IR 05000237/2019002
| ML19220B101 | |
| Person / Time | |
|---|---|
| Site: | Dresden |
| Issue date: | 08/08/2019 |
| From: | Kenneth Riemer NRC/RGN-III/DRP/B1 |
| To: | Bryan Hanson Exelon Generation Co, Exelon Nuclear |
| References | |
| IR 2019001, IR 2019002 | |
| Download: ML19220B101 (35) | |
Text
August 8, 2019
SUBJECT:
DRESDEN NUCLEAR POWER STATION, UNITS 2 AND 3INTEGRATED INSPECTION REPORT 05000237/2019002; 05000249/2019002; AND 07200037/2019001
Dear Mr. Hanson:
On June 30, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Dresden Nuclear Power Station, Units 2 and 3. On July 8, 2019, the NRC inspectors discussed the results of this inspection with Mr. P. Karaba, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.
The NRC inspectors did not identify any finding or violation of more than minor significance.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Kenneth R. Riemer, Chief Branch 1 Division of Reactor Projects
Docket Nos. 05000237; 05000249; and 07200037 License Nos. DPR-19 and DPR-25
Enclosure:
As stated
Inspection Report
Docket Numbers:
05000237; 05000249; and 07200037
License Numbers:
Report Numbers:
05000237/2019002; 05000249/2019002; and 07200037/2019001
Enterprise Identifiers: I-2019-002-0065 and I-2019-0001-0110
Licensee:
Exelon Generation Company LLC
Facility:
Dresden Nuclear Power Station, Units 2 and 3
Location:
Morris, IL
Inspection Dates:
April 01, 2019 to June 30, 2019
Inspectors:
J. Cassidy, Senior Health Physicist
J. Dalzell, Health Physicist
G. Edwards, Health Physicist
R. Elliott, Resident Inspector
N. Fields, Health Physicist
J. Havertape, Resident Inspector
A. Nguyen, Senior Resident Inspector
C. Phillips, Project Engineer
M. Porfirio, Illinois Emergency Management
C. St. Peters, Reactor Engineer
Approved By:
Kenneth R. Riemer, Chief
Branch 1
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Dresden Nuclear Power Station, Units 2 and 3, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors.
Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
No findings or violations of more than minor significance were identified.
Additional Tracking Items
Type Issue Number Title Report Section Status LER 05000249,05000237/2 019-001-00 LER 2019-001-00 for Dresden, Unit 2 and 3,
Secondary Containment Differential Pressure Exceeded Technical Specification due to Excess Ventilation Supply Flow.
71153 Closed
PLANT STATUS
Unit 2 began the inspection period at full power. On May 9, 2019, the reactor automatically scrammed due to a main turbine trip caused by a failure in the main turbine lubricating oil system. Unit 2 remained shut down in forced outage D2F57 for repair activities until May 13, 2019, when it synchronized back to the grid. The unit reached full power on May 17, 2019. On June 6, 2019, the unit was down powered to approximately 62 percent to conduct repairs on two Main Turbine Control Valve linear variable differential transducers (LVDTs) and perform a control rod sequence exchange. The unit returned to full power later that day and remained there for the rest of the inspection period.
Unit 3 began the inspection period at full power. On May 3, 2019, the unit was down powered to approximately 85 percent for repairs to the Main Turbine Control Valve #4 LVDT. The unit returned to full power the same day. On June 1, 2019, the unit was down powered to approximately 73 percent for quarterly turbine and main steam isolation valve testing, feedwater regulating valve maintenance, and control rod exercising and sequence exchange. The unit returned to full power on June 2, 2019, and remained there for the rest of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
External Flooding Sample (IP Section 03.04) (1 Sample)
- (1) On April 29, 2019, through May 3, 2019, during periods of heavy rain and river flooding, the inspectors evaluated readiness to cope with external flooding for the following areas: Cribhouse, Unit 2 and Unit 3 emergency core cooling system (ECCS) corner rooms and torus basements, and the 2/3 emergency diesel generator room.
Summer Readiness Sample (IP Section 03.01) (1 Sample)
The inspectors verified that the licensees procedures and associated plant features for operation of both offsite alternating current (AC) power systems and the onsite alternate AC power systems appropriately addressed measures to monitor and maintain continued availability and reliability.
- (1) On June 25, 2019, through June 28, 2019, the inspectors evaluated summer readiness of offsite and alternate AC power systems by performing walkdowns of the 345kV Switchyard, the Unit 2 and Unit 3 transformer yard, the Auxiliary Electrical Equipment Room, and the station battery rooms.
