IR 05000272/1986099

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SALP Repts 50-272/86-99 & 50-311/86-99 for Oct 1986 - Dec 1987
ML20148N812
Person / Time
Site: Salem, 05000000
Issue date: 02/05/1988
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18093A779 List:
References
50-272-86-99, 50-311-86-99, NUDOCS 8804080022
Download: ML20148N812 (69)


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U. S. NUCLEAR REGULATORY COMMISSION

REGION I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE INSPECTION REPORT NO. 50-272/86-99; 50-311/86-99 PUBLIC SERVICE ELECTRIC AND GAS COMPANY SALEM GENERATING STATION ASSESSMENT PERIOD: October 1, 1986 - December 31, 1987 SALP BOARD FEBRUARY 5, 1988 i

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8804000022 890329 PDR ADOCK 05000272 O PDR

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SUMMARY . . . . . . . . . . . . . . . . . 56 TABLE 3 - ENFORCEMENT ACTIVIl(. ..... ............. 57 TABLE 4 - LICENSEE EVENT REPORTS. . . . . . . . . . . . . . . . . . 61 TABLE 5 - SUMMARY OF LICENSING ACTIVITIES , . . . . . . . . . . . . 66

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I. INTRODUCTION Purpose and Overview The Systematic Assessment of Licensee Performance (SALP) is an integrated NRC staff effert to collect the available observations and data on a periodic basis and to evaluate licensee performance based upon this information. The SALP program is supplemental to the normal regulatory processes used to ensure compliance to NRC rules and regulations. The SALP program is intended to be sufficiently diagnostic to provide a rational basis for allocating NRC resources and to provide meaningful guidance to the licensee's management to promote quality and safety of plant operatio The NRC SALP Board, composed of the staff members listed below, met on February 5, 1988 to review the collection of performance obser-vations and data and to assess licensee performance in accordance with the guidance in NRC Manual Chapter 0516, "Systematic Assessment of Licensee Performance". A summary of the guidance and evaluation criteria is provided in Section II of this repor This report is the SALP Board's assessment of the licensee's safety performance at the Salem Generating Station for the period October 1, 1986 through December 31, 1987. It is noted that the summary findings and totals reflect a 15 month assessment perio The SALP Board was comprised of the following:

Chairman S. J. Collins, Deputy Director, Division of Reactor Projects (DRP)

Members W. F. Kane, Director, Division of Reacto. Projects (DRP) (part-time)

W. R. Butler, Project Director, PDI-2 (NRR) (part-time)

J. E. Richardson, Acting Deputy Director (DRS)

E. C. Wenzinger, Sr. , Chief, Reactor Projects Branch 2 (DRP)

R. M. Gallo, Chief, Operations Branch (DRS)

R. R. Bellamy, Chief, Facilities Radiological Safety and Safeguards Branch (DRSS) (part-time)

P. D. Swetland, Chief, Reactor Projects Branch 2B (DRP)

T. J. Kenny, Senior Resident Inspector, Salem (DRP)

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Other Attendees (non-voting)

R. R. Keimig, Chief, Safeguards Section (DRSS) (part-time)

W. J. Lazarus, Chief, Emergency Preparedness Section (DRSS)

(part-time)

W. J. Pasciak, Chief, Effluents Radiation Protection Section (DRSS)

(part-time)

M. M. Shanbaky, Chief, Facilities Radiation Protection Section (DRSS)

(part-time)

R. J. Summers, Project Engineer, Branch 2B (DRP) (part-time)

M. J. Cioffi, Radiation Specialist (DRSS) (part-time)

D. T. Wallace, Operations Engineer (ORS)

II. CRITERIA Licensee performance is assessed in selected functional areas. Functional areas normally represent areas significant to nuclear safety and the environmen One or more of the following evaluation criteria were used to assess each are . Management involvement and control in assuring qualit . Approach to resolution of technical issues from a safety standpoin , Responsiveness to NRC initiative . Enforcement histor . Operational events (including response to, analysis of, and corrective actions for).

i Staffing (includirg management). Training and qualification effectivenes i However, the SALP Board is not limited to these criteria and others may >

have been used where appropriat '

Based upon the SALP Board assessment each functional area evaluated _is classified into one of three performance categorie The definitions of '

these periormance categories are: i Category 1: Reduced NRC attention may be m ropriate. Licensee management attention and involvement are a n cessive and oriented toward '

nuclear safety; licensee resources are ample and effectively used such that a high level of performance with respect to operational safety is being achieve !

Category 2: NRC attention should be maintained at normal levels. Licensee HIanagement attention and involvement are evident and concerned with nuclear safety; licensee resources are adequate and reasonably effective 1 so that satisfactory performance with respect to operational safety is j being achieve Category 3: Both NRC and licensee attention should be increased. Licensee management attention or involvement is acceptable and considers nuclear safety, but weaknesses are evident; licensee resources appear strained or not effectively used such that minimally satisfactory performance with respect to operational safety is being achieve The SALP Board may determine to include an appraisal of the performance trend of a functional area. Normally, this performance trend is only used where both a definite trend of performance is discernible to the Board and <

the Board believes that continuation of the trend may result in a change of performance level. Improving (declining) trend is defined as:

Licensee performance was determined to be improving (declining) near the close of the assessment perio I

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i III. SUMMARY OF RESULTS Overall Summary The Salem facilities continue to operate in a safe, competent manne The leadership of site and corporate management in setting high goals with respect to plant safety and reliability is evident by the commit- !

ment of resources to identify and solve problems, the establishment of ownership and accountability for facility performance, and the prompt conservative approach to safety issues, particularly when continued plant operation was affected. The licensee's handling of service water corrosion / erosion problems, electrical coordination discrepancies and reactor vessel head leaks exemplfy this element of performanc Operator performance during routine and abnormal conditions has been good. Some instances of inattea. ion to detail and inadequate communications / interface with other departments have resulted in i plant trips or other events. While the frequency of trips has been ,

reduced, particularly for Unit 1; the number of trips for Unit 2 can be improved. Problems identified in the operator requalification program also require further licensee attentio The surveillance program satisfactorily implements a large number of 1 test requirements to assure reliable equipment operation. Weaknesses L in attention to detail and inter-department interface continue to result in a small, but growing number of missed or late surveillance There is an effective radiation protection program ensite, with

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challenging ALARA goals and adequate resources and management commit-ment to successfully achieve them. Not withstanding, recurrent weaknesses in the quality of radiation protection procedures and the implementation of laboratory quality controls need to be addresse Noteworthy good performance was recognized in the maintenance, security,

emergency planning, outages and assurance of quality areas. In each case, the licensee's aggressive approach to excellence, quality of training, and commitment of resources were exemplar In the engineering area, older plant problems such as inadequate implementation of new regulatory requirements and poor documentation of the design basis for the plants continue to affect overall performance. Recent licensee initiatives appear to be effective in identifying and correcting these problems. Nevertheless, the assess-

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ment of licensee performance in this area reflects the continuing concern over previous performance weaknesse The strength of the management team and the positive worker attitude contribute to the improving trend in licensee performance overal Recurring lapses in individual attention to detail particularly in the surveillance area, longstanding problems with radiation protection

'. procedures and quality control in the chemistry area, and continuing design and engineering support discrepancies indicate that further licensee emphasis in these steas is warranted, a

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8. Background Licensee Activities Unit 1 Unit 1 began this assessment period at 83% due to loading restrictions within the electrical plant. The restrictions were self imposed due to station transformer loading problems identified after the August 26, 1986 false loss of offsite powe Following manipulation of electrical loads between Unit 1 and 2, which conformed to licensee commitments to the NRC, the Unit operated at various power levels up to 100% until March 1, 1987, when a tanker struck and destroyed a 500 KV line from Hope Creek to Keeney, Delaware. The loss of this line restricted electrical output from Salem and Hope Creek because of the potential for off-site electrical line instability if another 500 KV line was lost with all three plants operating at full powe On March 8, 1987, the unit was removed from service for planned maintenance and the replacement of No. 1 Auxiliary Power Transformer. The unit was returned to service on March 15, !

after completion of this maintenance. Unit output was ;

restricted to 71% due to the loss of the 500 KV Keeney lin i On March 27, 1987, a new plant tripping device was energized allowing the units to return to 100% power. This device was installed to trip one operating unit, if another off-site high voltage line would be los The unit selected by the trip-a-unit device would trip, thus restricting nutput power from the Artificial Island (location of Hope Creek and Salem Generating Stations). To prevent undesired trips, the trip-a-unit device was disarmed and unit output reduced anytime l electrical storms in the area threatened high voltage line !

reliabilit '

On April 6, 1987, Steven Miltenberger was appointed to the position of Vice President - Nuclear Operations and Corbin l McNeill was promoted to Senior Vice President - Nuclea On June 2,1987, the unit tripped due to a lightning strike on l the line that had the trip-a-unit in servic The trip-a-unit had not been disarmed because the electrical storm intensity was below the criteria necessary to disarm. This forced the licensee to reevaluate the criteria for removing the trip-a-uni It was determined that such a lightning strike was not common and the criteria was not change On October 2, 1987, the unit was removed from service for a refueling butage and plant modifications. The licensee per-formed the following major changes to the facility: (1) removal of the RTD bypass loop; (2) installation of bottom mounted core exit thermocouples and the elimination of the instrument pene-trations on the reactor head; (3) removal of the boron injection tank, as well as other modifications. The unit remained in the refueling outage (Mode 5) at the end of this report period. The startup from the outage was delayed by a service water flooding event and the discovery of cracks in three spare control rod drive mechanism penetrations.

During this rating period Unit 1 participated in an IAEA sponsored program to monitor plant activities to prevent diversion of special material The staff and management enthusiastically supported these safeguards activities and performed in an exemplary manner.

Unit 2 Unit 2 began this report period operating at 65% power with No.

21 feed pump out of service. On October 2, 1986, the unit was removed from service for a refueling outage. While taking the unit off the line, the licensee successfully demonstrated a partial unit shutdown from outside the control room. Outage activities included: (1) An intrusion of resin into the Refueling Water Storage Water Storage Tank and eventually into the refueling cavity; (2) A complete assessment of all of the welds in the service water system related to the containment fan cooler units; (3) replacement of No. 21 component cooling water heat exchanger tubes; and other design changes and maintenance.

On December 23, 1986, during the restart from refueling, the unit tripped from 8% power while troubleshooting an electro-hydraulic control (tiHC) system failure. Repairs were made and the unit was brought on line on December 24, 1986. (The unit operation was restricted due to the same condition of the electrical plant that was delineated above for Unit 1.)

On December 28, 1986, the unit tripped from 77% power due to loss of level in No. 23 steam generator. The cause was a control system failure of the feedwater regulating control valve, w W h caused the valve to shut. On December 29, 1986, the unit was returned to servic )

On January 18, 1987, the unit was being taken off the line due to a main generator exciter ground fault alarm when at 3%, the unit tripped due to a high neutron flux signal which was

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returned to service on January 19, 1987.

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On March 12, 1987, the unit tripped from 96.5 power due to a main i generator loss of field. The event was caused by operatin1 the generator in an over excited conditio This was a new opera-

ting condition necessitated by the electrical pcoblems on the off-site electrical system with newly generated excitation curves and excitation metering that was not calibrated with the tolerances desired. The_ licensee reissued the curves, recali-brated the instrumentation, and restarted the unit on March 14,

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l 198 On April 7, 1987, the unit tripped from 85% due to loss of electro-hydraulic control system D.C. power. The problem was traced to a failed servo card which was replaced. The unit was ,

cooled down to repair a non-isolable valve in the reactor '

coolant system not caused by the trip. The licer.see also l identified a main generator stator water leak which was also '

repaired. The unit was returned to service on April 17, 198 !

