IR 05000261/2019003

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Integrated Inspection Report 05000261/2019003
ML19318F778
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 11/14/2019
From: Randy Musser
NRC/RGN-II/DRP/RPB3
To: Kapopoulos E
Duke Energy Progress
A. Wilson RGN-II/DRP
References
IR 2019003
Download: ML19318F778 (10)


Text

November 14, 2019

SUBJECT:

H.B. ROBINSON STEAM ELECTRIC PLANT - INTEGRATED INSPECTION REPORT 05000261/2019003

Dear Mr. Kapopoulos:

On September 30, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at H.B. Robinson Steam Electric Plant. On October 16, 2019, the NRC inspectors discussed the results of this inspection with Ms. Nicole Flippin, General Plant Manager, and other members of your staff. The results of this inspection are documented in the enclosed report.

No NRC-identified or self-revealing findings were identified during this inspection.

A licensee-identified violation which was determined to be of very low safety significance is documented in this report. We are treating this violation as a non-cited violation (NCV)

consistent with Section 2.3.2 of the Enforcement Policy.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Randall A. Musser, Chief Reactor Projects Branch 3 Division of Reactor Projects

Docket No. 05000261 License No. DPR-23

Enclosure:

As stated

Inspection Report

Docket Number:

05000261

License Number:

DPR-23

Report Number:

05000261/2019003

Enterprise Identifier:

I-2019-003-0017

Licensee:

Duke Energy Progress, LLC

Facility:

H.B. Robinson Steam Electric Plant

Location:

3581 West Entrance Road, Hartsville SC 29550

Inspection Dates:

July 1, 2019 to September 30, 2019

Inspectors:

A. Beasten, Resident Inspector

M. Fannon, Senior Resident Inspector Pwr/Tl

Approved By:

Randall A. Musser, Chief

Reactor Projects Branch 3

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at H.B. Robinson Steam Electric Plant in

accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs

program for overseeing the safe operation of commercial nuclear power reactors. Refer to

https://www.nrc.gov/reactors/operating/oversight.html for more information. A licensee-identified

non-cited violation is documented in report section: 71111.06.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

PLANT STATUS

Unit 2 began the inspection period at rated thermal power. On August 11, 2019, the unit

experienced an automatic reactor trip and turbine trip due to an electrical fault in the main

generator exciter. The unit was restarted on September 3, 2019 and was returned to rated

thermal power on September 6, 2019. The unit remained at or near rated thermal power for the

remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed plant status activities described in

IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem

Identification and Resolution. The inspectors reviewed selected procedures and records,

observed activities, and interviewed personnel to assess licensee performance and compliance

with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather Sample (IP Section 03.03) (1 Sample)

(1)

The inspectors evaluated readiness for impending adverse weather related to

Hurricane Dorian on September 1 through September 5, 2019

External Flooding Sample (IP Section 03.04) (1 Sample)

(1)

The inspectors evaluated readiness to cope with external flooding on

August 28, 2019

Lake Robinson dam and spillway tainter gates

71111.04Q - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

(1)

Spent fuel pool cooling, including service water pumps 'C' and 'D' and 'A' component

cooling water pump, for less than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> time to boil on July 10, 2019

(2)

Steam driven auxiliary feedwater system during the 'B' motor driven auxiliary

feedwater train maintenance outage on July 17, 2019

(3)

Dedicated shutdown emergency diesel generator following the turbine and reactor trip

on August 13 through 15, 2019

(4)

Emergency bus E-1 equipment and components while the dedicated shutdown diesel

generator was out of service for planned overhaul on August 20, 2019

71111.05A - Fire Protection (Annual)

Annual Inspection (IP Section 03.02) (1 Sample)

(1)

The inspectors evaluated fire brigade performance on August 9, 2019

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (5 Samples)

(1)

Fire zone 2, 'A' emergency diesel generator room, on July 2, 2019

(2)

Fire zone 3, safety injection pump room, on August 2, 2019

(3)

Fire zone 21, rod control room, on August 2, 2019

(4)

Fire zone 4, charging pump room, on August 6, 2019

(5)

Fire zone 8, boron injection tank room, on August 27, 2019

71111.06 - Flood Protection Measures

Inspection Activities - Underground Cables (IP Section 02.02c.) (1 Sample)

(1)

(1) M-50A and M-50B, on June 18, 2019

(2) M-35 and M-36, on June 18, 2019

71111.07A - Heat Sink Performance

Annual Review (IP Section 02.01) (1 Sample)

(1)

The 'A' component cooling water heat exchanger

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1)

