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Category:INSPECTION REPORT
MONTHYEARIR 05000298/19990121999-10-22022 October 1999 Insp Rept 50-298/99-12 on 990927-30.No Violations Noted. Major Areas Inspected:Licensee Emergency Preparedness Program & Included Review of Emergency Preparedness Performance Indicators IR 05000298/19990101999-10-14014 October 1999 Insp Rept 50-298/99-10 on 990920-24.No Violations Noted. Major Areas Inspected:Radiological Environ & Meteorological Monitoring Programs & Program for Unrestricted Release of Matl from Radiological Controlled Area IR 05000298/19990031999-10-0808 October 1999 Insp Rept 50-298/99-03 on 990823-27 & 990907-10.No Violations Noted.Major Areas Inspected:Methods Used for Identification,Cause Investigation & Correction of Quality Related Problems IR 05000298/19990071999-09-27027 September 1999 Insp Rept 50-298/99-07 on 990718-0828.No Violations Noted. Major Areas Inspected:Implementation of Reactor Safety & Emergency Preparedness Programs IR 05000298/19990091999-09-22022 September 1999 Insp Rept 50-298/99-09 on 990823-26.No Violations Noted. Major Areas Inspected:Radioactive Matl Processing & Shipping Programs & Occupational Radiation Safety Performance Indicator IR 05000298/19990081999-09-14014 September 1999 Insp Rept 50-298/99-08 on 990816-20.No Violations Noted. Major Areas Inspected:Access Authorization/Fitness-for-Duty (Behavior Observation) Program,Access Control of Personnel, Packages & Vehicles Into Protected & Vital Areas & PIs IR 05000298/19990061999-08-0909 August 1999 Insp Rept 50-298/99-06 on 990530-0717.No Violations Noted. Major Areas Inspected:Inspectors Performed Partial Walkdown of high-pressure Coolant Injection Sys,Including Components Located in Sys Pump Room IR 05000298/19990021999-07-21021 July 1999 Insp Rept 50-298/99-02 on 990628-0702.No Violations Noted. Major Areas Inspected:Licensed Operator Requalification Program to Determine Whether Program Incorporated Appropriate Requirements for Evaluation Operator IR 05000298/19990051999-06-16016 June 1999 Insp Rept 50-298/99-05 on 990502-29.Noncited Violations Identified.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000298/19990041999-05-19019 May 1999 Insp Rept 50-298/99-04 on 990321-0501.Non-cited Violations Identified.Major Areas Inspected:Operations,Maint & Plant Status.Emergency Procedures Failed to Instruct Operators When to Reduce Core Spray Pump Flow Following DBA IR 05000298/19990011999-05-0505 May 1999 Insp Rept 50-298/99-01 on 990207-0320.Non-cited Violations Noted.Major Areas Inspected:Operations & Maint ML20204D9811999-03-18018 March 1999 Insp Rept 50-298/98-09 on 981227-990206.Violations Noted. Major Areas Inspected:Operations,Maint & Engineering IR 05000298/19980081999-01-22022 January 1999 Insp Rept 50-298/98-08 on 980115-1226.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20199E1691999-01-0707 January 1999 Insp Rept 50-298/98-22 on 981116-1208.Violations Noted.Major Areas Inspected:Licensee Performance in Completing Engineering Strategy Action Item 3.2.e IR 05000298/19980151998-12-17017 December 1998 Insp Rept 50-298/98-15 on 980504-22 & 980608-26.Violations Noted.Major Areas Inspected:Safety Sys Engineering Insp Performed for Dgs,Vital Ac Eds & CR Emergency Filtration Sys IR 05000298/19980071998-12-11011 December 1998 Insp Rept 50-298/98-07 on 981004-1114.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19980211998-10-29029 October 1998 Insp Rept 50-298/98-21 on 981005-09.No Violations Noted. Major Areas Inspected:Third 10-yr Interval Inservice Insp Program,Including GE Reactor Insp Sys Automated Ultrasonic Exams of Reactor Vessel Circumferential Weld IR 05000298/19980061998-10-21021 October 1998 Insp Rept 50-298/98-06 on 980823-1003.No Violations Noted. Major Areas Inspected:Operations,Maintenance & Plant Support IR 05000298/19980201998-09-21021 September 1998 Insp Rept 50-298/98-20 on 980831-0904.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program IR 05000298/19980051998-09-18018 September 1998 Insp Rept 50-298/98-05 on 980712-0822.No Violations Noted. Major Areas Inspected:Operations,Maint & Engineering IR 05000298/19980041998-08-19019 August 1998 Errata to Insp Rept 50-298/98-04.Page 10 of Rept Was Inadvertently Omitted ML20237A6221998-08-10010 August 1998 Insp Rept 50-298/98-04 on 980531-0711.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19980181998-06-30030 June 1998 Insp Rept 50-298/98-18 on 980518-21 & 0608-11.No Violations Noted.Major Areas Inspected:Reviewed Radiation Protection Activities Including Exposure Controls,Controls of Radioactive Matls & Contamination IR 05000298/19980031998-06-23023 June 1998 Insp Rept 50-298/98-03 on 980419-0530.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19980161998-06-22022 June 1998 Insp Rept 50-298/98-16 on 980608-11.Weakness Noted.Major Areas Inspected:Licensee Performance & Capabilities During full-scale Biennial Exercise of Emergency Plan & Implementing Procedures IR 05000298/19980191998-06-17017 June 1998 Cancelled Insp Rept 50-298/98-19.Open Items Insp That Was Assigned NRC Insp Rept 50-298/98-19 Will Be Combined W/ Engineering Insp Documented in NRC Insp Rept 50-298/98-15 IR 05000298/19980021998-06-11011 June 1998 Errata to Insp Rept 50-298/98-02,dtd 980515.Changes Have Been Made to Fourth Paragraph IR 05000298/19980171998-05-26026 May 1998 Insp Rept 50-298/98-17 on 980504-08.Violations Noted.Major Areas Inspected:Plant Support ML20247L2721998-05-15015 May 1998 Insp Rept 50-298/98-02 on 980308-0418.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19980131998-04-17017 April 1998 Insp Rept 50-298/98-13 on 980406-09.No Violations Noted. Major Areas Inspected:Training & Qualifications,Quality Assurance Oversight,Facilities & Equipment,Procedural Guidance & Annual Repts IR 05000298/19980141998-04-17017 April 1998 Insp Rept 50-298/98-14 on 980406-09.No Violations Noted. Major Areas Inspected:Organization & Mgt Controls, Radioactive Effluent Monitoring & safety-related Air Cleaning Sys ML20216F8721998-04-14014 April 1998 Insp Rept 50-298/98-12 on 980316-19.No Violations Noted. Major Areas Inspected:Emergency Plan & Implementing Procedures,Emergency Facilities & Equipment,Organization & Mgt Control,Training & Audits IR 05000298/19980111998-04-0909 April 1998 Cancelled Insp Rept 50-298/98-11.No Rept Will Be Issued W/Subj Number IR 05000298/19980011998-03-31031 March 1998 Insp Rept 50-298/98-01 on 980125-0307.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19980101998-03-19019 March 1998 Insp Rept 50-298/98-10 on 980302-06.Violations Noted.Major Areas Inspected:Review of Access Authorization,Vehicle Access Control,Assessment Aids,Safeguards Event Logs,Plans & Procedures & Audit & self-assessment Programs IR 05000298/19970111998-02-23023 February 1998 Insp Rept 50-298/97-11 on 971214-980124.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19972011998-02-0505 February 1998 Insp Repts 50-298/97-201 on 971027-1121 & 1201-04.No Violations Noted.Major Areas Inspected:Rhr Sys & REC Sys ML20198L0471998-01-12012 January 1998 Insp Rept 50-298/97-10 on 971102-1213.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19970091997-12-19019 December 1997 Insp Rept 50-298/97-09 on 970921-1101.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19970191997-12-17017 December 1997 Insp Rept 50-298/97-19 on 971117-20.No Violations Noted. Major Areas Inspected:Implementation of Radiological Environ Monitoring & Meteorological Monitoring,Training & Qualifications,Qa Oversight,Facilities & Equipment IR 05000298/19970181997-12-17017 December 1997 Insp Rept 50-298/97-18 on 971020-1117.No Violations Noted. Major Areas Inspected:Maint & Engineering IR 05000298/19970171997-12-10010 December 1997 Insp Rept 50-298/97-17 on 971117-20.No Violations Noted. Major Areas Inspected:Licensed Operator Requalification Program Evaluation IR 05000298/19970081997-10-20020 October 1997 Insp Rept 50-298/97-08 on 970810-0920.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000298/19970161997-10-0909 October 1997 Insp Rept 50-298/97-16 on 970915-24.Violations Noted.Major Areas Inspected:Follow Up on Licensee Planned & Implemented Activities Associated W/Erosion/Corrosion Monitoring Program & Open NRC Items IR 05000298/19970121997-10-0303 October 1997 Insp Rept 50-298/97-12 on 970708-0905.Violations Being Considered for Escalated Ea.Major Areas Inspected:Evaluation of Licensee Performance Re Recognizing Documenting & Correcting Conditions Adverse to Quality ML20154F2061997-09-19019 September 1997 Partially Withheld Insp Rept 50-298/97-15 on 970818-22 (Ref 10CFR73.21).Violations Noted.Major Areas Inspected:Licensee Vehicle Barrier Sys Utilizing Technical Instruction 2515-132,dtd 960118 IR 05000298/19970131997-09-12012 September 1997 Insp Rept 50-298/97-13 on 970728-0814.Violation Noted.Major Areas Inspected:Surveillance Procedure IR 05000298/19970071997-09-0404 September 1997 Insp Rept 50-298/97-07 on 970629-0809.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support IR 05000298/19970141997-08-27027 August 1997 Insp Rept 50-298/97-14 on 970804-08.No Violations Noted. Major Areas Inspected:Licensee FFD Program Utilizing IP 81502, FFD Program, ML20149K8881997-07-25025 July 1997 Insp Rept 50-298/97-06 on 970518-0628.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support 1999-09-27
