IR 05000263/2024001
ML24117A352 | |
Person / Time | |
---|---|
Site: | Monticello |
Issue date: | 04/29/2024 |
From: | Richard Skokowski NRC/RGN-III/DORS/RPB3 |
To: | Hafen S Northern States Power Company, Minnesota |
References | |
IR 2024001 | |
Download: ML24117A352 (1) | |
Text
SUBJECT:
MONTICELLO NUCLEAR GENERATING PLANT - INTEGRATED INSPECTION REPORT 05000263/2024001
Dear Shawn Hafen:
On March 31, 2024, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Monticello Nuclear Generating Plant. On April 11, 2024, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.
No findings or violations of more than minor significance were identified during this inspection.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely, Richard A. Skokowski, Chief Reactor Projects Branch 3 Division of Operating Reactor Safety Docket No. 05000263 License No. DPR-22
Enclosure:
As stated
Inspection Report
Docket Number: 05000263
License Number: DPR-22
Report Number: 05000263/2024001
Enterprise Identifier: I-2024-001-0075
Licensee: Northern States Power Company, Minnesota
Facility: Monticello Nuclear Generating Plant
Location: Monticello, MN
Inspection Dates: January 01, 2024 to March 31, 2024
Inspectors: N. Bolling, Acting Resident Inspector T. McGowan, Resident Inspector C. Norton, Senior Resident Inspector J. Reed, Health Physicist
Approved By: Richard A. Skokowski, Chief Reactor Projects Branch 3 Division of Operating Reactor Safety
Enclosure
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Monticello Nuclear Generating Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
No findings or violations of more than minor significance were identified.
Additional Tracking Items
Type Issue Number Title Report Section Status LER 05000263/2023-002-00 LER 2023-002-00 for 71153 Closed Monticello Nuclear Generating Plant, Reactor Scram and Containment Isolation due to Valve Responses during Main Turbine Control Valve Testing
LER 05000263/2023-003-00 LER 2023-003-00 for 71153 Closed Monticello Nuclear Generating Plant, Condition Prohibited by Technical Specifications due to Inoperable Main Steam Line Low Pressure Isolation Switch
PLANT STATUS
Monticello began the inspection period at rated thermal power. On February 28, 2024, the unit tripped and entered Mode 4. On March 2, 2024, the licensee commenced a reactor startup, and synced to the grid on March 3, 2024. The unit returned at or near rated thermal power on March 5, 2024. On March 27, 2024, the licensee performed a shutdown to Mode 4 to replace a safety relief valve. On March 30, 2024, the licensee commenced a unit startup, and synced to the grid on March 31, 2024, and ended the inspection period at 31% of rated thermal power.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Impending Severe Weather Sample (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated the adequacy of the overall preparations to protect risk-significant systems from impending severe weather on January 10, 2024.
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (1 Sample)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Emergency diesel generator (EDG) 11 starting air and fuel oil systems prior to making EDG 12 inoperable for testing on January 30, 2024
71111.05 - Fire Protection
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (7 Samples)
The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:
- (1) Fire Zone 1-E, high pressure coolant injection (HPCI) room on January 4, 2024
- (2) Fire Zone 1-G, control rod drive pump room on January 4, 2024
- (3) Fire Zone 14-A, upper 4KV bus area (14 and 16) on January 5, 2024
- (4) Fire Zone 12-A, lower 4KV bus area (13 and 15) on January 5, 2024
- (5) Fire Zone 1-C, reactor core isolation cooling room on January 10, 2024
- (6) Fire Zone 2-H, west shutdown cooling area on January 12, 2024
- (7) Fire Zone 33, emergency filtration building third floor on January 12, 2024
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (2 Samples)
- (1) The inspectors observed and evaluated licensed operator performance in the control room during reactor startup to critical and the point of adding heat on March 2, 2024.
- (2) The inspectors observed and evaluated licensed operator performance in the control room during reactor startup on March 31, 2024.
