IR 05000255/1993029

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Forwards Insp Rept 50-255/93-29 on 931116-1216.No Violations Noted
ML18059A623
Person / Time
Site: Palisades 
Issue date: 01/04/1994
From: Kobetz T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Slade G
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
Shared Package
ML18059A624 List:
References
NUDOCS 9401120004
Download: ML18059A623 (14)


Text

,..

UNITED STATES NUCLEAR REGULATORY COMMISSION Docket No. 50-255 Consumers Power Company ATTN:

Gerald General Manager REGION Ill 801 WARRENVILLE ROAD LISLE. ILLINOIS 60532-4351 JAN Cl

-~'. IS.34 27780 Blue Star Memorial Highway Covert, MI 49043-9530

Dear Mr. Slade:

SUBJECT:

ROUTINE RESIDENT INSPECTION AT PALISADES NUCLEAR PLANT This.refers to the inspection conducted by Messrs**. M. E. Parker and D. G.

Passehl of this office, from November 16 through December 16, 1993.. The inspection included a review of authorized activities for your Palisades Nuclear Generating Facility. At the conclusion of the inspection, the findings were discussed with those members of your staff identified in the enclosed report.

Areas examined during the inspection are identified in the report.

Within these areas, the inspection consisted of a selective examination of procedures and representative records, interviews with personnel, and observation of activities in progress. The purpose of the inspection was to determine whether activities authorized by the license were conducted safely and in accordance with NRC requirements.

No violations of NRC requirements were identified during the course of this inspection.

In accordance with 10.CFR 2.790 of the Commission's regulations, a copy of this letter and the enclosed !nspection report will be placed in the NRC Public Document Room.

We will gladly discuss any questions you have concerning this inspection.

Enclosure:

Inspection Report

No. 50-255/93029(DRP}

See Attached Distribution

9401120004 940104

~:

PDR

ADOCK 05000255

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tz, Acting Chief

Rea or Projects Section 2A

Consumers Power Company

Distribution:

REGION I II

Report No. 50-255/93029(DRP)

Docket No. 50-255

License No. DPR-20

Licensee: Consumers Power Company

212 West Michigan Avenue.

Jackson, MI

49201

Facility Name:

Palisades Nuclear Generating Plant

Inspection At:

Palisades Site, Covert, Michigan

Inspection Conducted:

November 16 through December 16, 1993.

Inspectors:

M. E. Parker

D. G. Passehl

Approved 8~9 Chief

Reacto Projects Section 2A

Inspection Summary

Inspection from November 16 through December 16. 1993.

(Report No. 50-255/93029CDRPll

Date '

Areas Inspected: Routine, unannounced inspection by the resident inspectors

of actions on licensee event report followup, followup of events, operational

safety verification, maintenance, surveillance, cold weather preparations,

engineering and technical support, and Region III requests.

No Safety Issues

Management System (SIMS) items were reviewed.

Results:

No cited violations or deviations were identified in any of the

eight areas inspected.

The strengths, weaknesses, and Inspection Followup Items are discussed in

paragraph 1, "Management Interview."

9401120007 940104

--

PDR

ADDCK 05000255

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PDR

---.1~

.,

1.

DETAILS

Management Interview (71707)

The inspectors met with licensee representatives (denoted in paragraph

10) on December 16, 1993, and informally throughout the inspection

period to summarize the scope and findings of the inspection activities.

The inspectors also discussed the likely informational content of the

inspection report, with regard to documents or processes reviewed by the

inspectors.

The licensee did not identify any such documents or

processes as proprietary.

Highlights of the exit interview are discussed below:

a.

Strengths noted:

Improved housekeeping and material condition of engineered

safeguards rooms.

Repair of longstanding emergency diesel generator fluid

leaks.

b.

Weaknesses noted:

Slow response to internal audit finding,concerning

replacement of red flexible hose covers for the emergency

diesel generators.

Cold weather checklists need updating to accurately reflect

installed plant equipment.

c.

