IR 05000266/2019002

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Integrated Inspection Report 05000266/2019002 and 05000301/2019002
ML19214A097
Person / Time
Site: Point Beach  
Issue date: 07/30/2019
From: Eric Duncan
Reactor Projects Region 3 Branch 4
To: Craven R
Point Beach
References
IR 2019002
Download: ML19214A097 (30)


Text

July 30, 2019

SUBJECT:

POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2INTEGRATED INSPECTION REPORT 05000266/2019002 AND 05000301/2019002

Dear Mr. Craven:

On June 30, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Point Beach Nuclear Plant, Units 1 and 2. On July 22, 2019, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. The inspectors documented a licensee-identified violation which was determined to be of very low safety significance in this report. The NRC is treating this violation as non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest a violation or the significance or severity of a violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at Point Beach.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at Point Beach. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Eric R. Duncan, Chief Branch 4 Division of Reactor Projects

Docket Nos. 05000266 and 05000301 License Nos. DPR-24 and DPR-27

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000266 and 05000301

License Numbers:

DPR-24 and DPR-27

Report Numbers:

05000266/2019002 and 05000301/2019002

Enterprise Identifier: I-2019-002-0060

Licensee:

NextEra Energy Point Beach, LLC

Facility:

Point Beach Nuclear Plant

Location:

Two Rivers, WI

Inspection Dates:

April 1, 2019 to June 30, 2019

Inspectors:

K. Barclay, Resident Inspector

M. Domke, Reactor Inspector

G. Edwards, Health Physicist

T. Hartman, Senior Resident Inspector

D. Kimble, Senior Resident Inspector

D. Krause, Senior Resident Inspector

V. Myers, Senior Health Physicist

R. Ng, Project Engineer

Approved By:

Eric R. Duncan, Chief

Branch 4

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Point Beach in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. A Licensee-identified non-cited violation is documented in Report Section: 7115

List of Findings and Violations

Human Performance Error Causes Unplanned Pressurizer Pressure Drop Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green NCV 05000266/2019002-01 Open

[H.12] - Avoid Complacency 71111.20 A self-revealed finding of very low safety significance and an associated non-cited violation (NCV) of Technical Specification 5.4.1, Procedures, was identified when licensee personnel failed to adequately implement a procedure for the normal sequence of startup of the plant following a refueling outage. Specifically, the licensee exceeded the single step power limit of 3 percent when power was increased from 50.0 percent to 53.4 percent. The resulting temperature transient caused pressurizer pressure to drop below the Core Operating Limits Report (COLR) minimum pressure limit of 2205 pounds per square inch gauge (psig).

Additional Tracking Items

None.

PLANT STATUS

Unit 1 began the inspection period shutdown for a refueling outage. On April 18, 2019, Unit 1 was restarted. On April 19, 2019, Unit 1 was synchronized to the grid and on April 24, 2019, achieved full power. On May 16, 2019, Unit 1 was reduced in power to 43 percent to support main condenser water box cleaning. Unit 1 subsequently returned to full power on May 18, 2019, and remained at or near full power for the remainder of the inspection period.

Unit 2 began the inspection period at full power. On May 8, 2019, Unit 2 was reduced in power to 59 percent to support turbine stop valve testing. Following the completion of this testing, Unit 2 returned to full power on May 9, 2019. On May 28, 2019, Unit 2 was reduced in power to 60 percent to investigate elevated B steam generator feed pump vibrations. Following repairs, Unit 2 returned to full power on May 31, 2019, and remained at or near full power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Summer Readiness Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated the summer readiness of offsite and alternate alternating current (AC) power systems

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 1 Train B Component Cooling Water (CCW) pump on April 9, 2019
(2) Unit 1 Chemical and Volume Control System (CVCS) when credited as a shutdown inventory flowpath on April 11, 2019
(3) Unit 1 Turbine-Driven Auxiliary Feedwater (TDAFW) pump following testing on May 11, 2019

71111.04S - Equipment Alignment

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the Unit 1 and Unit 2 CCW systems on May 1, 2019

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (5 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Fire Zones 225 and 228 on April 10, 2019
(2) Fire Zones 306 and 307 on April 10, 2019
(3) Fire Zones 142 and 151 on May 22-23, 2019
(4) Fire Zones 156 and 156A on May 22-23, 2019
(5) Fire Zone 166 on May 22-23, 2019

71111.08P - Inservice Inspection Activities (PWR) PWR Inservice Inspection Activities Sample (IP Section 03.01)

(1) The inspectors verified that the Reactor Coolant System (RCS) boundary, steam generator tubes, reactor vessel internals, risk-significant piping system boundaries, and containment boundary were appropriately monitored for degradation and that repairs and replacements were appropriately fabricated, examined, and accepted by reviewing the following activities from March 25, 2019 to April 9, 2019:

03.01.a - Nondestructive Examination and Welding Activities.

  • Volumetric ultrasound examination of Reactor Coolant System (RCS)components RC-03-AS-1001-02, elbow-to-tee; RC-03-PS-1002-24, tee-to-pipe; RC-03-PS-1002-25, pipe-to-reducer, on 3-inch diameter piping located in the pressurizer upper cubicle of containment
  • Volumetric ultrasound examination of RCS components RC-03-PS-1001-08, pipe-to-elbow; RC-03-PS-1001-09, elbow-to-pipe; on 3-inch diameter piping located in the head laydown area of containment
  • Pressure boundary field welds W-2 and W-3 for Safety Injection (SI) system check valve 1SI-845E replacement for seat leakage per Work Order (WO)

===40479783

03.01.b - Pressurized Water Reactor Vessel Upper Head Penetration Examination Activities.