[Table view] Category:NRC-GENERATED
MONTHYEARIR 05000298/19990121999-10-22022 October 1999 Insp Rept 50-298/99-12 on 990927-30.No Violations Noted. Major Areas Inspected:Licensee Emergency Preparedness Program & Included Review of Emergency Preparedness Performance Indicators IR 05000298/19990101999-10-14014 October 1999 Insp Rept 50-298/99-10 on 990920-24.No Violations Noted. Major Areas Inspected:Radiological Environ & Meteorological Monitoring Programs & Program for Unrestricted Release of Matl from Radiological Controlled Area IR 05000298/19990031999-10-0808 October 1999 Insp Rept 50-298/99-03 on 990823-27 & 990907-10.No Violations Noted.Major Areas Inspected:Methods Used for Identification,Cause Investigation & Correction of Quality Related Problems IR 05000298/19990071999-09-27027 September 1999 Insp Rept 50-298/99-07 on 990718-0828.No Violations Noted. Major Areas Inspected:Implementation of Reactor Safety & Emergency Preparedness Programs IR 05000298/19990091999-09-22022 September 1999 Insp Rept 50-298/99-09 on 990823-26.No Violations Noted. Major Areas Inspected:Radioactive Matl Processing & Shipping Programs & Occupational Radiation Safety Performance Indicator IR 05000298/19990081999-09-14014 September 1999 Insp Rept 50-298/99-08 on 990816-20.No Violations Noted. Major Areas Inspected:Access Authorization/Fitness-for-Duty (Behavior Observation) Program,Access Control of Personnel, Packages & Vehicles Into Protected & Vital Areas & PIs IR 05000298/19990061999-08-0909 August 1999 Insp Rept 50-298/99-06 on 990530-0717.No Violations Noted. Major Areas Inspected:Inspectors Performed Partial Walkdown of high-pressure Coolant Injection Sys,Including Components Located in Sys Pump Room IR 05000298/19990021999-07-21021 July 1999 Insp Rept 50-298/99-02 on 990628-0702.No Violations Noted. Major Areas Inspected:Licensed Operator Requalification Program to Determine Whether Program Incorporated Appropriate Requirements for Evaluation Operator IR 05000298/19990051999-06-16016 June 1999 Insp Rept 50-298/99-05 on 990502-29.Noncited Violations Identified.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000298/19990041999-05-19019 May 1999 Insp Rept 50-298/99-04 on 990321-0501.Non-cited Violations Identified.Major Areas Inspected:Operations,Maint & Plant Status.Emergency Procedures Failed to Instruct Operators When to Reduce Core Spray Pump Flow Following DBA IR 05000298/19990011999-05-0505 May 1999 Insp Rept 50-298/99-01 on 990207-0320.Non-cited Violations Noted.Major Areas Inspected:Operations & Maint ML20204D9811999-03-18018 March 1999 Insp Rept 50-298/98-09 on 981227-990206.Violations Noted. Major Areas Inspected:Operations,Maint & Engineering IR 05000298/19980081999-01-22022 January 1999 Insp Rept 50-298/98-08 on 980115-1226.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20199E1691999-01-0707 January 1999 Insp Rept 50-298/98-22 on 981116-1208.Violations Noted.Major Areas Inspected:Licensee Performance in Completing Engineering Strategy Action Item 3.2.e IR 05000298/19980151998-12-17017 December 1998 Insp Rept 50-298/98-15 on 980504-22 & 980608-26.Violations Noted.Major Areas Inspected:Safety Sys Engineering Insp Performed for Dgs,Vital Ac Eds & CR Emergency Filtration Sys IR 05000298/19980071998-12-11011 December 1998 Insp Rept 50-298/98-07 on 981004-1114.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19980211998-10-29029 October 1998 Insp Rept 50-298/98-21 on 981005-09.No Violations Noted. Major Areas Inspected:Third 10-yr Interval Inservice Insp Program,Including GE Reactor Insp Sys Automated Ultrasonic Exams of Reactor Vessel Circumferential Weld IR 05000298/19980061998-10-21021 October 1998 Insp Rept 50-298/98-06 on 980823-1003.No Violations Noted. Major Areas Inspected:Operations,Maintenance & Plant Support IR 05000298/19980201998-09-21021 September 1998 Insp Rept 50-298/98-20 on 980831-0904.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program IR 05000298/19980051998-09-18018 September 1998 Insp Rept 50-298/98-05 on 980712-0822.No Violations Noted. Major Areas Inspected:Operations,Maint & Engineering IR 05000298/19980041998-08-19019 August 1998 Errata to Insp Rept 50-298/98-04.Page 10 of Rept Was Inadvertently Omitted ML20237A6221998-08-10010 August 1998 Insp Rept 50-298/98-04 on 980531-0711.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19980181998-06-30030 June 1998 Insp Rept 50-298/98-18 on 980518-21 & 0608-11.No Violations Noted.Major Areas Inspected:Reviewed Radiation Protection Activities Including Exposure Controls,Controls of Radioactive Matls & Contamination IR 05000298/19980031998-06-23023 June 1998 Insp Rept 50-298/98-03 on 980419-0530.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19980161998-06-22022 June 1998 Insp Rept 50-298/98-16 on 980608-11.Weakness Noted.Major Areas Inspected:Licensee Performance & Capabilities During full-scale Biennial Exercise of Emergency Plan & Implementing Procedures IR 05000298/19980191998-06-17017 June 1998 Cancelled Insp Rept 50-298/98-19.Open Items Insp That Was Assigned NRC Insp Rept 50-298/98-19 Will Be Combined W/ Engineering Insp Documented in NRC Insp Rept 50-298/98-15 IR 05000298/19980021998-06-11011 June 1998 Errata to Insp Rept 50-298/98-02,dtd 980515.Changes Have Been Made to Fourth Paragraph IR 05000298/19980171998-05-26026 May 1998 Insp Rept 50-298/98-17 on 980504-08.Violations Noted.Major Areas Inspected:Plant Support ML20247L2721998-05-15015 May 1998 Insp Rept 50-298/98-02 on 980308-0418.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19980131998-04-17017 April 1998 Insp Rept 50-298/98-13 on 980406-09.No Violations Noted. Major Areas Inspected:Training & Qualifications,Quality Assurance Oversight,Facilities & Equipment,Procedural Guidance & Annual Repts IR 05000298/19980141998-04-17017 April 1998 Insp Rept 50-298/98-14 on 980406-09.No Violations Noted. Major Areas Inspected:Organization & Mgt Controls, Radioactive Effluent Monitoring & safety-related Air Cleaning Sys ML20216F8721998-04-14014 April 1998 Insp Rept 50-298/98-12 on 980316-19.No Violations Noted. Major Areas Inspected:Emergency Plan & Implementing Procedures,Emergency Facilities & Equipment,Organization & Mgt Control,Training & Audits IR 05000298/19980111998-04-0909 April 1998 Cancelled Insp Rept 50-298/98-11.No Rept Will Be Issued W/Subj Number IR 05000298/19980011998-03-31031 March 1998 Insp Rept 50-298/98-01 on 980125-0307.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19980101998-03-19019 March 1998 Insp Rept 50-298/98-10 on 980302-06.Violations Noted.Major Areas Inspected:Review of Access Authorization,Vehicle Access Control,Assessment Aids,Safeguards Event Logs,Plans & Procedures & Audit & self-assessment Programs IR 05000298/19970111998-02-23023 February 1998 Insp Rept 50-298/97-11 on 971214-980124.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19972011998-02-0505 February 1998 Insp Repts 50-298/97-201 on 971027-1121 & 1201-04.No Violations Noted.Major Areas Inspected:Rhr Sys & REC Sys ML20198L0471998-01-12012 January 1998 Insp Rept 50-298/97-10 on 971102-1213.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19970091997-12-19019 December 1997 Insp Rept 50-298/97-09 on 970921-1101.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19970191997-12-17017 December 1997 Insp Rept 50-298/97-19 on 971117-20.No Violations Noted. Major Areas Inspected:Implementation of Radiological Environ Monitoring & Meteorological Monitoring,Training & Qualifications,Qa Oversight,Facilities & Equipment IR 05000298/19970181997-12-17017 December 1997 Insp Rept 50-298/97-18 on 971020-1117.No Violations Noted. Major Areas Inspected:Maint & Engineering IR 05000298/19970171997-12-10010 December 1997 Insp Rept 50-298/97-17 on 971117-20.No Violations Noted. Major Areas Inspected:Licensed Operator Requalification Program Evaluation IR 05000298/19970081997-10-20020 October 1997 Insp Rept 50-298/97-08 on 970810-0920.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000298/19970161997-10-0909 October 1997 Insp Rept 50-298/97-16 on 970915-24.Violations Noted.Major Areas Inspected:Follow Up on Licensee Planned & Implemented Activities Associated W/Erosion/Corrosion Monitoring Program & Open NRC Items IR 05000298/19970121997-10-0303 October 1997 Insp Rept 50-298/97-12 on 970708-0905.Violations Being Considered for Escalated Ea.Major Areas Inspected:Evaluation of Licensee Performance Re Recognizing Documenting & Correcting Conditions Adverse to Quality ML20154F2061997-09-19019 September 1997 Partially Withheld Insp Rept 50-298/97-15 on 970818-22 (Ref 10CFR73.21).Violations Noted.Major Areas Inspected:Licensee Vehicle Barrier Sys Utilizing Technical Instruction 2515-132,dtd 960118 IR 05000298/19970131997-09-12012 September 1997 Insp Rept 50-298/97-13 on 970728-0814.Violation Noted.Major Areas Inspected:Surveillance Procedure IR 05000298/19970071997-09-0404 September 1997 Insp Rept 50-298/97-07 on 970629-0809.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support IR 05000298/19970141997-08-27027 August 1997 Insp Rept 50-298/97-14 on 970804-08.No Violations Noted. Major Areas Inspected:Licensee FFD Program Utilizing IP 81502, FFD Program, ML20149K8881997-07-25025 July 1997 Insp Rept 50-298/97-06 on 970518-0628.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support 1999-09-27