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Unit 2 Division II low pressure coolant injection (LPCI) and containment cooling service water (CCSW) systems on April 1 and 2, 2019
- (2) Unit 3 core spray system on April 29 and 30, 2019
- (3) Unit 2 control rod drive system on May 10, 2019
71111.05Q - Fire Protection
Quarterly Inspection (IP Section 03.01) (5 Samples)
The inspectors evaluated fire protection program implementation in the following selected areas:
- (1) Fire Zone (FZ) 6.2, Unit 2/3 Computer Room and Auxiliary Electrical Equipment Room, Elevation 517 feet on April 9, 2019
- (2) FZ 8.2.4, Unit 2 and Unit 3 Cable Tunnel, Elevation 502 feet on April 10, 2019
- (3) FZ 8.2.5.E, Unit 3 Switchgear Area, Elevation 517 feet on May 1, 2019
- (4) FZ 11.2.3, Unit 2 High Pressure Coolant Injection (HPCI) Pump Room, Elevation 476 feet on May 1, 2019
- (5) FZ 11.1.2, Unit 3 Southeast Corner Room, Elevation 476 feet on May 1, 2019
71111.06 - Flood Protection Measures
Inspection Activities - Internal Flooding (IP Section 02.02a.) (1 Sample)
The inspectors evaluated internal flooding mitigation protections in the:
- (1) Unit 2 and Unit 3 CCSW Vaults
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (2 Samples)
- (1) The inspectors observed and evaluated licensed operator performance in the Control Room during an emergent downpower on Unit 3 to repair the turbine control valve #4 LVDT cable on May 3, 2019
- (2) The inspectors observed and evaluated licensed operator performance in the Control Room during the Unit 2 SCRAM on May 9, 2019, and subsequent startup activities on May 11, 2019, through May 13, 2019
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
- (1) The inspectors observed and evaluated annual exam senarios on May 15, 2019
71111.12 - Maintenance Effectiveness
Routine Maintenance Effectiveness Inspection (IP Section 02.01) (1 Sample)
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
- (1) Unit 2 and Unit 3 Reactor Building sumps and floor drain system
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
- (1) Planned elevated risk on Unit 2 for the Division I LPCI and CCSW system maintenance windows on April 1 and 2, 2019
- (2) Emergent elevated risk work to troubleshoot and repair the Unit 3 digital electrohydraulic control system controller failure on April 10, 2019
- (3) Planned elevated risk for the Unit 3 HPCI room cooler maintenance window and the emergent risk impacts due to human performance issues on April 29, 2019, through May 2, 2019
- (4) Emergent work to repair the Unit 3 turbine control valve #4 LVDT cable on May 2 and 3, 2019
- (5) Emergent work to identify and repair the Unit 2 main condenser in-leakage, to address the Unit 2 B steam jet air ejector system perturbation, and elevated plant risk for adverse weather on May 16 and 17, 2019
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 02.02) (5 Samples)
The inspectors evaluated the following operability determinations and functionality assessments:
(1)3A Reactor Building Closed Cooling Water System Heat Exchanger Flaw Assessment
- (2) Unit 3 Emergency Diesel Generator Pre-Lube Oil Line Support Clamp is Not Fully Engaged
- (3) Potential vulnerability identified within the Core Spray system initiation logic
- (4) Historical operability review of the Unit 2 Low Pressure ECCS Permissive Pressure Switch that did not pass its Technical Specification surveillance
- (5) Unit 1 Diesel Fire Pump did not meet its surveillance acceptance criteria
71111.19 - Post-Maintenance Testing
Post Maintenance Test Sample (IP Section 03.01) (6 Samples)
The inspectors evaluated the following post maintenance tests:
(1)3A service water pump leak checks and maintenance run on April 13, 2019
- (2) DOS 6600-01, Unit 3 Diesel Generator Surveillance Test on April 24, 2019
- (3) Diagnostic testing of AOV 2-2001-5, Unit 2 Drywell Equipment Drain Sump Valve, after emergent repairs on May 5 and 6, 2019
- (4) Unit 2 Average Power Range Monitor 6 calibrations and testing following power supply replacement on May 12, 2019
- (5) Unit 2 Source Range Monitor 23 calibration and testing following repair on May 9 and 10, 2019
- (6) DOS 2300-01, HPCI Valve Operability and Timing, after HPCI 2-2301-29 regulator replacement on June 18, 2019
71111.20 - Refueling and Other Outage Activities
Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)
- (1) D2F57, Unit 2 Forced Outage after a SCRAM from May 9, 2019, through May 17, 2019
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
FLEX Testing (IP Section 03.02)
- (1) Work Order (WO) 4882157 and WO 4882158, Annual A and B FLEX Barge Pump and Motor Operation Tests, on June 26, 2019
Inservice Testing (IP Section 03.01) (1 Sample)
- (1) DOS 1100-04, 2A Standby Liquid Control System Quarterly/Comprehensive Pump Test, on April 4, 2019
Surveillance Tests (other) (IP Section 03.01) (2 Samples)
- (1) DIS 1500-32, Unit 2 Division I & II LPCI ECCS Loss-of-Offsite-Power Selection Circuitry Logic System Functional Test, on April 17, 2019
- (2) DOS 7000-03, Local Leak Rate Testing of the Primary Containment Airlock, on May 12, 2019
71114.06 - Drill Evaluation
Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (2 Samples)
(1)2nd Quarter 2019 Focus Area Drill on June 6, 2019 (2)2019 Pre-Exercise Drill on June 25,
RADIATION SAFETY
71124.05 - Radiation Monitoring Instrumentation
Calibration and Testing Program (IP Section 02.02) (1 Sample)
The inspectors evaluated the calibration and testing program implementation.