  • Bare Metal Visual (BMV) examination of reactor vessel head nozzles 40, 28, 20, 16 and 32 03.01.c - Pressurized Water Reactor Boric Acid Corrosion Control Activities.
  • Boric acid leakage evaluation on charging system component 1P-2A charging pump discharge drain first off isolation, 18-021-E

03.01.d - Pressurized Water Reactor Steam Generator Tube Examination Activities.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

=

(1) The inspectors observed and evaluated licensed operator performance in the main control room during a Unit 1 reactor startup following a refueling outage on April 18, 2019

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated a licensed operator simulator scenario on May 27, 2019

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness Inspection (IP Section 02.01) (1 Sample)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) K-3B Service Air Compressor

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Unit 1 elevated risk due to lowered reactor inventory for reactor pressure vessel head placement, on April 9, 2019
(2) Elevated risk for G-05 Gas Turbine Generator maintenance and Service Water pump testing, on May 15, 2019
(3) Elevated risk for DY-0A Red Inverter maintenance and Unit 1 Emergency Core Cooling System (ECCS) testing, on June 19-20, 2019
(4) Elevated risk during Unit 1 Train B ECCS testing, on June 27, 2019

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 02.02) (5 Samples)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Unit 1 Steam Generator (SG) Snubber HS-9 Failed Functional Test on April 2, 2019
(2) Unit 1 Reactor Coolant Loop Flow Relay Found De-energized on April 26, 2019
(3) Unit 1 Train A Containment Sump Recirculation Valve Operator Corrosion on May 21, 2019
(4) Unit 1 Train A CCW Pump Elevated Vibrations on May 23, 2019
(5) Unit 1 RCS Flow Transmitter Error on June 5, 2019

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) EC 293289 - Flood Protection Lake Level Change on June 18, 2019

71111.19 - Post-Maintenance Testing

Post Maintenance Test Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the following post maintenance tests:

(1)1P-11B, Unit 1 Train B CCW pump following replacement/upgrade on April 9, 2019 (2)1DY-02 Inverter following maintenance on April 30, 2019 (3)1P-2A Charging Pump following maintenance on May 21, 2019

(4) K-3B Service Air Compressor following maintenance on May 23, 2019

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated Refueling Outage (RFO) U1R38 activities from March 22-April 17, 2019

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Containment Isolation Valve Testing (IP Section 03.01) (1 Sample)

(1) ORT 28, Demineralized Water Supply to Unit 1 Containment, on April 13, 2019

Inservice Testing (IP Section 03.01) (1 Sample)

(1) IT 45, Unit 2 Safety Injection Valves Train B, on April 11, 2019

Surveillance Tests (other) (IP Section 03.01) (3 Samples)

(1) IT 7C, P-32C Service Water Pump Quarterly Test, on March 5, 2019
(2) ORT 6, Unit 1 Containment Spray Sequence Test, on April 11, 2019
(3) IT 230, Unit 1 Leak Test of Class 1 Components Following a Refueling Shutdown, on April 16, 2019

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)

The inspectors evaluated the conduct of the following planned licensee Emergency Preparedness (EP) drill:

(1) A full scale EP site drill conducted on May 21,

RADIATION SAFETY

71124.01 - Radiological Hazard Assessment and Exposure Controls

Contamination and Radioactive Material Control (IP Section 02.03) (1 Sample)

The inspectors evaluated licensee processes for monitoring and controlling contamination and radioactive material.

(1) The inspectors verified the following sealed sources are accounted for and were intact:
  • 1113-7
  • 2602-9
  • 9121

High Radiation Area and Very High Radiation Area Controls (IP Section 02.05) (1 Sample)

(1) The inspectors evaluated risk-significant high radiation area and very high radiation area controls

Instructions to Workers (IP Section 02.02) (1 Sample)

The inspectors evaluated instructions to workers including radiation work permits used to access high radiation areas.

(1) Radiation Work Packages
  • 19-1064; Unit 1B Reactor Coolant Pump Impeller Change Out and Pump Bowl Inspection
  • 19-1053; Unit 1 Narrow Range Resistance Temperature Detector Replacement

Electronic Alarming Dosimeter Alarms

  • AR 02286293; Dosimeter Rate Alarm Received During Walk Down

Labeling of Containers

  • Unit 1 Containment 8 Elevation Hot Trash Container
  • Unit 1 Containment 66 Elevation Hot Trash Container
  • Auxiliary Building Trash Containers (Various Locations)

Radiation Worker Performance and Radiation Protection Technician Proficiency (IP Section 02.06) (1 Sample)

(1) The inspectors evaluated radiation worker performance and radiation protection technician proficiency

Radiological Hazard Assessment (IP Section 02.01) (1 Sample)

The inspectors evaluated radiological hazards assessments and controls.

(1) The inspectors reviewed the following:

Radiological Surveys

'B' Reactor Coolant Pump (RCP) Platform

  • Resistance Temperature Detector (RTD) Tent
  • Refuel Floor
  • Spent Fuel Pool
  • Reactor Cavity

Risk-Significant Radiological Work Activities

'B' RCP Internals Removal

  • RTD Removal and Repair

Air Sample Survey Records

  • 30-105
  • 30-108
  • 30-112
  • 30-106

Radiological Hazards Control and Work Coverage (IP Section 02.04) (1 Sample)

The inspectors evaluated in-plant radiological conditions during facility walkdowns and observation of radiological work activities.

(1) Radiological work package for areas with airborne radioactivity
  • 19-1064; Unit 1B RCP Impeller Change Out and Pump Bowl Inspection
  • 19-1053; Unit 1 Narrow Range RTD Replacement

71124.02 - Occupational ALARA Planning and Controls

Implementation of ALARA and Radiological Work Controls (IPSection 02.03) (1 Sample)

The inspectors reviewed as low as reasonably achievable practices and radiological work controls.

(1) The inspectors reviewed the following activities:
  • 19-1064; Unit 1B Reactor Coolant Pump Impeller Change Out and Pump Bowl Inspection
  • 19-1053; Unit 1 Narrow Range Resistance Temperature Detector Replacement

Radiation Worker Performance (IP Section 02.04) (1 Sample)

The inspectors evaluated radiation worker and radiation protection technician performance during:

(1)the observations of activities listed in Section 02.03

71124.03 - In-Plant Airborne Radioactivity Control and Mitigation

Engineering Controls (IP Section 02.01) (1 Sample)

The inspectors evaluated airborne controls and radioactive monitoring.