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On June 25, 1987, the unit was removed from service to investicate the reasons for a high vibration on No. 6 turbine bearin., and an unusual noise in the vicinity of No.- 22 moisture separator rehetter (MSR). The licensee performed a visual

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inspection of low pressure turbines, piping, and MSR's with no :

identified problems. A vibration analysis contractnr was '

brought to the site, anu on June 30, 1987 the unit was restarted !

and brought to 62f! power (the point where vibration and noise ;

began to accelerate). The source of the noise was pin pointed i j and the unit was once again removed from service. A transition 1 3 piece diaphragm gasket in a low pressure turtaine had failed. It '

i was replaced and the unit was placed in service on July 13, i

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On August 6, 1987, the unit tripped from 100% power when No. 24 j steam generator experienced a high-high level. The reason for
the high level was the operator's inattention to the feedwater control system which had been placed in manual because of an

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ongoing surveillance test. The operator was counseled and retrained, and the unit was returned to service on August 7, 198 ,

. On August 7, 1987, the licensee removed the unit from service after main output transformer oil samples indicated insulation breakdown in one of three inservice transformers. During this

! plant outage, the licensee also identified a small leak on the seal weld for #5 reactor vessel head instrument (conoseal)  ;

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penetratio The transformer was replaced with an on site spare, and the conoseal leak was reotire The unit was returned to service on August 27, 198 On October 24, 1987, the licensee removed thu unit from service when it could not be determined, therigh analysis and records search, that Class 1E electrical breaker coordination existe The licensee brought the unit to Mod; 5 and performed analyses and electrical modifications to the unit. On December 17, 1987, it was certified that breaker coordination existed. The Keeney 500 KV electrical line was also returned to service in December 1987, thereby removing the need for the trip-a-unit protectio The trip-a-unit equipment was de-ac;ivated for both units, Unit 2 was restarted and remained at 100% power through the end of this report perio . Inspection Activities i

Two NRC resident inspectors were assigned during the inspection period. The total of 4288 hours0.0496 days <br />1.191 hours <br />0.00709 weeks <br />0.00163 months <br /> (3430.4 annualized) was expended utilizing resident and region based inspector During the period, NRC team inspections were conducted as follows: Balance of Plant special inspection on the feedwater and conden' te systems (Inspection Report 272/87-18,

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311/87-20). Appendix "R" Fire Protection Team (Inspection Report 311/87-29), Electric Breaker Coordination cam (Inspection Report 272/87-15,311/87-35).

Inspection Activities and tne distribution of hours are shown in Tables 1 and 2. Enforcement activities are summarized in Table This report also discusses ' Training and Qualification Effec-tiveness" and "Assurance of Quality" as separatt functional areas. Although these topics, in themselves, are assessed in the other functional areas through their use as criteria, the i two areas provide a synopsis. For example, quality assurar t 1 effectiveness has been assessed on a day-to-day basis by resident inspectors and as an 'ategral aspect of specialist inspection- Although quality work is the responsibility of every emp'ios ee, one of the management tools to measure this

effectiveness is the use of quality assurance inspections and

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, audits. Other major factors that influence quality, such as involvement of first-line supervision, safety committees, and work attitudes, r e discussed in each area.

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11 Facility Performance Analysis Summary Category Category Last Period This Period Functional Area 10/1/85-09/30/86 10/1/86-12/31/87 Trend Plant Operations 2 2 -- Chemistry and Radiological Controls 1 2 -- Maintenance 1 1 -- Surveillance 2 2 -- Emergency Preparedness 1 1 -- Security and Safeguards 1 1 -- Refueling, Outage Management 2* 1 -- Engineering Support 2* 2 --

, Licensing Activities 2 2 --

1 Training and Qualification

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i Effectiveness 2 2 --

1 Assurance of Quality 2 1 --

  • These functional areas were combined in the last SALP,

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P Unplanned Shutdowns, Plant Trips, and Forced Outages Root Functional Date & Power Level '

Description Cause A re c ___

UNIT 1 3/8/87 - 100% The unit was removed from Equipment --

service to replace No. 1 failure /

Auxiliary Power Transformer design Restart: 3/15/87 6/2/87 - 100% Unit tr'p from trip-a-unit Lightning --

protection system due to a vai4d trip sensor actuatio Restart: 6/4/87 UNIT 2 12/23/86 - 8% Unit trip on turbine trip Personnel Operations due to loss of turbin error / poor  ;

control while reducing judgement j main turbine load with the EHC in a degraded operating condition Failure to maintain turbine load below the low power setpoint

Restart: 12/24/86 l

12/28/86 - 77% Unit trip on No. 23 low Equipment --

steam generator level due failure / random to a failed shut feed regulation valv Circuit card in the feed control system faile Rastart: 12/29/86 l i

1/18/87 - 3% Reactor trip on spurious Personnel Maintenance l High Neutron flux signal error:  !

uben a technician pulled Training  !

a fuse while trouble- deficienc J shoating a roa block l signal on the intermedi-ate rance instrumen This action was inapprop- '

i riate for the existing

plant condition.

! Restart: 1/19/87

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13 Unplanned Shutdowns, Plant Trips, and Forced Outages (Cont.)

Root Functional Date & Power Level Description Cause Area ___

3/12/87 - 96% Unit trip on turbine trip Design Engineering due to main generator loss Error Support of fiel Excitation metering was insufficient

. for operation in the over excited conditio Restart: 3/14/87 4/7/87 - 85% Ur't trip on turbine trip Equipment --

due to loss of DC power failure / random to the EHC syste EHC circuit card faile Restart: 4/17/87 6/25/87 - 62% Controlled shutdown to Equipment --

investigate high vibration anomaly:

and noise associated with Cause was not the main turbine, determine Restart: 6/30/87 7/3/87 - 62% Controlled shutdown to Equipment --

l correct main turbine failure / random l vibration caused by a i gasket failure at the I low pressure turbine inlet transition piec Restart: 7/13/87 8/6/87 - 100% Unit trip on high steam Personnel Operations generator level in #24 error:

steam generator with Operator the feed system inattention to in manual contrc detail, l

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Restart: 8/7/87 i

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.  : Unplanned Shutdowns, Plant Trips, and Forced Outages (Cont.)

Root Functional Date & Power Level Description Cause Area __,

8/7/87 Controlled shutdown due to Equipment --

impending failure of a main failure / random output transformer because of insulation breakdown due to agin This outage included the identification and repair of

  1. 5 conoseal leak on the reactor head, restart: 8/27/87 10/24/87 Centrolled shutdown due to Inadequate Engineering design documentation documentation Support problems related to of design basis, electric breaker coordinatio Restart: 12/17/87 ,

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NOTE: The root cause in this Table is the opinion of the SALP Board based on the inspector (s) description of the event; and may, in certain instances, differ from the LE i l

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IV. PERFORMANCE ANALYSIS Plant Operations (32.3*4,1385 Hours) Analysis Licensee performance in this area was rated as Category 2, and improving at the end of the previous SALP period. Weaknesses in the last period included an above average number of reactor trips (18), numerous fire protection deficiencies, and a number of operator error The licensee continues to have a strong management team committed to plant betterment, and which clearly recognizes safety issues and understands NRC policies and regulation .

There is consistent evidence of prior planning and the assign-ment of priorities by the licensee when dealing with plant operation Reviews, decisions and corrective actions are clear, timely and in keeping with NRC and industry standard Often the corrective actions for identified concerns such as the RWST resin intrusion, conoseti leak and transformer problems exceed requirement Licensee management at the corporate and station levels have been conservative and responsive regarding the operation of the Units. The licensee has shutdown and cooled down the units on four occasions (listed ua pages 6-9) during this assessment period to install, repair or modify systems, and to address safety related problems. Startup following these shutdowns and refueling outages was aoproved by the licensee only after all the identified concerns were fully resolve During this assessment period the licensee has exhibited their commitment to safety and the regulatory process by their prompt and thorough followup on: strike preparations, identification and followup corrective action on a resin intrusion into the l refueling water storage tank, reactor vessel head leaks and the I service water flooding event. The professionalism of the operators in the control room has been evident in the conduct of

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operations. However, during the conduct of licensed operator examinations, isolated instances of informality of operations )

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were observed. These instinces have included operators leaning i

against control board rails, control panel indications being obscured by procedures, and operators not wearing personnel

, monitoring devices as directed by licensee policy. Operator i

performance during plant trips and abnormal operating conditions remains prompt and competent. The housekeeping at the facility has been rated above average by NRC inspectors and managemen j

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Licensee weaknesses in this functional area manifest themselves principally in the area of personnel error and inattention to detail. In of seven trips resulted from inadequate operator i attention to abnormal operating conditions. Human error was also noted in events related to isolating a component on the wrong unit for maintenance and omission of post maintenance testing on a diesel generator prior to its return to servic This inattention to the operations interface with other departments also resulted in missed surveillance tests as described in Section D of this assessment. Also, there were instances nf fire watches not posted and sleeping fire watches identified by the license These problems indicate room for improvement in shift communication, interface with other depart-trents and more consistent attention to detail in operational activitie The number of reactor trips has been reduced from 18 in the '

previous SALP period to 7 in this assessment period, which was three months longer. As a result of the licensee's trip reduction eff orts, there was only one trip on Unit 1 and the remainder were on Unit Four trips were caused by equipment breakdowns, one as a result of a lightning strike, and two trips were related to human erro The staffing of the facility remains at a full complement and staff turnover is low. During this assessment period the Vice President of Nuclear was elevated to a Senior Vice President of Nuclear (a new position) and a new Vice President of Nuclear was hired. The Engineering and Plant Betterment Department was

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reorganized to provide more responsive support to the plant

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operating staff. These changes are detailed in Section H of i this repor The stability of the staff contributes to the l consistency in irnplementation of operational program The Station Operations Review Committee (50RC) meets frequently j but not excessively. The Committee was observed to be thorough '

and complete with their reviews of safety related issues and their tracking of issues that have not been concluded. The SORC committee reviews and assesses all unit trips and shutdowns for root cause and correction prior to unit restar The Nuclear Safety Review (NSR) group which consists of onsite and offsite safety review groups i: a full time dedicated organization, consisting of managers and eight full-time engineers. This organization provided effective oversight of the routine activities specified in technical specifications and ,

applicable industry standar *1 addition, they provided l independent assessment to men % went regarding the causes of !

significant operational occurrences and the incorrect I certification of breaker coordinatio l

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In summary, the operations organization is competent, responsive and highly motivated toward safe plant operation Tie licensee has an aggressive approach to resolve problems encountered in the operation of the unit In particular, a strong management team is evident, which fosters a safety

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conscious attitude and an accountability for performanc Operator response to events has been good, and trip frequency has decreased. However, human error due to inattention to detail or ptar interface communications continues to be a contributor to plant trips and other event RC and the safety review groups continue to be effectiv . Conclusion Ra.ti n g : 2 Trend: None 3. Board Recommendation

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Licensee: None NRC: None

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l 18 Chemistry and Radiological Controls (12.1*4, 525 Hours) Analysis This area was rated Category 1 last assessment period. Licensee strengths in the last assessment were noted in a strong commit-ment to minimize personnel exposures and reduce radwaste volum ,

Program improvements were also noted with renovations to the RC/ :

access control point. This included new computerized access j controls, the installation of sensitive personnel friskers to enhance the radioactive material control program, and additional office space for the radiation protection staf Weaknesses in the quality of radiation protection procedures and the need for improvement in the chemistry laboratory QA/QC program were l identifie During this review period, there were eight routine and reactive inspections in the radiological controls area. Routine inspection reviews included organization and staffing, training and qualifications, procedures, internal and external exposure contaols, the ALARA program, radiological and non-radiological chemistry, effluent controls and monitoring, and solid l

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radioactive waste management and transportatio One reactive inspection was conducted to review the circumstances of a primary water spill, hot particle contamination, and repetitive defeating of a locked high radiation door. Principal problems '

identified during this assessment period where failure to adhere

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to procedures, failure to establish procedures, and failure to maintain positive controls over locked high radiation area Weaknesses in the radiation protection procedures, highlighted ;

1 in the two previous SALPs were not fully resolved in this assess-

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ment period, in spite of licensee commitments to complete implementation of the new procedures prior to the beginning of the 1987 refueling outages. Further, problems were again i identified both in +he radiological and non-radiological

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i chemistry laboratory QA/QC areas. These continued unresolved issues indicate a weakness in licensee implementation of effective corrective action to NRC identified weaknesse Radiation Protection During this assessment period, the radiation protection organi-zation responsibilities were expanded to include chemistry. The planned change to the organization specifically impacts the j .echnician level, in that, a technician "pool" will perform both j chemistry and health physics function This was the status of

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19 the radiation protection organization in 1980, during the HP appraisal. A significant appraisal finding was a lack of tech-

nical depth within the technician pool for health physics activities. The concept of combining HP and chemistry functions was identified as a generic industry weakness which was corrected as a result of the NRC's HP apprain:Is of 1980. The appraisal cited insufficient time and experience given to HP tasks which were necessary to appreciate and develop the technical skills necessary to perform in an effective manne The licensee's subsequent actions to correct this deficiency were separation and dedication of technicians to health physics and chemistry. The proposal of the technician "pool" suggests a

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return to an organization which has already been shown to be detrimental for effective program performance throughout the industry. The impact of the technician "pool" on program performance, and the effectiveness of the training and qualifications program to support the "pool" will be evaluated in the futur An NRC identified concern for the previous two assessment periods regarding the consolidation, quality and consistency of cadiation protection procedures was not resolved ouring this assessment period. Further, the lack of well established, clearly defined procedures resulted in two cxamples of failure to adhere to the requirements of existing procedures. There was also one example of failure to establish procedures for the calibration and use of airborne radioactivity monitors. These )

violations, along with the delay over resolving this issue !

indicates a weakness in management implementation of effective ;

corrective action !

