IR 05000255/1993006

From kanterella
Jump to navigation Jump to search
Forwards Insp Rept 50-255/93-06 on 930405-08.No Violations Noted
ML18058B769
Person / Time
Site: Palisades Entergy icon.png
Issue date: 04/16/1993
From: Snell W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Slade G
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
Shared Package
ML18058B771 List:
References
NUDOCS 9304210364
Download: ML18058B769 (10)


Text

APR 16 1993 Docket No. 50-255 Consumers Power Company ATTN:

Gerald General Manager Palisades Nuclear Generating Plant 27780 Blue Star Memorial Highway Covert, MI 49043-9530

Dear Mr. Slade:

SUBJECT:

ROUTINE CHEMISTRY INSPECTION AT THE PALISADES NUCLEAR PLANT This refers to the routine safety inspection conducted by Dr. J. House of this office on April 5 thro~gh 8, 1993.

The inspection included a review of authorized activities for your Palisades facility.. At the conclusion of the inspection, the findings were discussed with those members of your staff identified in the enclosed report.

  • Areas examined duririg this inspection are identified in the report. Within the,se areas, the inspection consisted of a selective examination of procedures and representative records, observations, and interviews with personnel..

No violations of NRC requirements were identified during the course of this i nsp.ect ion.

  • In accordance with 10 CFR 2.790 of the Commission's regulations, a copy of this letter and the enclosed inspection report will be placed in the NRC Public Document Room:

We will gladly discuss any questions you have concerning this inspection.

Enclosure:

Inspection Report

No. 50-255/93006(DRSS)

See Attached Distribution

~

II

use

Riii.

/lb /93

J~en

r~.'!>

.

93()416

9304210DOC~ 05000255

.~DR

A

PDR

Sincerely,

Ori&inar Si&ne4 B_y William Snell

William Snell, Chief

Radiological Controls Section 2

Riii

~

Snell

4/.'-/.93

  • Consumers Power Company

Distribution

REGION I I I

Report No. 50-255/93006(DRSS)

Docket No. 50-255

licensee: Consumers Power Company

27780 Blue Star Memorial Highway

Covert, MI

49043 *

Facility Name:

P~lisades Nuclear Plant

Inspection At:

Palisades Site, Covert, MI

Inspection Conducted: April 5-8, 1993

Inspector: ~

&~

Approved by: w;)frl~t*e?Qe

Radiological Controls Section 2

Inspe~tion Summary

Date

License No. DPR-20

Inspection on April 5-8, 1993 (Report No. 50-255/93006(DRSS))

Areas Inspected:

Routine, announced inspection of the chemistry program

including:

audits,_quality assurance, chemistry comparisons, radiological

environmental monitoring program (REMP), dry cask fuel storage, and an

inspection followup item.

Results:

The licensee's performance in the chemistry comparison program was

excellent (31 agreements in 32 comparisons).

The laboratory QA/QC program was

well managed.

The water chemistry program and plant water quality were very

good; the licensee removed a total of only 30 pounds of sludge from both steam

generators at the end of the first refueling outage following steam generator

replacement which was very good. Audits were performance based and. thorough.

The REMP was well managed, and the radiation monitoring program for dry cask

fuel storage appeared adequate. * *

930421= 6~b~55

PDR

"

PDR

a

DETAILS

1.

Persons Contacted

  • B. Baker, Chemistry Supervisor

G. Foster, Mechanical Equipment Supervisor

  • K. Haas, Radiological Services Manager

D. Malone, Radiological Services Superintendent

  • J. McElrath, Chemical Engineering Section Head
  • M. Mennucci, Health Physics Technical Supervisor
  • T. Palmisano, Operations Manager
  • T. Popp, Project REMP Coordinator
  • M. Sullivan, Chemistry Performance Analyst
  • J. Heller, Senior Resident Inspector, NRC

The inspector contacted other licensee personnel during the inspection.

2.