(1) Installed Ventilation Systems
  • Unit 1 Containment Purge

Temporary Ventilation Systems

Portable or Installed Monitoring Systems

  • Continuous Air Monitors on the Refueling Floor
  • Continuous Air Monitors in the Auxiliary Building

Use of Respiratory Protection Devices (IP Section 02.02) (1 Sample)

The inspectors evaluated the licensees use of respiratory protection devices by:

(1) Evaluations for the Use of Respiratory Protection
  • 19-1053; Unit 1 Narrow Range Resistance Temperature Detector Replacement
  • 19-1064; Unit 1B Reactor Coolant Pump Impeller Change Out and Pump Bowl Inspection

Respiratory Protection Use During Work Activities

  • 19-1053; Unit 1 Narrow Range Resistance Temperature Detector Replacement
  • 19-1064; Unit 1B Reactor Coolant Pump Impeller Change Out and Pump Bowl Inspection

Medical Fitness for Use of Respiratory Protection Devices

  • Two individuals wearing respirators for RTD work

Observation of Donning, Doffing and Functional Test

  • Two individuals wearing respirators for RTD work

Respiratory Protection Device Evaluation

  • Three OptimAir powered air purifying respirators
  • Two OptimAir MM 2K respirators

71124.04 - Occupational Dose Assessment

External Dosimetry (IP Section 02.02) (1 Sample)

(1) The inspectors evaluated the external dosimetry program implementation

Internal Dosimetry (IP Section 02.03) (1 Sample)

The inspectors evaluated the internal dosimetry program implementation.

(1) Whole Body Counts
  • Dose assessment completed on April 8, 2017
  • Two dose assessments completed on October 29, 2017
  • Dose assessment completed on May 14, 2018

In-Vitro Internal Monitoring

  • None available

Dose Assessments Performed using Air Sampling and DAC-hr Monitoring

  • None available

Source Term Categorization (IP Section 02.01) (1 Sample)

(1) The inspectors evaluated the licensees characterization of the source term and use of scaling factors for the use of hard-to-detect radionuclide activity

Special Dosimetric Situations (IP Section 02.04) (1 Sample)

The inspectors evaluated the following special dosimetric situation:

(1) Declared Pregnant Workers
  • Declaration Date July 10, 2018

Effective Dose Equivalent for External Exposures

  • None available

Shallow Dose Equivalent

  • Dose assessment completed on October, 28, 2017
  • Dose assessment completed on March 9, 2018

Neutron Dose Assessment

  • None available

71124.06 - Radioactive Gaseous and Liquid Effluent Treatment

Instrumentation and Equipment (IP Section 02.04) (1 Sample)

The inspectors reviewed the following radioactive effluent discharge system surveillance test results:

(1) The inspectors reviewed effluent instrumentation and equipment

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

BI02: RCS Leak Rate Sample (IP Section 02.11)===

(1) Unit 1 (April 1, 2018 - March 31, 2019)
(2) Unit 2 (April 1, 2018 - March 31, 2019)

MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04) (2 Samples)

(1) Unit 1 (April 1, 2018 - March 31, 2019)
(2) Unit 2 (April 1, 2018 - March 31, 2019)

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program, trend reports, major equipment problem lists, system health reports, self-assessments, and additional documents, to identify trends that might indicate the existence of a more significant safety issue.

INSPECTION RESULTS

Licensee-Identified Non-Cited Violation 71152 This violation of very low safety significance was identified by the licensee and has been entered into the licensee corrective action program and is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Violation: Point Beach Nuclear Plant, Units 1 and 2, Renewed Facility Operating License Condition 4.F, required, in part, that the licensee implement and maintain in effect all provisions of the approved fire protection program that comply with 10 CFR 50.48(a) and 10 CFR 50.48(c), National Fire Protection Association Standard NFPA 805, as specified in the license amendment requests, and as approved in the Safety Evaluation Report (SER)dated September 8, 2016. National Fire Protection Association (NFPA) 805, Performance-Based Standard for Fire Protection for Light Water Reactor Electric Generating Plants, 2001 Edition, Section 3.3.1.2, Control of Combustible Materials, required, in part, that procedures for the control of transient combustibles shall be developed and implemented.

Licensee procedure NP 1.9.9, Transient Combustible Control, was developed by the licensee to implement the requirements of NFPA 805 for the control of transient combustibles. Revision 36 of NP 1.9.9, Step 4.12.3.b, stated, Except as permitted by Step 4.12.3.f, up to 100 pounds of Class A combustible materials may be brought into and left unattended in an Ordinary Risk fire zone without a TCCP [transient combustible control permit].

Contrary to the above, on April 4, 2019, the licensee failed to implement the requirements of Revision 36 of NP 1.9.9, Step 4.12.3.b associated with the control of transient combustibles.

Specifically, the licensee brought in and left unattended in excess of 1000 pounds of Class A combustible materials in the primary auxiliary building truck bay, an Ordinary Risk fire zone, without a TCCP. This amount of material significantly exceeded the 100 pound limit of Class A combustible material specified in Step 4.12.13.b of NPP 1.9.9 and the Class A combustible material did not qualify for the Step 4.12.3.f exemption.

Significance: Green.

Corrective Action References: AR 2308895

Observation: Semi-Annual Trend Review 71152 The licensee documented a trend in procedure use and adherence errors on March 1, March 29, and April 10, 2019. A licensee Recovery Plan, issued on April 15, 2019, included actions for first-line supervisors to emphasize procedure use and adherence within their work groups; managers to perform observations of procedure use and adherence in the field; and operations, maintenance, chemistry, engineering, and radiation protection departments to perform information sharing to reinforce human performance and procedure use and adherence.

The inspectors reviewed a licensee Interim Effectiveness Review that was issued on May 13, 2019, and that assessed the effectiveness of the Recovery Plan. The licensee concluded that their recovery actions were effective based on a reduction in the number of identified procedure use and adherence errors documented in condition reports.

The inspectors observed that although some improvements in procedure use and adherence were noted, challenges with procedure use and adherence, which were also documented in the previous semi-annual trend inspection, continued to be identified in the first and second quarter of 2019. For example, procedure use, and adherence errors associated with the control of transient combustibles during the Unit 1 refueling outage were observed. In particular, the inspectors identified three condition reports that identified a failure to obtain a required transient combustible permit, one of which is documented in this report as a finding of very low safety significance with an associated non-cited violation.

