IR 05000298/1993004

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SALP Cycle 012 Rept 50-298/93-04 for Period 930425-941022, Semiannual Plant Performance Review
ML20217G011
Person / Time
Site: Cooper Entergy icon.png
Issue date: 10/19/1993
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20217F876 List:
References
FOIA-97-148 50-298-93-04, 50-298-93-4, NUDOCS 9708070068
Download: ML20217G011 (6)


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-COOPER NUCLEAR-STATION EXECUTIVE SUMMARY SEMIANNUAL PLANT PERFORMANCE REVIEW 93 04 OCTOBER-19, 1993 SALP CYCLE 012

(APRIL 25, 1993 THRU October 22, 1994) OVERVIEW The licensee's overall performance has continued to be poor. Significant weaknesses were noted for. the identification and resolution of problems. -The quality assurance organization has been ineffective in identifying programmatic implementation weaknesse Plant management had not demonstrated the ability to promptly and effectively-react to multiple plant and personnel challenge Organizationa1 changes are in progress to return senior management. quality assurance and licensing to the sit .

I PERFORMANCE INDICATORS Quarter: 93-01 Analysis: -_The performance indicators are consistent with the assessments derived through the inspection program. Several safety system failures occurred because-of design inadequacies which have identified through its design reviews, personnel errors and degraded plant conditions. +The operatioral phase has continued to show good performance while the shutdown performance indicated increased challenges-to the plant and personne II SUMMARY-0F SIGNIFICANT REGULATORY ISSUES ~

'An escalated enforcement action with a proposed Civil Penalty of $200.000 was issued on October 13. 1993, which-addressed plant managements' apparent-continuing inability to aggressively pursue effectively identify, and resolve safety-related-equipment deficiencie .Two 01-investigations are open concerning a procedure change that permitted movement of. heavy loads,around the reactor-vessel without maintaining-secondary containment integrity, and that terminal lugs had been inadequately installed and.a CNS inspector failed to identify the discrepanc ; Tea 78na'7oaos MATTHEW 97-148 PDR ih] _() ! p O O (j f j

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I PLANT OPERATIONS PREVIOUS RATINGS SALP 92: 2 93: 2 OPPR 93-03: (NC) SPPR 93-04: (NC)

STRENGTHS: Good operator awareness of equipment available to mitigate events while the plant was shutdown for the refueling outag WEAKNESSES: Operators continued to demonstrate a poor questioning attitud Adverse plant conditions caused by building water in leakage were not promptly addressed. Inaccurate operator aides were not corrected and the actions recuired for a HPCI main control board annunciator were not reviewed and uncerstood. Management response to identified plant and personnel performance issues was slow with the problems continuing before action was take PERFORMANCE ASSESSMENT WITH RECOMMENDATIONS: The licensee's performance in

- this area remained mixed and indicated a high threshold for identifying problems. The day to day evolutions were handled well as was the initial challenges provided by the area flooding. However, the continuing lack of a questioning attitude by the operators and the failure of licensee management to promptly address plant and personnel issues resulted in unnecessary challenges to plant operatio An additional 100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> should be added to the 71707-RI to permit 30 RI hours for period remaining. A decrease in 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> charged to the 71707 core for each remaining period will be required. The Operational Safety Team Inspection will also address the above weakness and performance concerns, MAINTENANCE PREVIOUS RATINGS SALP 92: 1 93: 3-QPPR 92-03: (NC) SPPR 93-04: (NC)

STRENGTHS: None identified

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WEAKNESSES: Management expectations were not well established and maintenance personnel did not demonstrate an overall awareness of the existing management expectations. Inspection of relay racks did not identify the types of concerns expected from management. Maintenance activities performed during the refueling outage appear to have contributed to equipment problems occurring early in the operating cycl PERFORMANCE ASSESSMENT WITH RECOMMENDATIONS: The performance in this area remained consistent with the previous performance assessment. A lack of a questioning attitude continued throughout the maintenance area. Management-2-

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expectations were not well established and understood by maintenance personne The infrastructure to support maintenance activities does not appear to be well developed or maintaine Additional regional initiative 62703 maintenance observation hours (270)

should be added to the MI This will allow for the extensive maintenance observations which occurred under the core module early in the SALP cycle with the plant in a refueling outage and an additional 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> observation for the remaining periods (approximately 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> each period). An additional 81 hours9.375e-4 days <br />0.0225 hours <br />1.339286e-4 weeks <br />3.08205e-5 months <br /> regional initiative should be added to 61726 surveillance observation to supplement a decrease in the core hours from 15 to 11 each period and will allow for an additional 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> of surveillance observations each remaining period. The Operational Safety Team Inspection will also address the above weakness and performance concerns and assess if additional regional initiative hours are neede V ENGINEERING PREVIOUS RATINGS:

