transient combustibles and ignition sources, the material condition of fire protection equipment, and the material condition and operational status of fire barriers used to prevent fire damage or propagation.
Area conditions/configurations were evaluated based on information provided in the licensees Fire Hazards Analysis Report, August 2001. The inspectors also walked down the listed areas to verify that fire hoses, sprinklers, and portable fire extinguishers were installed at their designated locations, were in satisfactory physical condition, and were unobstructed. The inspectors also verified that the physical location and condition of fire detection devices were in accordance with the Fire Hazards Analysis Report.
Additionally, the inspectors reviewed passive features such as fire doors, fire dampers, and mechanical and electrical penetration seals to verify that they were located in accordance with Fire Hazards Analysis Report requirements and were in satisfactory physical condition.
b. Findings
No findings of significance were identified.
.2 Annual Resident Inspector Observation of Unannounced Fire Drill
a. Inspection Scope
The inspectors observed an unannounced drill associated with Unit 2 circulating water pump, 2P30B, on May 6, 2003, to evaluate the readiness of licensee personnel to respond to and fight fires. The inspectors observed licensee performance in donning protective clothing/turnout gear and self-contained breathing apparatus, deploying firefighting equipment and fire hoses to the scene of the fire, entering the fire area in a deliberate and controlled manner, maintaining clear and concise communications, checking for fire victims and propagation of fire and smoke into other plant areas, removing smoke, and using pre-planned firefighting strategies to evaluate the effectiveness of the firefighting brigade. The inspectors also reviewed post-drill critique comments to evaluate the licensees candor in self-critiquing firefighting performance and make recommendations for future improvement. Finally, the inspectors reviewed licensee monitoring and trending of the firefighting deficiencies and crew challenges to evaluate the rigor with which the licensee was attempting to identify and correct potential weaknesses.
b. Findings
No findings of significance were identified.
==1R06 Flood Protection Measures
==
.1 External Food Protection
a. Inspection Scope
During the week of April 26, 2003, the inspectors reviewed external flooding design bases documents, flooding mitigation equipment, and risk analyses to determine whether existing configurations and mitigation plans were consistent with design requirements and risk analysis assumptions. The inspectors walked down the following areas to assess the overall readiness of flood protection equipment and barriers.
- Circulating Water Pump House Wave Barrier Locations;
- Diesel Generator 3 & 4 Building;
- Cable Manholes 1, 2, 3, 10, 14, 16, and 19;
- Gas Turbine (GT) Generator Building;
- Switchyard; and
- Main Transformer Area.
The inspectors focused on the material condition of flood protection equipment, and the material condition and operational status of flood barriers used to mitigate flood damage or propagation. Flood protection features such as flood doors and door gaps, subsoil drains, and flood zone penetration seals were also inspected to verify that they were in satisfactory physical condition, unobstructed, and capable of providing an adequate flood barrier. The inspectors reviewed the licensees normal and abnormal operating procedures associated with flood identification and mitigation. Also, the inspectors reviewed annunciator response procedures associated with high sump level alarms and the associated lack of equipment calibration.
The inspectors reviewed several CAPs, including an action request (AR) identified during the inspectors plant walkdowns for the manholes. In addition, several other CAPs were also reviewed to determine the adequacy of the implemented and pending corrective actions.
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification
a. Inspection Scope
On May 27, 2003, the resident inspectors observed the simulator portion of operator requalification examinations to evaluate the adequacy and proficiency of licensed operator performance. The inspectors evaluated crew performance for clarity and formality of communication; the ability to take timely action in the safe direction; the prioritization, interpretation, and verification of alarms; the correct use and implementation of procedures, including alarm response procedures; timely control board operation and manipulation, including high-risk operator actions; and group dynamics for simulator examination Scenario 099. Finally, the inspectors observed the post-examination critique, evaluated crew involvement in the discussions, and reviewed CAP033108, During LOR [Licensed Operator Requalification] Training Notification to Offsite Was Not Met in 15 Minutes, to assess the rigor of the licensees self-critique process.
b. Findings
No findings of significance were identified.
1R12 Maintenance Rule (MR) Implementation
.1 Routine Resident Inspector Review of Selected Systems
a. Inspection Scope
The inspectors reviewed the implementation of the MR to verify that component and equipment failures were identified, entered, and scoped within the MR and that selected systems, structures, and components were properly categorized and classified as (a)(1) or (a)(2) in accordance with 10 CFR 50.65. The inspectors reviewed station logs, maintenance work orders (WOs), ARs, (a)(1) corrective action plans, functional failures, unavailability records, selected surveillance test procedures, and a sample of CAPs to verify that the licensee was identifying issues related to the MR at an appropriate threshold and that corrective actions were appropriate. The inspectors also walked down portions of systems to examine material condition, ensure the proper implementation of action plans, and to verify past functional failures had been corrected. Additionally, the inspectors reviewed the licensees performance criteria to verify that the criteria adequately reflected equipment performance needs and to verify that licensee changes to performance criteria were reflected in the licensees probabilistic risk assessment. Specific components and systems reviewed were:
- Reactor Coolant System (RCS) during the week of April 19, 2003;
- Reactor Protection System during the week of May 24, 2003; and
- EDG Ventilation System during the week of May 24, 2003.
b. Findings
No findings of significance were identified.
.2 Periodic Evaluation
a. Inspection Scope
The objective of the inspection was to:
- Verify that the licensee completed the periodic evaluation within the time constraints defined in 10 CFR 50.65, (i.e., once per refueling cycle, not to exceed 2 years); ensuring that the licensee reviewed its goals, monitoring, preventive maintenance activities, and industry operating experience; and made appropriate adjustments as a result of those reviews;
- Verify that the licensee balanced reliability and unavailability during the previous refueling cycle, including a review of safety significant structures, systems, and components (SSCs);
- Verify that the licensee met the (a)(1) goals, that corrective actions were appropriate to correct defective conditions, the use of industry operating experience, and that (a)(1) activities and related goals were adjusted as needed; and
- Verify that the licensee has established (a)(2) performance criteria, examined any SSCs that failed to meet their performance criteria, or reviewed any SSCs that have suffered repeated maintenance preventable functional failures (MPFF) including a verification that failed SSCs were considered for (a)(1).
The inspectors examined the last two periodic evaluation reports for 2001 and 2002.
To evaluate the effectiveness of (a)(1) and (a)(2) activities, the inspectors examined (a)(1) action plans, justifications for returning SSCs from (a)(1) to (a)(2), and a number of CAPs (contained in the list of documents at the end of this report). In addition, the inspectors reviewed the CAPs to verify that the threshold for identification of problems was at an appropriate level and the associated corrective actions were appropriate.
The inspectors focused the inspection on the following systems:
- Chemical and Volume Control (CV);
- Gas Turbine Generator (GT);
- Residual Heat Removal (RHR); and
- Safety Injection (SI).
The inspectors also reviewed two self-assessments that addressed MR implementation at Point Beach Nuclear Plant.
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessment and Emergent Work Evaluation
.1 Review of Equipment and Components Missed in Licensee Risk Assessments
a. Inspection Scope
During the weeks of June 2 and 9, 2003, the inspectors reviewed seven NRC-identified examples of risk assessments (RAs) for which the licensee had not considered components and equipment made unavailable during pre-planned work activities to evaluate the adequacy of the licensees risk assessment process. For each of the examples, the inspectors reviewed whether the appropriate risk categories had been entered, whether the licensee had implemented normal work controls or risk management actions (RMAs) in accordance with nuclear plant procedure (NP) 10.3.7, On-Line Safety Assessment, and whether key safety functions had been preserved.
b. Findings
Introduction.
The inspectors identified a Green Non-Cited Violation of 10 CFR 50.65(a)(4) for failure to implement required RMAs during calibration of volume control tank (VCT) level transmitters during September 2002 and January 2003.
Description.
On March 17, 2003, the inspectors identified that calibration of the Unit 1 VCT level transmitters,1LT-112 and 1LT-141, in accordance with licensee instrumentation and calibration procedure (ICP) 1ICP 13.010 on January 2-3, 2003, had rendered the transmitters unavailable to perform their intended function. The inspectors evaluated the risk impact of the transmitter unavailability and identified an increase in the instantaneous core damage frequency (CDF) from 1.4E-4 per year to 3.5E-4 per year, an increase from 4.1 to 10.3 times the average-maintenance CDF that had been unnoticed by the licensee, but which had remained in the licensee-defined Yellow risk category.
Similarly, the inspectors reviewed calibration of the Unit 2 VCT level transmitters. The calibrations, performed on September 9-10, 2002, resulted in an instantaneous CDF increase of 1.76E-4 per year. This event increased risk from the licensee-defined Green to Yellow category.
Licensee procedure NP 10.3.7, Step 4.2.2, defined the Yellow risk category and specified RMAs that were required to ensure that the assumptions in the probabilistic risk assessment model for equipment availability were not exceeded. As defined in Steps 4.2.2.b and 4.2.2.c, these RMAs included Shift Manager approval for pre-planned entries into the Yellow risk category; monitoring and shortening the duration of the activity; eliminating the overlap of two or more activities that compounded the risk impact; ensuring that personnel associated with the work activity had a heightened awareness of the risk impact; ensuring that work which challenged the availability of redundant operable equipment was avoided; and posting redundant equipment as protected. Both VCT level transmitter calibration activities were pre-planned and had been included in the list of scheduled activities for the applicable work week. Since the licensees risk assessments had not recognized the unavailability of the level transmitters as a result of performing the calibrations, appropriate RMAs as specified in NP 10.3.7, Steps 4.2.2.b and 4.2.2.c, for the Yellow risk category were not implemented as required.