The inspectors concluded that more time was required to determine whether the efforts to reduce procedure use and adherence errors were effective and sustainable.

Human Performance Error Causes Unplanned Pressurizer Pressure Drop Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events

Green NCV 05000266/2019002-01 Open

[H.12] - Avoid Complacency 71111.20 A self-revealed finding of very low safety significance and an associated non-cited violation (NCV) of Technical Specification 5.4.1, Procedures, was identified when licensee personnel failed to adequately implement a procedure for the normal sequence of startup of the plant following a refueling outage. Specifically, the licensee exceeded the single step power limit of 3 percent when power was increased from 50.0 percent to 53.4 percent. The resulting temperature transient caused pressurizer pressure to drop below the Core Operating Limits Report (COLR) minimum pressure limit of 2205 pounds per square inch gauge (psig).

Description:

On April 21, 2019, with Unit 1 at 49 percent following the U1R38 refueling outage, the licensee inadvertently commenced power ascension at a rate of 3 percent per minute instead of 3 percent per hour and stepped reactor power from 49 percent to 53.4 percent. A reactor operator communicated that the turbine ramp rate was being set for 3 percent per hour but misread an operator aid and inadvertently established a ramp rate of 3 percent per minute.

The reactor operator then requested a peer check for the ramp rate that had been established from a second reactor operator, who improperly concurred with the incorrect setting. The reactor operator informed the Unit 1 senior reactor operator (SRO) that the turbine ramp rate had been set and requested permission to commence the power ascension. The SRO gave permission to proceed and the power ascension was commenced. The reactor operator observed that the turbine setter display value had begun to increase, confirming that the ramp had commenced, and stated that the turbine was ramping up. About 2 minutes after the power ascension was initiated, the reactor operator noted that reactor coolant system (RCS) temperature was unexpectedly lowering and the second reactor operator communicated that RCS pressure was also unexpectedly lowering.

The second reactor operator subsequently suspended the power ascension by placing the turbine controls in hold.

The resulting temperature transient caused pressurizer pressure to drop below the Core Operating Limits Report (COLR) minimum pressure limit of 2205 psig required by Technical Specification (TS) Limiting Condition for Operation (LCO) 3.4.1, RCS Pressure, Temperature, and Flow Departure from Nucleate Boiling (DNB) Limits. The Technical Specification Action Condition (TSAC) required that when pressurizer pressure drops below the minimum pressure required by the COLR, that pressurizer pressure be restored to within the COLR limit of 2205 psig within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />. The licensee entered TSAC 3.4.1.a at 8:06 a.m.,

restored pressurizer pressure to within the COLR limit at 8:09 a.m., and subsequently exited the TSAC.

OP 1C, Startup To Power Operation Unit 1, Step 3.3.2, stated, in part, that the rate of core power change is not limited by the fuel up to the conditioned power level or the threshold power of 50 percent, whichever is greater. OP 1C also stated that to be conditioned above 50% power, the plant must have been operated in the current cycle at or above a given power level greater than 50 percent for at least 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> out of the last 7 days of power operation.

For the step change in power on April 21, the conditioned power level was not above 50 percent in the current cycle since the plant was restarting immediately following a refueling outage. Therefore, the threshold power level of 50 percent applied. OP 1C, Step 3.3.2, also stated, in part, that the following power limit increases shall not be exceeded: 4 percent over any 1-hour period; 7 percent over any 2-hour period; 10 percent over any 3-hour period; and no single step change in power of more than 3 percent of full power.

Corrective Actions: After identifying the issue, the licensee immediately halted the load ramp and reduced power to about 51 percent. The licensee contacted the fuel vendor, who validated that the step change in power did not adversely impact the fuel. Long-term corrective actions included revising the operator aid used to set the ramp rate and conducting a human performance investigation.

Corrective Action References: AR 2311530

Performance Assessment:

Performance Deficiency: The inspectors determined that the failure to adequately implement OP 1C, Startup To Power Operation Unit 1," Step 3.3.2, was contrary to TS 5.4.1, "Procedures, and was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Human Performance attribute of the Initiating Events cornerstone. The performance deficiency adversely affected the cornerstone objective of limiting the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the licensee violated the step change limits for power ascension and violated the COLR limit for pressurizer pressure.

Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors determined that the finding was of very low safety significance (i.e., Green) because they answered No to the Transient Initiators Question in Exhibit 1 - Initiating Events Screening Questions. Specifically, the finding did not cause a reactor trip, or the loss of mitigating equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition.

Cross-Cutting Aspect: H.12 - Avoid Complacency: Individuals recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Individuals implement appropriate error reduction tools. Specifically, the operators failed to implement appropriate error reduction tools.

Enforcement:

Violation: Technical Specification 5.4.1.a, of Technical Specification 5.4, Procedures, required, in part, that written procedures shall be established, implemented, and maintained covering the normal sequence of startup, operation, and shutdown of components, systems, and the overall plant. Point Beach Nuclear Plant Operating Procedure OP 1C, Startup To Power Operation Unit 1, is the procedure used in the normal sequence of startup of the overall plant subject to the requirements of Technical Specification 5.4.1.a. OP 1C, Step 3.3.2, stated, in part, that the rate of core power change is not limited by the fuel up to the conditioned power level or the threshold power of 50 percent, whichever is greater. OP 1C, Step 3.3.2 also stated, in part, that no single step in power shall exceed 3 percent of full power.

Contrary to the above, on April 21, 2019, the licensee failed to implement a procedure for the normal sequence of startup of the overall plant as required by Technical Specification 5.4.1.a.