Inspection Followup Items:

Licensee's actions in response to having an ungrounded rod

control system power source without an installed ground

detection system will be reviewed.

2.

Licensee Event Report Followup (92700, 92720)

The inspectors reviewed the following Licensee Event Reports (LERs) by

means of direct observation, discussions with licensee personnel, and

review of records.

The review addressed compliance to reporting

requirements and, as applicable, that immediate corrective action and

appropriate action to prevent recurrence had been accomplish~d.

a.

(Closed) LER 255/91013:

Operation of Plant with Leak in

Containment Spray Line Caused by Personnel Error:

On May 7, 1990,

the licensee identified a leak through a weld in a containment

spray header.

They determined that the leak did not require

repair before resuming power operation. Subsequent reviews found

  • 3.

that the plant had been in an unanalyzed condition outside the

design basis of the plant.

The containment spray header weld was repaired.

No violation is

warranted since this issue was one of the examples used for a

notice of violation and proposed imposition of civil penalty as

discussed in enforcement conference report 50-255/9102l(DRS).

This LER is closed.

b.

(Closed) LER 255/92002:

Equipment Not Channel Checked In

Accordance With Technical Specifications Tables 3.17.1 and 4.1.1.

and 4.0.4:

On December 16, 1991, with the plant shutdown, the

licensee discovered that channel checks for reactor coolant flow

and wide range nuclear power instrumentation were not being

performed as required by technical-specifications.

The root cause

was a procedural weakness which resulted in the inadequate

implementation of Technical Specification requirements.

Procedure SH0-1, "Operations Shift Items," was revised to ensure

that any required shiftly*channel checks are performed prior to

entry into a reactor operating condition or special operating

condition which requires that equipment be operable.

This LER is

closed.

No violations, deviations, unresolved, or inspection followup items were

identified in this area.

Followup of Events (93702)

During the inspection period, the licensee experienced one event which

required prompt notification of the NRC pursuant to 10 CFR 50.72.

The

inspectors pursued the event onsite with licensee and/or other NRC

officials. The inspectors verified that the notification was correct

and timely, that activities were conducted within regulatory

requirements, and that corrective actions would prevent future

recurrence.

The specific event was as follows:

December 7, 1993 -

Electrical Containment Penetrations Not In

Conformance Wit~ Final Safety Analysis Report

And Technical Specifications.

On December 7, 1993, a plant design engineer identified electrical

containment penetrations which failed to meet design features described

in Technical Specifications (TS) and the Final Safety Analysis Report

(FSAR).

The FSAR and TS describe these electrical containment

penetrations as being double barrier _design.

The FSAR also states that.

all containment penetrations are seismically designed and tornado

protected.

The electrical penetrations in the north and southwest

penetration rooms do not appear to meet all of these requirements.

Electrical penetration eighteen in the southwest penetration room and

electrical penetration eighteen in the north penetration room are

  • connected together by a nitrogen supply system.

This system provides an

inert-atmosphere to the penetrations for corrosion protection.

The

nitrogen supply bottles for the southwest room are located in the

turbine building; as such, the lines in the turbine building are not

seismically designed nor tornado protected.

In the north penetration

room a similar non-seismic nitrogen system exists. However, the

nitrogen bottles are connected to a header with a hose arrangement

rather than copper tubing.

The licensee and the inspectors are continuing to evaluate this issue.

The inspectors will evaluate corrective actions for this event when the

Licensee Event Report is issued.

No violations, deviations, unresolved, o~ inspection-followup items were

identified in this area.

4.

Operational Safety Verification (71707, 71710, 42700)

Routine facility operating activities were observed as conducted in the

plant and from the main control room.

Plant startup, steady power

operation, plant shutdown, and system lineup and operation were observed

as applicable.

The performance of reactor operators and senior reactor operators, shift

engineers, and auxiliary equipment operators was observed and evaluated.

Included in the review were procedure use and adherence, records and

logs, communications, shift/duty turnover, and the degree of

professionalism of control room activities.

Evaluation, corrective action, and response for off normal conditions

were examined.

