|
---|
Category:Letter
MONTHYEARML24283A1192024-10-28028 October 2024 Letter to Shawn Hafen, Re Monticello Subsequent License Renewal Schedule Change L-MT-24-038, Subsequent License Renewal Application Response to Request for Additional Information - 3rd Round RAI2024-10-15015 October 2024 Subsequent License Renewal Application Response to Request for Additional Information - 3rd Round RAI ML24277A0202024-10-0303 October 2024 Operator Licensing Examination Approval Monticello Nuclear Generating Plant, October 2024 ML24199A1752024-10-0101 October 2024 Issuance of Amendment No. 212 Revise Technical Specification 3.8.6, Battery Parameters, Surveillance Requirement 3.8.6.6 IR 05000263/20240112024-10-0101 October 2024 Biennial Problem Identification and Resolution Inspection Report 05000263/2024011 L-MT-24-025, Application to Revise Technical Specifications to Adopt TSTF-554, Revise Reactor Coolant Leakage Requirements2024-09-26026 September 2024 Application to Revise Technical Specifications to Adopt TSTF-554, Revise Reactor Coolant Leakage Requirements L-MT-24-029, Subsequent License Renewal Application Response to Request for Additional Information and Request for Confirmation of Information-Supplement to Set 1 Part 2 and Response to 2ci Round RAI2024-09-13013 September 2024 Subsequent License Renewal Application Response to Request for Additional Information and Request for Confirmation of Information-Supplement to Set 1 Part 2 and Response to 2ci Round RAI IR 05000263/20240052024-08-30030 August 2024 Updated Inspection Plan and Follow-Up Letter for Monticello Nuclear Generating Plant, Unit 1 (Report 05000263/2024005) L-MT-24-028, Response to RCI for RR-017 ISI Impracticality2024-08-28028 August 2024 Response to RCI for RR-017 ISI Impracticality ML24222A1822024-08-27027 August 2024 – Proposed Alternative Request VR-09 to the Inservice Testing Requirements of the ASME OM Code for Main Steam Safety Relief Valves 05000263/LER-2024-002, Low Pressure Coolant Injection Inoperable Due to Motor Valve Failure2024-08-27027 August 2024 Low Pressure Coolant Injection Inoperable Due to Motor Valve Failure IR 05000263/20244202024-08-21021 August 2024 Security Baseline Inspection Report 05000263/2024420 - Cover Letter IR 05000263/20240022024-08-14014 August 2024 Integrated Inspection Report 05000263/2024002 ML24218A2282024-08-0505 August 2024 Request for Confirmation of Information for Relief Request RR-017, Inservice Inspection Impracticality During the Fifth Ten-Year Interval ML24208A1502024-07-26026 July 2024 Independent Spent Fuel Storage Installation - Submittal of Quality Assurance Topical Report (NSPM-1) ML24215A2992024-07-23023 July 2024 Minnesota State Historic Preservation Office Comments on Monticello SLR Draft EIS ML24198A2372024-07-18018 July 2024 Information Request to Support Upcoming Biennial Problem Identification and Resolution (Pi&R) Inspection at Monticello Nuclear Generating Plant L-MT-24-022, – Preparation and Scheduling of Operator Licensing Examinations2024-07-0909 July 2024 – Preparation and Scheduling of Operator Licensing Examinations ML24164A2402024-06-10010 June 2024 Minnesota State Historic Preservation Office- Comments on Draft Monticello SLR Draft EIS L-MT-24-019, Submittal of ASME Section XI, Section IWB-3720 Analytical Evaluation in Accordance with 10 CFR 50.55a(b)(2)(xliii)2024-06-10010 June 2024 Submittal of ASME Section XI, Section IWB-3720 Analytical Evaluation in Accordance with 10 CFR 50.55a(b)(2)(xliii) L-MT-24-017, Response to Request for Additional Information Regarding License Amendment Request to Revise Monticello Technical Specification Surveillance Requirement 3.8.6.6 (EPID-L-2023-LLA-01602024-06-0404 June 2024 Response to Request for Additional Information Regarding License Amendment Request to Revise Monticello Technical Specification Surveillance Requirement 3.8.6.6 (EPID-L-2023-LLA-0160 ML24137A2792024-06-0303 June 2024 Audit Summary for License Amendment Request to Revise Technical Specification 