Licens~e Action on Previous Inspection Fihding CIP 84750)

(Closed) Open Item (50-255/91016-0ll:

The lice.nsee will split a liquid

radwaste sample and have their vendor laboratory analyze for tritium,

strontium-89, strontium-90, and gross beta.

The results will be sent to

Region III for comparison with results from the NRC reference

laboratory.

No comparisons could be made as the NRC reference

laboratory did not analyze the sample. This item is* closed.

3.. Management. Organiz~tion, and Training (IP 84750)

The chemistry superintendent reports to the operations manager.

A

.laboratory supervisor, a performance analyst, a chemistry support

specialist, a chemical engineering section head, and the environmental

coordinator report to the superintendent.

Five senior chemistry

technicians and six technicians report to the laboratory supervisor.

One of the technicians is on loan to the systems engineering group and

one technician is in training. All technicians, except for the one in

training, meet the American National Standards Institute Nl8.l-1971

criteria for technicians.

Due to low staff turnover, the laboratory has an experienced technical

staff with approximately 45% of the personnel at the senior technician

level. This is not an automatic promotion based on time in grade, but

is a promotion based on experience, knowledge, and laboratory skills and

requires the approval of chemistry supervision.

The laboratory has

strong ma.nagement support as evidenced by recent equipment purchases

including a new graphite furnace atomic absorption spectrophotometer and

modifications to an ion chromatograph.

The chemistry staff was very

capable and is a strength.

No violations or deviations were identified.

4.

Water Chemistry Control Program (IP 84750)

The licensee's water chemistry program conforms. to the Electric Power

Research Institute (EPRI) guidelines for primary and secondary water

chemistry. A review of selected trend chart data from the previous

12 months indicated t.hat primary system chemistry parameters were well

within the guidelines. Fluoride, chlbride, sulfate, and dissolved

oxygen levels averaged less than 20 parts per billion (ppb), 20 ppb,

20 ppb, and 2 ppb with EPRI guidelines of 50 ppb, 50 ppb, 50 ppb, and

5 ppb, respectjvely. Dissolved hydrogen was maintained within the EPRI

window.

The laboratory recently reduced the lower limit of detection

(LLD) for chloride, fluoride, and sulfate from 20 ppb to 1 ppb by

upgrading the Ion Chromatograph; This provides ~more realistic

estimate of these anions in the primary coolant since the actual

concentrations of these anions appeared to be much lower than the

previous d~tection limits of 20 ppb.

Secondary system chemistry was very good with steam generator (S/G)

blowdown levels of sodium, chloride, sulfate, silica, and conductivity

averaging l~ss than 4 ppb, 4 ppb, 3 ppb, 100 ppb, and 0.8 micro

Siemen/cm (µS/cm) with guidelines of 20 ppb,.20 ppb, 20 ppb, 300 ppb,

and 0.8 µS/cm, respectively. * Feedwater dissolved oxygen, iron, and

copper levels averaged less than 0.5 ppb, 2 ppb, and 2 ppb with

guideline levels of 5 ppb, 20 ppb, and 2 ppb,* respectively. Hydrazine

levels were ac(equate for removing dissolved oxygen from steam generator

feedwater.

Chemistry parameters were reviewed daily by chemistry

management and a ~eport of selected parameters was sent to plant

management.

The chemical engineering section prepares a monthly report

of chemistry trends and significant observations are forwarded to plant

management for review. A contractor reviews chemistry data daily and

prepares a monthly report for plant management.

The licensee's water

quality program is ex~ellent.

The chemistry department monitors corrosion products in the steam

generators. A licensee representative stated that during the last

refueling out~ge, 14 pounds of sludge was removed from one steam

.generator (S/G) and 16 pounds was removed from the other S/G.

This was

very good when compared with the previous (1987) sludge lancing of the

original steam generators during which approximately 4438 pounds of

sludge were removed from both generators.. In addition~ no S/G tubes had

  • to be plugged during the most recent outage.