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The external exposure control program is well defined and effectively implemented. The scheduling and execution of routine radiation surveys were thorough and well controlle Posting of radiologically controlled areas was effective, but there were repetitive instances of personnel defeating locked high radiation area doo The licensee's initial corrective actions in this case were not effective in identifying and correcting the root cause of this problem. Subsequent actions appear to have been more effectiv 'ne licensee raintains and implements a generally adequate and o

well defined internal exposure control program. Engineering I controls are effectively used to maintain airborne radioactivity I levels well below those requiting respirato.y protectio ,

However, violations were identified in the use and calibration I of air sampling equipment, proper analytical methods, documenta- l

tion and adherence to procedural requirements which relate to the str.tus of radiation protection procedures already discussed.

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i The licensee's ALARA program exhibited effecti<e performance i during the current period. Realistic annual and outage exposure '

goals were developed. A significant scope of work activities was undertaken during the Unit 1 1987 outage, including .

refueling, 10 year ISI, RTD bypass removal, steam generator '

activities, reactor coolant pump seal replacements and i pressurizer and reactor vessel instrumentation modification Pre-work ALARA planning was initiated early and ALARA reviews ,

were comprehensive and well documented. The licensee used audio :

and video equipment extensively, for monitoring work in high exposure areas, shielding, and mock-up training. Work

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evolutions and exposure tracking were closely monitored by HP technicians assigned to specif'c work package Unanticipated work activities, such as the secondary side steam generator "J" norzle replacements, conoseal head leak repair, pressurizer spray valve replacement, and CRD vent fan change-out during 1987 increased the original 1987 ALARA goal of 560 person-rem by 20* In spite of this, licensee exposure for this assessment period was 635 person rem for 1986, and about 675 person-rem for 1987. These exposure values (i.e., 2 units)

compare favorably with industry PWR annual averages (approxi-mately 400 person-rem / year / unit).

Radiological Effluent Control and Monitoring During the assessment period, one inspection was conducted in this area. The licensee is implementing an adequate program for liquid and gaseous radioactive effluent control. Radioactive effluent releases were made in accordance with procedures and technical specification requirements. Semi-annual Radioactive Effluent Release Reports were comprehensive. However, licensee ;

responsiveness to concerns identified during an NRC inspection i in this area during the previous assessment period, regarding a l programmatic upgrade in the radio-chemistry laboratory QA/QC l

, program, indicated a lack of thoroughness and management over-sigh Improvements in the interlaboratory QC program and laboratory QC procedures were not implemented from the initial commitment date of April 14, 1986 to the time of the inspection, March, 198 The licensee's commitment to upgrade the electrical power supply to the counting room has similarly been prolonge Also, the lack of management oversight was noted by the failure to resolve a licensee audit finding regarding the timeliness of radiochemistry procedure review because of the inability to escalate the audit finding to a management level sufficient for !

resolution. Within the chemistry organization, positions are I j identified and responsibilities define i l

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In the area of air cleaning systems testing, weaknesses were

' identified with respect to the thoroughness of management oversight and QA review. Tin.a spans of eleven months in one

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instance and one year in another had elapsed before final management and QA review were completed for the test results, indicating a lack of adequate attention to followup on potential problem No onsite inspections of the licensee's environmental monitoring program were conducted during this assessment period. However, routine surveillance and event repcrts were reviewed. These reviews indicated that a generally effective Radiological Environmental Monitoring Program was conducted by the license sampling frequencies, types of measurements, analytical sensi- ,

tivities and reporting schedules generally complied with technical specification requirements.

J Two LERs were submitted in this area during the assessment period. Both were related to technical specification surveillance requirements not being completed within the required time due to personnel erro Solid Radioactive Waste Management and Transportation During the assessment period, one inspection was conducted in this area. The licensee is implementing an effective program for solid radioactive waste management and trar.sportation. The licensee's organization in this area is defined in position descriptions and responubilities are clearly delineated. The staff is experienced and only minor use is made of consultants to upgrade the computer program used to classify radioactive 1 wast Licensee response to an NRC identified concern regarding '

training of all personnel with involvement in the radwaste area

was timely and thorough. Both Quality Assurance and Quality :

Control programs were thoroughly and comprehensively implemented. Procedures and check lists were well define !

Records were complete, well maintained and availabl Water Chemistry Controls Late in the assessment period, 'No inspections in the water

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chemistry controls area were conducted. Twelve out of 45 )

i i Brookhaven National Laboratory non-radiological chemistry '

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standard results comparisons were in disagreement. The disagreements were generally due to poor calibration techniques ,

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and procedures. These weaknesses are simil6* to those identi-fied in this area during the previous assess. bent period. This is an indication of a lack of attention to detail, as well as a weakness in management response to NRC identified concern In addition, some of the problems were the restili of the licensee's reliance upon contractor support personnel in the chemistry area

! rather than in-house staff expertis In the area of plant systems, the licensee has implemented a generally adequate water chemistry control program. Weaknesses in control of in-line instrumentation suggest a need for further emphasis in quality control of chemical measurements. Licensee initiated special task forces and contracted vendor audits have identified suggestions for program improvements, indicating licensee site management recognition of the need for improvement in water chemistry controls. Additional corporate support may be warranted to augment site initiatives in this area. Operating procedures ware generally conservative, resulting in few corrosion-related problems with primary and secondary water system In summary, the licensee's radiation protection program is generally acceptable. Strong performance continues to be noted in the control of personnel exposures through the implementation of an ef fective ALARA program, and in ef fluent controls, envi-ronmental monitoring, and solid radioactive waste management and transportatio In contrast, weaknesses persist regarding the quality of radiation protection procedures and in the chemistry laboratory QA/QC area. The licensee's failure to resolve these long standing NRC concerns indicates an inability to focus management attention to affect timely ccrrective actio . Conclusion Rating: 2 Trend: None 3. Board Recommendation Licensee: Provide and complete a schedule of radiation protection program procedure upgrade . Re-evaluate tne dual assignment of HP and chemistry technicians in light of HP appraisal findings in this are ,

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23 Improve radiological and nonradiological laboratory QA/QC and followup NRC and licensee audit identified weaknesses in these area ;

NRC: None a

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C. Maintenance (9.7%, 421 Hours) Analysis The last SALP assessment rated this area a Category 1 and i highlighted the new work order control system that had been incorporated into a computer system called the Managed Maintenance Information System (MMIS).

During this assessment period, the resident inspectors observed maintenance routinely. Two region-based inspections reviewed the maintenance, modification and retest programs. No viola-tions or concerns were identifie The planning for the maintenance department (mechanical, elec-trical and I&C) is performed by the planning department who also controls the MMIS. After the planning department determines when the work orders will be accomplished, a complete package including parts, procedures and tag out is turned over to the maintenance department for performance of the maintenance. The planning _ department, upon completion of the work, then returns tne system or systems to operational status. This system tends to eliminate duplication of work orders and gives more coordi-nation between departments when performing work on specific system The maintenance department routinely performs the maintenance in a timely, effective manner. Isolated problems have be3n iden-tified such as, troubleshooting of the EHC system and nuclear instrumentation system causing two reactor trips, recurrent packing leakage on feedwater isolation valves, and failure to perform /M's on warehouse stored rotating machinery. The licensee's actions in response to these issues were prompt and effectiv Non-safety related transformer problems were reviewed by region based inspectors during this assessment period. Preventive '

meosures instituted by the licensee include obtaining equipment for monitorir j and tracking transformer oil status. This action is aimed at preventing future occurrences, such as the failure ,

of a Generator Main Transformer at Hope Creek in 198 The '

licensee has taken positive steps in designing a continuous monitoring system that will provide a readily available status

of transformer parameter The implementation of these systems will allow the licensee to predict the optimum time for i preventive maintenance of the Station and Main Generator Transformers, and will aid in identifjing further tetions n?cessary to prevent future transformer failures.

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The licensee catalogs maintenance work requests into categories depending on parts availability, engineering ir.put, plant conditions, "in planning stage", and "scheduled to be worked".

The ratio of the number of work orders ready to work in conjunction with the plant conditions in which the work may be performed is manageable (about an eight day back log). Technical Specifications and "necessary for plant operation" work orders are usually performed within twenty four hour The maintenance department works closely with the systems engineers in identifying and correcting equipment deficiencies to return a unit to service, and installing minor design changes. Management encourages problem identification from any sourc The ioentification of calibration deficiencies for lead-lag controllers by training and vendor personnel, and the prompt corrective measures exemplify licenste performance in this are One inspection reviewed the inservice inspection, water chemistry controls, and radiological records for steam generator No. 13. Water chemistry has been well controlled throughout the life of the plant in order to provide extended life for the steam generator The effectiveness of these controls is evidenced by the extremely small number of tubes that have required plugging or repair. Steam generator 13 has only 16 tubes that have been plugged. Of tFese 16, 10 were plugged prior to service as a precaution against erosion. The licensee's prenntive actions have resulted in a high level of effectiveness in the area of steam generator maintenanc The licensee's continued application of a live loaded valve nacking program (which is now in effect on most of the valves w thin both units) is beginning to show positive results on ALARA and plant shutdown There are fewer primary and

secondary valve leaks, and less contaminated leakage in the sumps. The smaller time necessary to repack highly radioactive valves is helping keep radiation doses ALAR The licensee selected a manager, maintenance engineer and a staff engineer, and assigned them to a full time preventive maintenance project for six months. The team utilized working groups ranging from 6 to 12 people frcm Vice Presidents down to engineers to develop a program that will ultimately establish a reliability centered maintenance program for Artificial Islan The program will include predictive maintenance, enhanced preventative maintenance and a more structured root cause analysis feed back into the maintenance program. The program pilot system is scheduled '.o go into effect in 1988 with full scale development in 1989.

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During outages, maintenance related tasks were performed professionally and on time.. The maintenance department utilized contract personnel to enhance and expand the maintenance force in order to complete the larger outage workloa Also, the licensee is currently utilizing individuals from the QC department in the day to day work assignments ir, the maintenance area. The licensee hopes to make the individual worker and their peers responsible for QC of all work performed The on loan QC personnel is the beginning of the program to meet this goa In summary, the maintenance department management is aggressive and proactive. There is a consistent and structured approach to maintenance, utilizing well written procedures and technical manuals. The department resolves identified problems in a timely manner. The maintenance department is adequately staffed and competently traine . Conclusion Rating: 1 Trend: None 3. Board Recommendation Licensee: None NRC: None

0. Surveillance (11.1%, 479 Hours) Analysis

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During the last assessment period, surveillance was rated a

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Category 2. There were several missed or late surveillances

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which were caused by personnel error and lack of attention to

detai During this assessment period, a Containment Integrated Leak Rate Test (CILRT) for each Unit was witnessed by NRC specialist The resident inspectors reviewed routine serveillance activities regularl The test procedure and conduct of the CILRTs were consistent with the requirements specified in the technical specifications and station administrative procedures. The staff assigned to the performance of the tests were experienced in the evolution, utilized technically adequate procedures, and were supported by management. Implementation of the procedures was error free, as a result of step-by-step rehearsals prior to each major activit QA/QC involvement in these activities was thorough, and included surveillance tours, and the perfonnance of surveillances and audits by QC personnel that evidenced a high degree of knnwledge in the test '

During the assessment period, the post modification test program was reviewed noting that test procedures were properly approved, and technically adequate. Post modification testing was i observed to be conducted in an orderly fashion by knowledgeable !

personne One inspection was directed toward the Cycle 4 Startup Physics i Testing Program for Unit 2. This review indicated that the testing program has been implemented in an adequate manner. All ;

surveillance tests and I&C Work Orders that supported the cycle 4 startup were noted to be adequately preplanned and w"re properly executed. Management involvement in the program was evidenced by the high quality of the Refueling Test Sequence Procedure. In addition, test results were noted to have been adequately evaluated and documente At Salem surveillances are tracked by computer. The system j

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tracks about 2500 safety related surveillance tests per year, as i l well as all non safety related surveillances. The program is I sound and a written schedule is produced on a daily basis. Some i scheduling problems were identified because of the difference in I scheduling surveillances during plant shutdowns and outages, l l

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During these periods, the scheduling is manually accomplished by ,

schedulers. The licensee has recognized this problem and is developing a program to account for schedular differences during Unit shutdowns.