- (1) The inspectors reviewed the following:
Alarm Setpoint and Calibration Method Check of Personnel Contamination Monitors, Portal Monitors and Small Article Monitors
- Bicron-NE IPM9D; Serial Number (SN) IPM9-143
- Bicron-NE IPM9D; SN IPM9-154
- Canberra ARGOS 5AB; SN 1011-286
- Canberra ARGOS 5AB; SN 1011-277
- Thermo Small Article Monitoring 12; SN SAM12-151
- Thermo Small Article Monitoring 12; SN SAM12-152
Failure to Meet Calibration or Source Check Acceptance Criteria
- Mirion MGP AMP-100; SN 0020787
- Ludlum 177; SN 22697
- Thermo RM25; SN 79403
Walk Downs and Observations (IP Section 02.01) (1 Sample)
The inspectors evaluated radiation monitoring instrumentation during plant walkdowns.
- (1) The inspectors reviewed the following:
Portable Survey Instruments
- Ludlum 177; SN 32173
- Ludlum 177; SN 19267
- Ludlum 177; SN 36092
- Bicron RSO-5; SN 0022758
- Thermo Fischer RO 20; SN 078610
Source Check Demonstration
- Eberline RO20; SN 078046
- Rotem Ram Gam-1; SN 079477
- Ludlum 3; SN 0011111 Area Radiation Monitors and Continuous Air Monitors
- Unit 2 Reactor Building 517 Drywell Continuous Air Monitor
- Unit 3 Reactor Building 517 Drywell Continuous Air Monitor
- Unit 3 Area Radiation Monitor (ARM) Reactor 613 Spent Fuel Pool
- Unit 3 ARM Reactor 613 Spent Fuel Pool West Wall
- Max Recycle ARM Chemical Addition Room
Personnel Contamination Monitors, Portal Monitors and Small Article Monitors
- Canberra ARGOS 5AB; SN 1011-286
- Canberra ARGOS 5AB; SN 1011-277
- Canberra ARGOS 5AB; SN 1206-083
- Thermo Small Article Monitoring 12; SN SAM12-151
71124.06 - Radioactive Gaseous and Liquid Effluent Treatment
Calibration and Testing Program (Process & Effluent Monitors) (IP Section 02.02) (1 Sample)
The inspectors reviewed the following gaseous and liquid effluent monitor instrument calibrations and tests:
(1)
- WO 04618727-01 Unit 2/3 Quarterly Chimney Particulate, Iodine and Noble Gas Monitor
- WO 04669719-01 Unit 2/3 Quarterly Reactor Building Ventilation Particulate, Iodine, and Noble Gas Monitor Functional Test
Dose Calculations (IP Section 02.05) (1 Sample)
The inspectors reviewed the following to asses public dose:
- (1) The inspectors reviewed the following liquid and gaseous discharge permits to evaluate public dose calculations:
- G-20170801-586-C
- G-20170801-587-C
- G-20170801-582-C
- L-20170801-221-C
The inspectors also reviewed the following annual radiological effluent release reports:
- Corrected Dresden Nuclear Power Station 2017 Radioactive Effluent Release Report
- Dresden Nuclear Power Station 2018 Radioactive Effluent Release Report
Abnormal gaseous or liquid tank discharges
- None were available for review during this inspection
Instrumentation and Equipment (IP Section 02.04) (1 Sample)
The inspectors reviewed the following radioactive effluent discharge system surveillance test results:
(1)
- Stand-By Gas Treatment High Efficiency Particulate Filter Leak Test
- High Radiation Sample Sink High Efficiency Particulate Filter and Charcoal Testing
Sampling and Analysis (IP Section 02.03) (1 Sample)
The inspectors reviewed the following:
- (1) The inspectors reviewed the following radioactive effluent sampling and analysis activities:
- Unit 2 Reactor Building particulate, iodine, and noble gas sample collection
- Unit 3 Reactor Building particulate, iodine, and noble gas sample collection
- Station Chimney particulate and iodine sample collection
Effluent discharges
- None were available for review during this inspection
Walk Downs and Observations (IP Section 02.01) (1 Sample)
The inspectors walked down the following gaseous and liquid radioactive effluent monitoring and filtered ventilation systems to assess the material condition and verify proper alignment according to plant design:
(1)
- Unit 2 Reactor Building Gaseous Discharge System
- Unit 3 Reactor Building Gaseous Discharge System
- Storm Water Collection System
71124.07 - Radiological Environmental Monitoring Program
Groundwater Protection Initiative (GPI) Implementation (IP Section 02.02) (1 Sample)
- (1) The inspectors examined the remediation efforts associated with the 2014 Condensate Storage Tank Leak and other historical leaks at the facility.
Site Inspection (IP Section 02.01) (1 Sample)
The inspectors evaluated the radiological environmental monitoring program implementation.
- (1) The inspectors evaluated the radiological environmental monitoring program implementation.