3.8.6, Battery Parameters, Surveillance Requirement 3.8.6.6 ML24141A1292024-05-22022 May 2024 Northern States Power Company - Use of Encryption Software for Electronic Transmission of Safeguards Information ML24141A1782024-05-20020 May 2024 Information Request to Support the NRC Annual Baseline Emergency Action Level and Emergency Plan Changes Inspection L-MT-24-015, Response to Request for Additional Information - Alternative Request VR-09 for OMN-172024-05-16016 May 2024 Response to Request for Additional Information - Alternative Request VR-09 for OMN-17 L-MT-24-013, 2023 Annual Radiological Environmental Operating Report2024-05-14014 May 2024 2023 Annual Radiological Environmental Operating Report ML24135A1902024-05-14014 May 2024 Submittal of 2023 Annual Radioactive Effluent Release Report IR 05000263/20240102024-05-13013 May 2024 Age-Related Degrading Inspection Report 05000263/2024010 ML24128A0042024-05-0909 May 2024 Letter to Minnesota State Historic Preservation Office- Section 106 Consultation Regarding the Monticello Nuclear Generating Plant Subsequent License Renewal Application ML24127A1472024-05-0909 May 2024 Letter to Mille Lacs Band- Section 106 Consultation Regarding the Monticello Nuclear Generating Plant Subsequent License Renew. Application L-MT-24-016, 2023 Annual Report of Individual Monitoring for the Monticello Nuclear Generating Plant (MNGP)2024-05-0808 May 2024 2023 Annual Report of Individual Monitoring for the Monticello Nuclear Generating Plant (MNGP) ML24089A2382024-04-29029 April 2024 Summary of Nuclear Property Insurance IR 05000263/20240012024-04-29029 April 2024 Plan - Integrated Inspection Report 05000263/2024001 ML24115A2902024-04-25025 April 2024 Sec106 Tribal, Jackson-Street, Lonna-Spirit Lake Nation ML24115A2872024-04-25025 April 2024 Sec106 Tribal, Dupuis, Kevin-Fond Du Lac Band of Lake Superior Chippewa ML24115A2932024-04-25025 April 2024 Sec106 Tribal, Johnson, Grant-Prairie Island Indian Community ML24115A3062024-04-25025 April 2024 Sec106 Tribal, Wassana, Reggie-Cheyenne and Arapaho Tribes 05000263/LER-2024-001, Reactor Scram, Containment Isolation, and Cooldown Rate Outside of Limits Following Technician Adjustment of Wrong Component2024-04-25025 April 2024 Reactor Scram, Containment Isolation, and Cooldown Rate Outside of Limits Following Technician Adjustment of Wrong Component ML24115A3032024-04-25025 April 2024 Sec106 Tribal, Taylor, Louis-Lac Courte Oreilles Band of Lake Superior Chippewa Indians ML24115A3002024-04-25025 April 2024 Sec106 Tribal, Rhodd, Timothy-Iowa Tribe of Kansas and Nebraska ML24115A2972024-04-25025 April 2024 Sec106 Tribal, Miller, Cole-Shakopee Mdewakanton Sioux Community ML24115A2962024-04-25025 April 2024 Sec106 Tribal, Larsen, Robert-Lower Sioux Indian Community ML24115A2952024-04-25025 April 2024 Sec106 Tribal, Kakkak, Gena-Menominee Indian Tribe of Wisconsin ML24115A2982024-04-25025 April 2024 Sec106 Tribal, Reider, Anthony-Flandreau Santee Sioux Tribe ML24115A2912024-04-25025 April 2024 Sec106 Tribal, Jacskon, Sr., Faron-Leech Lake Band of Ojibwe ML24115A3052024-04-25025 April 2024 Sec106 Tribal, Vanzile, Jr., Robert-Sokaogon Chippewa Community ML24115A2992024-04-25025 April 2024 Sec106 Tribal, Renville, J. Garret-Sisseton Wahpeton Oyate of the Lake Travers Reservation ML24115A3022024-04-25025 April 2024 Sec106 Tribal, Stiffarm, Jeffrey-Fort Belknap Indian Community ML24115A3072024-04-25025 April 2024 Sec106 Tribal, Williams, Jr., James-Lac Vieux Desert Band of Lake Superior Chippewa Indians ML24115A2892024-04-25025 April 2024 Sec106 Tribal, Fowler, Thomas-St. Croix Chippewa of Wisconsin 2024-09-26