[Table view] Category:INSPECTION REPORT
MONTHYEARIR 05000298/19990121999-10-22022 October 1999 Insp Rept 50-298/99-12 on 990927-30.No Violations Noted. Major Areas Inspected:Licensee Emergency Preparedness Program & Included Review of Emergency Preparedness Performance Indicators IR 05000298/19990101999-10-14014 October 1999 Insp Rept 50-298/99-10 on 990920-24.No Violations Noted. Major Areas Inspected:Radiological Environ & Meteorological Monitoring Programs & Program for Unrestricted Release of Matl from Radiological Controlled Area IR 05000298/19990031999-10-0808 October 1999 Insp Rept 50-298/99-03 on 990823-27 & 990907-10.No Violations Noted.Major Areas Inspected:Methods Used for Identification,Cause Investigation & Correction of Quality Related Problems IR 05000298/19990071999-09-27027 September 1999 Insp Rept 50-298/99-07 on 990718-0828.No Violations Noted. Major Areas Inspected:Implementation of Reactor Safety & Emergency Preparedness Programs IR 05000298/19990091999-09-22022 September 1999 Insp Rept 50-298/99-09 on 990823-26.No Violations Noted. Major Areas Inspected:Radioactive Matl Processing & Shipping Programs & Occupational Radiation Safety Performance Indicator IR 05000298/19990081999-09-14014 September 1999 Insp Rept 50-298/99-08 on 990816-20.No Violations Noted. Major Areas Inspected:Access Authorization/Fitness-for-Duty (Behavior Observation) Program,Access Control of Personnel, Packages & Vehicles Into Protected & Vital Areas & PIs IR 05000298/19990061999-08-0909 August 1999 Insp Rept 50-298/99-06 on 990530-0717.No Violations Noted. Major Areas Inspected:Inspectors Performed Partial Walkdown of high-pressure Coolant Injection Sys,Including Components Located in Sys Pump Room IR 05000298/19990021999-07-21021 July 1999 Insp Rept 50-298/99-02 on 990628-0702.No Violations Noted. Major Areas Inspected:Licensed Operator Requalification Program to Determine Whether Program Incorporated Appropriate Requirements for Evaluation Operator IR 05000298/19990051999-06-16016 June 1999 Insp Rept 50-298/99-05 on 990502-29.Noncited Violations Identified.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000298/19990041999-05-19019 May 1999 Insp Rept 50-298/99-04 on 990321-0501.Non-cited Violations Identified.Major Areas Inspected:Operations,Maint & Plant Status.Emergency Procedures Failed to Instruct Operators When to Reduce Core Spray Pump Flow Following DBA IR 05000298/19990011999-05-0505 May 1999 Insp Rept 50-298/99-01 on 990207-0320.Non-cited Violations Noted.Major Areas Inspected:Operations & Maint ML20204D9811999-03-18018 March 1999 Insp Rept 50-298/98-09 on 981227-990206.Violations Noted. Major Areas Inspected:Operations,Maint & Engineering IR 05000298/19980081999-01-22022 January 1999 Insp Rept 50-298/98-08 on 980115-1226.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20199E1691999-01-0707 January 1999 Insp Rept 50-298/98-22 on 981116-1208.Violations Noted.Major Areas Inspected:Licensee Performance in Completing Engineering Strategy Action Item 3.2.e IR 05000298/19980151998-12-17017 December 1998 Insp Rept 50-298/98-15 on 980504-22 & 980608-26.Violations Noted.Major Areas Inspected:Safety Sys Engineering Insp Performed for Dgs,Vital Ac Eds & CR Emergency Filtration Sys IR 05000298/19980071998-12-11011 December 1998 Insp Rept 50-298/98-07 on 981004-1114.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19980211998-10-29029 October 1998 Insp Rept 50-298/98-21 on 981005-09.No Violations Noted. Major Areas Inspected:Third 10-yr Interval Inservice Insp Program,Including GE Reactor Insp Sys Automated Ultrasonic Exams of Reactor Vessel Circumferential Weld IR 05000298/19980061998-10-21021 October 1998 Insp Rept 50-298/98-06 on 980823-1003.No Violations Noted. Major Areas Inspected:Operations,Maintenance & Plant Support IR 05000298/19980201998-09-21021 September 1998 Insp Rept 50-298/98-20 on 980831-0904.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program IR 05000298/19980051998-09-18018 September 1998 Insp Rept 50-298/98-05 on 980712-0822.No Violations Noted. Major Areas Inspected:Operations,Maint & Engineering IR 05000298/19980041998-08-19019 August 1998 Errata to Insp Rept 50-298/98-04.Page 10 of Rept Was Inadvertently Omitted ML20237A6221998-08-10010 August 1998 Insp Rept 50-298/98-04 on 980531-0711.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19980181998-06-30030 June 1998 Insp Rept 50-298/98-18 on 980518-21 & 0608-11.No Violations Noted.Major Areas Inspected:Reviewed Radiation Protection Activities Including Exposure Controls,Controls of Radioactive Matls & Contamination IR 05000298/19980031998-06-23023 June 1998 Insp Rept 50-298/98-03 on 980419-0530.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19980161998-06-22022 June 1998 Insp Rept 50-298/98-16 on 980608-11.Weakness Noted.Major Areas Inspected:Licensee Performance & Capabilities During full-scale Biennial Exercise of Emergency Plan & Implementing Procedures IR 05000298/19980191998-06-17017 June 1998 Cancelled Insp Rept 50-298/98-19.Open Items Insp That Was Assigned NRC Insp Rept 50-298/98-19 Will Be Combined W/ Engineering Insp Documented in NRC Insp Rept 50-298/98-15 IR 05000298/19980021998-06-11011 June 1998 Errata to Insp Rept 50-298/98-02,dtd 980515.Changes Have Been Made to Fourth Paragraph IR 05000298/19980171998-05-26026 May 1998 Insp Rept 50-298/98-17 on 980504-08.Violations Noted.Major Areas Inspected:Plant Support ML20247L2721998-05-15015 May 1998 Insp Rept 50-298/98-02 on 980308-0418.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19980131998-04-17017 April 1998 Insp Rept 50-298/98-13 on 980406-09.No Violations Noted. Major Areas Inspected:Training & Qualifications,Quality Assurance Oversight,Facilities & Equipment,Procedural Guidance & Annual Repts IR 05000298/19980141998-04-17017 April 1998 Insp Rept 50-298/98-14 on 980406-09.No Violations Noted. Major Areas Inspected:Organization & Mgt Controls, Radioactive Effluent Monitoring & safety-related Air Cleaning Sys ML20216F8721998-04-14014 April 1998 Insp Rept 50-298/98-12 on 980316-19.No Violations Noted. Major Areas Inspected:Emergency Plan & Implementing Procedures,Emergency Facilities & Equipment,Organization & Mgt Control,Training & Audits IR 05000298/19980111998-04-0909 April 1998 Cancelled Insp Rept 50-298/98-11.No Rept Will Be Issued W/Subj Number IR 05000298/19980011998-03-31031 March 1998 Insp Rept 50-298/98-01 on 980125-0307.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19980101998-03-19019 March 1998 Insp Rept 50-298/98-10 on 980302-06.Violations Noted.Major Areas Inspected:Review of Access Authorization,Vehicle Access Control,Assessment Aids,Safeguards Event Logs,Plans & Procedures & Audit & self-assessment Programs IR 05000298/19970111998-02-23023 February 1998 Insp Rept 50-298/97-11 on 971214-980124.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19972011998-02-0505 February 1998 Insp Repts 50-298/97-201 on 971027-1121 & 1201-04.No Violations Noted.Major Areas Inspected:Rhr Sys & REC Sys ML20198L0471998-01-12012 January 1998 Insp Rept 50-298/97-10 on 971102-1213.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19970091997-12-19019 December 1997 Insp Rept 50-298/97-09 on 970921-1101.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19970191997-12-17017 December 1997 Insp Rept 50-298/97-19 on 971117-20.No Violations Noted. Major Areas Inspected:Implementation of Radiological Environ Monitoring & Meteorological Monitoring,Training & Qualifications,Qa Oversight,Facilities & Equipment IR 05000298/19970181997-12-17017 December 1997 Insp Rept 50-298/97-18 on 971020-1117.No Violations Noted. Major Areas Inspected:Maint & Engineering IR 05000298/19970171997-12-10010 December 1997 Insp Rept 50-298/97-17 on 971117-20.No Violations Noted. Major Areas Inspected:Licensed Operator Requalification Program Evaluation IR 05000298/19970081997-10-20020 October 1997 Insp Rept 50-298/97-08 on 970810-0920.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000298/19970161997-10-0909 October 1997 Insp Rept 50-298/97-16 on 970915-24.Violations Noted.Major Areas Inspected:Follow Up on Licensee Planned & Implemented Activities Associated W/Erosion/Corrosion Monitoring Program & Open NRC Items IR 05000298/19970121997-10-0303 October 1997 Insp Rept 50-298/97-12 on 970708-0905.Violations Being Considered for Escalated Ea.Major Areas Inspected:Evaluation of Licensee Performance Re Recognizing Documenting & Correcting Conditions Adverse to Quality ML20154F2061997-09-19019 September 1997 Partially Withheld Insp Rept 50-298/97-15 on 970818-22 (Ref 10CFR73.21).Violations Noted.Major Areas Inspected:Licensee Vehicle Barrier Sys Utilizing Technical Instruction 2515-132,dtd 960118 IR 05000298/19970131997-09-12012 September 1997 Insp Rept 50-298/97-13 on 970728-0814.Violation Noted.Major Areas Inspected:Surveillance Procedure IR 05000298/19970071997-09-0404 September 1997 Insp Rept 50-298/97-07 on 970629-0809.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support IR 05000298/19970141997-08-27027 August 1997 Insp Rept 50-298/97-14 on 970804-08.No Violations Noted. Major Areas Inspected:Licensee FFD Program Utilizing IP 81502, FFD Program, ML20149K8881997-07-25025 July 1997 Insp Rept 50-298/97-06 on 970518-0628.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support 1999-09-27