Other inspector-identified examples involving risk assessments that either did not consider the risk impact of equipment and components rendered unavailable by pre-planned work activities or assigned unavailable components to the incorrect Unit included:
- 480-volt safeguards bus undervoltage relay calibrations in accordance with routine maintenance procedures (RMPs) 1(2)RMP 9056-4(5). This observation affected six undervoltage relays associated with Unit 1 and six with Unit 2;
- Testing of Unit 2 instrument air primary containment isolation valves 2IA-3047 and 2IA-3048 in accordance with inservice test (IT) procedure 115. Two additional instrument air containment isolation valves associated with Unit 1 were also affected by this observation;
- 4160-volt safeguards bus undervoltage relay calibrations in accordance with 1(2)RMP 9056-6(7). This observation affected six undervoltage relays associated with Unit 1 and six with Unit 2;
- Assignment of an unavailable condenser steam dump to Unit 1 when the unavailable component actually applied to Unit 2; and
- Monthly testing of the diesel-driven fire pump in accordance with Procedure 0-PT-FP-002. During diesel cooldown, the back-up source of turbine-driven AFW pump bearing cooling was rendered unavailable.
The inspectors determined that the circumstances of each example had resulted in small changes in the CDF such that no additional RMAs had been required. Multiplying the instantaneous change in CDF by the duration of each activity, the inspectors determined that the seven examples collectively had resulted in an incremental core damage probability increase of approximately 7E-7.
Analysis.
The inspectors determined that failure to implement required RMAs during VCT level transmitter calibrations was a performance deficiency warranting a significance evaluation in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Disposition Screening, issued on February 21, 2003.
The inspectors determined that the issue was more than minor because, if left uncorrected, it would become a more significant safety concern if RAs that had not considered the impact of equipment and components rendered unavailable by pre-planned activities resulted in high risk levels without compensatory RMAs in place.
The inspectors used IMC 0609, Significance Determination Process [SDP],
Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations, regarding mitigating systems and determined that the finding was not a design or qualification deficiency, did not represent an actual loss of the safety function, or involve internal or external initiating events. Therefore, the finding screened as Green, a finding of very low safety significance.
Enforcement.
Section 10 CFR 50.65(a)(4) requires, in part, that before performing maintenance activities (including but not limited to surveillance, post-maintenance testing, and corrective and preventative maintenance), the licensee assess and manage the increase in risk that may result from the proposed maintenance activities.
Contrary to this, on September 9-10, 2002, for Unit 2, and on January 2-3, 2003, for Unit 1, the licensee failed to assess the risk associated with volume control tank level transmitter calibration activities performed in accordance with procedures 1(2)ICP 13.010. This resulted in the entry into higher risk configurations for which the licensee had not implemented additional risk management actions to obtain management approvals; monitor and shorten the calibration duration; eliminate the overlap of activities that could have compounded the risk impact; ensure that work activity personnel had a heightened awareness of the risk impact; and protect redundant equipment. Because of the very low safety significance, this violation is being treated as a Non-Cited Violation (NCV), consistent with Section VI.A of the NRC Enforcement Policy: NCV 50-266/301/03-03-01, Failure to Implement Risk Management Actions for Components Made Unavailable by Pre-Planned Work Activities. This issue was entered into the licensees CAP as CAP031681, Activities Missed in On-Line Risk Evaluations.
.2 Risk Review of Selected Work Week Activities
a. Inspection Scope
The inspectors reviewed the licensees evaluation of plant risk, scheduling, configuration control, and performance of maintenance associated with planned and emergent work activities to verify that scheduled and emergent work activities were adequately managed. In particular, the inspectors reviewed the program for conducting maintenance risk safety assessments to verify that the planning, risk management tools, and the assessment and management of on-line risk were adequate. The inspectors also reviewed actions to address increased on-line risk when equipment was out-of-service for maintenance, such as establishing compensatory actions, minimizing the duration of the activity, obtaining appropriate management approval, and informing appropriate plant staff, to verify that these actions were accomplished when on-line risk was increased due to maintenance on risk-significant systems, structures, and components. The inspectors also reviewed selected procedures to verify that execution did not render risk-modeled components unavailable. The maintenance risk assessments for work planned for the weeks beginning on the dates listed below were reviewed:
- April 6, 2003. This work included G05 GT repairs, recovery from a Unit 2 forced shutdown, 4160-volt safeguards bus relay calibrations, and D-105 battery performance testing;
- April 27, 2003. This work included undervoltage relay checks for B08/B09, SI valve testing, and reactor protection and safeguards logic testing;
- May 4, 2003. This work included A component cooling water (CCW) heat exchanger inspections and cleaning, SI system venting, D-106 station battery testing, and 4160-volt bus undervoltage relay calibrations. In addition, the inspectors reviewed CAP032992, 2A-04 Relay Work Not Included in Workweek X03 Risk Projection; which was written as a result of this inspection activity, and discussed the licensees failure to identify that the calibration of 4160-volt nonsafety-related undervoltage relays, associated with offsite power supplies to the safeguards buses, affected plant risk;
- May 11, 2003. This work included D-106 station battery testing, D-108 battery charger maintenance, SI and RHR pump and valve testing, and P-32E service water (SW) pump switch replacement activities. In addition, the inspectors reviewed CAP033074, Activities Evaluated for On-Line Risk in Work Week X04, which was written as a result of this inspection activity and discussed the licensees failure to identify that activities associated with 480-volt safety-related undervoltage relay calibrations and primary containment instrument air valve testing affected plant risk;
- June 8, 2003. This work included 1-DY-02 inverter maintenance for the entire week. The inspectors reviewed the equipment associated with 1-DY-02 and the effect on other work during the week on the risk profile. The inspector reviewed midweek changes that affected risk and the effects of errors made in the risk profile by work week planning staff. These errors were subsequently corrected by the shift technical advisor (STA);
- June 15, 2003. This work included battery charger D-09, CCW train B, battery charger D-07, and AFW pump and valve testing. The inspectors reviewed the possible combinations of concurrent work that could cause maintenance risk conditions to be categorized as Red, and verified that the licensee did not enter a Red risk situation. The inspectors reviewed the stop and start time for the various work associated with the risk possibilities; and
- June 22, 2003. This week included a review of the changes in the work week schedule due to red (high demand) electrical grid conditions. The inspectors verified that the rescheduling did not change the plants risk profile to Red. The inspectors reviewed the 1B-04 bus fuse replacement and plant configuration.
b. Findings
No findings of significance were identified.
1R14 Personnel Performance During Non-Routine Plant Evolutions and Events
.1 Cross Unit Leakage Caused Dilution on Unit 1
a. Inspection Scope
The inspectors reviewed operator action during an inadvertent Unit 1RCS dilution and reviewed licensee response to and investigation of the event afterwards. During the Unit 2 power reduction to 50 percent (begun at 12:18 a.m., May 24, 2003), operators placed the Unit 2 letdown orifice on line about 2:01 a.m. This increased the pressure in the Unit 2 gas stripper system from 40 to 50 pounds per square inch-gauge. The increase resulted in leakage from the Unit 2 side of the system to the Unit 1 side. The leakage resulted in pure water being added to the Unit 1 VCT, causing positive reactivity addition and VCT level increase indications. At 11:00 a.m. the Unit 1 reactor operator noted that there had not been a dilution planned during his shift and that VCT level had increased. The licensee initiated an investigation of the source of the dilution.
At 12:08 p.m., the licensee identified the leak which was determined to be through one of the gas stripper system crossconnect valves. The licensee isolated the leak at 12:54 p.m.
b. Findings
No findings of significance were identified.
.2 Unit 2 Main Feedwater Pump Casing Leak
a. Inspection Scope
During the week of May 23, 2003, the inspectors monitored operator actions for a secondary leak on the Unit 2 A main feedwater pump leak from a bolt hole in the upper casing to ensure plant and personnel safety were maintained. At 10:31 a.m.,
Unit 2 operators entered AOP 24, Secondary Steam Leak procedure, and reduced power. The steam leak began as a small wisp and increased to about 2 to 3 feet in length over the next several hours. The plant power was reduced to approximately 50 percent and the main feedwater pump was isolated and repaired.
b. Findings
No findings of significance were identified.
.3 Both Units Reduce Power Due to Fish Intrusion
a. Inspection Scope
During the week of June 30, 2003, the inspectors observed operators reduce power on both Units to 95 percent because of decreasing condenser vacuum, starting at 2:45 p.m. The vacuum problem was caused by a fish intrusion in the circulating water pump bays. Operators secured a Unit 1 circulating water pump and lined up the swing water box vacuum pump to maintain flow through the condenser. Unit 1 was then stabilized at 95 percent power. Auxiliary operators cleaned the strainers for the Unit 1 condenser water box vacuum priming pump and shifted the swing pump to Unit 2. Operators secured a Unit 2 circulating water pump but vacuum continued to be lost until the swing vacuum priming pump was shifted from Unit 1. The operators reduced power on Unit 2 to 90 percent.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations
.1 Multiple Battery Chargers Under Certain Conditions Could Trip
a. Inspection Scope
During the week of June 9, 2003, the inspectors assessed Operability Determination, OPR000063, Potential Tripping of Battery Chargers. The inspectors examined the effects of a problem with breaker coordination to determine the potential operability.