The licensee uses boric

  • acid to reduce corrosion and morpholine for pH control in the steam

generators.

  • The inspector compared boron concentrations in various plant systems

during the past 12 months with Technical Specification (T/S)

requirements.

The spent fuel pool concentration met the 1720 parts per

million (ppm) minimum; the boric acid storage tanks were within the T/S

range of 6.25-10%; the safety injection refueling water tank was within

the 1720-2500 ppm range; and the b~ron concentration in the safety

injection tanks were within the 1720-2500 ppm window.

No violations or deviations were identified.

5.

Chemistry Comparison Program CIP 84750).

6.

The inspector submitted chemistry samples to the licensee for analysis

  • as part of a program to evaluate the laboratory's capabilities to

monitor nonradiological chemistry. parameters in various plant systems

with respect to regulatory and administrative requirements. These

samples had been prepared and standardized for the NRC by the Analytical

Chemistry Division of Oak Ridge National Laboratory (ORNL).

The samples * *

were analyzed by the licensee using routine methods and equipment.

Three dilutions were prepared from each sample by licensee personnel in

order to bring the concentrations within the ranges normally analyzed by

the laboratory. A single analysis wa*s performed on each dilution in a

manner similar t6 that of routine samples.

Th~ results are presented in

Table 1 which also contains the criteria for agreement.

These criteria

are based on ORNL analyses of the standards and on the relative standard

deviations (RSD) derived from the results of nuclear power plants

participating in a 1986 interlaboratory comparison (Table 2.1,

NUREG/CR-5442, Evaluation of Non-Radiological Water Chemistry at Power

Reactors).

The acceptance criteria were that the licensee's value

should be within 2 Standard Deviations (SD) of the ORNL ~alue for

agreement and between 2 and 3 SD for qualified agreement.

A qualified

agreemen_t may indicate a bias in the assay.

The licensee analyzed ten unknowns at three concentrations and one at°

two contentrations. Of the 32 comparisons, 31 were agreements

(Table 1). The three hydrazine results had larger biases than are

usually. seen; however, only the middle hydrazine concentration was a

disagreement. *When the three hydrazine unknowns were redil uted and

analyzed with no calibration or reagent changes, the results

(agreements) were within two percent of the reference values ~hich was a

si.gnificant improvement.

This indicated that a dilution error produced

the original disagreement and biases. Overall, licensee performance in

the chemistry comparison program was excellent.

  • *

No violations or deviations were identified.

Chemistry Quality Assurance/Quality Control CIP 84750)

The inspector reviewed the chemistry quality assurance (QA) program

defined by Laboratory Quality Control Program, Procedure 1.3,

Revision 3, March 5, 1990.

The program incorporated statistically based

  • control charts, independent controls, and multiple point calibration

curves. Control charts were reviewed by technicians when performing an

assay and weekly by supervisors. Data from selected.control charts was

randomly scattered about the mean indicating that instrument performance

was under statistical control. Concentrations of the independent

controls were in the ranges of plant samples which is a good practice.

Control charts were manually plotted, were neat, and provided an easy

appraisal of instrument performance.

The 1 i censee had two* 1 aboratory cross check. programs.

The first was a

vendor supplied interlaboratory cross check program which.measured

overall laboratory performance. This program was well organized and

incorporated licensee developed acceptahce criteria which*were based on

industry standards.

Each unknown was analyzed by five technicians and

their results were compared to the acceptance criteria. Technicians

whose results were outside of the criteria reanalyzed the un~nowns. The

average values for the five technicians were then compared to the

vendor's values using the acceptance criteria. The second program was

an intralaboratory cross check program in which unknowns were prepared

by laboratory supervisors. Technicians were required *to be tested twice

per year in this program.

From a review of selected data it appeared

that all technicians were tested twice annually. lhe licensee's quality

assurance program was very well managed.

No violations or deviations were identified.

7.