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During this assessment period, there were ar. increased number of -

personnel errors related to missed or late surveillance Specific examples are: shift supervisors not issuing the surveillance packages to be performed, correct surveillance performed but on the wrong unit, engineering not providing valve numbers for expanded ASME Section XI valve tests, omission of tests on the fuel handling crane, and performance of an inadequate post test procedure. Although the number of these events (missed or late surveillances) is small in relation to the total !

number of tests performed yearly, these occurrences have increased during this assessment period. This indicates that corrective measures for previous missed or late surveillances have not been effective and more licensee oversight and attention to detail in the implementation of surveillances is warrante ,

The licensee's calibration program for gages and instrumentation was not consistently implemented to assure the accuracy of instruments used for plant operation. Technical specification ,

required instrumentation was calibrated and recorded during each I

surveillance by procedure. However, in the balance of plant '

(BOP) there were calibration stickers on some gages and instru-ments and not on others. The inconsistency was confusing to !

operators and supervisors as to the validity of readings taken from unlabeled gages, and to management and auditors measuring the effectiveness of the calibration program. Toward the end of

I this assessment period, the licensee had corrected the method for :

identifying calibrated gages and instrumentation. Technical L specification instruments remain as described above, instruments used to operate the B0P are now divided into information only instruments and instruments necessary for operation. The instruments necessary for operation are now calibrated on a '

three or five year cycle depending on their applicatio , Operators were updated to the new method of calibration being

performe In summary, no major discrepancies were identified in the sur-

, veillance area, and there appears to be a sound surveillance

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program in place. However, implementation problems related to i the applicability and support of the surveillance programs ;

} are the most frequently identified problems at Sale These ;

discrepancies identified both by the NRC and the licensee i indicate the need for better attention to detail.

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2. Conclu', ton Rating: 2 Trend: None 3. Board Recommendation Licensee: None NRC: None i

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E. Emergency Preparedness (1.1*., 47 Hours) Analysis There is a consolidated Emergency Plan for the Artificial Island complex, including the Salem and Hope Creek facilities. Conse-quently, the assessment of emergency preparedness is a combined evaluation of both facilities' emergency response capabilitie During the previous assessment period, the licensee was rated Category 1 in the area of Emergency Preparedness at Hope Creek and Sale This assessment was based on strong management commitment to the hardware and programmatic requirements of this functional area, and the performance of the licensee's staff during exercises at both Salem and Hope Cree During this assessment period, there were three announced inspections of Emergency Preparedness at Artificial Islan One inspection was the observation of a Hope Creek full participa-tion exercise. There was no exercise at Salem. In addition, four actual unusual events were deciared at Hope Creek and one at Sale Implementing procedures were correctly followed for '

all but one of the unusual events. On July 30, 1987, Hope Creek made a one hour notification to the NRC per 50.72(b) instead of declaring an unusual event. .The licensee detected the error within sixteen minutes and then declared the unusual event. The Hope Creek Event Classification Guide has been modified to avoid i a recurrence of this mitelassificatio '

Observations mada during the routine safety inspections at Hope Creek and Salem indicate regulatory requirements were fully satisfied. A drill testing various aspects of the program is ;

conducted at both Shlem and Hope Creek on a weekly basis. The high degree of training and experience is reflected in the ;

excellent performance noted during their annual exercis Emergency response training is current; 1,450 personnel are i qualified for one or more emergency response positions - 600 for i

each site and 250 for both sites. Operators received eight hours of emergency preparedness training including response to one l fast breaking scenario "run" on the Hope Creek simulator. Health Physicists demonstrated the ability to correctly use the four l available dose projection systems. A dosimetry comparison was made involving three of the licensee's systems, systems for both States and the NRC. The results were within acceptable limits.

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satisf actory result Independent audits are curren '

Executives and senior managers interface with State government officials. Safety parameter display systems (SPDS) are in place I i and functional at Hope Creek and Salem, a Post Implementation

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Appraisal for Salem has been conducted. No significant deficiencies have been identified to dat PSELG has put considerable effort into working with off-site authorities to complete final review and approval of off-site plans. Results of the annual public Alert and Notification system (sirens, etc.) test specified by FEMA were submitted during December 1986. FEMA has not complated the review. The Delaware Emergency Plan was given contingent, favorable reviews and comments per 44 CFR 350.12, pending acceptance by FEMA of the siren test data. New Jersey has submitted its plan for similar review. Tie licensee has developed a computerized data ,

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base for special needs residents (hearing and mobility impaired)

living within the ten mile Emergency Planning Zon Additional licensee strengths in this area are noted as follows:

(1) Contracts are in place to provide for plume aerial surveillance; (2) ten diverse, redundant communications systems are in place; and (3) a full-time, 37 person site fire department is available for emergency support, with half of them d

qualified as Emergency Medical Technicians. The staff is divided into shif ts and work around-the-cloc .

In summary, a strong management commitment to emergency

preparedness is evident by the hardware and comprehensive training program achievements in this area, and by licensee J

cooperation ith outside agencies toward approval of State

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Emergency Pians. Licensee effectiveness is demonstrated by the consistent hign quality performance of the staff during emergency exercise l j Conclusion Rating: 1 Trend: None i Board Recommendations Licensee: None

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NRC: None i

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32 Security and Safeguards (4.3*s, 187 Hours) Analysis There is a consolidated Security Plan for the Artificial Island i complex, including the Salem and Hope Creek facilities. Conse-quently, the assessment of security and safeguards is a combined evaluation of both facilities' protection capabilitie During the previous assessment periods, both the Salem and Hope Creek security programs were assessed as Category 1. These ratings were influenced by a well planned transition for the integration of the two security programs; a major upgrade of security systems to include the installation of an integratej security computer system and associated hardware, computert.ed access control devices, state-of-the-art assessment aids and new search equipment; and a strong security management staf Management's attention to, and involvement in, assuring the implementation of an effective and quality security program '

remained evident during this assessment period. The l'censee

was very effective in maintaining good support for the security

program from other functional groups at both stations. Frequent organizational interfaces and good working relationships were apparent from the professional attitude of all employess toward

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the security program, as well as the attention given by the maintenance groups to prevention and correction of problems with security systems and equipment.

3 As further evidence sf management's interest in an effective and <

i quality program, it was noted that all security shift l supervisors, who provide around-the-clock oversight of the contract security force, attended a special 30-day training  :

course on regulatory and security program requirements and objective In addition, security management continued to participate in nuclear industry groups engaged in security related matters.

J The licensee also continued to implement a self-initiated appraisal program carried out by security management and supervisory perscnnel . Adverse findings were promptly resolved ,

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and factored into the training and qualification program in an  !

effort to prevent their recurrenc The appraisal program is in addition to the NRC's required annual program audit that is conducted by experienced quality assurance personnel. The last

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l annual audit was comprehensive in both scope and depth. Audit l

findings were distributed to appropriate management personnel  !
for review, and corrective actions for deficiencies were prompt ,

d and effective. This also demonstrates the licensee's desire to 1 implement an effective and quality security program.

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c During this assansment period, the licens'e engaged a new contractor to provide the administration, supervision, and

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training of the security force. The new contractor was able to ;

t retain most of the incumbent members of the force. The change in contractors went smoothly as a result of good planning on the j part of the license Staffing of the security organization appears adequate, as ,

evidenced by a controlled use of overtime. The installation and i maintenance of state-of-the-art systems and equipment has !

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significantly reduced the use of compensatory posts for systems and equipment failures and, thus, reduced the need for extensive .

overtime. Both the licensee's proprietary supervisors and the i contractor's supervisors are well trained and experienced, and ,

exhibit a conservative and positive attitude toward securit Security force personnel are also well-trained and exhibit high morale and professionalism in carrying out their duties. The

licensee's efforts to establish and maintain such a professional

{ imageforthesecurityforceisanotherindicatorofthelicen- !

see s desire to implement an effective and quality security progra It is also reflected by the generally excellent state of cleanliness in all security facilitie !

The training and requalification program is well developed and !

carried out by a training administrator and two full-time instructors. In addition to initial and requalification train- '

, ing, on-the-job performance evaluations are conducted which test '

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the proficiency of individuals on general and specific security '

program requirements. The on-the-job performance evaluations !

have provided management the ability to review and enhance the performance and job knowledge of security personnel and to I

, correct deficiencies as they are detecte This is another '

initiative that is indicative of the licensee's desire to

] implement an effective progra '

i During the assessment period, there were two events involving

, security guards who were discovered being unattentive to duties.

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One (at Hope Creek) was discovered by the NRC Resident Inspector

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and the licensee was cited for the violation. The other (at Salem) security guard was discovered by the on duty security i shift supervisor, j In each case, the licensee took prompt and effective corrective !

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action. The associated security event reports submitted by the

licensee pursuant to 10 CFR 73.71c were conplete and well I

written, and required no further information from the licensee.

l' These events appear to be isolated cases of poor performance and do not indicate a programmatic problem. They occurred during j the latter part of the assessment period and until that time, i

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the licensee's overall good enforcement record during this period is attributed to management's involvement in the security program, the continuing self-appraisal program, comprehensive annual audits and the security training progra During this assessment period, the licensee submitted three

"temporary changes" to the Plans. These changes included compensatory measures to be implemented during construction of a building addition inside the protected area and during the special supervisory training program. The changes were clear and fully described the issue Prior to submittal of these changes, the licensee discussed them with Region I safeguards personnel at a licensee-requested meeting on site and at the Region I office. The licensee also provided its response to the August 4, 1986 Miscellaneous Amendments to 10 CFR 73.55 codificd by the NRC, and submitted the consolidations of the Salem and Hope Creek Security Plans, Safeguards Contingency Plans, and Training and Qualification Plans into the Artificial Island Security Plan, Safeguards Contingency Plan, and Training and Qualification Plan. The Artificial Island Plans were generally o' high quality; however, several discrepancies were identified '

during the NRC revie A management meeting was held with the i licensee during which the licansee was able to fully explain  !

each discrepancy and provide acceptable resolutions. The j licensee subsequently submitted amendments to the plans that resolved the discrepancies. Considering the magnitude of the effort involved in consolidating the Salem and Hope Creek plans into one, the discrepancies were considered by the NRC to be minor oversights that did not materially effect the quality of the Artificial Island Plans. The safeguards licensing group is adequately staffed with experienced personnel who are knowledge-able of NRC security program objectives and committed to main-taining an effective and high quality security progra Management involvement, advance planning, and the expenditure of necessary capital and personnel resources was noteworthy and indicative of l high level management suppor In summary, the licensee continued to implement a highly I effective and quality security program for Artificial Islan {

Management interest in the program remained evident through its continued support and attention to program needs.

2. Conclusion Rating: 1 Trend: None

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_NRC : None ,

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G. Refueling, Outage Management (7.6 , 322 Hours) Analysis The last SALP rated outages and engineering support as Category With regard to outages, the assessment addressed generally

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I effective outage planning, oversight and implementation. The newly organized planning department was highlighted as an unproven refueling cutage initiativ During this assessment period there were two refueling outages and four plant shutdowns as discussed in Section III.B of this repor Within the planning department there are groups of personnel dedicated to outage planning as well as daily operational maintenance planning. The outage planners dedicated to either Unit 1 or 2 (2 groups) maintain a living schedule, which is computerized. When outages are forthcoming, litcle notice is required to have a comprehensive schedule ready for work to be performed. The management within this organization is aggressive in the planning of outages and the work planned is generally completed on time. The four outages, one on Unit 1 ar.d three on !