Specifically, with the reactor at the threshold power of 50 percent, which was the greater of the conditioned power level and the threshold power level, the licensee exceeded the single step power increase limit of 3 percent of full power specified in OP 1C, Step 3.3.2, when a step change in power from 50 percent to 53.4 percent occurred.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On April 5, 2019, the inspectors presented the radiation protection inspection results to Mr. R. Craven, Site Director, and other members of the licensee staff.
  • On April 9, 2019, the inspectors presented the Inservice Inspection Exit to Mr. B. Wojak, Site Engineering Director and other members of the licensee staff.
  • On July 22, 2019, the inspectors presented the integrated inspection results to Mr. R. Craven and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.01

Corrective Action

Documents

Resulting from

Inspection

2314350

NRC Items Identified during Switchyard Walkdown

05/14/2019

Miscellaneous

PBNP-MISO-

NUC-001

Nuclear Plant Operating Agreement for Point Beach Nuclear

Plant

Procedures

NP 2.1.5

Electrical Communications, Switchyard Access and Work

Planning

NP 5.2.19

NERC Standard NUC-001 Nuclear Plant Interface

Coordination Agreement Control

71111.04

Drawings

110E018, Sheet 3 Auxiliary Coolant System

110E018, Sheet 5 CCW Minimum Flow Recirculation Cross Connect Details

M-201, Sheet 1

P&ID Main & Reheat Steam System

M-217, Sheet 1

P&ID Auxiliary Feedwater System

104

Miscellaneous

Shutdown Safety Assessment and Fire Inspection Checklist

04/11/2019

Procedures

1-CL-CC-001

Component Cooling Unit 1

CL 13E Part 1

Auxiliary Feedwater Valve Lineup Turbine-Driven Unit 1

CL 5A

Chemical and Volume Control System Unit 1

71111.04S

Drawings

110E018, Sheet 1 P&ID Auxiliary Coolant System

110E018, Sheet 2 P&ID Auxiliary Coolant System

110E018, Sheet 3 P&ID Auxiliary Coolant System

110E029, Sheet 1 P&ID Auxiliary Coolant System

110E029, Sheet 2 P&ID Auxiliary Coolant System

110E029, Sheet 3 P&ID Auxiliary Coolant System

110E029, Sheet 4 P&ID Auxiliary Coolant System

Procedures

1-CL-CC-001

Component Cooling Unit 1

2-CL-CC-001

Component Cooling Unit 2

71111.05Q Corrective Action

Documents

Resulting from

Inspection

2300129

Material Missing From Structural I Beams

1/31/2019

Fire Plans

PFP-0-CB

Control Building Elevation 8', 26', 44' and 66'

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

PFP-0-PAB-26

Auxiliary Building 26'

PFP-0-PAB-8

Primary Auxiliary Building Elevations 8' and Below

PFP-0-PAB-8

Pre-Fire Plan Primary Auxiliary Building Elevations 8' and

Below

71111.08P

Corrective Action

Documents

AR 2309189

Anomaly During U1R38 SG Tube Plug Installation

04/05/2019

AR 2309427

Debris Found on Unit 1 Reactor Pressure Vessel Closure

Head

04/08/2019

AR 2309430

Boric Acid Streaking from CETNA 37 on Unit 1 RPV Head

04/08/2019

AR 2309467

Boric Acid Streaking from CETNA 35 on Unit 1 RPV Head

04/08/2019

AR 2309598

Recordable Indication on RTD Bypass Piping Support RC-

2501R-14-102R

04/09/2019

Corrective Action

Documents

Resulting from

Inspection

AR 2307462

Weld Data Sheets in Incorrect Record

03/26/2019

AR 2309226

Incorrect Revision of Code Case N-729 Referenced in NDE

Procedure

04/05/2019

Engineering

Evaluations

17-198B-E

Safety Injection Pump Inboard Seal Leakoff Area and Pump

Skid Below

04/17/2018

18-021-E

1P-2A CHG Pump Discharge Header Drain First Off

Isolation/8/PAB/U1

03/27/2018

LTR-CECO-19-

29

Evaluation of Roll Expanded Mechanical Tube Plug

Extending from the Tubesheet in Tube R13C49 in SGA Cold

Leg at Point Beach Unit 1

04/08/2019

Miscellaneous

NPM 2007-0145

Documentation of Point Beach Nuclear Plants Position on

the Use of Liquid Penetrant and Magnetic Particle Materials

Contained in Aerosol Containers and Stored Under Ambient

Conditions

04/24/2007

NSAL-12-1

Nuclear Safety Advisory Letter for Steam Channel Head

Degradation

Revision 1

NSD-TB-94-03-

R0

Westinghouse Technical Bulletin for Steam Generator

Secondary Side Erosion-Corrosion

05/02/1994

SG-CDMP-19-3

Point Beach U1R38 Steam Generator Degradation

Assessment

Revision 1

NDE Reports

2019U1PT-001

Liquid Penetrant Examination of Component AC-601R-6-H4-

IWA

04/02/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Procedures

FP-PE-B31-

P1P1-GTSM-001

ASME-Welding Procedure Specification

Revision 6

FP-PE-B31-

P8P8-GTSM-037

ASME-Welding Procedure Specification

Revision 5

MRS-GEN-1217

Rolled Mechanical Plug Installation Using the Advanced

Rolling Tool and the Universal Platform Control Box

Revision 5

NDE-173

PDI Generic Procedure for the Ultrasonic Examination of

Austenitic Piping Welds

Revision 17

NDE-201

Radiographic Examination

Revision 6

NDE-451

Visible Dye Penetrant Examination Temperature

Applications 45°F to 125°F

Revision 30

Work Orders

WO 40459909 01

1AF-00195A/Replace Valve (Welding)