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
- (1) The inspectors observed and evaluated crew as found simulator exam on January 16, 2024.
71111.12 - Maintenance Effectiveness
Maintenance Effectiveness (IP Section 03.01) (2 Samples)
The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:
- (1) P111D, emergency service water (ESW) pump 14
- (2) F safety relief valve degrading tailpipe temperature on March 26, 2024
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:
- (1) Risk associated with the B feedwater regulating valve lockup on January 16, 2024
- (2) Risk associated with clamping C outboard main team isolation valve (MSIV)instrument air line on February 7, 2024
- (3) Risk associated with anticipated transient without scram reactor coolant pump trip reactor pressure restoration of setpoint after reactor SCRAM on February 29, 2024
- (4) Risk associated with cycling breaker 3A-CB1, reactor manual control system 120 VAC logic power supply on March 7, 2024
- (5) Risk associated with HPCI inboard steam isolation valve and failure of leak rate testing isolation valves on March 28, 2024
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 03.01) (6 Samples)
The inspectors evaluated the licensees justifications and actions associated with the following operability determinations and functionality assessments:
- (1) 501000081180, ESW 14 quarterly flow degradation
- (2) 501000080744, VD-9175B, B control room pressure control damper failed to open
- (3) 501000082034, inadvertent BKR 4300 operation
- (4) 501000082532, check valve failed during RHRSW quarterly
- (5) 501000082683, reactor pressure vessel bottom head cooldown rate >100 degrees per hour
- (6) 501000082407, LS-2-3-680F and LS-2-3-680H reactor feed pump and main turbine trip failure to reset
71111.18 - Plant Modifications
Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)
The inspectors evaluated the following temporary or permanent modifications:
- (1) VD-9175A emergency filtration train control room ventilation damper
71111.20 - Refueling and Other Outage Activities
Refueling/Other Outage Sample (IP Section 03.01) (2 Samples)
- (1) The inspectors evaluated forced outage MIF 3202 activities from February 28 to March 2, 2024.
- (2) The inspectors evaluated forced outage MIF 3203 activities from March 26 to 31, 2024.
71111.24 - Testing and Maintenance of Equipment Important to Risk
The inspectors evaluated the following testing and maintenance activities to verify system operability and/or functionality:
Post-Maintenance Testing (PMT) (IP Section 03.01) (10 Samples)
- (1) B.05.07-05, local manual control of feedwater regulating valves after repair of programable logic controller on January 20, 2024
- (2) Electric fire pump after replacement of the seal water PCV on February 27, 2024
- (3) K61D relay replacement, March 1, 2023
- (4) Reactor manual control system after power supply breaker exercising on March 7, 2024
- (5) HPCI governor actuator remote servo after maintenance on March 22, 2024
- (6) HPCI governor after maintenance on March 22, 2024
- (7) HPCI gland seal drain pump after maintenance on March 22, 2024
- (8) HPCI inlet steam trap drain after maintenance on March 22, 2024
- (9) HPCI exhaust pressure root valve after replacement on March 22, 2024
- (10) A Inboard MSIV after packing adjustment due to steam leak on March 31, 2024
Surveillance Testing (IP Section 03.01) (4 Samples)
- (1) Security system emergency generator operability check and alarm on January 8, 2024
- (2) EDG 12 quarterly test on January 29, 2024
- (3) Residual heat removal (RHR) pump 11 time delay over current relay calibration on March 5, 2024
- (4) 2-of-4 voter average power range monitor channel functional test on March 14, 2024
Inservice Testing (IST) (IP Section 03.01) (2 Samples)
- (1) RHR service water B pump testing on January 26, 2024
71114.06 - Drill Evaluation
Additional Drill and/or Training Evolution (1 Sample)
The inspectors evaluated:
- (1) Licensed operator requalification including emergency classification and notification on January 16,
RADIATION SAFETY
71124.08 - Radioactive Solid Waste Processing & Radioactive Material Handling,
Storage, & Transportation
Radioactive Material Storage (IP Section 03.01)