Walkdowns and calibration and maintenance record review
- Air Sampling Station D-03
- Air Sampling Station D-04
- Air Sampling Station D-07
- Thermoluminescent dosimeter (TLD) Monitoring Station D-03
- TLD Monitoring Station D-04
- TLD Monitoring Station D-07
The inspectors observed the following environmental sample collections and preparation:
- Water Sample DSP 34A
- Water Sample DSP 34B
Licensee actions in response to missed sample, inoperable sampler, lost TLD or anomalous measurement
- D-25 (MI) (Milk); 06/27/2018; Farmer Resting Cow, Grass Substituted
- D-04 (AP/AI) (Air Sampler); 10/19/2018; Low Reading of 67.5 Hours Due to Power Outage
- D-23 (WW) (Well Water); 06/08/2018; Home Vacant, Water Turned Off
Sampling program for the potential of licensed material entering groundwater
- Storm Water Collection System
- Monitoring Well MD-11
- Monitoring Well MW-DN-119I
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
MS06: Emergency AC Power Systems (IP Section 02.05)===
- (1) Unit 2, April 1, 2018 - March 31, 2019
- (2) Unit 3, April 1, 2018 - March 31, 2019
MS07: High Pressure Injection Systems (IP Section 02.06) (2 Samples)
- (1) Unit 2, April 1, 2018 - March 31, 2019
- (2) Unit 3, April 1, 2018 - March 31, 2019
OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)
- (1) May 1, 2018 - May 1, 2019
PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample.
(IP Section 02.16) (1 Sample)
- (1) October 1, 2018 - March 31, 2019
71152 - Problem Identification and Resolution
Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
- (1) Preventive maintenance and monitoring of the Reactor Protection Scheme (RPS)logic relays on Units 2 and 3
Semiannual Trend Review (IP Section 02.02) (1 Sample)
- (1) The inspectors reviewed the licensees corrective actions associated with an identified adverse trend in the area of Human Performance to ensure that it is not indicative of a more significant safety issue.
71153 - Follow-up of Events and Notices of Enforcement Discretion Event Follow-up (IP Section 03.01)
- (1) The inspectors completed a Post-SCRAM review following the Unit 2 Turbine/Reactor Trip on May 9, 2019.
Event Report (IP Section 03.02) (1 Sample)
The inspectors evaluated the following licensee event reports (LERs):
- (1) LER 05000237/2019-001-00, Secondary Containment Differential Pressure Exceeded Technical Specification Due To Excess Ventilation Supply Flow (ADAMS Accession: ML19091A046) The circumstances surrounding this LER are documented in the results section and this LER is closed.
OTHER ACTIVITIES
- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL
60855.1 - Operation of an Independent Spent Fuel Storage Installation at Operating Plants Operation of an Independent Spent Fuel Storage Installation at Operating Plants
- (1) The inspectors evaluated the licensees independent spent fuel storage installation cask loading activities on April 29th through May 3rd. Specifically, the inspectors observed the following activities:
- Fuel loading of MPC-68M-614
- Removal of the loaded transfer cask (HI-TRAC) from the spent fuel pool
- Lid-to-shell root pass welding
- Hydrostatic testing and non-destructive weld evaluations
- Canister processing including bulk water removal (blowdown) and forced helium dehydration
- Vent and drain port cover welding and non-destructive weld evaluations
- Helium leak testing
- Stack-up and download of the Multi-Purpose Canister from the HI-TRAC into the storage cask (HI-STORM)
- Radiological field surveys
The inspectors performed walkdowns of the East and West Independent Spent Fuel Storage Installation (ISFSI) pads, including independent radiation surveys, and walkdowns of the ISFSI haul path and vertical cask transporter.
The inspectors evaluated the following:
- Spent fuel selection for the four casks for this loading campaign
- Changes to the Emergency Plan related to the ISFSI Emergency Action Levels
- Selected corrective action program action requests
- Selected 72.48 screenings
- Change in canister drying method from vacuum drying to forced helium dehydration
INSPECTION RESULTS
Observation: Preventive Maintenance and Monitoring of the RPS Logic Relays 71152 On May 21, 2019, Unit 3 received a spurious Channel B Reactor Scram signal (half scram). During troubleshooting efforts, it was identified that the 3-0590-108F relay (Unit 3 Channel B RPS Scram Contactor) was chattering and tripped multiple times. Jumpers were installed around the B RPS Channel test switch, which was a source of high resistance in the past, and troubleshooting was conducted to take voltage readings along the B2 RPS logic string. High resistance and dirty contacts were found on the 3-0590-105D, Low Reactor Water Level, HFA relay. The contacts were burnished on the 3-0590-105D relay, as well as the other relays in the logic string, to ensure any resistance buildup was cleared before returning the system to service. Extent of condition voltage checks were completed on all RPS logic strings on both Unit 2 and Unit 3 and no other issues were identified.
The inspectors observed the licensees troubleshooting and extent of condition efforts. They also reviewed the licensees work group evaluation which included an evaluation of the stations maintenance practices for the components within the RPS logic strings since this was not the first instance of dirty contacts and high resistance causing spurious half scrams.
The inspectors reviewed industry operating experience and preventive maintenance templates to ensure the proper maintenance practices were being implemented. The inspectors determined that the licensee conducted a timely evaluation of the issue with sufficient detail to identify appropriate corrective actions. The extent of condition checks and evaluation were timely and of sufficient depth to ensure the risk to other components was appropriately addressed.