Audits CIP 84750)

8..

Surveillance S-AP-92-014 was.conducted March 3-June 30, 1992, to assess

the adequacy of hazardoui waste generation and control practices.

The

auditors reviewed chemical inventories, shelf lives, chemical usage,

types of chemical waste p~oduced, waste reduction, and disposal efforts~

There were no major _findings, although a number of minor observations

for program improvement were made.

Audit PT-92-07.assessed the

effectiveness of the Radiofogical Services Department in meeting

applicable T/S, procedures, *and regulatory criteria. Auditors reviewed

the REMP operation including procedures, equipment condition,

observation of $ample collection, and data acquisition. There were no

findings for the REMP.

The audit and surveillance were detailed; and

the audit teams appeared to be very knowledgeable.

No violations or deviations were identified.

Radiological Environmental Monitoring Program CIP 84750)

The inspector reviewed the Radiological Environmental Monitoring Program

(REMP) as defined by Procedure HP 10.1, Radiolog.ical Environmental

Monitoring Program Surveillances, Revision 3, January 1, 1993.

The 1991

Annua 1 Operating Report appeared to com*p ly with the REMP requirements.

All of the required samples were collected and analyzed, except as noted

in the repo~t. Missing samples were documented and the causes were

investigated as requited by procedure.

..

A tour of selected air sampling stations was conducted with the REMP

coordinator who was responsible for oversight of the REMP including

contractor performance in filter media changeriut and maintenance -0f the

air samplers.

The equipment was in very good condition and calibrations

were c,urrent.

The coordinator was a health physicist with power plant

.experience and was very knowledgeable of the REMP.

No violations or deviations were identified.

9:

Dry Fuel Storage Radiation Monitoring CIP 84750)

The dry fuel storage area is a concrete pad with a locked security fence

surrounding it. Three guard stations have been built around this fenced

area.

The dry fuel storage location is designated a radiological

controlled area (RCA) and will not be included tn the REMP.

This is a *

conservative approach as considerably more monitoring is required for an

RCA than is performed in the REMP, and the REMP program is designed to

detect any radiological releases from the plant including the dry fuel.

storage area. Monitoring wi 11 include contamination surveys,

thermoluminescent dosimeters (TLOs), and electronic dosimeters (EDs). *

TLDs and EDs will be placed at variotis locations around the fenced pad

including the guard stations and the administration building. The*

operations depa~tment will monitor cask vent tempefatures daily.

The

radiation monitoring plan appeared to be adequate.

No virilations or deviati6ns we~e identified.

10.

Inspection Followup Items

Inspection Followup Items are matters which have been discussed with the

licensee, which w111 be reviewed further by the inspector, a*nd whith

involve some action on the part of the NRC or licensee or both.

One

Inspection Followup Item is closed in Section 2.

11.

Exit Interview

The scope and findings of the inspection were reviewed with licensee

representatives (Section 1) at the conclusion of the inspection on

Aprjl 8, 1993.

The jnspector discussed the Ihspection Followup Item in

. Section 2, licensee performance in the chemistry comparison program *

along with observations on laboratory quality assurance, the water

chemistry program, radiation monitoring for dry fuel storage, and the

REMP.

During the exit interview, the inspector discussed the likely

informational content of the inspection report with regard to documents

or processes reviewed during the inspection.

Licensee representatives

did not identify any such documents or processes as proprietary.

Attachment: Table 1, Chemistry

Comparison Results, 2nd

Quarter 1993

"*

J

'"

TABLE 1

Nonradiological Chemistry Comparisons Results

Palisades Nuclear Generating Plant

April 5-8, 1993

Analyte

Method1 Conc2

Ratio3

Acceptance Ranges4

Result5

+/- 2RSD

+/- 3RSD

filU2

,---.