The inspectors observed and evaluated licensed operator performance in the control

room during plant startup activities on September 3, 2019

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness Inspection (IP Section 02.01) (2 Samples)

(1)

Dedicated shutdown diesel generator following recent overhaul

(2)

Water cooled condensing unit '1B' following recent failure

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)

(1)

'B' motor driven auxiliary feedwater system train maintenance outage on

July 17, 2019

(2)

Maintenance activities for the week of August 18, 2019, including the dedicated

shutdown diesel generator overhaul

(3)

Steam driven auxiliary feedwater system planned maintenance concurrent with MST-

021, Reactor Protection Logic Testing Train B, and MST-023, Safeguard Relay Rack

Train B, testing on September 10, 2019

(4)

230kV switchyard relay calibrations for the week of September 16, 2019

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 02.02) (5 Samples)

(1)

Nuclear condition report (NCR) 2281205, 'A' safety injection pump seal water line

vibrations on July 10, 2019

(2)

NCR 2266397, 'B' emergency pressurization failing to meet acceptance criteria for

control room envelope on July 31, 2019

(3)

NCR 2277990, underground cable vault M-36 water level above grating and on

cables on July 31, 2019

(4)

NCR 2283402, debris found in motor vent screen of 'C' service water pump on

August 2, 2019

(5)

NCR 2283172, 'A' diesel generator air compressor unloader tower porting off air on

August 6, 2019

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (5 Samples)

(1)

Work order (WO) 20224292, 'B' motor driven auxiliary feedwater train maintenance

outage on July 17, 2019

(2)

OST-908-4, Component Cooling Water Pump Test 'C', following planned

maintenance on the 'C' component cooling water pump on July 25, 2019

(3)

OP-306, Component Cooling Water System, following minor maintenance on the

'A' component cooling water pump on July 31, 2019

(4)

OP-602-1, DSDG Power Pack Replacement Break-In and Testing, following major

planned maintenance on August 23, 2019

(5)

WO 20240431, replace open limit switch on FCV-113A-LS-O, and WO 20240426,

replace open limit switch on FCV-113A-LS-C, on September 16, 2019

71111.22 - Surveillance Testing

Surveillance Tests (other) (IP Section 03.01) (2 Samples)

(1)

OST-108-1, Boric Acid Pump 'A' Inservice Test, on July 8, 2019

(2)

SP-1506, Control Room Integrated In-Leakage Tracer Test, performed from

March 28-31, 2019, however the final report from the vendor was not issued until

July, 2019

Inservice Testing (IP Section 03.01) (1 Sample)

(1)

OST-151-3, Safety Injection Subsystem Components Test Pump 'C', on

September 23, 2019

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01) (1 Sample)

(1)

Unplanned scrams from July 1, 2018 to June 30, 2019

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) (1 Sample)

(1)

Unplanned power changes from July 1, 2018 to June 30, 2019

MS08: Heat Removal Systems (IP Section 02.07) (1 Sample)

(1)

Heat removal systems (MS08) from July 1, 2018 to June 30, 2019

BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) (1 Sample)

(1)

RCS activity (B101) from July 1, 2018 to June 30, 2019

71152 - Problem Identification and Resolution

Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples)

(1)

NCR 2253155, Steam dumps group 1 loss of power MST-021

NCR 2147971, Bank 1 steam dump loss of indication

(2)

NCR 2256141, FCV-1424 remains open after stopping 'A' motor driven auxiliary

feedwater pump

71153 - Followup of Events and Notices of Enforcement Discretion

Personnel Performance (IP Section 03.03) (1 Sample)

(1)

The inspectors evaluated the licensees performance in response to a Unit 2

automatic reactor trip from rated thermal power due to a turbine trip that was a result

of a fault in the main generator exciter on August 11, 2019. A non-emergency event

report was submitted to the NRC (Event Notification 54212). The reactor trip was not

complex, with all systems responding normally post trip. The unit was restarted on

September 3, 2019 and was returned to rated thermal power on

September 6, 2019. The issue was placed in the corrective action program as NCR

2286376.

INSPECTION RESULTS

Licensee-Identified Non-Cited Violation

71111.06

This violation of very low safety significance was identified by the licensee and has been

entered into the licensee corrective action program and is being treated as a non-cited

violation, consistent with Section 2.3.2 of the Enforcement Policy.

Violation: Title 10 of CFR Part 50, Appendix B, Criterion III, Design Control, requires, in

part, that that measures shall be established to assure applicable regulatory requirements

and the design basis, as defined in section 50.2 and as specified in the license applications,

for those structures, systems, and components to which this appendix applies are correctly

translated into specifications, drawings, procedures, and instructions.