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000263/LER-2024-002, Low Pressure Coolant Injection Inoperable Due to Motor Valve Failure2024-08-27027 August 2024 Low Pressure Coolant Injection Inoperable Due to Motor Valve Failure 05000263/LER-2024-001, Reactor Scram, Containment Isolation, and Cooldown Rate Outside of Limits Following Technician Adjustment of Wrong Component2024-04-25025 April 2024 Reactor Scram, Containment Isolation, and Cooldown Rate Outside of Limits Following Technician Adjustment of Wrong Component 05000263/LER-2023-003, Condition Prohibited by Technical Specifications Due to Inoperable Main Steam Line Low Pressure Isolation Switch2023-12-0404 December 2023 Condition Prohibited by Technical Specifications Due to Inoperable Main Steam Line Low Pressure Isolation Switch 05000263/LER-2023-002, Reactor Scram and Containment Isolation Due to Valve Responses During Main Turbine Control Valve Testing2023-11-13013 November 2023 Reactor Scram and Containment Isolation Due to Valve Responses During Main Turbine Control Valve Testing 05000263/LER-2023-001, Main Steam Isolation Valve Leakage Exceeds Technical Specification Requirements Due to Stem Scoring2023-05-17017 May 2023 Main Steam Isolation Valve Leakage Exceeds Technical Specification Requirements Due to Stem Scoring 05000263/LER-2022-001, Loss of Control Room Envelope Operability2022-07-0707 July 2022 Loss of Control Room Envelope Operability 05000263/LER-2017-0062018-01-12012 January 2018 Loss of Reactor Protection System Scram Function During Main Steam Isolation Valve and Turbine Stop Valve Channel Functional Tests due to Use of a Test Fixture, LER 17-006-00 for Monticello Regarding Loss of Reactor Protection System Scram Function During Main Steam Isolation Valve and Turbine Stop Valve Channel Functional Tests Due to Use of a Test Fixture 05000263/LER-2017-0052017-09-20020 September 2017 Diesel Generator Emergency Service Water System Automatic Transfer to Alternate Shutdown Panel, LER 17-005-00 for Monticello Nuclear Generating Plant Regarding Diesel Generator Emergency Service Water System Automatic Transfer to Alternate Shutdown Panel 05000263/LER-2015-0042017-08-22022 August 2017 Past Inoperability of Turbine Stop Valve Scram Function Exceeded Technical Specification Requirements, LER 15-004-01 for Monticello Regarding Past Inoperability of Turbine Stop Valve Scram Function Exceeded Technical Specification Requirements 05000263/LER-2017-0042017-08-16016 August 2017 High Pressure Coolant Injection Steam Stop Valve Failed to Open During Test, LER 17-004-00 for Monticello Regarding High Pressure Coolant Injection Steam Stop Valve Failed to Open During Test 05000263/LER-2017-0032017-06-14014 June 2017 Main Steam Isolation Valve Leakage Exceeds Technical Specification Limits, LER 17-003-00 for Monticello Regarding Main Steam Isolation Valve Leakage Exceeds Technical Specification Limits 05000263/LER-2017-0022017-06-13013 June 2017 Main Steam Isolation Valve Closure Time Outside of Technical Specification Requirements, LER 17-002-00 for Monticello Nuclear Generating Plant Regarding Main Steam Isolation Valve Closure Time Outside of Technical Specification Requirements 05000263/LER-2017-0012017-06-13013 June 2017 Reactor Scram and Group II Isolation Due to 11 Reactor Feed Pump (RFP) Removal from Service with 12 RFP Isolated, LER 17-001-00 for Monticello Regarding Reactor Scram and Group II Isolation Due to 11 Reactor Feed Pump (RFP) Removal from Service with 12 RFP Isolated 05000263/LER-2016-0012017-05-25025 May 2017 High Pressure Coolant Injection System Cracked Pipe Nipple Caused Oil Leak, LER 16-001-02 for Monticello Regarding High Pressure Coolant Injection System Cracked Pipe Nipple Caused Oil Leak 05000263/LER-2016-0032017-05-25025 May 2017 HPCI Declared Inoperable Due to Excessive Water Level in Turbine, LER 16-003-01 for Monticello Regarding HPCI Declared Inoperable Due to Excessive Water Level in Turbine 05000263/LER-2016-0022016-09-30030 September 2016 Inadequate Appendix R Fire Barrier Impacts Safe Shutdown Capability, LER 16-002-00 for Monticello Regarding Inadequate Appendix R Fire Barrier Impacts Safe Shutdown Capability 05000263/LER-2014-0022016-07-13013 July 2016 Torus to Drywell Vacuum Breaker Did Not Indicate Closed During Testing, LER 14-002-01 for Monticello Regarding Torus to Drywell Vacuum Breaker