This included compliance to any reporting requirements.

Observations of the control room monitors, indicators, and recorders

were made to verify the operability of emergency systems, radiation

monitoring systems, and nuclear reactor protection systems.

Reviews' of

surveillance, equipment condition, and tagout logs were conducted.

Proper return to service of selected components was verified.

Periodic verification of Engineered Safety Features status was conducted

by the inspectors.

Equipment alignment was verified against plant

procedures and drawings and detailed walkdowns selectively verified:

equipment labeling, the absence of leaks, housekeeping, calibration

dates, operability of support systems, breaker and switch alignment, as

appropriate.

a.

General

The plant has been online since the end of the 1993 refueling

outage.

On December 9, 1993, reactor power was lowered slightly

to approximately 99.5 percent power to minimize the number of

reactor protective system variable high power pre-trip actuations.

b.

These pre-trip actuations were due to indicated delta-T power*

swings and actual core power has been stable.

The cause of the pre-trip alarms appears to be caused by

temperature swings in the primary coolant system hot legs as a

consequence of the low leakage core design instituted following

the recent refueling outage. Just prior to lowering reactor power

the plant had been averaging about one to two pre-trips per day.

The licensee has taken appropriate action, including obtaining

outside assistance, to investigate and correct the cause of this

condition. These actions were ongoing at the close of this

inspection period.

The inspectors will continue to follow the

licensee's actions regarding this issue.

All other primary system data indicates normal plant performance.

Based on chemistry data there are no known fuel pin leaks.

Activity levels of the primary coolant system are stable and are

closely monitored and reported daily.

Walkdown of Emergency Diesel Generator Systems

The inspectors performed a walkdown of the mechanical portions of

the emergency diesel generator (EDG) starting air, lube oil, fuel

oil, and jacket water systems. Applicable plant drawings and other

design doc~ment~ were used.

No significant discrepancies were

identified and both EDGs were in their proper standby lineups.

Additionally, the inspector observed that the licensee had taken

action to resolve some outstanding work orders and other material

condition concerns that were identified in a previous NRC

inspection report 50-255/93017(DRP).

Two observations were identified to the EDG system engineer:

(1)

Three hoses were installed in the fuel oil system on each

EDG that were not reflected on plant drawing M214, sheet 1.

Two of the hoses were installed at the suction to the fuel

oil booster pump and fuel oil priming pump.

The third hose

was installed on the return fuel oil line from the EDG to

the fuel oil reservoir in the base of the EDG.

(2)

Section 8.4.1.3 of the Final Safety Analysis Report listed

local alarms at each EDG with three missing from the list:

Low lube oil level

Engine trouble.

High/low fuel oil level

The system engineer agreed with the observations. Also, the red

flexible hose covers included in item (1) above appeared degraded.

.....

Licensee audit report in 1991 (QA-91-10) documented the same

observation. Although the response-to the audit report stated

that the hoses would be replaced in March/April 1992, no action

was taken nor was a reason for the delay evident.

However, there

were open work orders tracking completion of this action item.

Work to replace the hoses was completed prior to the close of this

inspection period.

The drawings will be updated to reflect the

installation of the hoses.

The licensee will evaluate the need to update Section 8.4.1.3 of

the FSAR to include the missing local alarms.

No violations, deviations, unresolved, or inspection followup items were

identified in this area.

5.

Maintenance (62703, 42700)

Maintenance activities in the plant were routinely inspected, including

both corrective maintenance (repairs) and preventive maintenance.

Mechanical, electrical, and instrument and control group maintenance

activities were included as available.

The focus of the inspection was to assure the maintenance activities

reviewed were conducted in acco~dance with approved procedures,

regulatory guides and industry codes or standards, and in conformance

with Technical Specifications. The following items were considered

during this review: the Limiting Conditions for Operation were met while

components or systems were removed from service; approvals were obtained

prior to jnitiating the work; activities were accomplished using

approved procedures; and post maintenance testing was performed as

applicable.

The following maintenance activities were observed:

a.