The condition could lead to a trip of feeder breakers for safety-related battery chargers D-09, D-107, D-108, and D-109, and could affect the plant recovery from a loss of offsite alternating current (AC) voltage with a SI signal, from a loss of AC voltage, or from a station blackout. The inspectors discussed the compensatory measures with operations staff and walked down affected equipment. The inspectors also interviewed selected system and electrical engineering personnel to understand fully the potential implications of the issue.
b. Findings
No findings of significance were identified.
.2 Pump Motor Terminal Equipment Qualification (EQ)
a. Inspection Scope
During the week of May 17, 2003, the inspectors reviewed the Operability Determination OPR 000059, EQ Pump Motor Splices Not Qualified/No Sound Reasons Documented, for the emergency core cooling system motors that require EQ in accordance with 10 CFR 50.49 to ensure that the connections meet the operability requirements. The inspectors reviewed the regulatory requirements and the basis for the changes in the material that was used for the terminal splices. The inspectors also interviewed the diesel and electrical cable engineers about the splices that had been changed during the life of the plant as to the possible application of the operability determination. The licensee operability determination of the EQ conditions verified that the terminals met the EQ requirements and were operable and the documentation was being corrected.
b. Findings
No findings of significance were identified.
.3 Intermediate and Power Range Instrument Cable Separation
a. Inspection Scope
During the week of May 24, 2003, the inspectors reviewed information regarding separation of the safety-related N-00044 power range instrument cables and the nonsafety-related N-00035 and N-00036 intermediate range cables. The inspectors verified that the plant was meeting the current licensing basis and Institute of Electrical and Electronics Engineers 384. The inspectors reviewed CAP032083, N44 Power Range Protective Circuit Isolation Compromised by Control Grade Signal, and Operability Determination OPR 00055, Separation Requirement Violation in 1C-130 and 2C-133; N-00044, N-00035, and N-00036; Unit 0," Revision 0 and Revision 1, to verify that the cables were not separated and discussed the issue with the electrical design and system engineers. The separation of nonsafety-related and safety-related cables of low amperage is covered by The Institute of Electrical and Electronics Engineers Standard 384, Criteria for Independence of Class IE Equipment and Circuits.
The safety-related sections of the nuclear instrument cables are separated either in different cable trays or with isolation amplifiers.
b. Findings
No findings of significance were identified.
.4 Incorrect Leak Detection Information in Approved Westinghouse Commercial Atomic
Power Report (WCAP)
a. Inspection Scope
During the week of May 24, 2003, the inspectors reviewed Operability Determination OPR000060, Incorrect Leak Determination Information in Approved WCAP, for impact on the decision by NRC to grant permission for CCW inside containment closed loop determination, power up-rate, and control room envelope changes. On May 13, the licensees licensing group discovered that WCAP 15065, 15105, and 15107 referred to containment leakage criteria for 1 gpm in 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. This information was considered by the NRC as part of a safety analysis to reclassify the CCW system as a closed system inside containment, but was not used in the final determination to allow the reclassification. The WCAPs should have stated that the leak detection system at Point Beach was required to identify 1 gpm in 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. The licensee contacted Westinghouse and the determination of operability did not change when the 4-hour criteria was applied.
b. Findings
No findings of significance were identified.
.5 Elevated Unit 2 A Steam Generator AFW Injection Line Temperatures Due to Check
Valve Backleakage
a. Inspection Scope
During the week of May 19, 2003, the inspectors reviewed Operability Determination OPR000061, Unit 2, Piping EB-10, Increased Temperatures on AFW Piping, to evaluate the impact of elevated injection line temperatures on the ability of the AFW system to provide design basis flows to the steam generators during accident and anticipated operational conditions. The inspectors examined thermography data, past material history, and selected WOs to determine which check valves were leaking. The inspectors considered the effects of localized cavitation causing loss of minimum pipe wall thicknesses and the formation of vapor pockets leading to potential waterhammer and steam binding concerns to verify that the system remained capable of performing the intended safety functions. The inspectors also verified that the licensees compensatory actions were adequate and sufficiently conservative to prevent American Society of Mechanical Engineers Code allowable stresses on the AFW injection line inside containment from being exceeded during seismic events. Finally, the inspectors reviewed CAP033025, Issues Encountered During Preparation of Operability Determination OPR 000061, Revision 0, and the licensees check valve repair plans to ensure that actions were being taken commensurate with the potential safety significance.
b. Findings
No findings of significance were identified.
.6 Instrument Air Rework
a. Inspection Scope
The inspectors reviewed CAP033625, New ASCO Solenoid Valve Fails Operational Check Following Pre-use Bench Test, concerning the new solenoid valve on the air compressor that failed twice, but passed the test on the bench and the operability determination for the instrument air system. The inspectors discussed corrective actions and follow-up investigations with the system engineer and learned that the internal valve for the four-way solenoid would not work using system pressure.
b. Findings
No findings of significance were identified.
.7 Failure of Valve 1CV-369A
a.
The inspectors reviewed the licensees documentation concerning the installation of valve 1CV-369A without proper documentation of a dye penetrant (PT) exam to verify that the valve met American National Standards Institute (ANSI) requirements. The inspectors reviewed CAP0131959, Vendor did not fulfill requirements of purchase order; CA02289799, Assess Adequacy of Installed 1CV-369A Without Documented PT Exam; Apparent Cause Evaluation (ACE) ACE 001263, Vendor Did Not Fulfill Requirements of Purchase Order; NP 9.9.6 (Quality Receipt) form FP-SC-RSI-02, Revision 0; OPR 000064, Purchase Specification Requirements Not Performed for 1CV-00369A Replacement Valve Operability Determination; PO 4500429607, Purchase Order for Edward Vogt Valve Company; and WO9937802, Replace CV-00369A, to verify that the valve met all of the requirements for the function it was to perform. The inspectors verified that the procurement process and quality validation requirements were established in procedures. The inspectors noted that the individual quality control specialist work had been reviewed and no other cases were identified.
The equipment met the ANSI standards and had been tested to ensure that it would perform its intended function.
b. Findings
No findings of significance were identified.
1R16 Operator Workarounds (OWAs)
.1 Remote Indicators for 1/2P-29 Discharge Motor-Operated Valves
a. Inspection Scope
During the week of June 9, 2003, the inspectors reviewed OWA 0-03R-004 AF to verify that the workaround was properly classified and dispositioned in accordance with the criteria of the licensees procedure. The workaround concerned the inability of the remote level indicators associated with 1/2P-29 [turbine-driven AFW pump] discharge motor-operated valves to stay within the calibration tolerance range of the local indication. The inspectors reviewed the adequacy of licensee actions to address the issue; examined the remote and local indicators to verify that all impacts were understood and evaluated the potential risk impacts to ensure that the workaround did not impact the operators ability to implement normal, abnormal, and emergency operating procedures.
b. Findings
No findings of significance were identified.
.2 Review of Charging Pump Trips on Return to Service
a. Inspection Scope
During the week of June 9, 2003, the inspectors reviewed OWA 2-02R-005 CV to verify that the workaround was properly classified and dispositioned in accordance with the criteria of the licensees procedure. The workaround concerned the frequent tripping of the charging pump from overspeed because of the inability to precisely set to optimum setting. The inspectors reviewed the adequacy of licensee actions to address the issue, and examined all impacts on the operators ability to implement normal, abnormal, and emergency operating procedures.
b. Findings
No findings of significance were identified.
1R19 Post-Maintenance Testing (PMT)
.1 SW Pump 32F Motor Replacement
a. Inspection Scope
During the week of May 17, 2003, the inspectors reviewed the documentation for the replacement of 32F SW pump motor. The inspectors reviewed the activity to ensure that the PMT was appropriate for the scope of work performed and that the SW pump remained capable of performing the intended safety function. The inspectors reviewed the completed test and WO documentation to determine the adequacy of the procedures used; to verify that the test data were complete, appropriately verified, and met the requirements of the test procedure; and to ensure the system had been restored to an operable status.
b. Findings
No findings of significance were identified.
.2 Instrument Air Compressor Unloader Solenoid Replacement
a. Inspection Scope
During the week of May 24, 2003, the inspectors reviewed the replacement and return to service of the unloader solenoid for the instrument air compressor K-2B. The inspectors reviewed the activity to ensure that the PMT was appropriate for the scope of work performed. The replacement solenoid was from a different manufacturer. The inspectors reviewed the engineering documentation to ensure that the replacement solenoid was comparable to the original. During the initial PMT, the operators found that the solenoid valve was not repositioning correctly and one of the Swagelok fittings was leaking. An addendum was developed for the work package and the PMT failed a second time. During the second PMT, the unloader valve did not position correctly. The work package was again returned to maintenance and a second rework was performed.
b. Findings
No findings of significance were identified.
.3 Unit 1 C Incore Flux Detector Replacement
a. Inspection Scope
During the week of May 19, 2003, the inspectors reviewed PMT activities associated with replacement of the Unit 1 C incore flux detector, 1FM-CH-C. The inspectors reviewed the PMT to ensure that it was appropriate for the scope of work performed and the detector remained capable of monitoring in-core conditions. The inspectors reviewed the completed troubleshooting and WO documentation to determine the adequacy of the procedures used; to verify that troubleshooting data were complete, appropriately verified, and met the requirements of the test procedure; to ensure the detector had been restored to an operable status; and to determine why the first attempt at replacing the detector had been unsuccessful.
b. Findings
No findings of significance were identified.