The corrective actions for the dirty contacts include enhanced monitoring and voltage checks during the quarterly surveillance activities that cycle these contacts. However, the inspectors did note that the frequencies of these surveillances are currently under revision per the Surveillance Frequency Control Program to move from quarterly to semi-annually and then eventually to yearly, which will decrease the potential effectiveness of them in timely detection of increased resistance across the contacts. The inspectors also noted that these relays used to have a replacement frequency of every 8 years, which was recently changed to an as-needed basis. This change was implemented based on changes to industry templates for HFA relay maintenance. Most relays for both units have been replaced within the last 5 to 8 years. Other components within the RPS logic strings, such as the test switches and RPS scram contactors, still have replacement frequencies corresponding to unit outages and industry templates. The inspectors determined that while the enhanced monitoring corrective actions seem reasonable, the changes in the surveillance frequencies and preventive maintenance practices will need to be monitored closely to ensure that equipment degradation can still be detected in a timely manner to prevent potential failures which could cause instability of the unit.
Observation: Semi-Annual Trend Review of Decline in Human Performance and Equipment Reliability 71152 The inspectors and licensee have identified declines in the areas of Human Performance and Equipment Reliability throughout the 6-month period from January 2019 through June 2019.
The licensee has completed or is in the processing of completing multiple causal products related to the declines in these areas. There have also been several external assessments throughout the first half of 2019 that have highlighted areas for improvement in the licensee's current plans to address these deficiencies. Following are some examples and overall summaries of the issues.
The licensee has experienced multiple equipment failures since the fall of 2018 that have included safety-related and nonsafety-related, but risk-significant, components. Some of the equipment failures have led to emergent unit down powers or unscheduled high-risk work windows to effect repairs. As an example, in May 2019, Unit 2 experienced a turbine trip and a subsequent reactor scram due to improper maintenance on a portion of the main turbine lube oil system, which starved couplings on one of the main turbine shaft components from being properly lubricated. The turbine tripped on low lube oil system pressure and the couplings and shaft in question were found to be severely degraded and overheated due to the lack of oil flow. The maintenance error was believed to have occurred in 2013 when a gasket that allowed lube oil to enter the coupling area of the shaft was not properly fabricated (missing a hole) and caused a lower than designed oil flow to the couplings. The root cause report for this event is still in progress and the residents will review this information as it gets finalized to determine if there is a performance deficiency.
The licensee has also experienced multiple events where underlying causes of the issues were determined to be lack of risk recognition or appropriate mitigation strategies for work.
An example of this was in January 2019, when the Unit 2 Reserve Auxiliary Transformer tripped during maintenance. Workers were installing a modification on the transformer and while performing that work came into contact with a relay on the door of the transformer. This contact resulted in the transformer tripping and the loads from the transformer automatically transferring to their backup source. The work was not screened as risk-significant and the impact of contact with this particular relay (or even its location in the cabinet) were not realized prior to work commencing in the field. This issue did have an associated violation that was documented in the first quarter 2019 report (2019001).
Another example was in April 2019, when maintenance personnel were performing work on the Unit 3 HPCI room cooler. They were attempting to drain the cooler when valves in the system were found to be leaking significantly onto components in the area. Directly underneath the cooler were junction boxes for some of the motor-operated valves in the HPCI system. One of these valves was the minimum flow valve and it opened when water intruded into the box. This caused the torus level on Unit 3 to rise. The operators in the control room did not identify this rise in torus level until the high-level alarms were received in the control room approximately 90 minutes later. This event illustrated both the lack of risk recognition and mitigation on behalf of the maintenance workers for the potential water impact on components in the area and also showed the human performance error of the operators in the control room for not properly monitoring their control boards to identify an abnormal condition. This issue was determined to not have an associated performance deficiency.
Minor Violation 71153 Minor Violation: On January 30, 2019, the licensee lost secondary containment when actions were taken, in accordance with Dresden Abnormal Operating procedure (DOA) 5700-01, Loss of Heating Boilers, Revision 25, to open the doors to the reactor building ventilation plenum after a trip of the heating boiler which was a performance deficiency. The licensee stated in LER 2019001-00 that the cause of the loss of secondary containment was inadequate procedural guidance in DOA 5700-01, Loss of Heating Boilers, Revision 25.
Technical Specification 5.4.1.a required that written procedures shall be established, implemented, and maintained covering the following activities: The applicable procedures recommended in Regulatory Guide 1.33, Revision 2; Appendix A, February 1978; Regulatory Guide 1.33, Revision 2; Appendix A, February 1978, Paragraph 6, Procedures for Combating Emergencies and Other Significant Events, Subparagraph r; and Other Expected Transients that may be Applicable, applied to DOA 5700-01.
The inspectors reviewed the licensees causal documentation and the corrective actions proposed and taken which were documented in Action Request 4215383, North RB DP
[reactor building differential pressure] Local Indication On 613 feet Not Accurate, dated January 30, 2019, and had no further concerns.
Screening: The inspectors determined the performance deficiency was minor. The inspectors answered no to all four questions from IMC 0612, Appendix B, Issue Screening, dated January 1, 2018, because the event only lasted a few moments.
Enforcement:
This failure to comply with Technical Specification 5.4.1.a constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On July 8, 2019, the inspectors presented the integrated inspection results to Mr. P. Karaba, Site Vice President, and other members of the licensee staff.
- On May 2, 2019, the inspectors presented the independent spent fuel storage installation inspection results to Mr. J. Stovall, Plant Manager, and other members of the licensee staff.