Emergency Diesel Generator (1-1), repair of several oil leaks and

hose replacement.

The inspector checked the licensee's progress on addressing a

small fuel oil fitting leak observed from.SV-1415, a one inch

s6lenoid valve in the fuel oil supply line to the emergency diesel

generator (EDG) 1-1 day tank.

The valve is about ten feet above

the floor with a tygon hose routed to a bucket to capture the

leakage. This was a material condition/housekeeping concern due

to the length of time the condition has existed.

It appears to

have been successfully repaired during a planned EDG maintenance

outage at the close of this inspection period.

A work request (No. 17640) was.submitted July 13, 1992, to repair

the valve and stop the leak.

The licensee has missed some prior

opportunities to repair this valve.

Since July 1992 there have

been at least two EDG maintenance outages when this valve could

have been fixed.

,,

6.

Upon further review the inspector found this valve had been worked

twice, just a few weeks prior to July 13, 1992.

The first work

activity in June 1992 replaced SV-1415 with a new model.

It was

subsequently found leaking and another repair attempt was made.

The valve was still found leaking through a fitting and was

scheduled for another repair attempt during the week of August 3,

1992, according to work request No. 017144.

However, the work was

never per,formed during this or subsequent EOG maintenance outages,

until December 1993.

Whether the leakage problem was due to valve

misapplication or poor maintenance work practices was unclear.

b:

Volume Control Tank Level Switch LS-0204

This level switch was found leaking at its flanged connection and

successfully repaired.

Good coord1nation and communication was

observed during the repair effort.

No violations, deviations, unresolved, or inspection followup items were

identified in this area.

Surveillance (61726, 42700)

The inspector reviewed technical specifications required surveillance

testing as described below, and verified that testing was performed in

accordance with adequate procedures, test instrumentation was

calibrated, limfting conditions for operation were met.

The inspector

further verified that the removal and restoration of the affected

components were properly accomplished, test results conformed with

technical specifications and procedure requirements, test results were

revi.ewed by personnel other than the individual directing the test, and

deficiencies identified during the testing were properly reviewed and

resolved by appropriate management personnel.

a.

QR-22, "Process Monitor Functional Checks - Quarterly," Rev.5

b.

DW0-13, "LLRT - local leak Rate Tests And Inner And Outer

Personnel Air lock Door Seals," Rev.7

c.

M0-7A-l,

"Em~rgen9 Diesel Generator 1-1 (K-6A)," Rev.29

d.

NMS-10, "Dual linear Power Current Measurements," Rev.6

No violations, deviations, unresolved, or inspection followup items were

identified in this area.

7.

Cold Weather Preparations (71714)

The inspector reviewed the licensee's cold weather protective measures

program.

The program was adequately implemented ensuring that safety-

rel ated systems are protected against cold weather.

n

'

The program consists of two operating checklists - CL-CWCL-1, Cold*

Weather Checklist," and CL-CWCL-2, "Cold Weather Checkltst

(Electrical)." The inspector conducted walkdowns of portions of both

checklists. There were no instances identified of unprotected safety-

related equipment.

Additionally, some components are routinely

monitored for the effects of cold weather through other plant procedures

or by auxiliary operator log sheets.

For example, temperatures of the

safety injection and refueling water storage tank and the condensate

storage tank are monitored shiftly by the operators.

One observation was that the blank checklists need to be updated to

accurately reflect plant conditions. There were eleven changes

requested on the completed copies or the checklists that would clean up

the documents and help prevent all the p~n and ink changes.

One other item noted was the standing "Radwaste Area Fuel Handling

Freeze Protection" control room alarm.

The associated alarm response

procedure directed the operators to ensure the steam supply to heating

coils VHX-7A and VHX-78 was functioning properly, or else initiate work

requests, as necessary. Heating coils VHX-7A and 78 supply heat to the

area around the spent fuel pool floor in the auxiliary building.

They

are not technical specification-related nor safety-related.

Followup indicated there were work requests in place to repair the

heating coils.