Unit 2 were performed on schedule and the Units were returned to service within a day of the scheduled time, with all planned work and in some cases additional work being performe )

Management has not hesitated in removing the Units from service l and cooling them down, if necessary, in order to facilitate repairs in the interest of personnel and nuclear safet Refwling outages are also preplanned. Design changes for the outage are identified far enough in advance that the design packages are delivered to prospective contractors for fixed price bidding in advance of the start of the outage. Management meetings, held three times daily during outages, address the issues and problem areas squarely, and determine responsible management to resolve the issues in a timely fashion. No instances were identified any area where safety was compromised for timely completion of a job or projec When the refueling outages have been prolonged, the reasons were usually unplanned factors that were identified as the outage progressed. When confronted with a contingency, the scheduling department was aggressive in factoring the newly identified work into the schedule. Examples of this are: (1) Identification, during routine steam generator inspections, that the "J" tube feed nozzles were degraded to an unacceptable level. The result was replacement of all "J" tubes in all steam generators;

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37 (2) flooding of the service water bay; (3) identification of cracks in the spare control rod drive mechanism penetrations; and (4) identification of degradation in the welds of the service water system inside containment, which resulted in all

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service water piping welds within the containment being examined and the necessary repairs being performe The planning department expanded their department to include an operations group that reviews, schedules and performs tag outs of equipment. This evolution is performed in the annex just outside of the control room. The group keeps the operations department informed of the work to be performed that day, either during an outage or when the unit is operating, by direct involvement with the operating shift. This arrangement reduces the traffic in the control room, thus minimizir.g disruptions in control room activitie In summary, management and the planning department are aggres-sive in preplanning outages. During outages, they are equally aggressive in seeing that work is performed satisfactorily, on schedule and without impacting personnel safety or nuclear safet . Conclusion Rating: 1 Trend: None 3. Board Recommendation Licensee: None 1 NRC: None

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H. Engineering Support (22.0*., 922 Hours) Analysis ihe last SALP assessment rated the combined outages and engi-neering support area as Category 2. fhat assessment discussed the organizational weaknesses within the Engineering Department, -

as well as specific areas (10 CFR 50.59 reviews and environmen-tal qualification) where engineering support had been weak. The last SALP also described new licensee initiatives planned to address these weaknesse The onsite system engineering group is directly involved in the  !

day to day operation of the facility and are engineers that have complete cognizance of a particular assigned system or system ,

Whenever there is an identified concern within the facility, the

! engineer assigned to the faulted system is alerte These j engineers are extremely knowledgeable of their assigned systems and have demonstrated this through clear identification of root i causes for; 1) Unit trips, 2) chemistry anomalies, especially l oxygen in the condensate system, and 3) system malfunction When design changes are instituted such as, the installation of new undervoltage relays which involved a technical specification change and the upgrading of procedures, the system engineer conducted training sessions for operators and I&C technicians to explain the changes. The engineers have also provided safety analyses and engineering evaluations for plant malfunctions such as, the resin that was found in the refueling water storage tank, and the reactor head penetration leak on Unit These evaluations were concise, thorough and technically sound.

"!

The nuclear fuel engineering support provided for plant oper-ations is timely, technically sound, and includes independent verifications for the assurance of qualit Procedures are technically adequate, and management support is evident by the l quality of personnel and the level of staffing. Another '

positive indicator in this area is the willingness of management to provide technical assistance for audits of fuel vendors.

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. The systems engineers and their management have provided assessments and information for NRC regulatory issues. These responses have been timely, thorough and have provided

information in excess of what was requested. The inspectors

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were able to assess and close out regulatory issues with confidence that the safety issues were thoroughly addresse I I

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One incident occurred, whore a steam generator (SG) was not fully drained which caused a reactor coolant spill when the SG was opened. The cause was attributed to changes made with regard to the operation of the Residual Heat Removal (RHR) System during a drained condition. To protect the RHR pump from vortexing, a higher minimum reactor vessel level was specified. However, engineers failed to recognize that the new high level specifi-cation would not allow the reactor coolant system loops to fully drain. Following the spill, the licensee's actions to correct the ancmaly were prompt and effectiv In previous SALPs the off-site engineering department has been identified as having weaknesses in design review interfaces, procedural development and the adequacy of the technical review process. Tnese weaknesses continued to be identified, but to a lesser extent during this assessment period. The implementation of site-based system engineers has improved the responsiveness to operational concerns, but interface problems with the offsite design organizations are still eviden Other NRC findings in this area were largely the result of the previous practices and do not necessarily reflect the current organization. Never-3 theless, for illustration these types of findings are discussed E in the next two paragraph Review of the approach and criteria for design and evaluation of pioing and surnort systems revealed several technical con-siderations which were either ignored or poorly addressed in the governing design documents. This conclusion is further supported b, the lad " " ntatiar, ;f pipin; ;te;;; ;r,el,se;. Tl.;

identification of an error in a contractor's technical report for U-bolt piping anchor assemblies and several concerns rclated to ISI of these anchor assemblies supports the conclusion of technical inadequacies in the mechanical engineering organizatio Though the licensee agreed to address these concerns, it was apparent that past reviews and approvals of documents and pro-cedures in these areas were lacking in depth and technical adequac Weaknesses in management's effectiveness were also noted in the 4 review of design interfaces during the process of design modification. Though the topic of interface between various engineering disciplines was included in the procedures for design modification, this guidance was vague and ineffectiv Two modifications initiated by the mechanical group, and involving the addition of load attachments to a building structure were completed without the interface or knowledge of the Civil / Structural discipline. These findings led to several problems and indicated that a programmatic weakness existed

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in the design interface area. The engineering department also failed to provide valve number changes for Section XI code modifications resulting in a missed surveillanc Significant deficiencies were identified by NRC and the licensee in the implementation of Appendix R fire protection requirements

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at Unit These problems include lack of separation and protection for redundant systems needed for safe shutdown of the plant, and inadequate breaker coordination for associated electrical circuit Potential violations are pending in these matter The importance of these fire protection issues is i emphasized because similar problems were identified at Unit 1 in 198 The licensee hired a consultant to review the fire protection program well after the date when compliance was required. Some of the deficiencies were identified by the licensee and reported to NRC prior to our inspection. Other problems such as the breaker coordination issue had not been focused on by licensee management. Compensatory measures were implemented by the licensee upon identification of individual problems. The tardiness of licensee verification of satisfactory fire protectior. measures and the unfamiliarity of licensee personnel with the requirements in this area indicated a lack of canagement emphasis and attention in the fire protection are Following NRC review of this area, the licensee reviewed the -

details of the identified problem areas. In most cases, accept- i

'

, able compensatory measures were identified to justify continued

'

i operation of the facilities until modifications could be implemente l However, uncertainties regarding electric breaker coordination .

rmited h. Um w l u. a r, a tJu n of Unit 2 pending verificati:n l of as-built and design parameters, and modifications to several ,

breaker cocedination relay These actions were completed on both units and verified by NRC prior to plant restar In a letter to the NRC, the licensee made an incorrect statement l regarding the existence of electric breaker coordinatio The

, NRC and the licensee performed special investigations which identified informality in communication between staff and management personnel, inadequate measures for deficiency reporting within the engineering organization, and inadequate

management of commitment tracking as causes for the mis-statement. This is another example of inadequate interface and communications between organizations and department Licensee management is presently implementing corrective actions for these concerns.

'

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!

l 41 During this assessment period a wrong assumption led to a delay '

in placing the fuel back into the vessel af ter the thermo-couple guide tube modification had been performed. The engi- .

j neering department took advantage of a shutdown on Unit 2 to take measurements for the modification and assumed that the

~

measurements on Unit I were the same. The result was some of the guide tubes were too long to allow the fuel to rest firmly ,

on the core support plate. The licensee performed an ,

investigation into the reason for the interference and identified the proble The licensee has taken corrective j measures to prevent recurrenc At the end of this SALP period, the licensee implemented further

, reorganization within the Engineering and Plant Betterment Department to institutionalize - project matrix organization ,

which successfully handled service water, and electrical system

'

problem recovery projects. The new matrix organization also ,

managed the Design Modification Packages (DCPs) for Units 1 and I

2 for the "Second Level of Undervoltage Protection for the Vital

'

Bus" system which were well , define The engineering study and calculations that established these modifications were complex, and required extensive calculations from the system to the component level. During the review of the DCPs, it was riear that Quality Control played an important role in verifying that

installation and test results reflected the requirements in the !

l DCP A review of engineering documentation indicated that the *

1 reports were detailed, and considered parameters such as cable ,

i and transformer losses that were not part of the original stud '

j All ure:t ;f O . p:; ram were well controlled and documente ,

i A review of as-built drawings verified that the drawings j

reflected the present confiouration of the plant undervoltage installation. An additional inspection found modification I

packages for the Unit 1 outage to be accurate, well organized

, and complete, with QA/QC involvement characterized by appropri-ate hold points and well defined acceptance criteri In September of 19S7, the NRC became aware of a potential problem with breaker coordination at the Salem Unit In '

I October of 1987, the licensee determined that the degree of breaker coordination fe- the electrical distribution system affecting safety relates equipment was not sufficiently

, established and documented to warrant continued operation of i

Unit 2. Site management subsequently shut down Unit Results of the NRC review of the breaker coordination issue indicated that the cause of the problem was primarily the {

inadequate maintenance of design basis documents for the unit '

3 The licensee's corrective actions were sufficiently i comprehensive to address the proble In particular, the

1

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4

. _ _

licensee's review included not only safety related circuit breakers, but also the potential impact of breaker coordination for non-safety related circuit The licensee's technical reviews were generally thorough and based on sound technical judgemen In addition, site staff's responses to NRC questions resulted in a satisfactory resolution for each of the problems identified. The licensee has also initiated efforts to improve the quality and retrieval capability for design basis document In conclusion, NRC inspections identified management support and overall quality in the engineering and technical support area NRC review of site events and breaker coordination problems indicate that site management responded in a thorough and effective manner. Continued deficiencies in the fire protection

! program indicate thtt further attention to this area is warranted.

Long standing dasign basis problems and interface issues with

<

operations and the off-site engineering organization are being addressed by ongoing long term corrective action program The t effectiveness of these initiative: will be assessed by future

'

NRC review, i

' Conclusion l Rating: 2 Trend: None Board Recommendation

, Licensee: None

. tRC:

j None ,

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-_ - _

.-.