10/13/2017

WO 40479783 01

1SI-845E/Cut Out and Replace Valve

10/17/2017

WO 40514558 01

Perform NDE/UT of Pressurizer Spray Piping Welds

10/13/2017

WO 40514567 02

Perform NDE/RC-03-PS-1001-08

10/12/2017

WO 40573724 01

Reactor Pressure Vessel Closure Head

01/17/2019

71111.11Q Corrective Action

Documents

2314216

Simulator Issue Negatively Affected LOC Evaluated

Scenario

5/13/2019

Procedures

OP 1B

Reactor Startup

OP-AA-100-1000

Conduct of Operations

71111.12

Corrective Action

Documents

263887

K-3B SA Compressor High Temp/Standby Compressor Start

05/11/2018

264862

K-3B Service Air Compressor Discharge Temp High Alarm

Received

05/17/2018

291891

K-3B Service Air Compressor Improper Operation

11/21/2018

297959

K-3B Service Air Compressor Rapid Motor Vibration

Increase

01/15/2019

2308290

NI System Maintenance Rule Evaluation Inconsistencies

Identified

04/01/2019

2316963

U1 CW System Exceeds Maintenance Rule Performance

Criteria

06/05/2019

2317207

SA System Exceeds Maintenance Rule Performance Criteria

06/07/2019

Corrective Action

Documents

Resulting from

2308290

NI System Maintenance Rule Evaluation Inconsistencies

Identified

4/1/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Inspection

Miscellaneous

Service Air Reliability Event Report

04/01/2017-

04/29/2019

71111.13

Corrective Action

Documents

Resulting from

Inspection

2319493

IT-90 Train B Test Moved PRA Risk Review Not Done In

Advance

06/27/2019

2319494

DGB Door 107 Not Self Latching

06/27/2019

Miscellaneous

Station Logs

05/15-

16/2019

Point Beach Station Unit 1 and 2 Daily Status Report

06/19/2019

Point Beach Station Unit 1 and 2 Daily Status Report

05/15/2019

PBNP Shutdown Safety Assessment and Fire Inspection

Checklist

04/11/2019

Current Risk Summary Reports; PBN Unit 1 and 2

06/18-

21/2019

Current Risk Summary Report; PBN Unit 1 and 2

05/15/2019

Current Risk Summary Reports; PBN Unit 1 and 2

06/27-

28/2019

Point Beach Station Unit 1 and 2 Daily Status Report

06/28/2019

71111.15

Calculations

CN-CPS-07-8

Point Beach Reactor Coolant Flow Instrumentation Setpoint

and Uncertainty Calculation (1C-41)

Corrective Action

Documents

2308372

Steam Generator Snubber HS-9 Failed Functional Test

04/01/2019

2312347

Relay 1RC-3A Found De-Energized During Visual Inspection 04/26/2019

2315175

1P-011A IST PMT Not Performed After 1P-011B Re-Piping

U1R38

05/21/2019

Corrective Action

Documents

Resulting from

Inspection

2311877

CR 02308372 Canceled Versus Processed

04/23/2019

2312945

Water Up to ISI-850A-O (Operator) in Tendon Gallery

05/01/2019

Drawings

617F354, Sheet

4A1

Schematic Diagram - Inputs, Reactor Protection System

Train "A," Unit 1

Miscellaneous

257

Model 1154 Alphaline Pressure Transmitter

Operability

Evaluations

165

SSC Affected by Condition: 1&2 SI-00850A&B, RHR Pump

Suction from Sump B

11/06/2005

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

2315095

1P-11A had Elevated Vibrations During IT-12 Train A

05/21/2019

Procedures

MA-AA-203-1000

Maintenance Testing

RMP 9061-3

Anker Holth Snubber Removal, Functional Testing, and

Installation

Work Orders

40573498

1ICP 4.2-1 - RCS Flow Transmitter Outage Calibration

04/04/2019

40608261 37

1FT-414, 1FT-415, 1FT-416, RC Loop B Flow Transmitters

Span Adjustment

04/17/2019

40665209

1P-11A CCW Pump - Coupling Alignment Verification

06/12/2019

71111.18

Calculations

2014-06279

Time Available to Respond to Rising Lake Level

Engineering

Changes

EC - 281811

External Wave Run-up Flood Mitigation Strategy

EC-293289

Basis for Changing Monitored Lake Level from the Highest

of All Reporting Stations to the Mean of All Reporting

Stations

06/05/2019

Miscellaneous

2316179

PBF-2124A - Maximum Converted Lake (Doc Dist)