.4 Unit 2 CCW Pump Rotating Assembly Replacement
a. Inspection Scope
During the week of June 2, 2003, the inspectors reviewed activities associated with the Unit 2, A CCW pump, 2P-11A, to ensure that the PMT was appropriate for the scope of work performed and the pump remained capable of performing the intended safety function. The inspectors also observed portions of the maintenance to examine the material condition of selected pump components. The inspectors reviewed the completed test and WO documentation to determine the adequacy of the procedures used; to verify that the test data were complete, appropriately verified, and met the requirements of the test procedure; and to ensure the system had been restored to an operable status. Finally, the inspectors observed the running pump following PMT activities to verify appropriate gland leakage and reviewed licensee activities to correct excessive oil consumption due to movement of an oil seal.
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing
.1 Missed Calibration of Degraded Voltage Relays
a. Inspection Scope
During the week of April 7, 2003, the inspectors reviewed the circumstances associated with missed Technical Specification (TS) Surveillance Requirement (SR) 3.3.4.3.b concerning calibration of 4160-volt safeguard bus degraded voltage relays to determine whether TS requirements had been satisfied. The inspectors reviewed compliance with TS SR 3.0.3 and the associated risk evaluation when, due to severe weather, performance of the surveillance was delayed for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The inspectors also reviewed routine maintenance and operations refueling test procedures to ensure that all portions of the safeguards circuitry associated with the degraded voltage relays were tested for 2-out-of-3 coincidence logic functions, electrical continuity, and the ability of relay contacts to change state.
b. Findings
No findings of significance were identified.
.2 Primary Leak Rate Calculation
a. Inspection Scope
During the week of April 26, 2003, the inspectors reviewed the RCS leak rate calculation program to determine whether TS requirements had been satisfied. The inspectors reviewed the daily calculations performed by the shift operating crew and the trend program and review performed by engineering. The inspector discussed alternative methods for identifying RCS leakage with the system engineer and discussed the draft procedures that were being written by the licensee.
b. Findings
No findings of significance were identified.
.3 Diesel Generator G01
a. Inspection Scope
During the week of May 24, 2003, the inspectors reviewed the diesel generator G01 quarterly testing and SW cooler cleaning to determine whether TS requirements had been satisfied. The inspectors reviewed the results of pole drop testing performed during the vibration trend testing and the reviews performed by engineering. The inspector discussed the vibration monitoring program with the system engineer.
b. Findings
No findings of significance were identified.
.4 Control Room Heating and Ventilation
a. Inspection Scope
During the week of June 20, 2003, the inspectors reviewed the control room ventilation quarterly testing to determine whether TS requirements had been satisfied. The inspectors reviewed the flow rate and differential pressure testing information performed during the surveillance testing and the reviews performed by engineering.
The inspectors reviewed the WOs associated with past performance problems.
b. Findings
No findings of significance were identified.
.5 Station Battery Tests
a. Inspection Scope
During the week of June 23, 2003, the inspectors reviewed the station battery D-106 Discharge Tests and Equalizing Charge and the Station Battery 92-day and 12-month surveillance tests to determine whether TS requirements had been satisfied. The inspectors reviewed the tests results, minor problems that were noted during testing, and the reviews performed by engineering staff. The inspector discussed the battery and DC system health with the system engineer.
b. Findings
No findings of significance were identified.
1R23 Temporary Plant Modifications
.1 Need for a Unit 2 Containment Cooling Fan Discharge Damper Temporary Modification
Not Identified In a Timely Manner
a. Inspection Scope
During the weeks of April 19 and 26, 2003, the inspectors reviewed the temporary modification package and WOs associated with the Unit 2, D containment cooling fan discharge damper, 2W-1D2-A, to verify that the modification was properly installed, had no effect on the operability of the safety-related equipment, and met design basis requirements. The inspectors interviewed selected maintenance, operations, and engineering personnel to assess the rigor of licensee communications and the opportunities to have identified containment cooling fan inoperability at the earliest opportunity. The inspectors also reviewed documentation associated with Operating Instruction (OI) 131, Performance Test of 2HX-15D1-D8 Containment Fan Cooler Unit 2, to determine when the 2W-1D2-A discharge damper degraded conditions were first noticed.
b. Findings
Introduction.
The inspectors identified a finding of very low significance for not taking appropriate and timely corrective actions to fully assess and correct degraded conditions associated with the safety-related Unit 2 containment cooling fan backdraft damper, 2W-1D2-A, during thermal performance testing on March 20, 2003. Despite the involvement of the test coordinator, control room operating supervisor, and system engineer, incomplete communications and coordination resulted in damper parts not being installed in the damper which affected damper operability. The condition adverse to quality was identified on April 2 when maintenance personnel identified the damper counterweight had not been installed in the damper. A Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, was identified.
Description.
Operating Instruction 131 was performed on March 20, 2003, to determine the heat removal capability of the Unit 2 containment fan coolers. During OI-131, Step 5.4.10, foreign material exclusion closeout activities, the test coordinator noticed and documented that the top louver on the 2W-1D2-A backdraft damper was disconnected from the positioning rod. The test coordinator also noticed that a 4-inch by 4-inch block of metal and two small brackets were lying on the containment cooling fan plenum floor and that while the top louver was shut, the lower louvers were all open. The test coordinator provided his observations to the control room operating supervisor (OS), who was a licensed senior reactor operator, after exiting primary containment. The control room OS recognized that the backdraft damper in question performed the safety-related function of closing to prevent airflow from the containment accident recirculation fan from flowing back through the normal cooling fan during loss-of-coolant or main steam line break design basis events inside containment. The OS contacted the system engineer during the evening of March 20, to inform him of the test coordinators observations and to gain engineering support for determining containment fan cooler operability prior to returning the fan to service. Based on the discussions with the system engineer and the test coordinator, the OS decided to declare the discharge damper operable and return the containment cooling fan to service. The OS based his decision on the premise that the top louver was already shut and the lower louvers were free to rotate. The OS reasoned that the top louver was already in the safety-related position and the lower louvers would still be able to shut to perform the intended safety function.
On April 2, 2003, a mechanic noticed a counterweight on a table in a radiologically controlled machine shop in the primary auxiliary building. The mechanic recognized that the counterweight, the same 4-inch by 4-inch block of metal that had been noticed by the test coordinator on March 20, was from a safety-related backdraft damper. The mechanic informed the system engineer who discussed the mechanics observation with operating crew. The containment accident recirculation fan, 2W-1D1, and the containment cooling fan, 2W-1D2, were declared out-of-service at 2:05 p.m. the same day. Subsequent containment entries confirmed that the counterweight had detached from the 2W-1D2-A discharge damper, several of the louver bearings appeared to have seized resulting in the damper being stuck in the partially open position, the damper linkage was detached from the top louver, the top louver was closed with the remaining louvers being partially open, and that some force was required to close the damper.
Temporary Modification 03-012, 2W-001D2-A Damper Closure, was subsequently prepared and installed by the morning of April 3, to secure the damper in the closed, safety-related position, thereby returning the containment fan cooler to an operable condition.
During document reviews and interviews with the test coordinator, OS, system engineer, and the mechanic who identified the counterweight lying in the machine shop, the inspectors found that, despite the communications that occurred,
- The system engineer was not aware that loose parts had been found on the cooling fan plenum floor during the test coordinators foreign material closeout activities. The system engineer stated that he had recommended returning the cooling fan to service based on the premise that the upper louver was already in the safety-related position and the lower louvers were free to rotate;
- Neither the test coordinator, OS, or system engineer recognized that the 4-inch by 4-inch block of metal found on the containment cooling fan plenum floor on March 20, 2003, was a counterweight associated with the discharge damper, 2W-1D2-A. When the counterweight became detached from the discharge damper the configuration of the safety-related component changed. Thus, a formal operability evaluation should have been completed prior to returning the containment fan cooler to service in the existing condition;
- Additional expertise, beyond the system engineer and test coordinator, was not obtained on the evening of March 20. Organizationally, the licensee did not require a system engineer to physically inspect the discharge damper or the parts found on the plenum floor or request mechanical maintenance personnel to inspect the same. Had system engineering or mechanical maintenance inspections occurred, the inspectors considered it likely that the degraded damper condition would have been identified and an operability evaluation performed prior to returning the containment cooling fan to service;
- The OI-131 post-maintenance test was not written to verify that the safety-related function of the 2W-1D2-A discharge damper could be met.
Specifically, Steps 5.4.14 and 5.4.20 started both the containment accident recirculation fan and the containment cooling fan to check for normal air flow rates. None of the OI-131 PMT steps ran the containment accident recirculation fan alone such that closure of the 2W-1D2-A discharge damper could be verified;
- Neither the OS or test coordinator checked to see if the lower louvers were difficult to rotate on March 20. Inspections on April 2, revealed that the lower louvers could only be closed when some force was applied and that bearing damage had occurred; and
- The test coordinator did not have specific containment fan cooling system knowledge and did not identify the 4-inch by 4-inch block of metal as the 2W-1D2-A discharge damper counterweight.
Analysis.
The inspectors determined that not taking appropriate and timely corrective actions to fully assess and correct the degraded conditions associated with the safety-related Unit 2 containment cooling fan backdraft damper, 2W-1D2-A, on March 20, 2003, was a performance deficiency warranting a significance evaluation in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Disposition Screening, issued on February 21, 2003. The inspectors determined that the issue was more than minor because: 1) it affected the reactor safety barrier integrity cornerstone objective of maintaining the functionality of primary containment in that the reliability and availability of the Unit 2, D containment cooling fan, a risk significant large-early-release component, was affected, and 2) if left uncorrected, would become a more significant safety concern in subsequent years if components relied upon to perform safety-related functions were returned to service prior to fully assessing and correcting degraded conditions.