- On May 3, 2019, the inspectors presented the radiation protection inspection results to Mr. J. Stovall, Plant Manager, and other members of the licensee staff.
- On June 27, 2019, the inspectors presented the Radiation Protection Inspection Results to Mr. P. Karaba, Site Vice President, and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
60855.1
ALARA Plans
DR-0-19-00204/5
2019 Dry Cask Activities (4 Casks)
03/13/2019
Calculations
DRE00-0022
Expanded Analysis to Address Change to HI-STORM
Overpack
DRE06-0037
Dose Versus Distance from a Single Cask at the Dresden
DRE06-0038
HI-STORM CoC Radiation Protection Program Dose Rate
Limits for Dresden
DRE15-0011
Thermal Evaluation of HI-STORM Under Flood Condition at
Dresden
03/11/2015
DRE18-0012
Independent Spent Fuel Storage Installation (ISFSI)
Expansion - Construction Pad Design
DRE19-0001
Cask Loading Design Analysis
01/15/2019
DRE19-0002
Dresden Unit 2 Fuel Selection Packages for 2019 Campaign
- ISFSI
01/28/2019
DRE19-0003
Dresden Unit 2 Fuel Selection Package Alternate
Assemblies for 2019 Campaign - ISFSI
01/28/2019
Corrective Action
Documents
Selected ISFSI-Related Action Requests Generated Since
May 30, 2016
NOSA-DRE-16-
Independent Spent Fuel Storage Installation Audit Report
11/02/2016
NOSA-DRE-18-
Independent Spent Fuel Storage Installation Audit Report
2/04/2018
Dresden Spent Fuel Loading Campaign (SFLC) Readiness
Assessment
03/08/2019
Corrective Action
Documents
Resulting from
Inspection
2/3-7900 HMPL2 High Mast Pole Light One Fixture is Out
05/01/2019
NRC ID'ed Record of PM WO Missing Procedure
05/03/2019
Recommended Clarification of Source Term Limits in FSPS
05/20/2019
Engineering
Changes
26654
Dresden 2019 Dry Cask Storage Fuel Selection Packages -
2/21/2019
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
26911
Spent Fuel Casks for the 2019 Loading Campaign
Dry Cask Storage - East ISFSI Screen Replacements
2
FHD Skid Evaluation for Dry Cask Processing
2/04/2019
Issue Major Revision 001 to DRE06-0036 West ISFSI Fire
Hazard Analysis
07/03/2018
ECR 440769
Railroad Track Inspection
04/08/2019
Miscellaneous
05/18/2017
Registration of Use of Casks to Store Spent Fuel
06/16/2016
Registration of Use of Casks to Store Spent Fuel
05/05/2017
Registration of Use of Casks to Store Spent Fuel
06/06/2017
Registration of Use of Casks to Store Spent Fuel
05/17/2018
Registration of Use of Casks to Store Spent Fuel
06/14/2018
CFR 72.48 Evaluation Summary Report
11/18/2017
Dresden Nuclear Power Station Units 1, 2, and 3 East ISFSI
CFR 72.212 Evaluation Report
Dresden Nuclear Power Station Units 1, 2, and 3 West ISFSI
CFR 72.212 Evaluation Report
Selected 72.48 Screenings Performed Since May 30, 2016
Environmental Dosimetry Reports for 2016, 2017, and 2018
Non-Destructive Inspector Certification Records for Mass
Spectrometer Leak Testing Personnel
Certifications and Examinations for Visual and Liquid
Penetrant Inspection Personnel
03/21/2019
Qualifications for Welding Personnel
Fuel Handlers Dry Cask Storage Qualifications
04/22/2019
Re: Railroad Track Inspection
04/07/2019
Table of Gamma and Neutron Sources of the Bundles
Selected for MPC-68-613
05/20/2019
1305096
QCGS Rail Pockets
06/20/2005
243699
Receipt 243699 Cat ID 1407896-3, 1459940-3 Container,
Cask, Storage, Concrete, HI-STORM (Receipt Docs and
Checklists)
01/09/2019
2.48-547
Procedure DFP 0800-65, Revision 14, Spent Fuel Cask Site
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Transportation
Addendum 3
Emergency Action Levels for Dresden
Quality Assurance Topical Report
Required Reviews and Approvals
03/25/2019
SVPLTR: #16-
0049
Dresden Nuclear Power Station Independent Spent Fuel
Storage Installation Annual Radioactive Material Effluent
Release Report
09/01/2016
SVPLTR: #17-
0040
Dresden Nuclear Power Station Independent Spent Fuel
Storage Installation Annual Radioactive Effluent Release
Report
09/18/2017
SVPLTR: 18-
25
Dresden Nuclear Power Station Independent Spent Fuel
Storage Installation Annual Radioactive Effluent Release
Report
08/15/2018
NDE Reports
Helium Leak Test Report Vent and Drain Port Cover Plates
05/02/2019
Liquid Penetrant Examination Data Sheet Reactor Building
Crane Hook
2/21/2019
Magnetic Particle Examination Data Sheet Reactor Building
Crane Hook
2/22/2019
Report No.