The inspectors evaluated the licensees performance in controlling, labeling, and securing the following radioactive materials:
- (1) 10 CFR 37 material storage locations
- (2) Radioactive materials stored outside the protected area
Radioactive Waste System Walkdown (IP Section 03.02) (2 Samples)
The inspectors walked down the following accessible portions of the solid radioactive waste systems and evaluated system configuration and functionality:
- (1) Condensates resin processing system
- (2) Reactor water clean-up (RWCU) system
Waste Characterization and Classification (IP Section 03.03) (2 Samples)
The inspectors evaluated the following characterization and classification of radioactive waste:
- (1) RWCU
- (2) Dry active waste (DAW)
Shipping Records (IP Section 03.05) (4 Samples)
The inspectors evaluated the following non-excepted radioactive material shipments through a record review:
- (1) Radioactive material shipment 23-57 containing control rod drive mechanisms in a general design package
- (2) Radioactive waste shipment 23-99 containing powder resin of class A waste in a general design package
- (3) Radioactive material shipment 24-04 containing control rod drive equipment in a general design package
- (4) Radioactive waste shipment 23-92 containing powder resin of class A waste in a general design package
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01)===
- (1) January 1, 2023, through December 31, 2023
IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) (1 Sample)
- (1) January 1, 2023, through December 31, 2023
IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (1 Sample)
- (1) January 1, 2023, through December 31, 2023
71153 - Follow Up of Events and Notices of Enforcement Discretion Event Follow up (IP Section 03.01)
- (1) The inspectors evaluated a reactor SCRAM with recirculation pump trip and licensees response on February 28, 2024.
Event Report (IP Section 03.02) (2 Samples)
The inspectors evaluated the following licensee event reports (LERs):
- (1) LER 05000263/2023-002-00, Reactor Scram and Containment Isolation due to Valve Responses during Main Turbine Control Valve Testing (ADAMS Accession No. ML23317A359). The inspectors determined that the cause of the condition described in the LER was not reasonably within the licensee's ability to foresee and correct, and therefore was not reasonably preventable. No performance deficiency nor violation of NRC requirements was identified. This LER is Closed.
- (2) LER 05000263/2023-003-00, Condition Prohibited by Technical Specifications due to Inoperable Main Steam Line Low Pressure Isolation Switch (ADAMS Accession No. ML23338A184). The inspectors determined that the cause of the condition described in the LER was not reasonably within the licensees ability to foresee and correct, and therefore was not reasonably preventable. The inspection conclusions associated with this LER are documented in this report under Inspection Results Section. This LER is Closed.
INSPECTION RESULTS
Minor Violation 71153 LER 05000263/2023-003-00, Condition Prohibited by Technical Specifications due to Inoperable Main Steam Line Low Pressure Isolation Switch
Minor Violation: The inspectors reviewed LER 05000263/2023-003-00, Condition Prohibited by Technical Specification (TS) due to Inoperable Main Steam Line Low Pressure Isolation Switch, for the licensees failure to comply with the actions required in TS limiting condition for operation (LCO) 3.3.6.1. Specifically, on October 7, 2023, at 0228 when the reactor entered Mode 1, the licensee failed to enter TS LCO 3.3.6.1 Condition A for One or more required channels inoperable, when the B1 main steam line low pressure isolation switch reset prior to its allowed TS value. This condition existed until it was discovered and corrected on October 10, 2023, at 0901 when the B1 main steam line low pressure isolation switch was recalibrated using TS Surveillance Requirement (SR) 3.3.6.1.4. As a result, the licensee operated in a condition prohibited by TS by failing to place the affected channel in trip within the required time in TS LCO 3.3.6.1 Condition A and subsequently failing to transition to Mode 2 by the required time in TS LCO 3.3.6.1 Condition E.