The inspectors used IMC 0609, Significance Determination Process, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations, regarding containment barriers and determined that the finding did not represent a degradation of the radiological barrier function of the control room, auxiliary building, or spent fuel pool; did not represent a degradation of the barrier function of the control room against smoke or a toxic atmosphere; did not represent an actual open pathway in the physical integrity of reactor containment or an actual reduction of the atmospheric pressure control function of the reactor containment. Therefore, the finding screened as Green, a finding of very low safety significance.
Enforcement.
Criterion XVI, Corrective Action, of 10 CFR Part 50, Appendix B, requires, in part, that measures be established to assure that conditions adverse to quality are promptly identified and corrected and that corrective actions be taken to preclude repetition. Contrary to this, on March 20, 2003, the licensee failed to fully assess and correct the degraded conditions associated with the Unit 2, D containment cooling fan discharge damper, 2W-1D2-A, despite finding parts of the damper assembly on the containment cooling fan plenum floor and senior reactor operator, test coordinator, and system engineering discussions on the degraded condition having occurred. The degraded condition was not fully assessed until 13 days later when, on April 2, a licensee mechanic noticed a 2W-1D2-A discharge damper counterweight in a radiologically controlled machine shop in the primary auxiliary building and questioned the origin of the component.
Since the other three Unit 2 containment fan cooling units and two containment spray systems had remained operable between March 20 and April 2, 2003, the ability to provide containment atmosphere cooling to limit post-accident pressures and temperatures to less than design values continued to be met. Accordingly, this violation is being treated as an NCV (NCV 50-301/03-03-03) consistent with Section VI.A. of the NRC Enforcement Policy. This violation was entered into the licensees Corrective action system as CAP031978, Backdraft Damper Degraded, 2W-001D2-A.
.2 Temporary Modification 03-014, Installation of Sump Pumps in Manholes #1 and #2
a. Inspection Scope
During the week of June 9, 2003, the inspectors reviewed the temporary modification package associated with Temporary Modification 03-014, Installation of Sump Pumps in Manholes, to determine the potential impact on cable reliability and plant operations.
The inspectors reviewed the design document process and work that was performed.
The inspectors interviewed plant staff about this process and reviewed the separate processes to ensure that the process did not allow closure without the actions being complete.
b. Findings
No findings of significance were identified.
.3 Temporary Modification 03-15, Cable Manhole Sump Pump Installation
a. Inspection Scope
During the week of June 20, 2003, the inspectors reviewed the temporary modification package associated with Temporary Modification 03-015, Installation of Sump Pumps in Manholes 3, 10, 14, 16, and 19, to determine the potential impact on cable reliability and plant operations. The inspectors reviewed the design document process and work that was performed. The inspectors questioned the plant staff about this process and reviewed the separate processes to ensure that the process did not allow closure without the actions being complete.
b. Findings
No findings of significance were identified.
Cornerstone: Emergency Preparedness
1EP4 Emergency Action Level and Emergency Plan Changes
a. Inspection Scope
The inspector reviewed Revisions 46 and 47 to Section 5, Revisions 44, 45, and 46 to Section 6, and Revision 45 to Section 7 of the Point Beach Nuclear Plants Emergency Plan to determine whether changes identified in these revisions reduced the effectiveness of the licensees emergency planning, pending onsite inspection of the implementation of these changes.
b. Findings
No findings of significance were identified.
1EP6 Drill Evaluation
.1 Resident Inspector Observation of Emergency Preparedness Drill
a. Inspection Scope
On June 5, 2003, the inspectors observed an emergency preparedness drill to evaluate the adequacy of the licensees drill conduct and critique performance. The inspectors observed the drill from the control room (simulator), technical support center, operations support center, and emergency operations facility to evaluate emergency preparedness performance at multiple locations. The inspectors also attended control room and technical support center critique sessions immediately following the drill termination on June 5, to evaluate the licensees identification of emergency planning weaknesses and deficiencies. The inspectors reviewed Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 2, Section 2.4, Emergency Preparedness Cornerstone, to aid in determining the adequacy of the licensees critique process and whether certain NRC Drill/Exercise Performance opportunities were successful.
b. Findings
No findings of significance were identified.
RADIATION SAFETY
Cornerstone: Public Radiation Safety
2PS3 Radiological Environmental Monitoring and Radioactive Material Control Programs (71122.03)
.1 Review of Environmental Monitoring Reports and Data
a. Inspection Scope
The inspectors reviewed the 2002 Annual Environmental Monitoring Report. Sampling location commitments, monitoring and measurement frequencies, land use census, the vendor laboratorys Interlaboratory Comparison Program, and data analysis were assessed. Anomalous results including data, missed samples, and inoperable or lost equipment were evaluated. The inspectors reviewed the Radiological Environmental Monitoring Program (REMP) to verify that the licensees program was implemented as required by the Radiological Environmental Technical Specifications/Offsite Dose Calculation Manual (RETS/ODCM), and associated TSs, and that changes, if any, did not affect the licensees ability to monitor the impacts of radioactive effluent releases on the environment. The inspectors reviewed the most recent quality assessment of the licensees REMP vendor to verify that the vendor laboratory performance was consistent with licensee and NRC requirements.
b. Findings
No findings of significance were identified.
.2 Walkdowns of Radiological Environmental Monitoring Stations and Meteorological
Tower
a. Inspection Scope
The inspectors conducted a walkdown of selected environmental air, water, vegetation, and soil sampling stations and thermoluminescent dosimeters locations to verify that the locations were consistent with their descriptions in the RETS/ODCM and to evaluate the equipment material condition and operability. The inspectors also conducted a walkdown of the primary meteorological monitoring site to validate that sensors were adequately positioned and operable. The inspectors reviewed the CY 2002 Annual Environmental Monitoring Report to evaluate the onsite meteorological monitoring programs data recovery rates, routine calibration and maintenance activities, and non-scheduled maintenance activities. The inspectors verified that the meteorological instrumentation was operable, and was calibrated and maintained in accordance with licensee procedures. The inspectors also reviewed indications of wind speed, wind direction, and atmospheric stability measurements to verify that the indications were available in the Control Room and that the instrument indications were operable.
b. Findings
No findings of significance were identified.
.3 Review of REMP Sample Collection and Analysis
a. Inspection Scope
The inspectors accompanied the licensee REMP technician to observe the collection and preparation of air particulate filters, iodine sampling cartridges, and lake water samples to verify that representative samples were being collected in accordance with procedures and the RETS/ODCM. The inspectors observed the technician perform air sampler field check maintenance to verify that the air samplers were functioning in accordance with procedures. Selected air sampler calibration and maintenance records for CY 2001 and 2002 were reviewed to verify that the equipment was being maintained as required. The environmental sample collection program was compared with the RETS/ODCM to verify that samples were representative of the licensees release pathways. Additionally, the inspectors reviewed results of the vendor Interlaboratory Comparison Program to verify that the vendor was capable of performing adequate radiochemical measurements.
b. Findings
No findings of significance were identified.
.4 Unrestricted Release of Material From the Radiologically Controlled Area
a. Inspection Scope
The inspectors evaluated the licensees controls, procedures, and practices for the unrestricted release of material from radiologically controlled areas and conducted reviews to verify that:
- (1) radiation monitoring instrumentation used to perform surveys for unrestricted release of materials was appropriate;
- (2) instrument sensitivities were consistent with NRC guidance contained in Inspection and Enforcement Circular 81-07, Control of Radioactively Contaminated Material, and in NUREG/CR-5569, Health Physics Positions Data Base, for both surface contaminated and volumetrically contaminated materials;
- (3) criteria for survey and release conformed to NRC requirements;
- (4) licensee procedures were technically sound and provided clear guidance for survey methodologies; and
- (5) radiation protection (RP)staff adequately implemented station procedures.
The inspectors reviewed the circumstances of the May 14, 2003, discovery of a previously unaccounted for and installed strontium-90/yttrium-90 RMS area monitor check source found in the instrument and control (I&C) training laboratory. This laboratory was located outside the protected area, but within the owner controlled area.
Specifically, the inspectors reviewed the licensees initial CAP, investigative documents (including worker statements and a timeline of the event), and survey data. The incident was discussed with the RP manager and several other members of the RP staff.
b. Findings
Introduction.
A self-revealing Green finding and an associated NCV were identified for the failure to maintain control of licensed radioactive material that was not in storage (i.e., a previously unaccounted for and installed strontium-90/yttrium-90 RMS area monitor check source) which was discovered in an I&C training lab.
Description.
On May 14, 2003, during RMS training in the licensees training building, an I&C instructor handed out several RMS area monitor detectors for hands-on use by trainees. While inspecting the internals of a detector (serial number (S/N) 666), one of the trainees noticed that a radioactive check source (S/N CS-20) containing approximately 1 microcurie strontium-90/yttrium-90, was still installed in the detector and reported this to the instructor. The instructor immediately removed the source from the classroom and put it under control in the I&C lab. The RP group was notified and the source was controlled per the licensees source control procedure.
The I&C training lab is located in the licensees training building which is located outside of the protected area, but is within the owner controlled area of the station.
Instrument and control staff surmised that the RMS detector and source were part of original plant equipment installed in the 1970s that was replaced in the early 1980s, and were probably stored in the old I&C training lab in the North Service Building until 1999. The RMS detector found with the check source had been moved out to the training building in 1999 along with four other RMS detectors. These detectors had been moved out of the protected area along with a large amount of other I&C training lab equipment through the vehicle access gate. The I&C personnel were not aware at that time that one of the detectors still had a check source installed.