Did Not Indicate Closed During Testing 05000263/LER-2014-0032016-07-13013 July 2016 Torus to Drywell Vacuum Breaker Dual Indication During Testing, LER 14-003-01 for Monticello Nuclear Generating Plant RE: Torus to Drywell Vacuum Breaker Dual Indication During Testing 05000263/LER-2015-0072016-01-21021 January 2016 Loss of Residual Heat Removal Capability, LER 15-007-00 for Monticello Regarding Loss of Residual Heat Removal Capability 05000263/LER-2015-0062016-01-21021 January 2016 - Reactor Scram due to Group 1 Isolation from Foreign Material in the Main Steam Flow Instrument Line, LER 15-006-00 for Monticello Regarding Reactor Scram due to Group 1 Isolation from Foreign Material in the Main Steam Flow Instrument Line ML1015505712009-09-12012 September 2009 Event Notification for Monticello on State Offsite Notification Due to Not Meeting Permit Requirements L-MT-05-035, LER 50-004-00 for Monticello Nuclear Generating Plant Regarding Voluntary LER for Control Rod Drive Insert Line Leakage2005-05-12012 May 2005 LER 50-004-00 for Monticello Nuclear Generating Plant Regarding Voluntary LER for Control Rod Drive Insert Line Leakage ML0216100952002-05-15015 May 2002 LERs 02-001-01 & 02-002-01 for Monticello Nuclear Generating Plant Re Mechanical Pressure Regulator Failure Causes Reactor Scram & Application of Instrument Deviation Acceptance Criteria Allowed As-Found Settings to Be Outside Tech Spec Val 2024-08-27
[Table view] |
LER-2023-002, Reactor Scram and Containment Isolation Due to Valve Responses During Main Turbine Control Valve Testing |
Event date: |
|
---|
Report date: |
|
---|
Reporting criterion: |
10 CFR 50.73(a)(2)(iv)(A), System Actuation |
---|
2632023002R00 - NRC Website |
|
text
(l Xcel Energy* 2807 West County Road 75 Monticello, MN 55362
November 13, 2023 L-MT-23-048 10 CFR 50.73
ATTN: Document Control Desk U.S. Nuclear Regulatory Commission Washington, DC 20555-0001
Monticello Nuclear Generating Plant Docket No. 50-263 Renewed Facility Operating License No. DPR-22
Monticello Nuclear Generating Plant Licensee Event Report 2023-002-00
Northern States Power Company, a Minnesota corporation, doing business as Xcel Energy (hereafter "NSPM"), hereby submits Licensee Event Report (LER) 50-263/2023-002-00 per 10 CFR 50.73(a)(2)(iv)(A).
If you have any questions about this submittal, please contact Carrie Seipp, Senior Regulatory Engineer, at 612-330-5576.
Summary of Commitments
This letter makes no new commitments and no revisions to existing commitments.
r:-) /,,,- az: __ _
/1/-/ -. 1J, / b"' "' * '-------" '
Greg D Brown Plant Manager, Monticello Nuclear Generating Plant Northern States Power Company - Minnesota
Enclosure
cc : Administrator, Region 111, USNRC Project Manager, Monticello, USNRC Resident Inspector, Monticello, USNRC State of Minnesota ENCLOSURE
MONTICELLO NUCLEAR GENERATING PLANT LICENSEE EVENT REPORT 50 -263/2023- 002-00
3 pages follow
Abstract
On September 27, 2023 at 1041 CDT, with Monticello Nuclear Generating Plant in Mode 1 at approximately 75 percent power for the semiannual Turbine Control Valve (CV) test, an unplanned Reactor Scram, Group I Primary Containment Isolation, and Group II Primary Containment Isolation occurred.
The cause of the Reactor Scram was exceeding the Reactor Pressure Vessel (RPV) high pressure scram setpoint during CV testing. CV-1, CV-2 and CV-3 percentage open did not increase enough when CV-4 was closed for testing. The reduction in steam flow caused the RPV pressure to exceed the scram setpoint. Subsequently, an expected low RPV level caused the Group II Primary Containment Isolation. The cause of the Group I Primary Containment Isolation was a transient in the steam line high flow instrumentation sensing lines for the C Main Steam Line.
Corrective actions included inspection and adjustment of the four CVs to within manufacturer's specifications. Channel calibration and functional tests were performed to verify that all C Main Steam Line flow instruments met requirements.