914601-614-01
Report of Nondestructive Examination Lid to Shell Weld
05/02/2019
Report No.
914601-614-02
Report of Nondestructive Examination Lid to Shell Weld
05/02/2019
Report No.
914601-614-03
Report of Nondestructive Examination Lid to Shell Weld
05/02/2019
Report No.
914601-614-04
Report of Nondestructive Examination Lid to Shell Weld
05/02/2019
Procedures
Environmental Dosimetry - Performance Specifications,
Testing, and Data Analysis
DFP 0800-65
Spent Fuel Cask Site Transportation
DFP 0800-68
HI-TRAC Preparations
DFP 0800-69
HI-TRAC Movement Within the Unit 2/3 Reactor Building
DFP 0800-70
HI-TRAC Loading Operations
DFP 0800-74
Helium Cooldown System Operation and MPC Reflood
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
DFP 0800-82
HI-TRAC/MPC Unloading Operations in the Unit 2/3 Reactor
Building
DRS 6021-33
Independent Spent Fuel Storage Installation Radiation
Survey
GQP - 9.0
Training, Qualification, Examination, and Certification of
NDE Personnel in Accordance with SNT-TC-1A and CP-189
GQP - 9.2
High Temperature Liquid Penetrant Examination and
Acceptance Standards for Welds, Base Materials and
Cladding (50 degrees - 350 degrees Fahrenheit)
GQP - 9.6
Visual Examination of Welds
H2-MON-002
Hydrogen Monitoring for Holtec Canisters
Exelon 72.48 Review Process
Rigging and Lifting Program
Control of Heavy Loads Program
MA-DR-MM-4-
58904
Dry Cask Storage Special Lifting Device Inspection/Testing
MSLT-MPC-
EXELON-MW
Helium Mass Spectrometer Leak Test Procedure
Multipurpose Canister
Fuel Selection for Dry Cask Storage Process Description
Fuel Selection and Documentation for Dry Cask Loading
Dry Cask Storage/ISFSI Inspection Surveillance Program
OU-MW-671-200
MPC Processing Forced Helium Dehydration (FHD) for
PI-CN-STR-OP-
EXE-H-01
Closure Welding of Holtec Multi-Purpose Canisters at Exelon
Facilities
Area Dosimeter Surveillance
Holtec HI-TRAC Radiation Survey
0, 2
Holtec HI-STORM Radiation Survey
Radiation
Surveys
East and West ISFSI Pad Surveys for 2016, 2017, and 2018
DRS 6021-33
Data Sheet 2 West ISFSI Radiation Survey
04/23/2019
Dresden HI-TRAC Radiation Survey
04/19/2019
Dresden HI-STORM Radiation Survey
04/23/2019
RP-DR-300-102,
HI-STAR Serial Number 100-004, 100-005, 100-006, 100-
10/03/2018
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
1, 2,
and 4
007, and 100-Prototype
Work Orders
01318757
Dresden 2/3 3 Year Com ISFSI Integrity Survey
06/03/2013
01654645
Dresden 2/3 3 Year Com ISFSI Integrity Survey
07/08/2016
4645034-02
Annual Inspection of Lifting and Rigging Equipment
06/19/2018
4648865
FH D2/3 14M Com HI-TRAC Trunnions Test
06/12/2018
4649346-01
2/3 14M Com ISFSI Test of HI-STORM Lift Bracket
06/18/2018
4650779
RXS D2/3 14M Inspection of MPC Lift Cleat 2/3-08209-2B
06/13/2018
4650780
D2/3 14M Inspection of MPC Lift Cleat 2/3-08209-2A
06/13/2018
4655193-01
RXS D2/3 AN Com Test of U2/3 RB 125 Ton Lift Yoke
06/27/2018
4698079
D2/3 14M Com ISFSI HI-STORM/HI-TRAC Cask
Surveillance
10/24/2018
4756601-01
D2/3 1Y Com OSHA Reactor Bldg Overhead Crane
2/22/2019
4756602-01
D2/3 1Y Com OSHA Insp Crane - RX Bldg Overhead
2/26/2019
4766851-01
D2/3 AN ISFSI 4-Point Transporter Preventive Maint Inspect
2/19/2019
4871389-01
EWP MM D2/3 30D PM Reactor Building Overhead Crane
Insp
2/01/2019
4871389-02
MM Perform Walkdown to Determine Status of D2/3 RB
Crane
01/28/2019
Corrective Action
Documents
1706696
Cable Conduit Above 2B Circulating Water Pump In-Ground
Leak
09/05/2014
2597308
NRC Degradation Question/East Wall of U2 HPCI Rm
2/07/2015
2736431
Continued Flood Seal Water In-Leakage in Unit 2/3 EDG Rm 11/02/2016
4162035
Dresden 2019 AR for Site Summer Readiness Actions
08/08/2018
4188768
2/3 EDG Rm. Flood Seal Increased Water In-Leakage Stains 10/29/2018
4188820
Roof Drain Active Leak Identified in 2/3 EDG Room
10/29/2018
209887
24/48 Volt DC System Summer Readiness
01/10/2019
28613
Unexpected Alarm, C-11, Main Transformer 3 Trouble
03/12/2019
242417