I. Licensing Activities Analysis '

During the previous SALP period, the licensee was rated as Category 2 with a consistent trend in this functional area. The ,

previous SALP report noted good management overview in the area as evidenced by. timely submittals, when changes to the technical specifications were needed to coalesce with the units' operation The previous SALP also noted certain weaknesses in the quality of the technical justifications for licensing actions that were

, submitte At the beginning of the current SALP period, the licensing backlog for Salem, Units 1 and 2 were 44 and 45, respectivel These items represented a mixture of licensee and NRC staff initiatives. During the SALP period, 16 licensing items were completed for Unit 1 and 13 for Unit Nine new items were added for Unit 1 and 10 for Unit 2. This lef t a backlog of 37 items for Unit 1 and 42 items for Unit 2 at the end of the SALP perio The licensee's activities in this functional area are conducted

, by a well trained group, generally efficient in operation. The

'

licensing group exhibited a high degree of cooperation with the NR The good communications between the licensing group and the NRC has been helpful in processing licensing action The licensee continues to be active in industry groups, most notably the Westinghouse Owners Grou With regard to NRC initiatives, the licensee's responses to NRC's requests for additional information have generally been

,

~

responsive and technically accurate, though sometimes not timely with respect to the need for completing the review. During the current SALP period, the NRC initiated its Safety Issues Management System to improve its tracking of implementation j sc5edules associated with safety issues. The licensee was

'

responsive to this initiative and provided updated information i on two occasions, the most recent in September, 198 D; ring the current SALP period, the licensee's effectiveness relating to licensing activities appeared to decline. Weak-

'

nesses were noted in schedular planning which resulted in late licensee submittals and responses. As an example, in mid-May the licensee submitted a proposed change requesting replacement ,

of the existing KTD by pass system with a newly designed syste i I

,

The request should have been submitted in February or March 198 l Very early discussion between the licensee and the NRC had

I l

- - - - - - _ - _ - - _ _ - - - - - - -

made the licensee aware that NRC review would be lengthy (6 months) because of the complexity of the issue. The licensee intended to implement the modification on Unit I during the next refueling outage scheduled late in September 1987. As a result of the late submittal, an expedited NRC review was necessary in order for the amendment to be issued in November, barely in time to permit implementation of the new design on Unit Other examples of submittals which were not tendered in a timely manner included the second 10 year interval ISI program and corrected analyses in support of Appendix R exemptions. Increased licensee emphasis on planning and completing license action mile-stones appears to be needed to improve performance in this are Other than the shortcomings with the timeliness of some submittals, the licensee maintains good technical capability to resolve the problem areas which arise during the NRC review proces In addition, the licensee utilizes the services of other outside nuclear support groups who may be required to assist in problem resolution or to utilize new and proven techniques to enhance the operation and safety of the plan In summary, the licensee continues to provide excellent cooperation with the NRC and maintains a knowledgeable licensing staf License cnange requests are prioritized so that license amendments may be processed and issued on dates that coalesce with the olants' operational schedule This process has been generally successful; the exceptions usually resulted from a lack cf effective planning. Licensee submittals during the SALP pericd exhibited improved technical justification . Conclusion Rating: 2 Trend: None Board Recommendation

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Licensee: None NRC: None l

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45 Training and Qualification Effectiveness

, Analysis This area was rated Category 2 in the last SALP assessment, A strong commitment to training was noted with weaknesses

"

identified in the success of initial license candidates; and, a

inadequate training leading to several reactor trip During this assessment period, management involvement and control in assuring a high quality of training continued, as evidenced by improvements in the Nuclear Training Department laboratories such as, the addition of Nuclear Instrumentation

, and rod control unit facilities to be used for maintenance training; and offering six month System Engineer's training

~

courses to QA personne A common weakness which was noted in many functional areas involves attention to cetail by 'icensee employees. The increasing proportion of personnel errors is indicative of a need to improve awareness and performance in this are In addition, one plant trip was related to inadequate technician 4 training. Overall, however, the satisfactory completion of the '

majority of activities conducted onsite reflects positively on the quality of the INP0 accredited training programs. In particular, the strong licensee performance in the maintenance, ,

J emergency planning and security areas was due, in part, to the l training and qualification effectiveness in these area The QA/QC involvement with the non-licensed training program is characterized by thorough and comprehensive audits. These audits routinely address the qualifications and training of non-licensed personnel and timely corrective actions for those activities which are not adequat Three operator licensing examinations were administered during the reporting period. One reactor operator candidate and eight senior reactor operator candidates were examined; seven of these candidates received their license. During the simulator portion of initial licensing examinations, it was observed that the operators were generally familiar with their responsibilities; and with the required actions during emergencies, both indivi-dually and as a team. The operator candidates also demonstrated a familiarity with the use of E0Ps, specifically in the application

, of prerequisites, precautions, initial conditiuns and transitions.

, The Fe;ruary 1987 examination resulted in a concern directed toward the level of training received by operators regarding the 3 differences between the Unit 1 and Unit 2 Technical Specifications (T.S.). Insufficient understanding of these differences led to an unsatisfactory rating for an individual being examined for Unit The lack of understanding by this candidate and other operators in the control room indicates that l _ __ . _ _ _ -

other licensed personnel may need additional training on the unique requirements of the Unit 2 Technical Specification The NRC administered requalification written and operating examinations to se/en senior reactor cperators (SR0s) and five reactor operators (R0s) in June 1987. Two SR0s and three R0s passed all portions of the examinations. The requalification program evaluation resulted in an unsatisfactory rating for the program. This determination was based on the low pass rate of operators being administered the exams. Some of the areas of weakness identified during the review consisted Of: operator informality during the simulator scenarios which was demonstrated in several ways, among them, lack of supervision during certain safety significant evolutions including bistable tripping; and the performance of a procedure out of sequenc In addition, several operators demonstrated a lack of knowledge of radiation monitoring equipment, and an inability to operate the Unit 2 Radiation Monitoring System compute In response to the unsatisfactory rating of the requalification program, site management organi:ed an Examination Review Team to determine the root cause of the examination failures. Short and long term corrective actions were devised by the licensee, and included in part: remedial training and reexamination, Operations Directive revisions that standardize the use of procedures, an increased emphasis on the understanding of the bases for procedural steps, incorporation into the requalification program of specific topics that require further training, and increased management attention toward simulator training and control room conduc Overall, training programs are characterized by a strong commit-ment and responsiveness to the needs of site personnel. Security, maintenance and emergency training were noted as particularly effective. However, some general weaknesses were identified in the effectiveness of training prog' rams as indicated by the licensee operator requalification program results; operator informality; and the overall training program effectiveness in reducing the frequency of personnel error . Conclusion Rating: 2 Trend: None 3. Board Recommendation ,

I Licensee: None i

NRC: None

.

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K. Assurance of Quality Analysis Assurance of Quality is a summary assessment of management oversight and effectiveness in implementation of the quality assurance program, and administrative controls affecting qualit Activities affecting the assurance of quality as they apply specifically to a functional area are addressed under each of the separate functional area Consequently, this functional 4 area is not an assessment of the quality assurance department alone, but is an overall evaluation of the effectiveness of l management's initiatives, programs, and policies which affect or

assure qualit Corporate and station managers remain visible and actively involved in station activities commensurate with their level of responsibilit Station management meets daily to discuss the problem areas within the plant. These meetings are also attended by corporate managers on occasion. Operational direction and day to day operational activities are the outcome of these meetings. Corporate and station management make plant walkthroughs frequently and are sensitive to plant cleanliness and safety. Management is sensitive to safety issues, and NRC and INPO identified concern
The licensee stresses doing jobs correctly the first time and first line supervisors are frequently found at the job site. To emphasize and asses; U.e wplo.ei.Louvn of this philosophj the licensee uses the following: Danners, signs, and slogans are i displayed throughout the plant that address management's approach to Assurance of Quality. These signs are updated frequently with different QA/QC type messages. Quality control ;

personnel have been assigned to the maintenance department to 1'

oversee quality assurance on a day to day basis. These assigned individuals are independent of maintenance, however they do I assessments and evaluations to improve or enhance maintenance i activitie The Employee Involvement Pregram (EIP) instituted

,

last year is still in full force at the station. This is a program that facilitates management / worker interfaces and rewards

.

' good performance. There is also a Quality Awareness Committee comprised of nuclear department volunteers who periodically issue a "Quality Gram" to promote improvements in quality performance, and finally a Quality Concerns Reporting Program that enables plant personnel to confidentially express quality i concerns to be investigated by licensee QA personnel. The above i programs are generally ef fective, however, t.he large proportion l l,

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48  ;

<

of personnel error related events identified by the licensee points to weakness in the attention to detail at the worker and first line supervisory level ; There were two region based inspections performed within the

'

QA/QC organization. Warehouse storage conditions, records of item locations, and original equipment manufacturer (OEM) ,

storage requirements were observed to be adequate. The identification by NRC personnel of incomplete preventive maintenance for various motors in storage focused additional licensee attention toward the preventive maintenance of these items. The licensee acknowledged this problem, and has established a Site Service Group to develop a program to streamline the processing of documents necessary for the performance of preventive maintenance activities for stored component The Nuclear QA Audit Group is well organized and manage The

,

licensee utilizes the Offsite Safety Review Committee and consultants as a team spproach to review the site audit program on a regular basis. These reviews are effective in identifying quality concerns as evidenced by in-depth and comprehensive annual reports issued by the teams. The QA organization performs quarterly surveillance overviews on all plant departments which provide plant management with a useful assessment of the department performanc These overviews are keyed to SALP identified or INP0 identified concerns. QA also

monitors contractor activities during outages, and has issued work stoppages when working conditions have become degrade These are considered strengths, however weaknesses were identified in 10 CFR Appendix B violations, mainly in the engineering of certain systems discussed in the engineering section of this report, and the wrong gasket used when replacing a hand hole gasket on No. 23 steam generator. Both of these issues have been resolve As discussed in the chemistry and radiological controls analysis, weaknesses were observed in the control of radio-chemistry laboratory QA/QC program and should be addresse I As discussed in the engineering section, design basis retention

and document control has been a main contributor to NRC concerns during this assessment period; specifically with regard to

', breaker coordination, followup on hangers installed in the 1979 and 1980 period, concrete walls and improper breaker settings of j Unit 2 diesel generators. The licensee is aware of this issue and is beginning to address the methods for recovery of such

records in the futur I ,

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_ .. -_ -- . - _ _

49  :

L In sum. mary, the sensitivity to Assurance of Quality is evident ;

'

at all worker levels and throughout management at the Salem Station. When safety issues are identified the licensee responds in a prompt thorough and effective manner in order to provide NRC management with an accurate assessment of the concern, and a prompt conservative approach to resolutio ,

'

2. Conclusion

Rating: 1 I

Trend: None 3. Board Recommendation

,

Licensee: None '

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NRC: None

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.

.

V. SUPPORTING DATA AND SUMMARY Investigations and Allegations Review Six allegations were received, followed up and closed during this !

assessment period. The allegations involved: (1) contractor labor

supervisor extorting money from laborers and using illegal drugs; (2)

Inadequate repair of service water piping; (3) Improper use of weld overlay and procadores; (4) Improper surveillance testing of service water pumps; (5) Guards being overworked; and (6) Equioment damaged to discredit contractors and get then removed from the sit All six allegations were found to be unsubstantiate Escalated Enforcement Actions I Civil Penalties None Orders None Confirmatory A.ction Letters

_

None "er.apmera Gnt e n encu

, November 11,19E6 - Meeting in Region I office to discuss licensee's i,

corrective actions taken to prevent events similar to the false loss of offsite power event that occurred on August 26, 198 February 24, March 10, and March 17, 1987 - Meetings at Salem to discuss the Salem electrical distribution syste '

July 16, 1987 - Meeting in Region I office to discuss the Consolidated Artificial Island Emergency Pla September 29, 1987 - Meeting in Region I to discuss Unit 2 reactor vessel head leak and proposed schedule for replacement of service

,

water piping, d

November 3, 1937 - Meeting in Region I to discuss the electrical distribution system and breaker coordination as related to Appendix

R " .

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l

D. Licensee Event Reports l

Forty-five LERs were submitted by the two Salem units during this

period. The LERs are listed in Table 4. The causal analyses of the l LERs are as follows
(1) Eighteen LERs were attributed to personnel i error (three plant trips); (2) Twelve LERs were a result of licensee identified plant conditions discovered during plant walkdowns and engineering evaluations; (3) Six LERs were attributed to procedural -

errors and were a product of omission of key information necessary to perform the operations for which they were written (one plant trip);

(4) Five LERs were attributed to equipment failure (two plant trips),

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!

4 i Table 1

'

INSPECTION REPORT ACTIVITIES

'

! REPORT NUMBERS TYPE TOTAL INSPECTION DATES INSPECTI0tj HOURS R DESCRIPTION

]

I 86-28 86-28 RESIDENT 94 ROUTINE RESIDENT INSPECTION 10/01/F6 10/27/S6 86-30 86-32 SPECIALIST 44 INSPECTION OF CONTINGENCY PLAN EVENTS AND

'

10/15/86 10/16/86 GUIDANCE FOR OPERATIONAL INTERFACES

,4 86-31 86-34 RESIDENT 131 ROUTINE RESIDENT INSPECTION 10/28/86 11/24/86  !

.

86-32 86-36 RESIDENT 155 ROUTINE RESIDENT INSPECTION

,

11/25/86 12/31/86 86-33 SPECIALIST 33 INSPECTION OF THE RADIOLOGICAL SAFETY

! 11/04/86 11/07/86 PROGRAM i i 86-35 SPECIALIST 73 INSPECTION OF TEST WITNESSING AND 11/19/86 .

] 11/27/86 PRELIMINA,RY EVALUATION OF CONTAINMENT '

INTEGRATED LEAK RATE TEST AND TOURS OF ;

t THE FACILITY  ;

87-01 I j 87-01 RESIDENT 106 ROUTINE RESIDENT INSPECTION 01/01e o,, u t/26, c,,

)  :

I 87-02 87-02 SPECIALIST 47 INSPECTION OF LICENSEE ACTIVITIES IN I i 01/12/87 01/16/87 RESPONSE TO OPEN ITEMS RELATING TO IE I i '

BULLETINS 79-02 AND 79-14

'

!