[Table view] Category:UTILITY
MONTHYEARIR 05000298/19900331990-11-0606 November 1990 Insp Rept 50-298/90-33 on 900904-1016.Noncited Violation Identified.Major Areas Inspected:Operational Safety Verification,Monthly Surveillance & Maint Observations, Review of Previously Identified Insp Findings IR 05000298/19900301990-09-27027 September 1990 Insp Rept 50-298/90-30 on 900827-31.Violations Noted.Major Areas Inspected:Licensee Water Chemistry & Radiochemistry Program,Including Water Chemistry & Radiochemistry Confirmatory Measurements IR 05000298/19900311990-09-26026 September 1990 Sys Entry & Retest Insp Rept 50-298/90-31 on 900910-14 & 17. No Violations Noted.Major Areas Inspected:Sys Entry Retest in Areas of Design Changes,Temporary Design Changes & Maint Activities IR 05000298/19900321990-09-14014 September 1990 Advises That Insp Rept 50-298/90-32 Canceled,Therefore,No Insp Rept Issued for Number IR 05000298/19900261990-08-0808 August 1990 Insp Rept 50-298/90-26 on 900616-0715.One Unresolved Item Identified.Major Areas Inspected:Operational Safety Verification,Monthly Maint & Surveillance Observations,Esf Walkdown & Onsite Followup of Written Repts IR 05000298/19900271990-07-20020 July 1990 Insp Rept 50-298/90-27 on 900709-13.No Violations or Deviations Noted.Major Areas Inspected:Licensee Startup Testing Following Refueling & Followup on Corrective Actions for Violation & Deviation IR 05000298/19900201990-07-18018 July 1990 Insp Rept 50-298/90-20 on 900611-15 & 25-29.No Violations or Deviations Noted.Major Areas Inspected:Quality Verification Function,Including Corrective Action & Audit Programs IR 05000298/19900221990-06-30030 June 1990 Insp Rept 50-298/90-22 on 900516-0615.No Violations or Deviations Noted.Major Areas Inspected:Operational Safety Verification,Monthly Surveillance & Maint Observation,Onsite Followup of Written Repts & IE Notice Followup IR 05000298/19900181990-06-15015 June 1990 Insp Rept 50-298/90-18 on 900416-0515.No Violations or Deviations Noted.Major Areas Inspected:Operational Safety Verification,Monthly Surveillance Observation,Complex Surveillance,Monthly Maint Observation & LER IR 05000298/19890241989-09-0606 September 1989 Insp Rept 50-298/89-24 on 890731-0804.Deviations Noted.Major Areas Inspected:Triennial post-fire Safe Shutdown Capability Reverification & Assessment & Implementation of Fire Protection Program IR 05000298/19890271989-09-0505 September 1989 Insp Rept 50-298/89-27 on 890821-25.No Violations Noted. Major Areas Inspected:Surveillance Procedures & Records IR 05000298/19890261989-08-28028 August 1989 Partially Withheld Insp Rept 50-298/89-26 on 890717-21 (Ref 10CFR73.21).No Violations or Deviations Noted.Major Areas Inspected:Physical Security Plan & Procedures,Mgt Effectiveness,Audits,Testing & Maint & Alarms IR 05000298/19890301989-08-24024 August 1989 Insp Rept 50-298/89-30 on 890807-11.Violation Noted.Major Areas Inspected:Qa Program Re Document Control IR 05000298/19890281989-08-18018 August 1989 Insp Rept 50-298/89-28 on 890731-0804.Violations Noted.Major Areas Inspected:Implementation of ATWS Requirements & Licensee Actions on Findings of Previous Insps ML20246G3441989-08-15015 August 1989 Insp Rept 50-298/89-25 on 890701-31.Violation Noted.Major Areas Inspected:Previously Identified Items,Ler Followup, Operational Safety Verification & Monthly Surveillance & Maint Observation IR 05000298/19890211989-07-26026 July 1989 Insp Rept 50-298/89-21 on 890626-30.No Violations or Deviations Noted.Major Areas Inspected:Licensee Liquid, Gaseous & Solid Radwaste Sys IR 05000298/19890221989-07-20020 July 1989 Insp Rept 50-298/89-22 on 890601-30.Violations Noted.Major Areas Inspected:Operational Safety Verification,Monthly Surveillance & Maint Observations & Onsite Followup of Events IR 05000298/19890231989-07-20020 July 1989 Insp Rept 50-298/89-23 on 890626-30.No Violations or Deviations Noted.Major Areas Inspected:Plant Mods & Licensed Operator Training Program IR 05000298/19890181989-06-15015 June 1989 Insp Rept 50-298/89-18 on 890416-0531.Violations Noted.Major Areas Inspected:Operational Safety Verification,Monthly Surveillance & Maint Observations,Installation & Testing of Mods & Refueling Activities ML20244C8001989-06-0202 June 1989 Insp Rept 50-298/89-19 on 890501-05 & 15-19.Violation Noted. Major Areas Inspected:Licensee Actions in Response to NRC Requirements for Motor Operated Valve Testing & Programs for Instrument Calibr & Piping Supports ML20244C9491989-06-0202 June 1989 Insp Rept 50-298/89-16 on 890501-05.Violations Noted.No Deviations Noted.Major Areas Inspected:Selected Areas of Radiation Protection Program as Set Forth in Core Insp Program,As Related to Outage Activities IR 05000298/19890201989-05-25025 May 1989 Reactive Insp Rept 50-298/89-20 on 890515-19.No Violations or Deviations Noted.One Weakness Identified.Major Areas Inspected:Commitments Made Re Facility Welding Program Enhancements IR 05000298/19890171989-05-15015 May 1989 Insp Rept 50-298/89-17 on 890501-05.Violations Noted.Major Areas Inspected:Action on Previously Identified Insp Findings,Inservice Insp & Welding IR 05000298/19890111989-05-0909 May 1989 Insp Rept 50-298/89-11 on 890301-15.No Violations Noted. Major Areas Inspected:Plant Status,Followup of Lers, Operational Safety Verification,Monthly Surveillance & Maint Observations,Balance of Plant Insp & QA Implementation IR 05000298/19890151989-04-27027 April 1989 Insp Rept 50-298/89-15 on 890410-14.Violations Noted.Major Areas Inspected:Welding Activities IR 05000298/19890101989-04-21021 April 1989 Insp Rept 50-298/89-10 on 890327-31.No Violations or Deviations Noted.Major Areas Inspected:Selected Areas in Radiation Protection Program as Set Forth in Core Insp Program (83750) IR 05000298/19890131989-04-12012 April 1989 Insp Rept 50-298/89-13 on 890327-30.No Violations or Deviations Noted.Major Areas Inspected:Licensee Actions Resulting from NRC Info Notice 86-053 Re Improper Installation of Heat Shrinkable Tubing at Nuclear Plants IR 05000298/19890031989-04-10010 April 1989 Insp Rept 50-298/89-03 on 890213-17.Violations Noted.Major Areas Inspected:Unresolved Items from Safety Sys Functional Insp,Including Emergency Electrical Sys,Auxiliary Support Sys & Other Related Issues IR 05000298/19890071989-03-14014 March 1989 Insp Rept 50-298/89-07 on 890206-28.Violation Noted.Major Areas Inspected:Followup of Previously Identified Insp Findings,Operational Safety Verification & Monthly Surveillance & Maint Observations IR 05000298/19880321989-03-0707 March 1989 Informs That Insp Rept 50-298/88-32 Cancelled,Therefore No Insp Rept Will Be Issued for Rept ML20246H4661989-03-0101 March 1989 Partially Withheld Insp Rept 50-298/89-06 on 890206-10 (Ref 10CFR73.21).Violations Noted.Major Areas Inspected:Physical Security Program Including,Mgt Support,Security Program Plan & Audits & Protected Area Physical Barriers IR 05000298/19890051989-03-0101 March 1989 Insp Rept 50-298/89-05 on 890123-27 & 0206-10.Violation Noted.Major Areas Inspected:Action on Previously Identified Insp Findings & Licensee self-assessment Capability ML20235Y7271989-02-28028 February 1989 Insp Rept 50-289/89-09 on 890213-16.Potential Violation Noted.Major Areas Inspected:Diesel Generator Air Sys Failures IR 05000298/19890081989-02-28028 February 1989 Insp Rept 50-298/89-08 on 890215-17.No Violations or Deviations Noted.Major Areas Inspected:Operational Status of Emergency Preparedness Program,Including Changes to EPIPs & Changes to Emergency Facilities,Equipment & Instrumentation ML20235T8481989-02-27027 February 1989 Insp Rept 50-298/89-02 on 890123-27.Violation Noted.Major Areas Inspected:Engineering & Technical Support Capabilities & Activities IR 05000298/19890041989-02-23023 February 1989 Insp Rept 50-298/89-04 on 890123-27.No Violations or Deviations Noted.Major Areas Inspected:Solid Radwaste & Radioactive Matls Transportation Programs ML20235R7661989-02-23023 February 1989 Insp Rept 50-298/89-01 on 890101-0205.Deviation Noted.Major Areas Inspected:Plant Status,Operational Safety Verification,Monthly Surveillance & Maint Observations & Safety Sys Walkdown IR 05000298/19880271988-11-30030 November 1988 Insp Rept 50-298/88-27 on 881024-28.Violation Noted.Major Areas Inspected:Licensee Chemistry/Radiochemistry Program & Water Chemistry & Radiochemistry Confirmatory Measurements ML20206L7931988-11-15015 November 1988 Insp Rept 50-298/88-31 on 881001-31.Violations Noted.Major Areas Inspected:Followup of Plant Events,Operational Safety Verification,Access Control,Monthly Surveillance & Maint Observations & Emergency Excercise ML20206K5921988-11-14014 November 1988 Insp Rept 50-298/88-29 on 881017-20.No Violations or Deviations Noted.Major Areas Inspected:Licensee Performance & Capabilties During Annual Exercise of Emergency Plan & Procedures ML20206A6431988-11-0707 November 1988 Insp Rept 50-298/88-24 on 880912-23.Violation & Unresolved Item Noted.Major Areas Inspected:Followup of Previous Insp Findings,Onsite Review Committee,Offsite Review Committee & Equipment Qualification/Seismic Design of Agastat Relays, IR 05000298/19880281988-10-19019 October 1988 Insp Rept 50-298/88-28 on 880901-30.Violations Noted.Major Areas Inspected:Ler Followup,Transportation,Facility Mods, Operational Safety Verification & Monthly Surveillance & Maint Observations IR 05000298/19880261988-10-18018 October 1988 Insp Rept 50-298/88-26 on 880606-0921.Violations Noted. Major Areas Inspected:Licensee Actions on Previously Identified Items Re Equipment Qualification IR 05000298/19880251988-09-12012 September 1988 Insp Rept 50-298/88-25 on 880801-31.No Violations Noted. Major Areas Inspected:Info Notices Followup,Operational Safety Verification,Monthly Surveillance & Maint, Observations,Esf Walkdown & Security IR 05000298/19882001988-09-0606 September 1988 Insp Rept 50-298/88-200 on 880627-0715.No Violations Noted. Major Areas Inspected:Review of Emergency Operating Procedures Validation & Verification Program,Training Program & Walk Down in Control Room & Plant IR 05000298/19880231988-08-0808 August 1988 Insp Rept 50-298/88-23 on 880705-31.No Violations Noted. Major Areas Inspected:Ler Followup,Operational Safety Verification,Monthly Surveillance & Maint Observations, Radiological Protection & Security IR 05000298/19880211988-08-0505 August 1988 Insp Rept 50-298/88-21 on 880620-24 & 880711-15.No Violations or Deviations Noted.Major Areas Inspected:Action on Previous Insp Findings & Licensee Implementation of Inservice Testing Program for Pumps & Valves ML20151V1821988-08-0303 August 1988 Insp Rept 50-298/88-22 on 880705-08.No Violations Noted. Major Areas Inspected:Assessment Aids,Contingency Plan Implementation & Matl Control & Accountability.Details Withheld (Ref 10CFR2.790) IR 05000298/19880191988-08-0303 August 1988 Insp Rept 50-298/88-19 on 880613-17.No Violations or Deviations Noted.Major Areas Inspected:Nonlicensed Staff Training,Qa Annual Review (Procurement,Receipt Insp & Audits) & Licensee Actions on Previous Concerns ML20151Q9141988-07-15015 July 1988 Insp Rept 50-298/88-20 on 880601-0704.Violations Noted.Major Areas Inspected:Operational Safety Verification,Monthly Surveillance & Maint Observations.Esf Walkdown,Ie Bulletin 88-005 Followup,Radiological Protection & Security 1990-09-27
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000298/19990121999-10-22022 October 1999 Insp Rept 50-298/99-12 on 990927-30.No Violations Noted. Major Areas Inspected:Licensee Emergency Preparedness Program & Included Review of Emergency Preparedness Performance Indicators IR 05000298/19990101999-10-14014 October 1999 Insp Rept 50-298/99-10 on 990920-24.No Violations Noted. Major Areas Inspected:Radiological Environ & Meteorological Monitoring Programs & Program for Unrestricted Release of Matl from Radiological Controlled Area IR 05000298/19990031999-10-0808 October 1999 Insp Rept 50-298/99-03 on 990823-27 & 990907-10.No Violations Noted.Major Areas Inspected:Methods Used for Identification,Cause Investigation & Correction of Quality Related Problems IR 05000298/19990071999-09-27027 September 1999 Insp Rept 50-298/99-07 on 990718-0828.No Violations Noted. Major Areas Inspected:Implementation of Reactor Safety & Emergency Preparedness Programs PNO-IV-99-040, on 990924,licensee Was Replacing Motor Operator for Suction Valve on B Recirculation Loop.After Completing Repairs,Operators Plan to Restart Reactor.Info Has Been Discussed with Licensee1999-09-24024 September 1999 PNO-IV-99-040:on 990924,licensee Was Replacing Motor Operator for Suction Valve on B Recirculation Loop.After Completing Repairs,Operators Plan to Restart Reactor.Info Has Been Discussed with Licensee IR 05000298/19990091999-09-22022 September 1999 Insp Rept 50-298/99-09 on 990823-26.No Violations Noted. Major Areas Inspected:Radioactive Matl Processing & Shipping Programs & Occupational Radiation Safety Performance Indicator IR 05000298/19990081999-09-14014 September 1999 Insp Rept 50-298/99-08 on 990816-20.No Violations Noted. Major Areas Inspected:Access Authorization/Fitness-for-Duty (Behavior Observation) Program,Access Control of Personnel, Packages & Vehicles Into Protected & Vital Areas & PIs IR 05000298/19990061999-08-0909 August 1999 Insp Rept 50-298/99-06 on 990530-0717.No Violations Noted. Major Areas Inspected:Inspectors Performed Partial Walkdown of high-pressure Coolant Injection Sys,Including Components Located in Sys Pump Room IR 05000298/19990021999-07-21021 July 1999 Insp Rept 50-298/99-02 on 990628-0702.No Violations Noted. Major Areas Inspected:Licensed Operator Requalification Program to Determine Whether Program Incorporated Appropriate Requirements for Evaluation Operator IR 05000298/19990051999-06-16016 June 1999 Insp Rept 50-298/99-05 on 990502-29.Noncited Violations Identified.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000298/19990041999-05-19019 May 1999 Insp Rept 50-298/99-04 on 990321-0501.Non-cited Violations Identified.Major Areas Inspected:Operations,Maint & Plant Status.Emergency Procedures Failed to Instruct Operators When to Reduce Core Spray Pump Flow Following DBA IR 05000298/19990011999-05-0505 May 1999 Insp Rept 50-298/99-01 on 990207-0320.Non-cited Violations Noted.Major Areas Inspected:Operations & Maint ML20204D9811999-03-18018 March 1999 Insp Rept 50-298/98-09 on 981227-990206.Violations Noted. Major Areas Inspected:Operations,Maint & Engineering IR 05000298/19993011999-03-0909 March 1999 NRC Operator Licensing Exam Rept 50-298/99-301 (Including Completed & Graded Tests) for Tests Administered on 990212. Exam Results:Four Reactor Operator License Applicants Passed Exam IR 05000298/19980081999-01-22022 January 1999 Insp Rept 50-298/98-08 on 980115-1226.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20202E3261999-01-22022 January 1999 Notice of Violation from Insp on 981115-1226.Violation Noted:Licensee Failed to Take Effective Measures to Preclude Repetition of Inadvertent Opening of torus-to-drywell Vacuum Breaker Documented in LER 50-298/97-007 IR 05000298/19960041999-01-0707 January 1999 Notice of Violation from Insp on 981116-1208.Violation Noted:Deviations from Plant Design Basis Identified as Result of Investigation Following Issuance of Violation 50-298/9604-1013 Not Properly Corrected ML20199E1691999-01-0707 January 1999 Insp Rept 50-298/98-22 on 981116-1208.Violations Noted.Major Areas Inspected:Licensee Performance in Completing Engineering Strategy Action Item 3.2.e IR 05000298/19980151998-12-17017 December 1998 Insp Rept 50-298/98-15 on 980504-22 & 980608-26.Violations Noted.Major Areas Inspected:Safety Sys Engineering Insp Performed for Dgs,Vital Ac Eds & CR Emergency Filtration Sys ML20198J3531998-12-17017 December 1998 Notice of Violation from Insp on 980504-22 & 0608-26. Violation Noted:As of October 1997,licensee Failed to Provide Procedures to Implement Compensatory Measures for Standby Liquid Control Tank Heater Failure,Per USAR ML20197J7321998-12-11011 December 1998 Notice of Violation from Insp on 981004-1114.Violation Noted:On 981001,inspectors Identified That Between 980125- 980125 & 0916,licensee Failed to Properly Maintain Procedures Governing Operation of Reactor Equipment Cooling IR 05000298/19980071998-12-11011 December 1998 Insp Rept 50-298/98-07 on 981004-1114.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19980211998-10-29029 October 1998 Insp Rept 50-298/98-21 on 981005-09.No Violations Noted. Major Areas Inspected:Third 10-yr Interval Inservice Insp Program,Including GE Reactor Insp Sys Automated Ultrasonic Exams of Reactor Vessel Circumferential Weld IR 05000298/19980061998-10-21021 October 1998 Insp Rept 50-298/98-06 on 980823-1003.No Violations Noted. Major Areas Inspected:Operations,Maintenance & Plant Support IR 05000298/19980201998-09-21021 September 1998 Insp Rept 50-298/98-20 on 980831-0904.