This event was self-revealing when, on May 14, 2003, an RP technician retrieved the source from the training building and placed it into the cleanside source storage room in the protected area. The check source, which is a sealed source and is labeled Caution, Radioactive Material with a yellow and magenta sticker is a one-half inch disc electroplated with strontium-90/yttrium-90. Four more RMS detectors that were also being used for training were searched and no additional check sources were found. Radiation protection management was notified of this event. The licensee performed searches of the I&C training classroom, laboratory, and other training areas to determine if any additional equipment that may have had radioactive materials was present. None were found. The licensee performed contamination surveys on the strontium-90/yttrium-90 source, RMS detector S/N 666, and the other four RMS detectors, to verify there was no detectable loose surface contamination present. None was detected. The licensee also performed extensive radiation and contamination surveys of the training building classrooms and associated storage areas to verify there was no additional detectable radioactive material in any of the above mentioned locations.
The licensee determined that it did not possess any historical records (i.e., maintenance logs, manufacturerss purchase/sales information, or source receipts) or other documentation associated with RMS detector S/N 666. The licensees apparent cause evaluation cited a lack of an effective source control program prior to 1998. Contributing factors cited were inadequate searches of the I&C training lab storage area and the I&C storeroom in the North Service Building during 1997 and 1998. Also cited as a contributing factor was a lack of an effective detector/source control matching methodology (i.e., the numbers of detectors were not matched with numbers of existing sources) which did not exist at the time of these searches.
Analysis.
The inspectors determined that the issue was associated with the Program and Process attribute of the Public Radiation Safety Cornerstone and affected the cornerstone objective in ensuring adequate protection of public health and safety from exposure to radioactive materials released into the public domain. Also, the issue involved an occurrence in the licensees radioactive material control program that is contrary to both NRC regulations and licensee procedures. Therefore, the issue was more than minor and represents a finding which was evaluated using the SDP for the Public Radiation Safety Cornerstone.
The inspectors determined that the licensee failed to prevent the inadvertent release and/or loss of control of licensed radioactive material to an unrestricted area that could cause an actual or credible radiation dose to member of the public. As such, the inspectors determined, utilizing Manual Chapter 0609, Appendix D, Public Radiation Safety SDP, that the finding involved radioactive material control, but transportation was not involved. The public radiation exposure was not greater than 0.005 rem (5 millirem) and the licensee did not have more than five radioactive material control occurrences (in the previous eight quarters). Consequently, the inspectors concluded that the SDP assessment for this finding was of very low safety significance (Green).
Enforcement.
Section 10 CFR 20.1802 requires that the licensee control and maintain constant surveillance of licensed material that is in a controlled or unrestricted area and that is not in storage. On May 14, 2003, the licensee failed to maintain control of licensed radioactive material (i.e., an uninventoried, internal strontium-90/yttrium-90 RMS area monitor check source) which was discovered in an I&C training lab. This failure constitutes a violation of 10 CFR 20.1802. However, because the licensee documented this issue in its corrective action program (CAP No. 032907) and because the violation is of very low safety significance, it is being treated as an NCV (NCV 50-266/301/03-03-02).
.5 Identification and Resolution of Problems
a. Inspection Scope
The inspectors reviewed CAPs, the results of the licensees REMP self-assessment performed during the second quarter of 2002, and Nuclear Oversight (quality assurance) observation reports addressing the REMP to determine if problems were being identified and entered into the CAP for timely resolution. The inspectors also reviewed the licensees pre-inspection readiness evaluation of the REMP, which evaluated the current state of the program and the completion status of the previous self-assessment items. The inspectors also reviewed the licensees overall management of the REMP, including attention to details of the sampling program and the vendor laboratory, in order to evaluate the effectiveness of the REMP in collection and analysis of samples for the detection of offsite radiological contamination.
b. Findings
No findings of significance were identified.
SAFEGUARDS
Cornerstone: Physical Protection
3PP2 Access Control (Identification, Authorization and Search of Personnel, Packages, and Vehicles) (71130.04)
a. Inspection Scope
The inspectors reviewed the licensees protected area access control testing and maintenance procedures. The inspectors observed licensee testing of all protected area access control equipment to determine if testing and maintenance practices were performance based. On two occasions, the inspectors observed in-processing search of personnel, packages, and vehicles to determine whether search practices were conducted in accordance with regulatory requirements.
The inspectors reviewed security-related event reports and safeguard log entries associated with the access control program from April 2002 through June 15, 2003.
The inspectors also reviewed the licensees CAP to determine if security-related issues associated with the access control program were appropriately identified and resolved.
b. Findings
No findings of significance were identified.
3PP3 Response to Contingency Event (71130.03)
a. Inspection Scope
The inspectors walked down the licensees protected area intrusion alarm system to identify potential vulnerabilities. The inspectors, accompanied by licensee security representatives, observed testing of inspector and licensee selected protected area intrusion alarm zones. Alarm zone detection was evaluated by conducting various testing methods.
The inspectors also reviewed the effectiveness of alarm station personnel to recognize and identify activities in the protected area alarm detection zones on the assessment monitors. The inspectors also reviewed the field of view provided by the assessment aids to ensure compliance with the licensees security plan.
The inspectors also reviewed a sample of licensee force-on-force drill records, and interviewed security management personnel to determine if the licensee had appropriately identified and resolved issues associated with the contingency response program.
b. Findings
No findings of significance were identified.
3PP4 Security Plan Changes (71130.04)
a. Inspection Scope
The inspectors reviewed revisions dated May 19, 2003, to the Point Beach Plant Security and Safeguard Contingency Plan to verify that changes did not decrease the effectiveness of the submitted document. The referenced revision was submitted in accordance with 10 CFR 50.54(p) by a licensee letter dated May 19, 2003.
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES
4OA1 Performance Indicator (PI) Verification
a. Inspection Scope
During the week of June 9, 2003, the inspectors reviewed portions of the Units 1 and 2, 2002 and 2003 data obtained for the High Pressure Safety Injection System Unavailability PIs using the definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 2.
The inspectors reviewed station log entries, selected procedures, and system engineer data sheets to verify that planned and unplanned unavailability hours were characterized correctly in determining PI results. The inspectors also performed independent calculations to verify PI data.
b. Findings
No findings of significance were identified.
.2 Unplanned Scrams per 7,000 Critical Hours
a. Inspection Scope
During the week of June 9, 2003, the inspectors reviewed licensee records to verify the Unplanned Scrams per 7,000 Critical Hours PIs for Units 1 and 2 for 2002 and 2003.
The inspectors used the definitions and guidance contained in NEI 99-02, Revision 2, for this review.
The inspectors reviewed station log entries, Licensee Event Reports (LERs), and PI coordinator data sheets to verify that all unplanned scrams had been characterized correctly in determining PI results.
b. Findings
No findings of significance were identified.
.3 Scrams With Loss of Normal Heat Removal
a. Inspection Scope
During the week of June 9, 2003, the inspectors reviewed portions of the Units 1 and 2, 2002 and 2003 data for the Scrams With Loss of Normal Heat Removal PIs using the definitions and guidance contained in NEI 99-02, Revision 2.
The inspectors reviewed station log entries, LERs, and PI coordinator data sheets to verify that all scrams with loss of normal heat removal had been characterized correctly in determining PI results.
b. Findings
No findings of significance were identified.
.4 RETS/ODCM Radiological Effluent Occurrence
a. Inspection Scope
The inspector reviewed selected CAPs for 2002 and 2003 and offsite dose calculations (3rd quarter 2002 through 1st quarter 2003) to identify any occurrences that were not identified by the licensee and to verify that the licensee had accurately reported the PI for the public radiation safety cornerstone. The inspector discussed the RETS/ODCM PI data collection and analysis process with the data steward for this indicator, to verify that the program was implemented consistent with industry guidelines provided in NEI 99-02, Revision 2, and licensee procedures.
b. Findings
No findings of significance were identified.
.5 Safeguards Strategic Area
a. Inspection Scope
The inspectors sampled licensee submittals for the PI listed below for the period from April 2002 through May 2003. To verify the accuracy of the PI data requested during that period, PI definition and guidance contained in Revision 2 of NEI 99-02 were used.
The following PIs were reviewed:
- Fitness-for-Duty Personnel Reliability;
- Personnel Screening Program; and
- Protected Area Security Equipment.
A sample of plant reports related to security events, security shift activity logs, and fitness-for-duty reports were also reviewed.
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems
.1 Control Room Operator Performance During Plant Evolutions
a. Inspection Scope
During April 5 through April 26, 2003, the inspectors observed operator actions during routine and non-routine evolutions to assess the performance of the operations crews.
The inspectors observed the crews during a Unit 2 loss of condenser vacuum event and subsequent startup activities.
b. Findings and Observations
During a Unit 2 plant shutdown due to loss of condenser vacuum, the operators failed to recognize that the TS surveillance related to the P-6 and P-10 interlocks needed to be performed within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> of shutdown. The surveillance was subsequently performed within TS-required time limits.
During the Unit 2 approach to criticality at 3:20 a.m. on April 6, the indicated value for 2F-466 (Loop A Feedwater Flow to Control Flow Indicator) changed from 0 to approximately 0.7 X 106 pounds per hour and an alarm was received. The operators were slow to recognize that the indication had failed. Specifically, the alarm was acknowledged at 3:20 a.m., but the indication failure was not acted upon until 21/2 hours later.
While neither event resulted in a finding or violation, they were indicative of a lack of attention to detail and slow evaluations of an abnormal condition.