05/30/2019

PBF-2124a

Maximum Converted Lake Level Calculation

PBF-2124a

Average Converted Lake Level Calculation

PCR 2316179

CFR 50.59 Screening Form: PBF-2124a, Maximum

Converted Lake Level Calculation

06/05/2019

Procedures

AOP-13C

Severe Weather Conditions

71111.19

Corrective Action

Documents

2304474

PMT Failed on HX-105A

03/05/2019

2304487

Leakage on HX-105A

03/06/2019

2305348

PMT for WO 40543692, 2P-10A Coupling Lubrication

03/12/2019

2306539

Work Planning/Manage: PMT Guidance Inadequate

03/20/2019

2308538

1CV-296 1HX-2 Regen Hx To Aux Spray Valve Has No PMT

Task

04/02/2019

2315175

1P-011A IST PMT Not Performed After 1P-011B Re-Piping

U1R38

05/21/2019

Procedures

IT 12A

CC Pumps and Valves While Aligned for RHR Operation

(Cold Shutdown) Unit 1

Work Orders

2312548

K-2 Relay Found With Broken Center Post

04/29/2019

40543692 02

2P-010A/OPS PMT

01/17/2019

40582325 01

B52-DB50-011; Breaker Maintenance Per RMP-9303 and

RMP-9369-1

03/05/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

40611338

1DY-02, Maintain and Inspect Inverter

04/25/2019

40624975

1P-002A-Z/Replace Signal Conditioner Module

05/21/2019

40626242 02

1B52-13A; Setup and Stage Spare Breaker

05/02/2019

40664989 03

K-3B/Replace 1st and 2nd Stage Discharge Check Valves

06/27/2019

40664989 04

K-3B/OPS PMT

05/23/2019

WO 40104553-49

1P-011B - Operations PMT - RTS

71111.20

Corrective Action

Documents

2310563

Deficiencies Noted During CL 20/20A Walkdown

4/14/2019

2310581

CL-20 CTMT Walkdown Items Identified

4/15/2019

Corrective Action

Documents

Resulting from

Inspection

2310884

NRC Observations During NOP/NOT & Key Way Walkdown

04/16/2019

Drawings

500B728; Sheet

Main Control Board Component Wiring

541F091; Sheet 1 P&ID Reactor Coolant System

541F091; Sheet 2 P&ID Reactor Coolant System

Engineering

Changes

EC 292423

Point Beach Unit 1 Cycle 39 Core Reload Modifications

Miscellaneous

PBNP Shutdown Safety Assessment and Fire Inspection

Checklist

03/26 -

04/15/2019

Spent Fuel Pool Map After U1R38 Core Offload

4/30/2019

Spent Fuel Pool Map After U1R38 Outage

4/30/2019

Point Beach Component Move Sheet; U1R38 Core Reload

4/7-9/2019

Point Beach Component Move Sheet; U1R38 Core Offload

3/27-31/2019

Point Beach Component Move Sheet; U1R38 Insert Moves

3/31/2019

Point Beach Component Move Sheet; U1R38 Fuel Cleaning

3/31-

4/2/2019

Fatigue Management Work History from 03/23/2019 to

04/12/2019

04/12/2019

Outage Work Schedules for Operations, Maintenance, and

Fire Brigade

04/12/2019

AF AF-4000-O

Clearance Package

4/11/2019,

4/15/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

OP-3C Accum

Out

Clearance Package

4/15/2019

Procedures

ARB 1C04 1C 2-8 Alarm Response Book; BA Flow Deviation or Potential

Dilution in Progress

CL 2A

Defueled to Mode 6 Checklist

04/07/2019

CL 2B

Mode 6 to Mode 5 Checklist

04/07/2019

CL 2C

Mode 5 to Mode 4 Checklist

04/10/2019

CL 2D

Mode 4 to Mode 3 Checklist

04/16/2019

CL 2E

Mode 3 to Mode 2 Checklist

04/18/2019

CL 2F

Mode 2 to Mode 1 Checklist

04/18/2019

OP 1C Unit 1

Startup to Power Operation

OP 3C Unit 1

Hot Standby to Cold Shutdown Unit 1

03/26/2019

Work Orders

40511562

1ICP 6.15 - Perform Steps 5.1 through 5.5.7

9/1/2017

WO 40521042

1ICP 13.14 - Core Exit T/C Recorder Calibration

2/18/2017

WO 40573349

1ICP 2.8-1 NI Axial Offset Calibration

4/22/2019

71111.22

Corrective Action

Documents

296665

South SW Header Flowmeter Calibration

01/04/2019

2304475

P-32C SW Pump Performance Outside Acceptance Criteria

03/05/2019

2305377

Service Water South Header Flow Appears High

03/12/2019

2305380

Calibration of the SW South Header Flow Meter

03/12/2019

Corrective Action

Documents

Resulting from

Inspection

2310121

Procedure Use and Adherence Issue

04/11/2019

2310869

Rebaselining of P-32A and P-32C Improvements

04/16/2019

Miscellaneous

291226

10CFR50 Appendix J Program Routing Task - 2018-2019

04/14/2019

IST Program

Document

Inservice Testing Program Document

SCR 2014-0011

Revisions to IT 07C Following Rebaselining of P032C,

Service Water Pump

01/17/2014

Procedures

1-PT-RCS-1

Reactor Coolant System Pressure Test - Inside/Outside

Containment Unit 1

IT 230

Leak Test of Class 1 Components Following a Refueling

Shutdown Unit 1

IT 45 Train B

Safety Injection Valves Train B Unit 2

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

OI 58

Leak Testing of Containment Isolation Valves - Unit 1 and 2

General Instructions and Information

ORT 6

Containment Spray Sequence Test Unit 1

Work Orders

40573810 01

ORT 28, Cont DI H2O

04/13/2019

40610316 01

IT-07C, P-32C Service Water Pump Comprehensive Test

03/06/2019

71114.06

Corrective Action

Documents

2315151

EP Drill - Accountability in NES

05/21/2019

2315188

EP Pre-Existing Accountability

05/21/2019

2315195

NA Identified Gaps - EP Pre-Exercise (TSC)

05/21/2019

Miscellaneous

PBN EPR 192

001D

Emergency Preparedness (EP) Drill Manual for the 2019 EP

Pre-Exercise

05/21/2019

71124.01

Corrective Action

Documents

255246

Source Leak Check Documentation Gaps

03/21/2018

270541

Neutron Correction Factor Not Auto Adding Correctly

06/29/2018

285855

Dosimeter - Rate Alarm Encountered During Snubber

Inspection

10/15/2018

286293

Dosimeter Rate Alarm Received During Walk Down

10/17/2018

2308787

Unanticipated Dose Rate Alarm

04/03/2019

2309081

Unanticipated Rate Alarms Received During U-1 'A' S/G

Sludge

04/05/2019

Procedures

RP-AA-100-1002

Radiation Worker Instruction and Responsibilities

Revision 8

RP-AA-102-1000

Alpha Monitoring

Revision 4

Radiation

Surveys30-105

Airborne Radioactivity Survey

04/03/2019

30-106

Airborne Radioactivity Survey

04/03/2019

30-108

Airborne Radioactivity Survey

04/03/2019

30-112

Airborne Radioactivity Survey

04/03/2019

PBPROD-M-

20190300-20

Unit 1 Reactor Cavity - Upper Level - Initial Entry

03/22/2019

PBPROD-M-

20190325-30

U-1 Reactor Upper Cavity - Post Decon on Floor

03/25/2019

PBPROD-M-

20190331-39

66' U-1 Containment Shiftly Routine

03/31/2019

PBPROD-M-

20190401

66' U-1 Containment Shiftly Routine

04/01/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

PBPROD-M-

20190402-40

U1 Daily Outage Routines Spent Fuel Pool

04/02/2019

PBPROD-M-

20190402-55

Unit 1 Containment B Elevation 10 Foot Platform

04/02/2019

PBPROD-M-

20190403-21

Unit 1 B Cold Leg RTD Manifold Removal

04/02/2019

PBPROD-M-

20190403-25

BG C/L RTD Rebuild Tent

04/03/2019

PBPROD-M-

20190404-2

Reactor Coolant Pump Lower, B Side U1 Post

Shielding/Contamination Survey

04/04/2019

PBPROD-M-

20190404-30

Reactor Coolant Pump Lower, B Side U1 Job Coverage

04/04/2019

PBPROD-M-

20190404-32

Reactor Coolant Pump Lower, B Side U1 Impeller Removal

04/04/2019

PBPROD-M-

20190404-41

U1 Daily Outage Routines Spent Fuel Pool

04/04/2019

Radiation Work

Permits (RWPs)