87-03 87-04 RESIDENT 130 ROUTINE RESIDENT INSPECTION  :

j 01/27/87 02/23/87 l

i 87-03 RESIDENT 24 SPECIAL INSPECTION OF OPERATION OUTSIDE j 01/12/87 01/23/87 THE DESIGN BASIS ANALYSIS AS DESCRIBED IN j IE INFORMATION NOTICE 87-01 l J t

87-04 87-10 SPECIALIST 34 INSPECTION OF THE LICENSEE'S RADIOLOGICAL i j 03/16/87 03/20/87 EFFLUENTS CONTROL PROGRAM l 87-05 SPECIALIST 31 CYCLE 4 STARTUP PHYSICS TESTING PROGPM i j 02/03/87 02/06/87 87-05 87-07 SPECIALIST 36 ROUTINE INSPECTION OF THE RADIATION ,

1l 02/24/87 02/27/87 PROTECTION PROGRAM i

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_ _ _ _ _ . .-. _ .

i Table 1 (cont.)

!

INSPECTION REPORT ACTIVITIES

"

REPORT NUMBERS TYPE TOTAL INSPECTION DATES INSPECTION HOURS DESCRIPTION d

87-06 87-11 RESIDENT 89 ROUTINE RESIDENT INSPECTION

,

03/24/87 04/20/87

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87-07 87-08 RESIDENT 140 ROUTINE RESIDENT INSPECTION 02/24/87 03/23/87 87-08 87-09 SPECIALIST 110 INSPECTION OF LICENSEE'S ENGINEERING 04/07/87 04/10/87 0FFICE AND SALEM 1 AND 2 PLANT SITES 87-09 87-12 SPECIALIST 42 ROUTINE INSPECTION OF THE LICENSEE'S 04/13/87 04/16/87 EMERGENCY PREPAREDNESS PROGRAM CONDUCTED APRIL 13-16, 1987 87-10 87-13 SPECIALIST 39 INSPECTION OF STAFF TRAINING AND LICENSEE 04/16/87 04/16/87 ACTION ON PREVIOUS INSPECTION FINDINGS *

87-11 S7-14 SPECIALIST 17 EFFECTIVENESS OF QUALITY CONTROL &

j 04/15/87 04/20/87 QUALITY ASSURANCE ACTIVITIES IN i

PROCUREMENT & PREVENTATIVE MAINTENANCE FOR STORED ITEMS

]

87-12 87-15 RESIDENT 190 ROUTINE RESIDENT INSFECTION i 04/21/87 05/18/87

'

87-13 87-16 SPECIALIST S3 NUCLEAR ENGINEERING INCLUDING IN-PLANT 05/18/87 05/22/87 REACTOR ENGINEERING AND, QA/QC INTERFACES, INVOLVEMENT AND OVERVIEW  !

l 87-14 87-17 SPECIALIST 62 ROUTINE PHYSICAL SECURITY INSPECTION 05/18/87 05/21/87

.l l 87-15 87-18 RESIDENT 112 ROUTINE RESIDENT INSPECTION  :

j 05/19/87 06/15/87 87-16 87-19 SPECIALIST 33 INSPECTION OF LICENSEE'S ANALYSIS, VITAL l 06/01/87 06/05/87

'

BUS RECORD LEVEL PROTECTION SYSTEMS, QA INTERFACE, SURVEILLANCE PROCEDURES & l

ELECTRICAL DISTRIBUTION SYSTEM i 87-17 CANCELLED 87-18 87-20 RESIDENT 192 SPECIAL TEAM INSPECTION ON FEE 0 WATER AND

):

06/15/87 06/19/87 CONDENSATE SYSTEMS

!

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. - . . - . -

!

S4 Table 1 (cont.)  ;

a p INSPECTION REPORT ACTIVITIES

, l

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REPORT NUMBERS TYPE TOTAL

, INSPECTION DATES INSPECTION HOURS DESCRIPTION 87-19 87-21 RESIDENT 138 ROUTINE RESIDENT INSPECTION 06/16/87 07/20/87

, 87-2n 87-22 SPECIALIST 34 INSPECTION OF LICENSEE'S RADI0 ACTIVE 06/29/87 07/02/87 WASTE PREPARATION, PACKAGING AND SHIPPING l PROGRAM i 87-21 87-26 SPECIALIST 0 OPERATORS EXAMINATIONS GIVEN !

06/15/87 06/19/87 87-22 87-23 SPECIALIST 5 A MEETING BETWEEN PSE&G AND NRC REGION I 07/16/87 07/16/87 TO DISCUSS CONSOLIDATED EMERGENCY PLAN l 87-23 87-24 SPECIALIST 76 INSDECTION OF THE LICENSEE'S RADIATION 07/27/87 07/31/87 PROTECTION PROGRAM ,

87-24 87-25 RESIDENT 223 ROUTINE RESIDENT INSPECTION 1 07/21/87 08/24/87 l

87-25 87-27 RESIDENT 204 ROUTINE RESIDENT INSPECTION j l 08/25/87 09/28/87 l

87-26 SPECIALIST 0 WRITTEN AND OPERATING EXAMINATIONS i

.

09/15/87 09/17/87 ACMINISTERED TO FOUR SENIOR REACTOR i

!

OPERATOR CANDIDATES t l

1 87-27 SPECIALIST 38 POST MODIFICATION TEST PROGRAM FOR ;

09/21/87 09/25/87 REFUELING OUTAGE l

j

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87-28 87-30 RESIDENT 226 ROUTINE RESIDENT INSPECTION 09/29/87 11/02/87 '

,

) 87-29 SPECIALIST 37 STEAM GENERATOR INSERVICE INSPECTION ,

i 10/26/87 10/30/87 '

l 87-29 SPECIALIST 258 FIRE PROTCCTION/ APPENDIX "R" l 09/14/87 09/18/87 87-30 87-31 SPECIALIST 107 INSPECTION OF RADIOLOGICAL CONTROLS 10/19/87 10/23/87 PROGRAM 87-31 87-32 SPECIALIST 115 INSPECTION OF LICENSEE'S ACTIONS ON 10/26/87 10/30/87 PREVIOUS NRC FINDINGS

I l,

Table 1 (cont.)

INSPECTION REPORT ACTIVITIES

REPORT NUMBERS TYPE TOTAL INSPECTION DATES IN,SPECTION HOURS DESCRIPTION i 87-32 87-33 RESIDENT 183 ROUTINE RESIDENT INSPECTION 11/03/87 11/30/87 i 87-33 87-34 SPECIALIST 68 INSPECTION OF THE NON RADIOLOGICAL j 11/16/87 11/20/87 CHEMISTRY PROGRAM

l 87-3A SPECIALIST 38 OUTAGE MODIFICATIONS FOLLOWUP 11/16/87 11/20/87

87-35 87-35 SPECIALIST 320 FOLLOWUP ON APPENDIX "R" BREAKER l !!/30/87 12/04/87 CC r,0! NATION ISSUE 87-36 87-36 RESIDENT 97 ROUTINE RESIDENT INSPECTION 12/01/87 12/31/87 87-37 87-37 SPECIALIST 41 INSPECTION OF RADIOLOGICAL SAFETY 12/14/87 12/18/87 PROGRAM J 37-38 SPECIALIST 28 ILRT ASSESSMENT 12/20/87 12/23/87 l

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Table 2 SALEM 1&2 INSPECTION HOUR SUMMARY

AREA _ , , . _ . _

HOURS HOURS ANNUALIZE0 PERCENT !

OPERATIONS 1395 110 .3 RADCON/ CHEMISTRY 525 42 .1 !

i l MAINTENANCE 421 33 .7 SURVEILLANCE 479 38 .1

'

EMERGENCY PRE .7 1.1 3 SEC/ SAFEGUARDS 187 14 .3

'

i OUTAGES 322 25 .4 l ENGINEERING 922 73 .0 ;

TOTALS: TSU hA30T 100 1

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. _ _ - - _ _ _ _ - - _ _ _ _ . _ _ _ _ _ _ _ _ _ - _ _ _ . _ - _ _ _ - - _ - _ - _ _ _ _ _ - _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ - _ _ _ _ - _ _ _ _ _ _ _ _ - - - _ _ _ - _ _ _ _ .

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Table 3

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SALEM 1&2 t

.

ENFORCEMENT ACTIVITY

!

A. Violations versus Functional Area by Severity Level '

I

.

FUNCTIONAL No. of Violations in Each Severity Level !

AREA 1 2 3 4 5 DEV TOTAL i m = = _,

-

=== -- -

OPERATIONS 1 3 4 l RADCON/ CHEMISTRY 3 3 ,

!

MAINTdNANCE 1 1 :

,

SURVEILLANCE O l

EMERGENCY PRE O SEC/ SAFEGUARDS 0 i

!

OUTAGES 0 ENGINEERING SUPPORT 5 5 ;

'

LICENSING 0 ASSURANCE OF QUALITY 0 TRAINING 6 QUALIFICA110N 0

" " " ~

TOTALS: U f~ 5~ IT

Note: Four other violations pending from NRC Fire Protection Team Inspection 50-311/87-29.

4

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) Table 3 (cont.) .

!

j Sumary of Violations .

! INSPECTION REPORTS REQUIREMENT SEVERITY FUNCTIONAL ,

_ INSPECTION DATES, VIOLATE 0_, LEVEL _ AREA , DESCRIPTION [

,

87-02 87-02 CRITERION !!! 5 ENGINEERING NO PPOCEDURES FOR [

01/12/S7-1/16/37 10CFR50 IMPLEMENTING i i

APPENDIX B SYSTEM DESIGN  :

INTERFACE MEASURES l

CRITERION V 5 ENGINEERING PIPING AND PIPE 10CFR50 SUPPORT DESIGN ,

! APPENDIX B ACTIVITIES WERE  ;

i NOT PERFORMED IN

,

ACCORDANCE WITH i

!

APPROVED PROCEDURES <

'

d CRITERION VI 5 ENGINEERING DOCUMENTS FOR 10CFR50 DESIGN MODIFICA- '

APPENDIX B TIONS WERE NOT MAINTAINED IN

-

ACCORDANCE WITH .

REQUIREMENTS l

'

!

87-03 87-04 T.S. 4.6.1. OPERATIONS TESTING DID NOT 01/27/87 02/23/87

'

DOCUMENT

) CONTAINMENT ,

'

! INTEGRITY EVERY 31 I

OAYS J

87-03 T.S. 3.5. CPERATIONS INOPERABILITY OF .;

01/12/87 BOTH EMERGENCY ,

CORE COOLING SYSTEM .

AND RESIDUAL HEAT  !

'

REMOVAL SYSTEM. THE

SYSTEM COULD ONL/

l INJECT WATER TO TWO

, VS FOUR LOOPS i 4  !

l  !

),

i I

l l

l l

!

,

-, - ~ .

. , , - - . , . , - , , , - .,. - - - , ~ _ . . - - - - . -

- __ - - _ . - .--. - _-

.

- . - - . . . -. - - . -. .- - - .--

'

i t

'

j 59

!

i j i Table 3 (cont.) i

! INSPECTION REPORTS REQUIREMENT SEVERITY FUNCTIONAL I i INSPECTION DATE VIOLATED _ _ LEVEL , AREA , DESCRIPTION l t

87-06 87-11 T.S. 4. OPERATIONS MISSED  !

1 03/24/87 04/20/87 SURVEILLANCE  !

l PERTAINING TO  !

l

!

OVERLOAD CUT 0FF ON

! A CRANE THAT CAN TRAVEL OVER SPENT l FUEL i

-

a 87-08 87-09 CRITERION Y 5 ENGINEERING WRITTEN PROCEDURES ;

i 04/07/87 04/10/87 10CFR50 PROVIDING THE  !