SALP 92: 2 93: 2D OPPR 93-03: (-) SPPR 93-04: (-)

STRENGTHS: Good support from the corporate engineering offic WEAKNESSES: Weaknesses were noted with problem resolution. The corrective action overview group was not effective in assessing service water degradatio The GL89-10 was not well implemented and the quality assurance oversight provided was not effective. The licensee's initial response to the MOV and relay rack problems did not demonstrate an awareness for the potential safety significance. Management's expectations for the initial evaluation and resolution of the relay rack issue were not inadequately defined within the engineering department. The status of the BWR level indication modifications were not communicated outside the engineering organization. The task team's coordination of work activities to validate MOV pinion gear assumptions was not well coordinate PERFORMANCE ASSESSMENT WITH RECOMMENDATIONS: Performance in this area has continued to decline. Oversight activities were not effective in identifying GL 89-10 program implementation weaknesse Plant management response to the MOV and relay rack issues were not well defined until after significant NRC involvement occurre The intra and inter communications have remained poo No change to the MIP is recommended. The Operational Safety Team Inspection will address the above weakness and performance concern _ _ .

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VI PLANT SUPPORT

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PREVIOUS RATINGS SALP 93: SPPR 93-04: (NA)

STRENGTHS: Strong radiological controls program for ALARA and exposure contro The security organization effectively implemented the emergency site access for a NOU Proper compensatory posting was implemented for degraded security boundar The emergency plan was well implemented for the NOU WEAKNESSES: Plant housekeeping activities during the refueling outage and-flooding event were poo PERFORMANCE ASSESSMENT WITH RECOMMENDATIONS: Performance in this area was very good with the exception of housekeeping activitie A lack of management involvement and the general acceptance of the housekeeping conditions contributed to this issu An additional 100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> should be added to onsite LER followup 92700-01 RI to accommodate open LER followup. All previously established hours have been expended. One hundred and fifty hours should be added to open item followup 92701-01 RI for remaining items. The Operational Safety Team Inspection will address the above weakness and performance concern VIII. TIA STATUS 92TIA001 Adequacy of Cooper emergency plan procedure Complete prior to 11/30/93 (TAC # M86982)

93TIA002 Movement of heavy loads around the reactor vessel without secondary containmen TS determination due 11/1/93. The generic review of the TS applicaMlity is due 12/93 93TIA003 Thermolag radiant energy shield, -Complete by 12/31/93

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I MAJOR SITE ACTIVITIES COMPLETED Corrective action inspection (298/93-17)

PLANNED Operational Safety Team Inspection Operational Security Readiness Evaluation Service Water System Operational Performance Inspection

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COOPER NUCLEAR STATION SEMIANNUAL PLANT PERFORMANCE REVIEW 93 04 0CTOBER 19, 1993 SUMMARY OF HIP CHANGES MODULE TITLE AREA ADD /- FM TO DELTA CHANGE 93802-HT OSTI ALL Add 0 600 +600 62703-RI Maintenance Maint Add 0 270 +270 71707-RI Ops Safety Ver Ops Add 312 412 +100 61726-R1 Surveillance Maint Add 0 81 +81 92700-RI LER Followup PS Add 60 160 +100 92701-RI Followup PS Add 60 210 +150 73755-RI ISI Data Review Eng Add 0 34 +34 NET CHANGE +1335 JUSTIFICATIONS 93802 Operational Safety Team Inspection to assess licensee performance based on concerns raised following the corrective action special inspectio Maintenance inspection to accommodate extensive core inspections which occurred early in the SALP cycle with the plant in a refueling outag Surveillance observations to supplement the core effort through the end of the SALP cycle and provide for additional RI surveillance effort each period to address SALP Report identified weaknesse Additional hours to supplement the core program through the end of the SALP cycle and also provide additional inspection effort to address the numerous weaknesses identified in addition the SALP report assessmen Additional hours required to permit continued followup of open LER .- _ _ . - _ _ _ . . . _ . - _ . . _ _ . _ _ _ _ _ _ . . _ _ . _ . _ . _ _ _ . _ . . _ . . .

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-92701 LAdditional hours required to permit continued followup of open

, inspection finding i 73755 Add ISI data review module because of next ISI observation j activity not expected until next SALP cycl ! ,

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