Screening: The inspectors determined the performance deficiency was minor.
Enforcement:
This failure to comply with Technical Specification 3.3.6.1 constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On April 11, 2024, the inspectors presented the integrated inspection results to Shawn Hafen, and other members of the licensee staff.
- On March 7, 2024, the inspectors presented the radiation protection baseline inspection results to K. Lorensen, Director Site Performance and Operations Support, and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection Type Designation Description or Title Revision or
Procedure Date
71111.01 Procedures 1444 Pre and Post Severe Weather Inspection Checklist 84
71111.04 Procedures 2154-14 Fuel Oil System Prestart Valve Checklist 20
2154-28 Diesel Generator Air Start System Prestart Valve Checklist 12
71111.05 Fire Plans Strategy A.13-12-Lower 4 KV Bus Area (13&15) 19
A
Strategy A.3-01-C RCIC Room and Appendix R Cable Enclosure 11
Strategy A.3-01-E HPCI Room - Reactor Building Elevation 896' 9
Strategy A.3-01-G Fire Zone 1-G, CRD Pump Room 5
Strategy A.3-02-H West Shutdown Cooling Area 10
Strategy A.3-14-A Upper 4KV Bus Area (14&16) 18
Strategy A.3-33 EFT Building Third Floor 13
71111.11Q Corrective Action 501000082463 IRM 12 HI HI Light on C-36 During SU 03/03/2024
Documents
Resulting from
Inspection
Miscellaneous RQ-SS-203 Loss of Control Rod Drive, Loss of Load Center 103, Bus 15 0
Lockout, Reactor Water Cleanup Leak Requiring Blowdown
Procedures 1371 Drywell Prestart Inspection 14
2159 Predicted Critical for Plant Startup 13
2167 Plant Startup 110
2167-04 Startup Checklist for Surveillance Requirements 12
2167-05 Startup Checklist for Transition from Mode 2 to Mode 1 5
2300 Reactivity Adjustment 27
253 B Defeat/Reinstall Drywell Personal Airlock Interlocks 11
71111.12 Procedures 0255-11-III-4 ESW 14 Quarterly Pump and Valve Tests 69
71111.13 Corrective Action 501000080923 B FRV Lockup 01/17/2024
Documents 501000080960 CV-6-12B-IL Amber Light Not Lit 01/17/2024
501000080971 PRA Model for Main FRV Configuration 01/17/2024
501000080986 Challenge Board Materials Timeliness 01/18/2024
Engineering 601000004946 Replace HPCI-1 and HPCI-2 0
Evaluations
Inspection Type Designation Description or Title Revision or
Procedure Date
Miscellaneous 700136403 Weld Control Record HPCI-1/HPCI-2 03/28/2024
FP-PA-HU-05 Type 2-Operational Decision Making Issue 02/06/2024
Evaluation - AO-2-86C (13 OTBD MSIV) Pilot Air Line
FP-WM-IRM-01 Planning and Approval of High Risk or Scheduled Risk 02/29/2024
Work - Restore Set-Point PIS-2-3-678C
Procedures B.05.07-03 Local Manual Control of Main FW Reg Valves 29
C.6-005-B-40 FW Control Valve Locked 4
Work Orders 7000091883 3A-CB1-Cycle Breaker 0
700130106-0020 ATWS RCP Trip Reactor Pressure 1
700136403-0030 M-2035 Upstream Test/Drain 0
71111.15 Calculations16-062 Development of Test Acceptance Criteria Basis for Monticello 0A
FSW Pumps
Corrective Action 501000058253 V-D-9175A Failed to Open 05/19/2022
Documents 501000068971 V-EAC-14A Tripped During CRV Swap 01/09/2023
501000075980 VD-9175B Didnt Open When B CRV Placed in Service 08/13/2023