APPENDIX B SCOPE AND l l ACCEPTANCE CRITERIA ,

WAS NOT DOCUMENTED ;

FOR 1980 SURVEY OF

8 LOCK WALLS i CRITERION XVII 5 ENGINEERING NO RECORDE0, l l 10CFR50 CONTROLLED ,

1 APPENDIX B CALCULATIONS WERE l l AVAILABLE FOR

, MASONRY WALLS l l MODIFICATIONS 87-11 S7-14 CRITERION XIII 4 MAINTdNANCE NO COMPLETED OATA 04/15/87 04/20/87 10CFR50 SHEET! TO DOCUMENT ,

APPENDIX B ROTATION OF l

'

CRITICAL EQUIPMENT IN STORERSM 37-15 87-1B T.S. 4.5.2b 4 OPERATIONS OPERABILITY OF 1 05/19/87 06/15/S7 EMERGENCY CORE l COOLING SYSTEM NOT !

DEMONSTRATED WITHIN l 31 DAYS

]

87-29 REPORT NOT ISSUED -

4 POTENTIAL VIOLATIONS j 09/14/87 09/18/87 i

s J

i

!

J

]

- - _ - .- _

-. - - - _._ - - .- - .- . - - - .- - - _ .

Table 3 (cont.)

INSPECTION REPORTS REQUIREMENT SEVERITY FUNCTIONAL INSPECTION OATE VIOLATE 0_ LEVEL _ AREA m, DESCRIPTION 87-30 87-31 T.S. 6.12 4 RADCON LOCKED HIGH 10/19/87 10/23/87 RADIATION DOORS WERE DEFECTED AND LEFT UNLOCKED T.S. 6.11 4 RADCON PRE-JOB BRIEFINGS WERE NOT BEING CONDUCTED AND MPC-HOUR METERS WERE NOT USED T.S. RADCON FAILURE TO ESTABLISH PROCEDURES FOR CALIBRATION USE AND DATA EVALUATION OF SL4 (MPC-HOUR METERS)

_

_. ,

Table 4 SALEM 1&2 LICENSEE EVENT REPORTS A. LER_by Functional Area Number by Cause Codes FU"CTIONAL AREA A B C D E X TOTAL OPERATI0d5 2 1 3 2 2 10 RADCON/ CHEMISTRY 4 4 MAINTENANCE 2 2 1 2 7 SURVEILLANCE 10 1 1 12 EMERGENCY PRE SEC/ SAFEGUARDS -

REFUELING, OUTAGE HANAGEMENT -

ENGINEERING SUPPORT 1 10 1 12 LICEN0!N3 A;T!'.' T :: -

TRAININ3 AND 00ALIFICATION -

ASSURANCE OF QUALITY -

~'TOTALY Is I6 }" "5 7 "5 i$f Legend: A - Personnel Error B - Design Error C - External Cause 0 - Defective Procedure E - Equipment Failure X - Other

Table 4 (cont.) LER Synopsis SALEM 1 LER NUMBER EVENT DATE CAUSE CODE DESCRIPTION 96-019 10/01/86 B T.S. 3.7.11 NON COMPLIANCE - FIRE BARRIER WALL IMPAIRMENT DISCOVERED 86-020 11/08/86 A T.S. SURVEILLANCE 4.7.7.1A -

SURVEILLANCE NOT COMPLETED WITHIN TIME - DUE TO PERSONNEL ERROR 86-021 11/12/86 A T.S. SURVEILLANCE 4.3.3.9 - DETECTOR 1R41C FUNCTIONAL TEST NOT IN TIME DUE TO PERSONNEL ERROR 87-001 01/30/87 A UNIT NO.1 REFUE'ING WATER STORAGE BORON CONCENTRATION OUT OF SPECIFICATION DUE TO PERSONNEL ERROR 87-002 03/12/87 A LOSS OF CONTROL OF A HIGH RADIATION AREA LOCKED 000R DUE TO PERSONNEL ERROR 87-003 03/26/87 0 CONTAINMENT PRESSURE / VACUUM RELIEF VALVES OPEN BEYOND 1000 HOUR LIMIT DUE TO PROCEDURAL INADEQUACY 87-004 04/10/87 A DIESEL GENERATOR MISSED SURVEILLANCE 00E TO INADEQUATE POST MAINTENANCE TESTIhG CAUSED BY PERSONNEL ERROR 67-005 04/23/87 A 1F GROUP BUS UNDERFREQUENCY PROTECTION INOPERABLE DUE TO MISPOSITIONED KNIFE SWITCH 87-006 , 05/25/87 X BOTH TRAINS OF HIGH HEAD SI DECLARED INOPERABLE - T.S. 3.0.5 ENTERE".87-007 06/02/87 C TURBINE TRIP /TX. TRIP FROM 100% -

5021 DEANS LINE CROSS TRIP SCHEME -

LIGHTING STRIKE f

87-008 06/03/87 A FAILURE TO IMPLEMENT PORTIONS OF THE INSERVICE TESTING PROGRAM

Table 4 (cont.)

LER NUMBER EVENT DATE CAUSE CODE DESCRIPTION 87-009 06/04/87 X T.S. 3.7.11 NON COMPLIANCE - IMPAIRED FIRE BARRIER PENETRATIONS DISCOVERED 87-010 06/10/87 8 NON COMPLIANCE WITH 10CFR50 APPENDIX A CRITERIA FOR SEPARATION OF SAFETY RELATED COMP.87-011 09/17/87 B POTENTIALLY INADEQUATE BREAKER C0 ORDINATION 87-012 09/30/87 D REACTOR TRIP SYSTEM INSTRUMENTATION NOT BEING PUT IN TRIP WITHIN THE REQUIRED TIME FRAME 87-013 10/02/87 E TRIP FROM SOURCE RANGES HIGH NEUTRON FLUX DUE TO WATER IN THE DETECTOR 87-014 10/08/87 A LOSS OF CONTROL OF A LOCKED HIGH RADIATION AREA DOOR DUE TO PERSONNEL ERROR 87-015 10/23/87 A TECHNICAL SPECIFICATION 3.8.1.28 -

NON COMPLIANCE DUE TO PERSONNEL ERROR 87-016 11/02/87 E F0,;ER CPERATED RELIEF STOP VALVE CABLING FOUND DEGRADED - INADEQUATC DESIGN REVIEW 87-017 11/13/87 B DISCOVERED LEAKAGE PATHS FROM 13 (23)

AFW PUMP COMPARTMENT 87-018 12/09/87 D LEAD / LAG AND DERIVATIVE AMPLIFIERS IMPROPERLY CALIBRATED DUE TO PROCEDURAL INADEQUACY 87-019 12/27/87 X WASTE GAS OXYGEN GREATER THAN 2% FOR GREATER THAN 48 HOURS I

Table 4 (cont.)

SALEM 2 LER NUMBER EVENT DATE CAUSE CODE DESCRIPTION 86-010 10/16/86 B T.S. 3.7.11 NON COMPLIANCE - FIRE BARRIER PENETRATION DISCOVERED IMPAIRED 86-011 11/17/86 A T.S. SURVEILLANCE 4.9.7 - NOT PERFORMED WITHIN SPECIFIED TIME DUE TO PERSONNEL ERROR 86-012 11/21/86 E CONTAINMENT SYSTEM - TYPE B & C LEAK RATE OUT-0F-SPECIFICATION DUE TO

,

VALVE 2PR25 EXCESSIVE LEAKAGE 86-013 12/23/86 A TURBINE REACTOR TRIP FROM 8% ON P-7 INTERLOCK DUE TO TURBINE OVERSPEED 86-014 12/28/86 E REACTOR TRIP FROM 77% POWER ON STEAM FLOW / FEED FLOW MISMATCH & 23 SG LOW LEVEL DUE TO VALVE 23BF19 CONTROL PROBLEMS87-001 01/13/87 0 LOSS OF RHR INJECTION CAPABILITY TO TWO COLD LEGS DUE TO TECHNICAL SPECIFICATION MISINTERPRETATION 87-002 01/18/87 A REACTOR TRIP FROM 3% POWER ON ERR 0NEOUS HIGH NEUTRON FLUX SIGNAL DUE TO PERSONNEL ERROR 87-003 02/26/87 A UNIT 2 FUEL HANDLING CRANE MISSED SURVEILLANCE OUE TO PERSONNEL ERROR i

87-004 03/12/87 X GENERATOR-TURBINE / REACTOR TRIP DUE TO LOSS OF FIELD ON THE MAIN GENERATOR l

87-005 04/07/87 E TURBINE / REACTOR TRIP FROM 85% POWER l DUE TO LOSS OF DC CONTROL POWER TO I

'

TURBINE ELECTRO HYDRAULIC CONTROL SYSTEM BY A FAILED SERVO CARD 87-006 05/06/87 A T.S. 3.7.10.3 NON COMPLIANCE -

INADEQUATE FIRE WATCH DUE TO PERSONNEL ERROR

- - -

)

Table 4 (cont.)

LER NUMBER EVENT DATE CAUSE CODE DESCRIPTION 87-007 05/11/87 8 T.S. 3.7.11 NON COMPLIANCE -

DISCOVERY OF FIRE BARRIER IMPAIRMENT 87-008 05/19/87 A MISSED T.S. SURVEILLANCE 4.5.2.8 DUE TO PERSONNEL ERROR - T.S. 3. ENTERED 87-009 06/19/87 B APPENDIX R CRITERIA NON-CONFORMANCE 87-010 06/23/87 A FIRE BARRIER IMPAIRMENT -

NON COMPLIANCE DUE TO PERSONNEL ERROR 87-011 08/06/87 A REACTOR TRIP - NO. 24 STEAM GENERATOR HIGH-HIGH LEVEL 87-012 09/30/87 X RHR PUMP ROOM FLOOD CURB MISSING DUE TO PERSONNEL ERROR 87-013 10/02/87 D T.S. SURVEILLANCE 4.8.1.3. A MISSED DUE TO INADEQUATE PROCEDURAL CONTROL

,87-014 10/22/87 B INCORRECT DIESEL GENERATOR INFEED BREAKER SETPOINT DUE TO INADEQUATE DOCUMENTATION CONTROL 87-015 11/27/87 B POTENTIAL FOR CERTAIN SW MCC CONTROL CIRCUITS TO PICK UP STARTER COIL 87-016 12/07/87 A 2A DIESEL GENERATOR SURVEILLANCE MISSED DUE TO PERSONNEL ERROR 87-017 12/08/87 0 1EChNICAL SPECIFICATION NON COMPLIANCE !

DUE TO PROCEDURAL IN ADEQUACY 87-018 12/23/87 A LATE SURVEILLANCE ON FUNCTIONAL TEST OF WASTE GAS MONITORS I

l l

,

I l

\

Table 5 SUMMARY OF LICENSING ACTIVITIES A. NRR LICENSEE MEETINGS 1/ 6/87 AE0D Meeting on False Loss of Offsite Power Transient 5/21/87 Control Room Design Review Meeting 6/15/87 RTD Bypass Modification Meeting 7/ 9/87 RTO Bypass Modification Meeting 11/24/87 North Anna Steam Generator Event Meeting B. NRR SITE VISITS 10/22-28/86 LPM observation of refueling outage activities 2/18/87 Licensing actions scheduling 5/28/87 Site access training for LPM 9/ 2/87 SIMS Data review 9/28/87 SIMS Data and licensing actions schedule review C. CCK4ISSION CRIEFINGS None D. SCHEDULAR EXTENSIONS GRANTED None E. RELIEFS GRANIED 6/24/87 Interim Relief from certain ASME Code testing requirements - Unit 1 12/29/87 Extension of 6/24/87 Interim Relief F. EXEMPTIONS GRANTED 9/ 4/87 Exemption from 10 CFR 50, Appendix J, III.D.2(b)(ii)

_

._ _ -

Table 5 (Cont.)

SUMMARY OF LICENSING ACTIVITIES _ LICENSEE AMENDMENTS ISSUED Date Unit 1 Unit 2 Title 2/26/07 76 50 Reduce $,' of Active Fuel Reds 3/31/87 77 51 Operate Fuel Handling Crane i

4/ 7/87 78 52 Delete Baron Injection Tank 4/10/87 79 53 Accident Monitoring 6/19/87 80 54 Delete Maximum Fuel Weight i 8/24/87 81 -

Facility Attachment

< 9/23/87 82 -

Replace Fxy Limits

'

) 10/16/87 83 55 Change RWST Boron Concentration

, 11/16/87 84 56 RTD Bypass Modification v EMERGENCY CHANGES TO TECHNICAL SPECIFICATIONS None ORDERS ISSUED None

_ _ - _ _ _ _ _ - - -