Contrary to the above, from June 18, 2018 to June 19, 2019, the licensee failed to maintain

Class 1E (safety-related) electrical cables in an environment for which they are

designed. Specifically, the low-voltage safety related cables associated with the A and B

service water pumps and power and limit switches were submerged in water, a condition for

which they are not qualified. The licensee took immediate actions to lower the water levels in

underground cable vaults where submerged cables were discovered and conduct pump-

downs of the safety-related underground cable vaults on an increased scheduled frequency.

Significance/Severity: Green. This performance deficiency was associated with the

Mitigating Systems Cornerstone. The performance deficiency was related to the equipment

reliability attribute and failure to maintain the cables in the environment for which they were

designed adversely impacted the cornerstone objective to ensure the availability, reliability,

and capability of systems that respond to initiating events to prevent undesirable

consequences. Specifically, the submergence of the safety-related cables adversely

impacted the service life of the cables and could cause the A train service water system to

be inoperable in the event a cable failed as a result of continuous submergence. The finding

screened as having very low safety significance (Green) because it did not represent an

actual loss of function in the service water system.

Corrective Action References: This issue was being tracked in the licensees corrective

action program by NCR 02277990.

Observation: Observation

71152

The Inspectors reviewed the licensees response to a relay failure of the A motor driven

auxiliary feedwater (MDAFW) pump discharge flow control valve, NCR 02256147. On

February 5, 2019, following post-maintenance testing on the A MDAFW pump, FCV-1424

failed to close as expected when the pump was secured. FCV-1424 is a discharge flow

control valve that adjusts the flow from the MDAFW pump to the steam generators. The

failure was unrelated to maintenance activities that had occurred earlier that

day. Troubleshooting identified that the relay did not open when de-energized. Following

relay replacement, all tests were completed successfully.

The Inspectors questioned the licensees investigation into the failure. The relay was to be

sent offsite for failure analysis, however an onsite visual inspection was determined to be

sufficient. The inspection revealed that the number 2 normally closed contact was bent which

caused the relay to bind internally. The licensee concluded that the relay had been installed

with the bent contact bar and was therefore a manufacturing defect. No extent of condition

was performed as it was determined to be an isolated failure. Although this relay had been

purchased with 10 others from Westinghouse, the licensee had not notified Westinghouse of

the defect. Additionally, the other 10 relays had not been located or inspected.

Based on these inspector questions, NCR 02277990 was reopened on April 3, 2019, and the

failure cause was changed to inadequate relay installation. Although the installation

procedure contained instructions to verify that the contacts were aligned correctly both prior

to and after installation, the licensee initiated a procedure revision to clarify that all contacts

and should be inspected both before and after installation. Given this new information, the

inspectors questioned how the defect was introduced. The licensee maintained that it had

been installed with the defect. The inspectors also questioned the capability of the A

MDAFW pump to perform its intended safety function with a defective relay installed in the

system. The licensee maintained that the pump would perform its safety function since the

internal binding from the bent contact bar would not have prevented the relay from

energizing, and valve FCV-1424 would have performed its safety function. The inspectors

questioned the licensees operability conclusions given only a visual examination of the relay

and inquired to the status of the other 10 relays received in the same purchase order. An

extent of condition was performed on the B MDAFW pump and no issues were noted on that

relay. Work orders have been initiated to inspect the remaining relays installed in the plant.

In response to additional inspector questions, the licensee sent the relay out for forensic

testing in May, 2019. The testing could not replicate the failure, however there was evidence

of gouge marks on the bent contact that could have been caused by a screwdriver or other

tool used during installation. Based on the results of the forensics testing, the inspectors

concluded the licensees determination that the A MDAFW pump would have performed its

safety function was adequate. While the licensees final corrective actions were adequate,

the inspectors determined that the initial cause evaluation and investigative process lacked

technical rigor. The initial failure determination (manufacturing defect) proved to be incorrect

and was not challenged internally so no initial extent of condition was performed, and the

defective relay was replaced without further investigation or corrective action. Through

inspector follow-up the licensee subsequently applied the appropriate level of technical rigor

to the investigation.

EXIT MEETINGS AND DEBRIEFS

The inspectors confirmed that proprietary information was controlled to protect from public

disclosure.

  • On October 16, 2019, the inspectors presented the integrated inspection results to

Ms. Nicole Flippin, General Plant Manager, and other members of the licensee staff.