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program IR 05000298/19980051998-09-18018 September 1998 Insp Rept 50-298/98-05 on 980712-0822.No Violations Noted. Major Areas Inspected:Operations,Maint & Engineering IR 05000298/19980041998-08-19019 August 1998 Errata to Insp Rept 50-298/98-04.Page 10 of Rept Was Inadvertently Omitted IR 05000298/19980991998-08-17017 August 1998 SALP Rept 50-298/98-99 for Cooper Nuclear Station for Period of 970112-980711 ML20237A6221998-08-10010 August 1998 Insp Rept 50-298/98-04 on 980531-0711.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19980181998-06-30030 June 1998 Insp Rept 50-298/98-18 on 980518-21 & 0608-11.No Violations Noted.Major Areas Inspected:Reviewed Radiation Protection Activities Including Exposure Controls,Controls of Radioactive Matls & Contamination IR 05000298/19980031998-06-23023 June 1998 Insp Rept 50-298/98-03 on 980419-0530.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 07100022/20120311998-06-23023 June 1998 Notice of Violation from Insp on 980419-0530.Violation Noted:No Explanation Was Included in Subsequent Annual Radioactive Matls Release Rept & Condition Was Not Repaired in Timely Manner from 971022-1231 IR 05000298/19980161998-06-22022 June 1998 Insp Rept 50-298/98-16 on 980608-11.Weakness Noted.Major Areas Inspected:Licensee Performance & Capabilities During full-scale Biennial Exercise of Emergency Plan & Implementing Procedures IR 05000298/19980191998-06-17017 June 1998 Cancelled Insp Rept 50-298/98-19.Open Items Insp That Was Assigned NRC Insp Rept 50-298/98-19 Will Be Combined W/ Engineering Insp Documented in NRC Insp Rept 50-298/98-15 IR 05000298/19980021998-06-11011 June 1998 Errata to Insp Rept 50-298/98-02,dtd 980515.Changes Have Been Made to Fourth Paragraph ML20249C2481998-05-26026 May 1998 Notice of Violation from Insp on 980504-08.Violation Noted: on 980506,inspector Observed Group of Visitors Enter Protected Area That Were Not Issued Visitor Badges,Did Not Card in & Did Not Enter Protected Area Through Turnstiles IR 05000298/19980171998-05-26026 May 1998 Insp Rept 50-298/98-17 on 980504-08.Violations Noted.Major Areas Inspected:Plant Support ML20247L2451998-05-15015 May 1998 Notice of Violation from Insp on 980308-0418.Violation Noted:Procedure 7.2.63 Was Inappropriate to Circumstances & Had No Appropriate Acceptance Criteria,In That Required Torque Value Not Given in Flange Bolt Work Instructions ML20247L2721998-05-15015 May 1998 Insp Rept 50-298/98-02 on 980308-0418.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000298/19980141998-04-17017 April 1998 Insp Rept 50-298/98-14 on 980406-09.No Violations Noted. Major Areas Inspected:Organization & Mgt Controls, Radioactive Effluent Monitoring & safety-related Air Cleaning Sys IR 05000298/19980131998-04-17017 April 1998 Insp Rept 50-298/98-13 on 980406-09.No Violations Noted. Major Areas Inspected:Training & Qualifications,Quality Assurance Oversight,Facilities & Equipment,Procedural Guidance & Annual Repts ML20216F8721998-04-14014 April 1998 Insp Rept 50-298/98-12 on 980316-19.No Violations Noted. Major Areas Inspected:Emergency Plan & Implementing Procedures,Emergency Facilities & Equipment,Organization & Mgt Control,Training & Audits IR 05000298/19980111998-04-0909 April 1998 Cancelled Insp Rept 50-298/98-11.No Rept Will Be Issued W/Subj Number IR 05000298/19980011998-03-31031 March 1998 Insp Rept 50-298/98-01 on 980125-0307.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20217A3681998-03-19019 March 1998 Notice of Violation from Insp on 980302-06.Violation Noted:On Five Separate Occasions,Licensee Mgt Called in Workers to Perform Back Shift Work W/O Providing Transportation or Administering Breathalyser Test IR 05000298/19980101998-03-19019 March 1998 Insp Rept 50-298/98-10 on 980302-06.Violations Noted.Major Areas Inspected:Review of Access Authorization,Vehicle Access Control,Assessment Aids,Safeguards Event Logs,Plans & Procedures & Audit & self-assessment Programs IR 05000298/19970111998-02-23023 February 1998 Insp Rept 50-298/97-11 on 971214-980124.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20203F8751998-02-23023 February 1998 Notice of Violation from Insp on 971214-980124.Violation Noted:On 971222,while MSL High RM Was Inoperable & Primary Containment Integrity Was Required,Licensee Opened Both Reactor Water Sample Valves IR 05000298/19972011998-02-0505 February 1998 Insp Repts 50-298/97-201 on 971027-1121 & 1201-04.No Violations Noted.Major Areas Inspected:Rhr Sys & REC Sys ML20198L0391998-01-12012 January 1998 Notice of Violation from Insp on 971102-1213.Violation Noted:As of 971213,Procedure 6.SC.502,Rev 2,was Not Appropriate to Circumstances in That Did Not Include Appropriate Acceptance Criteria 1999-09-27
[Table view] |
Inspection Report - Cooper - 1989022 |
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3 O.S.. NUCLEAR. REGULATORY COMMISSION; 4
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- ..NRC ' Inspection Report: - . 50-298/89-22 ' ,
Operating' License: ;DPR-46 l
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' Docket: 50-298; d
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4 Licensee: Nebraska Public Power' District (NPPD) ' '
P.O.' Box 499i ,
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~ Columbus, Nebraska- .
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i Co'oper Nuclear' Station (CNS)
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Inspection At: CNS, Nemaha: County, Nebraska m; .
- LInspection' Conducted: ' June 1-30, 1989
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. Inspectors: 2 . '7 a 6'
~ gG. A" Pick, Resident -Inspector,. Project
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Section C, Division of Reactor. Projects j
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W. R.Menneii, Senior Resident Inspector, 1/w/99 Date; /
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Project Section C, Division of Reactor Projects ;1
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.j Contributing . U Personnel: M. E. - Murphy, Reactor Inspector, Test Program" .
- e 'E Section, Division of Reactor Safety S. F. Kobylarz, Environmental,and Energy Services Company i j
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Approved: m _-- ' 7/2a[ft)
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JE'tT Constable, Chief Project-Section C, , D6t I a s Division.of Reactor Projects ,
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-2-Inspection Summary Inspection Conducted June 1-30, 1989 (Report 50-298/89-22)
Areas Inspected: Routine, unannounced inspection of followup of previously identified items, operational safety verification, monthly surveillance and maintenance observations, and onsite followup of event Results: Within the areas inspected, one apparent violation was identified (inadequate design control, paragraph 4).
Startup activities were conducted in a safe, conservative manner and good communication was evident among the operators. The diesel generator sequential loading test was completed successfully by knowledgeable and proficient personnel. The activities related to identifying and correcting the diesel generator petcock valves issue was comprehensive. The air compressor maintenance procedure was well written with excellent guidance. Licensee actions for correcting unqualified splices found in installed instrument racks were prompt and addressed the root cause. The licensee notified General Electric of the prc'alem who in turn notified other BWR licensees of the potential generic issu An inadvertent feedwater injection event occurred when a throttle valve was assumed to be closed when it was actually partially open. The licensee did not evaluate the reason the valve was partially open until prompted by the inspector l
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-3-DETAILS Persons Contacted Principal Licensee Employees
- G. R. Horn, Division Manager of Nuclear Operations
- R. L. Gardner, Maintenance Manager
- J. V. Sayer, Radiological Manager
- H. T. Hitch, Plant Services Manager
- R. Brungardt, Operations Manager
- J. R. Flaherty, Plant Engineering Supervisor
- G. R. Smith, Licensing Supervisor .
- L. E. Bray, Regulatory Compliance Specialist i
- Denotes those present during the exit interview conducted on July 6, 198 The inspectors also interviewed other licensee employees and contractors during the inspection perio . Plant Statqs The reactor achieved criticality at 2:37 p.m. on June 16, 1989, after a 10-week refueling outage. After minor adjustments to outage installed feedwater control system components, the plant reached 100 percent power operation on June 29, 198 . Followup On Previously Identified Inspection Findings (92701 and 92702) j (Closed)UnresolvedItem(298/8710-08): This item concerned the lack of a voltage study to demonstrate that critical 120 Vac electrical components would be provided adequate voltage during accident condition The inspectors reviewed the CNS 120 Vac Load Study, Applied Power i Associates (APA) Project 117.28, which was prepared in response to a j finding in the 1987 Safety Systems Functional Inspection (SSFI). The APA J study reanalyzed the worst case circuit operating loads and determined !