Fluoride

A

IC

0.956.. 0.875-1.125

0. 813-1.187.A

B

0.955

0. 875-1.125

0. 813-1.187

A

c

0;950

0.875-1.125

0. 813-1.187

A

Chloride

A

IC

0.954

0. 933-:-1. 067

0. 900-1.100

A.

B

0.916

0. 919-1. 081

0.887-1.113

A+

c

0.946

0.926-:-1.074

0.895-1.105 *A

Sulfate

A

IC

0.925

0.895-1.105

0.842-1.158

A

B

. 0.927

0.895-1.105

0. 868-1.132

A

c

. 20

0.959

0. 900-1.100

0.867-1.133

A.

Iron

G

AA/FU

1.076

0. 904-1. 096 * 0.854-1.146

A

H

l.o3e

0.903-1.097

0.857-1.143

A

I

1.047

0. 903-1. 097

0.855-1.145

A

Copper

G

AA/FU

1.031

0. 904-1. 095

0.859-1.141

A

H

0.963

0. 904-1. 096

0.857-1.143

A

I.

0.. 973

0. 904-1. 096

0.857-1.143

A

Sodium

J

AA/FU

1.047

0. 863-1.137

0.784-1.216

A

K

1.013

0.859-1.141

0.788-1.212

A

L

0.997

0.862-1.138

0. 789-1. 211

A

Lithium

JJ

AA/FL

500

1.099

0. 859-1.141

0. 788-1.212

A

KK

1000

1.045

0.859-1.141

0. 788-1. 212

A

LL

2000

1.026

0.868,.-1.142

0.787-1.213

A

Ammonia

M

Spec

1000

0.984

0. 902-1. 098

0.. 856-1.147

A

N

3000

1.045

0. 902-1. 098

0.856-1.147

A

5000

1.048

0. 902-1. 098

0.856-1.147

A

Hydrazine

p

Spec

0.901

0.922-1.078

0. 888-1.118

A+

Q

100

0.864

0. 922-1. 078

0. 888-1.118

D

R

250

1.070

0.922-1.078

0.888-1.118

A

Rerun

p

Spec

0.989

0.922-1.078

0. 888-1.118

A

Q

100

1.006

0. 922-1. 078

0. 888-1.118

A

R

250

0.986

0.922-1.078

0. 888-1.118

A

Analyte

Method1 Conc2

Ratio3

Acceptance Ra~ges

Result5

+/- 2RSD.

+/- 3RSD

Silica

T

Spec

u

100

250

1.001

1.053

0.906-1.094 * 0.859-1.141

A

0.909-1.091

0.860-1.136

A

RIDTI

Boron

D Titr

1000

1.004

0.979-1.021

0. 968-1. 032

E

3000

1.028

0.979-1.021

0. 968-1. 032

F

5000

1.009

0.979-1.021

0. 968-1. 032

E

Rerun 3000

1.005

0.979-1.021

0. 968-1. 032

1.

Methods: Titr - Titration

IC

- Ion Chromatography

Spec - Ultraviolet/Visible Spectrophotometry

AA/FL

Atomic Absorption Spectrophotometry

- Flame

AA/FU

Atomic Absorption Spectrophotometry

Furnace

2.

Cone: Approximate concentr~tion analyzed.

3.

Ratio-of Licensee mean value to NRC mean value.

A

A+

A

A

4.

  • The relative standard deviations {RSD) in the sixth and seventh columns.*

represent~ the trieffjcient of variation obtained from averaging licensee

data from the preceding cycle {Table 2.1 of NUREG/CR-5244).

A result is

considered to be_in agreement if it falls within the +/-2 SD range; a

qualified agreement if it lies outside +/-2 SD, but within +/-3 SD;*and in

disagreement if it is outside the +/-3 SD range.

5.

Result:

A = Agreement: Licensee value is within +/-2 SDs of the NRC mean

value.

  • A+ = Qualified agreement, licensee is between +/-2 and +/-3 SDs of

the NRC value.

D =Disagreement: licensee value is outside +/-3 SDs.

2