.2 Apparent Cause Evaluations (ACEs) Associated With Risk Modeling Errors
a. Inspection Scope
During the weeks of June 2 and 9, 2003, the inspectors reviewed four ACEs (1043, 1204, 1208, and 1238) associated with risk modeling errors occurring between November 2002 and May 2003. The ACEs were reviewed to ensure that the full extent of the issue had been identified, an adequate evaluation performed, and appropriate and effective corrective actions had been specified and prioritized. The inspectors evaluated the ACEs against the requirements of the licensees corrective action program as delineated in NP 5.3.1, Action Request Process, to determine whether the ACE had been the appropriate mechanism to have evaluated the contributing and root causes associated with the risk modeling errors.
b. Findings and Observations
There were no findings identified with the four ACEs reviewed; however, the inspectors determined that the first three evaluations had not identified an important contributing cause associated with the risk modeling errors. Namely, that probabilistic risk engineering, production planning, or on-shift operations personnel had not reviewed and examined pre-planned work activities to a sufficient level to recognize the unavailability of all components and equipment modeled in the licensees risk assessment tool, Safety Monitor. The fourth ACE (ACE 1238, initiated on March 19 and completed on May 2) recognized this need and created an appropriate action item that was linked to the sites Excellence Plan.
Finally, the inspectors reviewed the number of CAPs relating to Safety Monitor that had been initiated since the beginning of 2001. Data for the first 6 months of 2003 revealed a 314 percent increase over the number of Safety Monitor CAPs written for all of 2002 and a 162 percent increase for all of 2001. The inspectors considered that the 4 ACEs and the historic CAP data highlighted the need for the licensee to use the Safety Monitor risk assessment tool in a manner consistent with its full capabilities.
4OA3 Event Follow-up
.1 Unit 2 Rapid Power Reduction Due To Loss Of Condenser Vacuum
a. Inspection Scope
The inspectors observed the response to and reviewed the circumstances associated with a loss of condenser vacuum event on Unit 2 that occurred on April 5, 2003, to evaluate degraded plant conditions and licensee actions taken to mitigate the transient.
The inspectors reviewed plant response which included low feedwater suction pressure alarms; a condensate pump auto-start and subsequent trip due to overcurrent conditions; heater drain tank pump trips on low tank levels; steam jet air ejector steam supply isolations and low flow conditions through the steam jet air ejector condensers; and equipment failures associated with the A condensate pump discharge check valve and the condensate pump minimum recirculation flow control valve to determine if equipment had responded as expected. The inspectors also reviewed the operating crews decision to trip the main generator, shut the main steam isolation valves, and transition RCS temperature control to the steam generator atmospheric steam dumps to evaluate the timeliness of the crews actions as vacuum conditions continued to deteriorate. The inspectors reviewed a mode transition checklist and the initial root cause evaluation report for the loss of condenser vacuum to determine if equipment malfunctions had been sufficiently understood and corrected to support plant restart activities on April 8-9, 2003. Finally, the inspectors performed walkdowns of portions of the condensate and feedwater systems during power ascension activities to verify that equipment malfunctions had been properly diagnosed and corrected.
b. Findings
No findings of significance were identified.
.2 Loss of Emergency Plan Sirens
a. Inspection Scope
The inspectors observed the response to, and reviewed the circumstances associated with a loss of emergency plan sirens. At 11:30 a.m. on April 3, 2003 the control room notified the inspectors that 56 percent of the emergency plan sirens were lost due to power outages. Plant staff made a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> notification based on calls to state and county officials, and an 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> notification based on loss of greater than 50 percent of the sirens. The power outages were caused by severe ice storms in the area. Sirens became available as power was restored to the affected areas.
b. Findings
No findings of significance were identified.
.3 (Closed) LER 50-301/03-001-00:
Containment Accident Backdraft Damper Failure Results in Condition Prohibited by TS 3.6.6.C.
On April 2, 2003, a licensee mechanic identified a backdraft damper counterweight on a table top in a radiologically controlled machine shop. This led to the determination that the backdraft damper associated with Unit 2 W-1D2 containment cooling fan was substantially degraded. The function of the damper was to close when the 2W-1D2 fan was not operating so as to prevent the diversion of air flow through the normal cooling fan when the 2W-1D1 Containment Accident Fan was operating. Based on additional inspections conducted on April 2, the 2W-1D1 Containment Accident Recirculation Fan and the 2W-1D2 Containment Cooling Fan were declared out of service. Limiting Condition for Operation 3.6.6 was declared not met and TS Action Condition 3.6.6.C was entered for one accident fan cooler unit not operable. A temporary modification was completed to secure the damper in the closed position and the containment fan cooler was returned to service.
Further investigation determined that the degraded condition of the backdraft damper should have been identified during performance of a heat exchanger performance test on March 20, 2003. The failure to identify the condition of the damper was due to incomplete communication regarding the detached parts and the failure to recognize other indications of damper degradation. More detail and the regulatory disposition of this LER is provided in Section 1R23.1 of this report. No new findings of significance were identified by the inspectors in reviewing this LER. The licensee documented the failure to identify the degraded condition of the backdraft damper in CAP031978. This LER is closed.
.4 (Closed) LER 50-301/03-002-00:
Reactor Shutdown Required Due to Technical Specification TSAC 3.1.6.B.2 Not Met.
On April 5, 2003, operators commenced a planned power reduction of Unit 2 to approximately 52 percent to enable the removal of a single feed water train for the purpose of performing main feedwater pump lube oil cleaning. During the power reduction, problems were encountered with the condensate and feedwater systems requiring a rapid power reduction in an attempt to recover main feed pump suction pressure. After receiving a low condenser vacuum alarm, the shift manager ordered a manual trip of the Unit 2 turbine. The main steam isolation valves were subsequently shut and RCS temperature control was transferred to the steam generator atmospheric steam dumps.
Three hours and 32 minutes after opening the Unit 2 generator output breaker, operators noted that the difference between the Unit 2 control rod bank C and control rod bank D was 126 steps. Technical Specification LCO 3.1.6, Control Bank Insertion Limits, required the control banks to be within the insertion, sequence difference, and overlap limits specified in the Core Operating Limits Report. Figure 3 of the Unit 2 Core Operating Limits Report specified the sequence limit as 125 steps. At the time of discovery, control bank C was at 194 steps and bank D at 68 steps, a difference of 126 steps. Since the licensee was unable to meet the TS Action Condition 3.1.6.B.2 to restore control bank sequence and overlap to within the limits within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />, TS Action Condition 3.1.6.C was entered requiring the reactor to be in Mode 2 with the reactor subcritical within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. At 5:30 a.m. on April 6, Unit 2 entered Mode 3 and LCO 3.1.6.C.1 was considered met.
This LER was reviewed by the inspectors and no findings of significance were identified. The licensee documented the forced shutdown in CAP032039. This LER is closed.
.5 (Closed) LER 50-301/03-003-00:
Failure to Place Instrument Channel in Trip as Specified by LCO 3.3.1 Required Action D.1.
On April 8, 2003, Unit 2 was in Mode 2 with a reactor startup in progress when a steam generator feedwater flow alarm was received from flow indicator 2FI-466. The feedwater flow instrument had drifted out of calibration due to sensing line flashing causing the alarm. The feedwater flow instrument was required by TS Table 3.3.1-1, Item 14, Steam Generator Water Level Coincident with Steam Flow/Feed Flow Mismatch, to be operable in Modes 1 and 2. The sensing line flashing rendered the feedwater flow instrument incapable of properly indicating flow resulting in LCO 3.3.1 not being met for 2FI-466. The required action for this condition, LCO 3.3.1 Condition D, required placing the channel in trip within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> or placing the reactor in Mode 3 within 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />.
Operators did not discern the significance of this condition until about 21/2 hours after the receipt of the initial alarm. This was due to the operators attention being focused on the activities associated with reactor criticality that were ongoing at the time. The operators reasoned that, since the feedwater system was secured, the feedwater flow alarm did not warrant their immediate attention while reactor startup was in progress.
The operators failed to recognize that the reactor was in a Mode of operation in which this parameter was required by TSs. Although the channel was not placed in trip within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> of receipt of the initial alarm, it was restored to operable status within the 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> allowed by TSs to exit the Mode of applicability. Thus, the requirements of TS 3.3.1 were met and no violation of regulatory requirements occurred. Since the initial operator response to this condition was not appropriate, the licensee decided to voluntarily submit this LER as a condition of generic interest despite the subject condition not meeting the criteria for required reporting.
This LER was reviewed by the inspectors and no findings of significance were identified. The licensee documented the failure of operators to recognize a TS requirement in a timely manner in CAP032070. This LER is closed.
.6 (Closed) LER 50-266, 301/03-001-00:
As-Found Condition of Degraded Grid Voltage Relays Not Within TS Limits.
On April 4, 2003, the licensee identified that both Point Beach Units had been operated for an extended period with setpoints for the degraded voltage relays less that the TS setting. The set points were incorrectly set because the surveillance procedures for the relays, 1(2)RMP 9056-1 and 1(2)RMP 9056-2, had been revised to specify a test instrument with an accuracy tolerance greater than the accuracy tolerance of the test instrument assumed in the setpoint calculation, N-93-098. The cause of this event was that the licensee did not adequately consider and evaluate the differences in accuracy tolerance of the measuring instruments during the procedure revision process. The licensee subsequently performed the surveillance for these relays on April 6, 2003, for Unit 2 and April 7, 2003, for Unit 1. The as-found relay drop-out voltages for all of the 12 degraded grid voltage relays were found to be less than the TS required setting. In addition, 2 of the 12 relays were found to have setpoints that were less than the analytical minimums established by calculation N-93-002. The two relays were both on the 1A-05 bus and potentially impacted an EDG exhaust fan and a standby swing battery charger. The license reasoned that the safety impact of the two relays was minimal since the swing battery charger was not normally in service and the diesel exhaust fan would have been able to start and run since the as-found relay trip point was only slightly lower than industry standard specifications. Finally, a probabilistic risk assessment of the delay in performing the degraded voltage relay surveillance determined that the surveillance delay was not risk significant. Further detail regarding this missed SR is provided in Section 1R22.1. This licensee-identified finding involved a violation of TS SR 3.3.4.3.b. The enforcement aspects of the violation are discussed in Section 4OA7. This LER is closed.