501000077303 VD-9175B Does Not Open 10/02/2023
501000078405 0255-11-III-4 Flow Less Than 71.0 gpm 10/30/2024
501000080176 VD-9175B Failed to Open 12/20/2023
501000080744 VD-9175B Failed to Open 01/10/2024
501000081180 14 ESW Quarterly Flow Degradation 01/23/2024
501000082034 Inadvertent BKR 4300 Operation 02/18/2024
501000082407 High Level Trips Not Clearing 03/01/2024
501000082532 Check Valve Failed During RHRSW Quarterly 03/05/2024
501000082683 RPV Bottom Head Cooldown Rate>100/hr 03/08/2024
501000082684 Further Evaluation Needed for 501000082683 03/09/2024
Drawings NH-170037 Main Control Room CRV/EFT System 84
Engineering 2400420.401 Initial Operability Summary for the MNGP Reactor Pressure 03/08/2024
Evaluations Vessel Bottom Head
Procedures 0255-05-IA-1-1 A RHRSW Quarterly Pump and Valve Tests 93
255-11-III-4 14 ESW Quarterly Pump and Valve Tests 69
B.09.07-05 Operations Manual Section: 480 Volt Station Auxiliary 65
EC 13410 Evaluate Failure of SW-21-1, 21-2, 22-1, and 22-2 through 0
3/4 Inch Keep Fill Lines
Inspection Type Designation Description or Title Revision or
Procedure Date
71111.18 Drawings ECR4849-NX-Control Panel C243A Wiring Diagram 0-76
20010-29
ECR4849-NX-Control Panel C243A Wiring Diagram 0-E
20010-32
NE-93503-18 Damper VD-9175A Control Scheme V211 Channel 1 8
NE-93527 Loop Diagram Outlet Flow From V-ERF-14-A/B Flow Control 76
Engineering ECR Modify EFT Hydramotor Damper Logic 0
Changes 601000004849
71111.20 Procedures 2140 Deinerting Primary Containment 36
2167 Plant Startup 110
2167-03 Startup Transition from Mode 4 to Mode 2 23
204 Plant Shutdown 83
2300 Reactivity Maneuvering Steps 0
2404-03 Shutdown Checklist Transition from Mode 3 to Mode 4 7
B.03.04-05 D.1. Shutdown Cooling Mode-Loop A Startup 96
OSP-CRD-0539-Control Rod Testing 6
A
OSP-NIS-0042 IRM Functional Test 3
OSP-NIS-0047 SRM Functional Test 5
71111.24 Corrective Action 501000080637 Over Crank Alarm Received 01/08/2024
Documents
Procedures 0187-02 Emergency Diesel Generator 12/Emergency Service Water 111
Quarterly Pump and Valve Tests
255-04-IA-2 RHR System Cold Shutdown Valve Operability Tests 36
255-05-IA-1-2 B RHRSW Quarterly Pump and Valve Tests 93
255-06-IA-1 HPCI Quarterly Pump and Valve Tests 113
255-06-IA-1 HPCI Quarterly Pump and Valve Tests 113
298-02 Security System Emergency Generator Operability 32
Check & Alarm
1069 HPCI Flow Control System Dynamic Test Procedure 29
4850-504-PM 152-504, 11 RHR Pump Relay Maintenance, Calibration and 14
Trip Testing
B.08.05-05 Start P-110 Electric Fire Pump 52
Inspection Type Designation Description or Title Revision or
Procedure Date
ISP-NIP-0586 2-of-4 Voter Channel Functional Check 8
OPS MAN Main Steam 44
B.02.04-05
OPs Man Rod Worth Minimizer 24
B.05.02-05
OPS Man Startup of RHRSW Pump 50
B.08.01.03-05
OSP-MSC-0542-Breaker Alignment and Indicating Power Availability 1
Verification of Required Offsite Circuits
PCV-3163 Seal Water PCV to Electric Fire Pump (P-110) 0
PMT/RTS
Work Orders 700080595-0020 Replace Relay K61D 5
700091883 PMT/RTS Instructions After RMCS 120 Control Power Breaker 03/07/2024