them to be lower than originally assume J Based on the original APA voltage study a new feeder cable needed to be installed for certain loads. Field measurements determined that adequate operating voltage was present with the existing cable; therefore, a r.ew feeder cable will not be installed. The new operating load calculations have resolved the concern for minimum operating voltage. This item is : '
considered close (Closed) Deviation 298/8818-01: Nuclear Performance Procedure (NPP) 10.9,
" Control Rod Scram Time Evaluation," Revision 14, did not include a
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~ requirement in the prerequisites section for performance by appropriately trained personne The licensee reviewed the qualifications of the personnel who performed NPP 10.9 during the 1988 refueling outage startup. These individuals were found to have been qualified station nuclear engineers, meeting the requirement for performance by appropriately trained personnel. The NRC inspector reviewed NPP 10.9, Revision 15, dated September 30, 1988. This revision incorporated a prerequisite identifying the qualifications required for performance. This item is considered close (Closed)OpenItem 298/8818-02: This item was open pending revision of NPP 10.16, " Shutdown Margin Evaluation," to clarify administrative items and to require the fuel vendor to submit a cycle management report which would be formatted to agree with CNS procedure The licensee has revised NPP 10.16 to clarify the specific criteria for shutdown margin demonstration as well as how it is satisfied. The fuel vendor has agreed with the licensee on a revised shutdown margin demonstration section for the Cooper Cycle Management Report. These revisions were in place for the 1989 refueling outage startup. This item is considered close . Operational Safety Verification (71707)
The inspectors observed operational activities throughout the inspection period. Proper control room staffing was maintained and control room activities and conduct were observed to be well controlled. The inspectors observed selected shift turnover meetings and noted that information concerning plant status was properly corraunicated to the oncoming operators. Control room access was controlled during the perio Discussions with operators determined that they were cognizant of plant status. Limiting Conditions for Operations were properly entered when equipment was declared inoperable for maintenance, and acceptance testing was properly performed and reviewed prior to declaring equipment operabl )
On June 4,1989, while opening reactor feedwater pump (RFP) suction valves, feedwater was inadvertently discharged into the reactor vesse The "A" RFP discharge throttle valve indicated closed; however, it was partially open which allowed flow to the reactor vessel. The refuel pool increased and an estimated 250 gallons of water flowed into ventilation ducts. The ducts are located vertically alongside the refueling pool in order to take suction off the pool surface to capture potentially escaping radioactive gases. Operators closed the discharge throttle valve upon noticing the refuel pool level increase.
i MaintenanceWorkRequest(MWR) 89-2720 was issued to investigate and J repair, as necessary, the discrepancy between the control room indication and the actual valve position. The packing gland follower appeared to be cocked. The electric shop stroked the valve and found the valve operation acceptable. No adjustment of the packing gland follower was needed. The l l
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-5-inspector expressed a concern that a nonconformance report (NCR) was not issued to' identify and correct the root cause of the discrepancy between
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the control room indicator and the actual valve position. In response to the inspector's concern, training will be provided to reemphasize the importance of assuring throttle valves are fully closed in accordance with procedure Since the valve handles for the RFP discharge valves are different from other thrcttle valve handles, the control room panel will be enhanced to clearly identify the feedwater discharge valves as throttle s valve The inspector observed the performance, in part, of:the reactor pressure boundary hydrostatic test. The test was performed on June 12, 1989, as
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required by ASME code. General Operating Procedure (GOP) 2.1.14, "ASME Class I-N System Leakage Test," Revision 21, dated June 10, 1989, was utilized to control the test' activities. The heatup and pressurization were maintained within pressure and temperature limits of the reactor vessel. The hydrostatic test revealed a' few minor leaks through valve packings which are allowed by the code. These leaks were subsequently repaire The inspector observed the plant startup on Juna'16, 1989, to approximately 100 psi. The startup activities _were conducted in accordance with GOP 2.1.1, " Cold Startup Procedure," Revision 54, dated November 9, 1988, NPP 10.13,'" Control Rod Sequence and Movement Control,"
Revhion 19, dated February 2, 1989, and other necessary system operating i proceduras (S0P). Approximately 4 weeks prior to the'startup, as work activities-in a system were completed, the systems were lined up, and shift supervisor (SS) initials on a checklist signified the lineup was ready for startup. This prevented a rush at the end of the outage and allowed for better control of system statu An onsite review committee meeting was held to implement GOP 2.1.1.1, " Plant Startup Review and Authorization," Revision 3, dated September 22, 1988. Implementation of the procedure assured that procedures, documents, commitments, and other required items were completed prior to startup. Completion of GOP 2.1.1.2, " Technical Specification Pre-Startup Checks," Revision 9, dated March 2, 1989, provided the SS with a means to assure all TS items were in place prior to startup. The inspector reviewed GOPs 2.1.1, 2.1.1.1, and 2.1.L 2 signatures and determined that required information was complet During the startup, the licensed operators communicated well and pertinent information exchange occurred. The control room supervisor kept
' distractions to a minimum. System operating procedures were available and were' utilized. The inspector verified that: the control rod withdraw sequence was utilized, surveillance tests required to be performed prior to startup were complete, procedures had been revised to reflect changes made to the facility, and Technical Specifications were followe On June 25, 1989, the feedwater control system (FWCS) experienced a feedwater control signal failure and the newly installed feedwater controllers went into Feedwater Hold, i.e., locked up at last speed
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tracked. The ' operations crew appeared to be surprised that the FWCS annunciator did not respond as expected. Discussions with an instrument and control (I&C) technician familiar with the new FWCS annunciator configuration provided the shift supervisor with sufficient understanding for corrective actions to be taken. The operators became concerned, since in the new configuration, corrective actions to clear the annunciator alarm condition could result in blowing a fuse, and automatically placing the feedwater pump in manual control. There was no longer a way to determine whether the control signal failure condition had cleared; consequently, when turning the feedwater pump lockout switch to reset the alarm condition a fuse would blow if the control signal failure had not cleare The above condition was created when the annunciator upgrade modification performed during the refueling outage could not be completed due to software / hardware incompatibility. An on-the-spot change (OSC) was written on April 20, 1989, to parallel the RFP Turbine Track and Hold Alarm to the Feedwater Control Signal Failure annunciator window. The OSC also required connection of the RFP Turbine Control Trouble Alarm to a spare annunciator windo The inspector verified that training on the feedwater control system had been conducted prior to the outage and that procedures had been changed to include operation of the modified FWCS. However, training had not been conducted to inform the operators of the new response of the feedwater annunciators and what the annunciators mean. Additionally, appropriate procedures had not been altered to reflect the OSC and no annunciator procedure was issued to describe Ntions regarding the RFP Turbine Control Trouble Alarm windo The CNS design change program has procedures which require that training be conducted and that procedures be modified to reflect the plant modifications. Specifically, Engineering Procedure 3.4, " Station Modifications," Revision 9, dated May 25, 1989, requires that Attar W .: B be completed ensuring that design change (DC) related items such as procedures and training be completed or determined to be "not applicable."
Engineering Procedure 3.4.11. " Status Reports," Revision 0, dated (
December 5,1988, requires that, after DC installation or prior to i required system operability (startup in this instance) whichever occurs first, that records be turned over to various departments so that
- procedures and training can be conducted as necessary. Additionally, an OSC, as defined in Engineering Procedure 3.4.10. " Revision, Amendments, and On-the-Spot Changes," Revision 0, dated December 5, 1988, does not i
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require additional training nor changes to the necessary procedure CFR 50, Appendix B, Criterion III, requires that measures be established to assure that the design basis for structures, systems, and components l are correctly translated into specifications, drawings, procedures, and l l
instructions and that design changes, including field changes, shall be i subject to design control measures commensurate with those applied to the original design. The failure of the licensee's established programs to
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assure that required training was provided to licensed operators and to modify required procedures when a change was made to Design Change i Package 88-036,isanapparentviolation(298/8922-01).
The inspectors verified that selected activities of the licensee's l radiological . protection program were implemented in confonnance with {
facility policies, procedures, and regalatory requirements. Radiation {
and/or contaminated areas were properly posted and controlled. Health ]
physics personnel were prompt in reposting radiation areas affected by the '
startup. Radiation work permits contained appropriate information to ensure that work could be performed in a safe and controlled manne Health physics personnel were observed to be touring work areas, ensuring proper implementation of ALARA and radiological control requirement Radiation monitors were properly utilized to check for contaminatio The inspectors observed security prsonnel performing. vehicle, personnel, and package searches. Vehicles were properly authorized and controlled or escorted within the protected area. The inspectors conducted site tours to. ensure that compensatory measures were properly implemented as require The licensee continued implementatf on of the security equipment upgrad Personnel access was observed to be controlled in accordance with established procedures. Interviews with security personnel demonstrated J that they were cognizant of their responsibilities. The PA barrier had adequate illumination and the isolation zones were free of transient material A violation for inadequate design control was identified in this area. In I addition, the inspector expressed a concern for an apparent failure to I
take corrective actions to address the root cause related to an inadvertent injection of feedwater into the reactor vessel. Startup activities were conducted well with good communications among the ,
operations staf No other violations or deviations were identifie . Monthly Surveillance Observations (61726)
The inspectors observed the performance of and/or reviewed the following surveillance procedures (SPs): j SP 6.3.4.3, " Sequent * 1 Loading of Emergency Diesel Generators," ,
Revision 27, dated June 8, 1989. This surveillance functionally tests the emergency start ant, loading sequence for the emergency diesel generators .