EVENT DESCRIPTION
On September 27, 2023 Monticello Nuclear Generating Plant (MNGP) was operating in Mode 1 and approximately 75 percent power for the semiannual Turbine-Generator Operational Tests. At 1041 Central Daylight Time (CDT), while cycling closed the Turbine Control Valve 4 (CV-4) per the Turbine CV Test, an unplanned Reactor Scram, Group I Primary Containment Isolation, and Group II Primary Containment Isolation occurred.
This event is reportable under 10 CFR 50.73(a)(2)(iv)(A) for an event or condition that resulted in the automatic actuation of the Reactor Protection System (RPS) [EIIS CODE: JC] including reactor scram and containment isolation signals affecting containment isolation valves in more than one system and multiple Main Steam Isolation Valves (MSIVs) [EIIS CODE: ISV].
EVENT ANALYSIS
The Turbine Control Valves (CVs) [EIIS CODE: FCV] are a part of the MNGP Main Turbine System [EIIS CODE: TA].
The CVs control reactor pressure, in conjunction with the turbine bypass valves, by adjusting position to control steam flow.
During the semiannual Turbine-Generator Operational Tests, reactor power is reduced to approximately 75 percent to allow for testing of each of the four CVs. While one CV is stroked closed, the other three CVs are expected to increase percent open to compensate for the increased reactor pressure. While stroking CV-4 closed per the procedure, the percent open of CV-1 and CV-2 initially increased then stalled and CV-3 percent open did not change. In turn, total steam flow through the CVs lowered and the reactor pressure exceeded the (RPV) high pressure scram setpoint, resulting in an automatic Reactor Scram. The RPV water level lowered to below the Group II isolation setpoint as expected, resulting in a Group II Primary Containment Isolation. Additionally, a Main Steam Line high flow condition was sensed in C Main Steam Line, resulting in a Group I Primary Containment Isolation and closure of the Main Steam Isolation Valves. There were no structures, systems, or components (SSCs) whose inoperability contributed to this event.
ASSESSMENT OF SAFETY CONSEQUENCES
All safety systems functioned properly during the transient. All control rods fully inserted during the scram. The High Pressure Coolant Injection (HPCI) system was placed in service to control RPV pressure, but HPCI did not inject into the RPV and was not needed to control RPV water level.
There were no radiological, environmental, or industrial impacts associated with this event. The health and safety of the public and site personnel were not impacted during this event.
CAUSE OF THE EVENT
The cause of the RPV high pressure scram setpoint being exceeded was attributed to performance of Control Valve testing with the operating CVs just below the transition point between the large outer piston and the smaller inner piston of the actuator. The transition requires an increased hydraulic pressure to continue moving the CV in the open direction. In the test configuration, this can result in the CV stalling at the transition point. The transition point can occur at a slightly different percentage open for each valve based on control valve actuator settings, linkage tolerances, and valve wear.
During troubleshooting of the event, it was identified that maintenance performed on the CVs in April 2023 changed the transition points for the valves which affected how the valves respond to system demand at test conditions. Troubleshooting identified that only CV-4 was above the transition point prior to the close stroke test of the other CVs. That is, CV-4 did not move through the transition point and performed the largest percentage open adjustments to control reactor pressure during close stroke testing of CV-1, CV-2, and CV-3. However, CV-1, CV-2, and CV-3 were operating just below their transition points during testing. When CV-4 was stroked closed, CV-1, CV-2, and CV-3 were not able to overcome the transition point to increase the percent open enough, and without the increased steam flow, the RPV pressure exceeded the Reactor Scram setpoint. As expected, the RPV water level lowered to below the Group II isolation setpoint, res ulting in a Group II Primary Containment Isolation.
The cause of the Group I Primary Containment Isolation was a sensed, rather than actual, high steam line flow on the C Main Steam Line. Plant process computer data showed a transient on the C Main Steam Line flow transmitter. This transient was sensed as high flow by the Group I isolation high steam flow logic. No actual steam leak existed as determined via redundant indications and system walkdown.
CORRECTIVE ACTIONS
CV-1, CV-2, CV-3, and CV-4 were inspected and adjusted to the manufacturer's recommended control valve actuator settings, including adjustment of the operating cylinder closed end overtravel and control valve cracking points. Hysteresis testing confirmed that actuator transition points were within manufacturer's specifications. The valves were retested satisfactorily.
Channel calibration and functional tests were performed to verify that all C Main Steam Line flow instruments met requirements. No adjustments were needed.
PREVIOUS SIMILAR EVENTS
No previous similar events have occurred at MNGP in the prior 3 years.