Cycling
700112498-0010 Security System EDG - Annual Check 01/08/2024
700133351-0070 MT:1CFW:CV-6-12B, B Main Feed Water Regulation Valve 1
700136470-0010 11 INBD MSIV AO-2-80-A Adjust Packing 2
71114.06 Procedures FP-EP-EPIP-01 ERO Position Checklist 0
71124.08 Corrective Action 501000073443 Class B RW Shipment to Non-QSL Location 05/09/2023
Documents 501000078865 NOS: Issues in Rad Waste Shipment Record 11/09/2023
501000079937 Rad Waste Drumming Aisle 12/11/2023
501000081633 Lost Part 61 Paperwork 02/04/2024
Corrective Action 501000082538 Storage of RAM Outside PA 03/05/2024
Documents 501000082591 Records Legibility Issues 03/05/2024
Resulting from 501000082605 Shipment 23-92 Documentation 03/06/2024
Inspection 501000082628 Accurate Records Submission 06/06/2024
Engineering ECR RDS-1000 Replacement 03/23/2023
Changes 601000003555
Engineering 20-002 Evaluation of Used Oil for Radiological Contamination 00
Evaluations
Procedures 5863 Dewatering Resins in Waste Liners 31
FP-RP-RW-001 Additional Security Measures for Transportation of Radioactive 09
Material Part 37 Category 1 Quantities
Inspection Type Designation Description or Title Revision or
Procedure Date
FP-RP-RW-02 Radioactive Shipping Procedure 25
FP-RP-RW-03 10CFR37 Material Accountability 04
FP-RP-RW-09 Rad Waste Streams and Scaling Factors 00
PCP-01 Process Control Program for Wet Radioactive Wastes 02
R.06.09 Storage and Inventory of Radioactive Material Outside the 26
Power Block
Self-Assessments 600001146487 NRC Inspection Activities for IP71124.08. 12/15/2023
606000002023 71124.08 Radioactive Solid Waste Processing and 12/05/2023
Radioactive Material Handling, Storage, and Transportation
Shipping Records 2022 RWCU 10CFR61 Analysis for Reactor Water Clean-Up 08/08/2022
50/50 Mix
23-57 Shipping Papers for Twelve Control Rod Drive Mechanisms 05/09/2023
23-92 Shipping Papers for Dewatered Powder Resin 08/18/2023
23-99 Shipping Papers for Dewatered Powder Resin 09/22/2023
24-04 Shipping Papers for CRD Handling System Tooling 01/16/2024
L101029 10CFR61 Analysis for Secondary Resin Waste Stream 02/05/2024
L101029-3 10CFR61 Analysis for Dry Active Waste (DAW) 02/05/2024
Work Orders 700120331-0010 Semiannual Source Inventory and Smear Test 12/13/2023
71151 Miscellaneous QF0445 Monthly Operating Report - Generation Occurrences, 18
January 2023 - December 2023
71153 Drawings NF-36790 Reactor Vessel Thermocouple Locations & Expansion Lead 77
Miscellaneous FP-E-TS-01 Troubleshooting Plan PCIS - Group 1 Isolation 9
FP-PA-CSE-01 Cause Evaluation Template Reactor Scram Number 141 21
FP-PA-CSE-01 Equipment Cause Evaluation PS-2-134B Out of As-Found 12
FP-PA-HU-05 Type 2 - Operational Decision Making Issue Evaluation Group 11
Isolation on Main Steam Line High Flow
Operability FP-OP-OL-01 Past Operability Review PS-2-134B 5
Evaluations
Procedures 0058-B Main Steam Line Low Pressure Group 1 Isolation Instrument 17
Test and Calibration (RX in Run)
0118 Reactor Vessel Temperature Monitoring 23
B.01.04-05 Reactor Recirculation System H.6 Stratification Recovery 61
FP-OP-REP-01 Event Reporting and Notification Process 13
14