4OA4 Cross-Cutting Findings
.1 A finding described in Section 1R13.1 of this report had, as its primary cause, a human
performance deficiency. The deficiency concerned the failure of probabilistic risk assessment, production planning, and on-shift personnel to use the full capabilities of the risk assessment tool to recognize the unavailability and risk impact of components associated with pre-planned work activities.
.2 A finding described in Section 1R23.1 of this report had, as its primary cause, a human
performance deficiency. The deficiency concerned incomplete communications and coordination during thermal performance testing activities on March 20, 2003. This resulted in plant staff not taking appropriate and timely corrective actions to fully assess and correct degraded conditions associated with the safety-related Unit 2 containment cooling fan backdraft damper, 2W-1D2-A. The condition adverse to quality was identified 13 days later when, on April 2, 2003, a mechanic identified a 2W-1D2-A damper counterweight amongst other controlled material in a radiologically controlled machine shop.
4OA5 Other
.1 (Closed) URI 50-266/01-08-01; URI 50-301/01-08-01:
Ultrasonic Testing (UT)
Equipment Essential Variable Tolerances. The inspectors had opened this URI to review the licensees implementation of the Performance Demonstration Initiative UT examination techniques. Specifically, the inspectors had questioned the licensees decision to exempt UT equipment of the same make and model as that used during the procedure qualification from essential variable tolerance testing. The inspectors were concerned that a manufacturer may produce UT equipment of the same model that varied beyond the essential variable ranges required by Article VIII-4110, of Appendix VIII of the American Society of Mechanical Engineers Code and which would go undetected due to the lack of confirmatory testing. On March 18, 2003, the Performance Demonstration Steering Committee Chairman sent a letter to the NRC, which generically endorsed the practice of reliance on the original equipment manufacturers quality control standards. Since the licensees practice was consistent with that endorsed by the Performance Demonstration Initiative Steering Committee, it remains under review by the Office of Nuclear Reactor Regulation, and it will be addressed by other NRC processes, the inspectors considered this URI closed.
.2 (Closed) Apparent Violation (AV) 50-266/01-17-01; 50-301/01-17-01:
Potential Common Mode Failure of AFW Pumps Due to Inadequate Procedural Guidance. This violation was issued to the licensee in a Notice of Violation attached to a letter dated July 12, 2002. In response letters dated August 12 and September 26, 2002, the licensee described its corrective actions, which included procedure revisions, problem-specific training of operators, the installation of pneumatic backup for the AFW system recirculation line flow control valves, and reclassification of the open function of the flow control valves as safety-related. These actions and others were reviewed by the resident inspectors and as part of a special NRC inspection (Inspection Report 50-266/02-15; 50-301/02-15) and found acceptable to correct the problem.
.3 (Closed) AV 50-266/01-17-02; 50-301/01-17-02:
Failure to Identify and Correct Problem Associated With Potential Common Mode Failure of AFW Pumps. This corrective action problem was combined with the procedural inadequacy problem discussed above and issued to the licensee in a Notice of Violation attached to a letter dated July 12, 2002. As discussed above, corrective actions have been taken by the licensee and reviewed, in part, by the NRC.
4OA6 Meetings
.1 Exit Meeting
On July 1, 2003, the resident inspectors presented the inspection results to Mr. A. Cayia and other members of his staff, who acknowledged the findings. The licensee did not identify any information provided to, or reviewed by the inspectors as proprietary in nature.
.2 Interim Exit Meetings
Interim exits were conducted for:
- Safeguards Inspection with Mr. B. Kopetsky on April 16, 2003.
- Maintenance Rule Implementation - Periodic Evaluation with Mr. A. Cayia on May 1, 2003.
- Radiation Protection inspection with Mr. A. Cayia on May 17, 2003. A follow-up telephone discussion was held with the RP manager on June 19 regarding the source found in a radiation detector used for training.
- Safeguards Inspection with Mr. D. Fadel on June 18, 2003.
- Emergency preparedness with Ms. R. Millner on June 20, 2003.
4OA7 Licensee-Identified Violations
The following violations of very low safety significance (Green) were identified by the licensee and are violations of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as NCVs.
Cornerstone: Mitigating Systems
- Technical Specification Surveillance Requirement (SR) 3.3.4.3.b requires that the 4160-volt bus degraded voltage relays be calibrated at least once per 18 months. Contrary to the above, the licensee missed this SR in June 2002 for the Unit 2, 4160-volt safeguards buses 2A05 and 2A06 and in August 2002 for the Unit 1, 4160-volt safeguards buses 1A05 and 1A06. Specifically, a test instrument with inadequate calibration tolerances was used such that the ability of the degraded voltage relays to have met TS requirements was not demonstrated at the required frequency. The licensee entered this issue into its corrective action program as CAP032002, Potential to Exceed Tech Spec Limit of 3937 V at A05 and A06.
- 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part, that measures be established to assure that applicable regulatory requirements and design basis are correctly translated into specifications, drawings, procedures, and instructions. Contrary to the above, as of June 9, 2003, the design requirement to manually restore safety-related battery chargers within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> was not correctly translated into specifications, procedures or instructions for the DC system. Specifically, multiple feeder breakers to the battery chargers could trip under initiating event scenarios because the current limiter was set too high.
The licensee entered the condition into its corrective action program as CAP033447, Issues Associated with Battery Charger Current Limit Setpoint.
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
- A. Cayia, Site Vice-President
- J. Jensen, Plant Manager
- J. Anderson, Business Support Manager
- G. Arent, Licensing Manager
- D. Argall, Kewaunee/Point Beach Security Specialist
- J. Boesch, Maintenance Manager
- D. Fadel, Director of Engineering
- M. Fencl, Kewaunee/Point Beach Security Manager
- F. Flentje, Senior Regulatory Compliance Specialist
- J. Gerondale, NMC Security Consultant
- M. Holzmann, Nuclear Oversight Supervisor
- N. Hoefert, Engineering Programs Manager
- R. Hopkins, Internal Assessment Supervisor
- C. Jilek, Point Beach Maintenance Rule Coordinator
- T. Kendall, Program Engineering
- B. Kopetsky, Security Coordinator, Point Beach
- C. Krause, Regulatory Compliance
- K. Locke, Regulatory Compliance
- R. Millner, Emergency Preparedness Manager
- T. Petrowsky, Design Engineer Manager
- D. Schoon, Operations Manager
- J. Schweitzer, Production Planning Manager
- M. Shug, Assistant Operations Manager
- C. Sizemore, Training Supervisor
- P. Smith, Operations Training Supervisor
- J. Strharsky, Planning and Scheduling Manager
- T. Taylor, Site Assessment Manager
- S. Thomas, Radiation Protection Manager
- R. Turner, Inservice Inspection Coordinator
Nuclear Regulatory Commission
- D. Spaulding, Point Beach Project Manager, NRR
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
50-266/301/03-03-01 NCV Failure to Implement Risk Management Actions for Components Made Unavailable by Pre-Planned Work Activities (Section 1R13)
50-266/301/03-03-02 NCV Failure to Maintain Control of Licensed Radioactive Material in an Unrestricted Area and That was not in Storage (Section 2PS3)
50-301/03-03-03 NCV Need for a Unit 2 Containment Cooling Fan Discharge Damper Temporary Modification Not Identified In a Timely Manner (Section 1R23.1)
Closed
50-266/301/03-03-01 NCV Failure to Implement Risk Management Actions for Components Made Unavailable by Pre-Planned Work Activities (Section 1R13)
50-266/301/03-03-02 NCV Failure to Maintain Control of Licensed Radioactive Material in an Unrestricted Area and That was not in Storage (Section 2PS3)
50-301/03-03-03 NCV Need for a Unit 2 Containment Cooling Fan Discharge Damper Temporary Modification Not Identified In a Timely Manner (Section 1R23.1)
50-266/01-08-01; 50-301/01-08-01 URI Ultrasonic Equipment Essential Variable Tolerances (Section 4OA5.1)
50-301/03-001-00 LER Containment Accident Backdraft Damper Failure Results in Condition Prohibited by TS 3.6.6.C (Section 4OA3.3)
50-301/03-002-00 LER Rector Shutdown Required due to Technical Specification TSAC 3.1.6.B.2 not Met (Section 4OA3.4)
50-301/03-003-00 LER Failure to Place Instrument Channel in Trip as Specified by LCO 3.3.1 Required Action D.1 (Section 4OA3.5)
50-266/301/03-001-00 LER As-Found Condition of Degraded Grid Voltage Relays not Within TS Limits (Section 4OA3.6)
50-266/01-17-01; 50-
301/01-17-01 AV Potential Common Mode Failure of AFW Pumps Due to Inadequate Procedural Guidance (Section 4OA5.2)
50-266/01-17-02; 50-301/01-17-02 AV Failure to Identify and Correct Problem Associated With Potential Common Mode Failure of AFW Pumps (Section 4OA5.3)