(EDG). Also, the residual heat removal pumps and core spray pumps I emergency start features were tested. This is a complex surveillance which involved approximately 20 individuals and had data taken and verified at a minimum of 5 locations. All equipment performed as designed and the accepter.ce criteria were met. The June 12, 1989, test of EDG No. 2 wr, observed and the procedure reviewed. The procedure and data ,
for the EDG No. I testing was reviewed. The operators involved with the j EDG No. 2 test were knowledgeable and familiar with the surveillance purposes, steps, and requirement l
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SP 6.3.10.2, " Instrument Line Flow Check Valve Test," Revision 16, dated September 1, 1988. The inspector observed the performance of this procedure, in part, on June 12, 1989. This procedure tests the Marotta excess flow check valves once per operating cycle to ensure that upon a postulated instrument line break, the leakage would be maintained between 0.2 and 0.7 gallons per minute (gpm), thereby, not exceeding ASME Section XI requirements. Sixty-eight valves were tested with four with leakage greater than 0.7 gpm. Corrective actions were taken to bring the four valves within specification. Two crews tested the valves with each crew consisting of I&C technicians and operations staff personnel. This work was conducted in contaminated 'reas with spills expected to occur due to the testing. ALARA principles were followed and all spills were promptly cleaned up. This test is conducted each outage prior to startup in conjunction with the reactor pressure boundary hydrostatic test. The test was well coordinated 4nd execute SP 6.2.3.L1, "Drywell Floor Drain Sump 1F Flow Loop Calibration Test,"
Revision 1, dated November 9, 1988. This procedure was performed on June 26, 1989, to comply with TS Protective Instrument surveillance requirements. The inspector reviewed the completed procedure. All signoffs were completed. One discrepancy was annotated, then deleted without a stated reason for deletion of the comment. Discussions with the I&C technician revealed that he had inadvertently placed test leads into the incorrect test jacks. This action resulted in erroneous data. After utilizing the correct test jacks, the data was within toleranc SP 6.2.3.2.1, "Drywell Equipment Drain Sump IG Flow Loop Calibration Test," Revision 1, dated November 9, 1988. The inspector observed the performance of this test conducted on June 26, 1989. All required signatures had been obtained on this TS required surveillance. Good communication between technicians was evident. Measuring and test instruments utilized were calibrate NPP 10.9, " Control Rod Scram Time Evaluation," Revision 17, dated April 27,1989. The inspector observed, in part, the performance of this procedure on June 19, 1989. This test was performed to meet TS requirements and ASME,Section XI, inservice Testing requirements. The scram times were obtained by utilizing the process computer. Discussions with the licensed operators performing the test and the reactor engineers indicated that they had a thorough understanding of the. limitations, precautions, and prerequisites associated with the testing. No discrepancies were identified during the testing. All data were within specification No violations or deviations were identifie . Monthly Maintenance Observation (62703)
On June 27-28, 1989, the inspector observed the performance of Preventative Maintenance Activity (PM) 03873. The annual PM involved the disassembly, inspection, and replacement, as needed, of parts on the "B" Air j f
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Compressor. Maintenance Procedure (MP) 7.2.27, " Air Compressor Maintenance," Revision 3, dated February 6,1986, was used in the performance of the PM. The procedure was adequate and was sectioned L in a logical manner. For example, sections existed for: piston removal T
'and replacement; water cleaning jackets; removal of the intercooler and installation and Acleaning of the Type (of the cylinder NL nonlubricated)
channel valves; and disassembly, repair, and assembly of the Type A NL
. valves. The mechanics were experienced and.followed proper safety practice During a maintenance run of one of the EDGs, a petcock valve in an individual cylinder exhaust pipe sheared. .The inspector reviewed corrective actions identified by the license Investigation by the licensee determined that a'. hairline crack must have existed since original installation. .The failure was thought to have occurred due to stress by additional forces placed on the valve over time by the mechanics conducting engine analysis. The failure of the petcock valves would not render the EDGs inoperable. All adapter plates and petcock valves were replaced on both EDGs. Two additional petcock valves were broken during removal. Radiographic examinations were performed on the remaining 29 valves. Indications were found on one other valve. The 28 valves without indications were returned to spare The manner in which the air compressor maintenance procedure was written combined with the skills, knowledge, and abilities possessed by the technicians allowed for a well conducted maintenance activity. The ,
activities related to identifying and correcting the EDG petcock valves issue ~was comprehensiv No violations or deviations were identifie . Onsite Followup of Events (Unqualified Wire and Splices Found in EQ Equipment) (93702)
- While working.to complete DC 87-190, to update the limit switches of air operated valves (A0V) to seismic requirements as required in Regulatory
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'to Assess Plant and Environs Conditions During and following an Accident,"
- the licensee discovered four switches with unqualified wire. These wires were replaced with environmentally qualified (EQ) wire in accordance with DC 87-190 installation instructions. The licensee conducted a walkdown of all- A0Vs required to be environmentally qualified and identified five-additional limit. switches with unqualified wire. Replacement of the wire wasaccomplishedunderEquipmentSpecificationChange(ESC)89-18 To determine if the problem was isolated to the indication circuits of A0Vs, the licensee initiated a random sampling inspection of local terminal boxes. This resulted in the finding of questionable wire, which was later identified as instrument pigtails. This discovery led to the evaluation of additional EQ equipnent. The list of actual iteme to be walked down was developed by using the following elimination criteria:
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All cabling to the component has already been walked down Component uses a conduit seal spliced directly to known field cable l Component does not require cable for the performance of its safety function
Component is located within a qualified assembly _
i Equipment is a generic support item which is required only to support the operation of other components
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Component or cable has been recently installed and cable information is available from the design package Component was purchased / supplied with qualified interconnecting cables
No local terminal boxes are used
Jumpers are not used, field cables were connected directly to equipment terminals (These criteria were extracted from the licensee's document titled,
"Walkdown of EQ Jumper Cables")
Eliminating the items that met any of the preceding criteria resulted in a list of 150 items to be inspected. These items, uniquely, had a locally mounted terminal box requiring a jumper to interface the component to the field wire. The items were: ASCO - solenoid operated valves (S0Vs),
Barton pressure switches, Yarway switches, various small motors (e.g.,
valve operators), Target Rock - S0Vs, PCI pres:;ure switches, Woodward Governor controls, and other miscellaneous items (e.g., ball flow switches).
The walkdown of the 150 items was performed and document? under MWR 89-2495. This inspection resulted in two findings: (1) PVC wire in high pressure coolant injection (HPCI)-LS-91A and -B, did not have qualification documentation in place, and (2) one type of wire leading from a terminal box with a different type wire termit; ting at the Barton pressure switche The HPCI PVC wire, even though it was judged to be qualified based on partial testing and analysis, was replaced by an amendment to ESC 89-18 Further investigation of the difference in wires associated with the Barton switches revealed the presence of unqualified splices. These were found in conduit LBs between the local terminal box and the instrumen This discovery prompted the licensee to perform another walkdown of the original 150 items to lc,ok specifically for unqualified splices. The reinspection established that all unqualified splices were isolated to
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-11-Barton instruments. To provide further assurance that all unqualified local splices had been identified, the licensee performed another walkdown utilizing a random sample of the previously exempted items. This walkdown did not reveal any other unqualified configuration The licensee investigated the possible sources of the splices and why they had not been identified during previous EQ qualification inspections. It was verified that during prior walkdowns, cable qualification was verified only to the rack-mounted terminal boxes. Because of the short run of conduit to the instruments and the fact that the integrity of the q instrument would have to be broken to inspect the instrument terminal a board, it was assumed that qualified cable existed from the terminal box !
to the instrument terminal boar The unqualified splices do not appear on the drawings for the instruments j or for the racks. The drawings reference General Electric (GE) Design Specification 209A4351. This specification states, " Connections to external devices are to be on terminal blocks located in NEMA Type 12 enclosed steel terminal cabinets." The specification does not address splices, and splicing in general was not addressed by any original ;
construction practices except for the specific prohibition of splici power cable The instrument racks were originally provided to the site by GE under the blanket " Nuclear Steam Supply System" Contract E66-31. A review, by the licensee, of the receiving documentation for this contract verified '
traceability to the original rack manufacturer, HUIC0 Incorporated of Pasco, Washington. Rack construction and instrument installation was based on GE Specification 209A4351 and they were delivered to GE under Purchase Order 282-Y-7044. The racks were installed under Contract E70-3, which made connections to the field side of the terminal box. No records were found to indicate the rack wiring was modified during original installatio It was identified by the licensee, during a maintenance history review, that four switches had been replaced since original instrument rack installation. These switch changes were made by lead lifting and landing at the instrument terminal board, leaving the spliced lead between the terminal box and instrument undisturbe The licensee concluded that the original contractor spliced the pigtails to the GE wire to avoid disassembling the switch. The splices, therefore, existed in the conduit when the instrument racks were received at CN NPPD Letter NLS8900225, dated June 8, 1989, advised GE that a potential generic manufacturing problem existed. It further advised GE that there i was a possible need to report this in accordance with the requirements of )
10 CFR Part 21. In a letter dated June 30, 1989, GE responded stating,
"Because each plant has unique individual plant EQ requirements, ano GF
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Additionally, GE was to notify all BWR owners of this Potentially ReportableCondition(PRC). The information in the PRC summarized what was found at CNS and stated that single conditions may exist at other utilities which have GE supplied instrument rack During field observations of the spliced cable replacement by the inspectors, it was noted that numerous similar splices in non-EQ instrument leads existed. The licensee was asked if this condition had been evaluated for effects on safety-related functions. The licensee's representatives informed the inrpectors that if a non-EQ instrument could affect safety-related functions then the instrument would have been classified as EQ and designated as such on the Master Equipment Lis This was the policy adopted during the development of the original EQ classificatio Replacement of all EQ instrument cables with nonqualified splices was completed prior to startup on June 16, 1989. The licensee was finalizing a justification for continued operation (JCO) while shut down. A JC0 was not needed for startup, since the pressure switches were made operable by changing out the unqualified wire prior to startup. An operability evaluation for Nonconformance Report 89-111 was also being processe The licensee took decisive and prompt action to identify the extent of the nonqualified spices. . The licensee also provided information to GE so that other license holders with similar configurations could be notified. No violations or deviotions were identifie . Exit Interviews (30703)
An exit interview was conducted on July 6, 1989, with licensee representatives identified in paragraph 1. During the interview, the inspectors reviewed the scope and findings of the inspection. Other meetings between the inspectors and licensee management were held periodically during the inspection period to discuss identified concern The licensee did not identify as proprietary any information provided to, or reviewed by, the inspector ;
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