However, it appears the licensee has experienced

difficulty in repairing the heating coils. The problem is that the

steam inlet valves for the coils (CV-1547A and CV-15478) have a history

of improper operation, possibly due to system design or poor

maintenance.

No violations, deviations, unresolved, or inspection followup items were

identified in this area.

8.

Engineering and Technical Support (37700,92705)

The inspector monitored engineering and technical support activities at

the site and, on occasion, as provided to the site from the corporate

office. The purpose was to assess the adequacy of these functions in

contributing properly to other functions such as operations,

maintenante, testing~ lraining, fire protection, and configuration

management.

The inspector checked the status of the licensee's investigation into a

related event that occurred at another nuclear facility.

On November 13, 1993, the Fort Calhoun Nuclear Plant was near the end of

a refueling outage when they experienced an uncontrolled withdrawal of a

control rod.

The unexpected control motion was the result of the

contacts used to control rod motion being bypassed due to two grounds

that developed in unfavorable locations.

The licensee was unaware of

  • the presence of the grounds until the undesired control rod motion

occurred because no ground detection system was installed at Fort

Calhoun.

The Palisades staff found that a similar problem could exist at their

facility. A control rod or even a group of rods could be inadvertently

raised or lowered as a result of two grounds developing in strategic

locations.

In reviewing this event, the inspectors noted that maintenance practices

on the control rod drive system appears good.

This should help reduce

the likelihood of a ground.

All accessible control rod drive cabling

was walked down at the end of the most recent refueling outage.

In

recent years, various cables and connectors in the system were replaced.

In addition, control room operators have-redundant indication of

unexpected control rod movement in the alarms, lights, computer

printouts, etc. Action could then be taken to remove power to the

control rod drive motors.

The event has been analyzed and is found in Section 14.2 of the Final

Safety Analysis Report (FSAR).

The FSAR discusses the uncontrolled

withdrawal of a control rod or a group of control rods from various

reactor conditions.

The licensee's response on this issue was excellent. They immediately

began to work through Combustion Engineering and the Fort Calhoun

licensee to understand the problem and formulate a plan of action.

The

licensee is still considering several actions in response to this issue,

including installing a ground detection feature within the control rod

drive system.

This is considered an inspection followup item

(255/93029-0l(DRS)) pending NRC review of the licensee's actions.

One inspection followup item was identified, and no violations,

deviations, or unresolved items were identified in this ~rea.

9.

Region III Requests (92705)

J

The inspector responded to a request to determine whether the licensee

uses Automatic Timing and Controls Company (ATC) relays in their

emergency diesel generator (DG) load sequencer circuitry.

The request

was in response to relay failures in the DG loading scheme at another

U.S. nuclear facility.

This concern does not exist at Palisades.

Palisades has three such

relays installed in a nonsafety related application.

They are used for

chlorination in the secondary plant...

No violations, deviations, unresolved, or inspection followup items were

identified in this area.

10.

Persons Contacted

Consumers Power Company

G. B.

  • R. D.
  • R. M.

D. D.

  • T. J.
  • D. W.

K. M.

R. B.

K. E.

  • C. R.

-- -*J. c.

  • H. A.

J. L.

D. J.

J. H.

Slade, Plant General Manager

Orosz, Nuclear Engineering & Construction Manager

Rice, Director, NPAD

Hice, Nuclear Training Manager

Palmisano, Plant Operations Manager

Rogers, Safety & Licensing Director

Haas~ Radiological Services Manager

Kasper, Maintenance Manager _

Osborne, System Engineering Manager

Ritt, Administrative Manager

Griggs, Human Resource Director

Heavin, Controller

Hanson, Operations Superintendent

Malone, Radiological Services Superintendent

Kuemin, Licensing Administrator

Nuclear Regulatory Commission CNRC)

  • M. E. Parker, Senior Resident Inspector
  • D. G. Passehl, Resident Inspector
  • Denotes those present at the e~it meeting on December 16, 1993.

In addition, the inspectors interviewed other licensee personnel

including shift supervisors, control operators and engineering

personnel.

10