19-1021

B RCP Maintenance Seal Replacement

Revision 2

19-1053

Unit 1 Narrow Range RTD Replacement

Revision 2

19-1056

FOSAR Activities

Revision 1

19-1057

S/G Eddy Current Testing

Revision 00

19-1064

Unit 1B RCP Impeller Change Out and Pump Bowl

Inspection

Revision 1

71124.02

ALARA Plans

R-003

Replace B Loop Hot Leg RTD Manifold and Refurbish B

Cold Leg Manifold (Mechanical Cut-Out and Replace)

03/29/2019

R-023

B RCP Rotating Element Change-Out

04/01/2019

R005

B RCP Seal, Motor Replacement and Maintenance

03/07/2019

R011

Steam Generator Eddy Current

03/06/2019

Corrective Action

Documents

2308213

Narrow Range RTD Replacement Work is Tracking Above

Estimate

03/31/2019

2308215

Additional Dose Needed for Added Scope on RV Head Work

03/31/2019

2309059

Dose Estimate Adjustment Needed on FOSAR Work

04/04/2019

Procedures

RP-AA-104-1000

ALARA Implementing Procedure

Revision 15

71124.03

ALARA Plans

Respirator Assessment for Radiation Work Permit 19-1064

04/01/2019

Respirator Assessment for Radiation Work Permit 19-1053

03/29/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Corrective Action

Documents

290219

HPIP 3.58.1 Air Sampling Process Instruction Review

11/09/2018

Miscellaneous

HP-100-101718

Review of Steam Generator Channel Head Ventilation

Practices

10/18/2018

Procedures

NISP-RP-008

Use and Control of HEPA Filtration and Vacuum Equipment Revision 1

NP 4.2.32

Respiratory Protection Program

Revision 18

Self-Assessments 02256550-02

Shared Ownership Gaps - Respiratory Protection Program

05/03/2018

AR 02294511-04

2018 Annual Respiratory Protection Program Assessment

01/11/2019

71124.04

Calculations

High Level Contamination Report and Associated Dose

Calculations for RWP 17-1027

10/28/2017

High Level Contamination Report and Associated Dose

Calculations for RWP 17-1016

10/28/2017

Whole Body Count Evaluation for Radiation Protection

Individual

04/08/2017

Whole Body Count Evaluation for Radiation Protection

Individual

10/29/2017

Whole Body Count Evaluation for BHI Individual

10/29/2017

Whole Body Count Evaluation for Maintenance Individual

05/14/2018

Corrective Action

Documents

253282

WBC Procedural Guidance Not Updated Following

Evaluation

03/08/2018

255763

Error in DACDOS Calculation

03/23/2018

Procedures

NP 4.2.15

Fetal Protection Policy Implementation

Revision 7

71124.06

Calculations

Calibration Factor Steam Line Monitors

06/21/1983

2013-0018

Radiological Effluent Initiating Condition Values For

Emergency Action Level RS1 and RG1

Revision 03

99-0106

Dose Rate Calculations for Steam Line Monitors Calibration

Factor

Revision 0

Miscellaneous

Permanent Procedure and Procedure Revision Review and

Approval for HPCAL 3.7, Steam Line Radiation Monitor

Calibration Procedure

04/21/1993

Permanent Procedure and Procedure Revision Review and

Approval for HPCAL 3.7, Steam Line Radiation Monitor

Calibration Procedure

08/20/1990

349-17-1

Certificate of Gamma Standard Source for Cs-137 Source

08/01/1989

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Number 349-17-1

65089-10

Certificate of Radioactivity Calibration for Kr-85 Source

Number 65089-10

10/01/1981

SDD-RASCAL-

20140110

Unified RASCAL Interface Technical Design Description

Revision 02

SRS-RASCAL-

20140110

Requirements Specification Unified RASCAL Interface

Revision 02

Procedures

HPCAL 3.17

SPING Calibration Procedure

Revision 0

Work Orders

4035767401

1RE-231 Calibration

03/18/2016

4046900301

RM-SPRING-23 Calibration

2/13/2017

4046911302

RM-SPING23 Pre-Calibration

2/13/2017

4047338801

1RE-231 Calibration

10/15/2017

71152

Corrective Action

Documents

286174

Thermal Loading from Design-Basis Accident Exceeds

Platform [Capacity]

10/16/2018

297419

Unit 2 Manway Platforms Thermal Loading Results

01/10/2019

2303987

Management Escalation: Procedure Use and Adherence

Gap

03/01/2019

2307731

MOV Diagnostic of 1SI-860C

03/28/2019

2307741

Maintenance Department Clock Reset

03/28/2019

2308008

Cognitive Trend: Procedure Use and Adherence

03/29/2019

2308185

Trend AR - BHI Human Performance Behaviors

03/31/2019

2308252

Combustible Liquid Quantity Exceeds TCCP Limit

03/31/2019

2308260

Compressed Flammable Gas Cylinders Exceed Limit

03/31/2019

2308895

Untreated Wood in PAB Truck Bay

04/04/2019

2309962

Escalation: Procedure Use and Adherence

04/10/2019

2311488

Data Entry Error During Generation of NIS Currents

04/20/2019

2311530

Unit 1 Enters LCO 3.4.1 PZR Pressure Less than 2205

04/21/2019

Corrective Action

Documents

Resulting from

Inspection

2314702

OP 3A, Power Operations to Hot Standby Step Performance

05/16/2019

Fire Plans

PFP-0-PAB 26

Pre-Fire Plan Unit 1 & Unit 2 Auxiliary Building 26

PFP-1-TB 8

Pre-Fire Plan Unit 1 Turbine Hall Building Elevation 8'

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Procedures

1RESP 6.1

Core Power Distribution and Nuclear Power Range

Calibration Unit 1

04/20/2019

NP 1.9.9

Transient Combustible Control

OP 3A Unit 1

Power Operation to Hot Standby Unit 1

Self-Assessments 2304521-01

Negative Trend in Fleet Engineering Program

Implementation

05/14/2019

2304925

PBN L1A on HU Recovery Effectiveness (RWA 02304925-

01)

03/28/2019