Extent of Condition for Loss of Oil Flow Alarm Functional
Checks for Unit 3 MPT 3
04/22/2019
253344
Both Unit 2 and Unit 3 ASD Heat Exchangers Plugging with
Cottonwood
05/31/2019
254371
Potential Design Issue/No Loss of Oil Flow Alarm on MPT 3
06/4/2019
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
255268
345kV Switchyard Battery Room High Temperature
06/7/2019
256896
May 2019 Lake Inspection Piezometer Wells
05/13/2019
258139
Transformer 3 Oil Cooler Fins have Cottonwood Buildup
06/20/2019
258559
Transformer 2 Oil Cooler Fins have Cottonwood Buildup
06/21/2019
258585
No Loss of Oil Flow Alarms Received for MPT 3
06/21/2019
258761
3B ASD Heat Exchanger Fins are Clogged
06/22/2019
259095
Cottonwood Accumulation for AEER HVAC System
06/24/2019
260114
06/27/2019
260501
Unit 3 Battery Room HVAC Filters Need Replacement
06/29/2019
Drawings
Flood Elevation Drawings, FL-1, -32, -33, -34, -37, -41
Electrical Installation Cribhouse Plans, Elevations 490 Feet
Inches and 517 Feet 6 Inches
BV
Electrical Installation Cribhouse Plans, Elevations 490 Feet
Inches and 517 Feet 6 Inches
Engineering
Changes
391644
Reactor and Diesel Building Flood Barriers
005
391644
Reactor and Diesel Building Flood Barriers
Procedures
DAN 902(3)-3 H-
DAN 902(3)-4 C-
LPCI/CS East Sump Lvl Hi
DAN 902(3)-4 D-
LPCI/CS West Sump Lvl Hi
DAN 902-7 A-16
Unit 2/3 Cribhouse Water Level High
DAN 903-8 C-11
Main Transformer 3 Trouble
DAN 923-4 A-3
DAN 923-4 B-2
U2 W REFD Sump LVL Hi-Hi
DAN 923-4 C-3
DAN 923-4 D-2
DMS 1600-04
Torus Water Tight Door, Surveillance and Maintenance
DOA 0010-04
Floods
DOA 6100-01
Main Transformer Trouble
DOS 1300-04
Operation of the Isolation Condenser External Flood
Emergency Make-up Pump
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Structures Monitoring
ER-DR-450-1001
Dresden Structures Monitoring Instructions
FSG-60
FLEX Flood Pump Deployment/Operation
FSG-62
FLEX Generator Deployment During a Flood
MA-DR-MM-6-
00101
Maintenance Activities for Site Flooding
OP-AA-108-111-
1101
Severe Weather and Natural Disaster Guidelines
OP-DR-108-111-
1001
Hot Weather Strategy
Seasonal Readiness
WC-DR-8003-
1003
Dresden Station Units 2 and 3 Nuclear Plant Interface
Requirements Procedure
Self-Assessments 3950787
Flood Seals
2/03/2017
Work Orders
01554979
Ground Water Intrusion in the 2/3 EDG Room
04/18/2019
01568782
Roof Drain Piping Leaking Into 2/3 EDG
01/28/2017
01781687
Inspect Flood Seals Unit 2/3 EDG Area: Outside Walls
10/25/2016
01877924
Inspect Flood Seals RB E&W Corner Rm Walls Against
Torus
10/26/2017
01964803
Inspect Flood Seals Unit 2/3 EDG Area: Outside Walls
11/08/2018
01965935
Inspect Flood Seals RB S Wall & E&W Corner RMS Adj to
Torus
11/08/2018
0988022
Cribhouse High Water Level Switch Functional Test
2/2/2016
4817860
Inspect/Clean Fire Pump Bay and Downstream Screens
2/13/2019
Corrective Action
Documents
203143
CRD Drawing Changes for PP Suction Relief Vlv Piping
2/13/2018
1563954
Air Leaking From Valve Positioner
09/26/2013
2607096
U2 CRD System Parameters Minor Fluctuations at Steady
State
01/03/2016
2677670
U2 CRD Drive Water PCV 2-0302-8 Abnormal
Noise/Vibration
06/03/2016
3974685
U2 A CRD FCV, FCV 2-0302-6A, Will Not Cycle Full Open
2/16/2017
4138726
PMC: CRD Pump Suction Relief Valves Should be Replaced
05/17/2018
4146075
2A CRD Pump Discharge MOV Valve Leak (2-0301-2A)
06/11/2018
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
4174268
DPS Leak on CRD FCV 2-0302-13A-8A
09/18/2018
4180224
U2 CRD Sys A Stab Insert FCV Degrading
10/04/2018
Drawings
M-27
Diagram of Core Spray Piping
AAN
Engineering
Changes
EC 439035 and
26747
Update CRD Drawings M-34 Sheet 1, M-40, M-365 Sheet
and M-370 Drawing Changes for PP Suction Relief VLV
Piping/AR 4203143
Procedures
DOP 0300-01
Control Rod Drive System Start Up and Operation
DOP 0300-E1
Unit 2 Control Rod Drive Electrical
DOP 0300-M1
Unit 2 Control Rod Drive Hydraulic System
DOP 1400-M1/E1
Unit 3 Core Spray System
DOP 1500-E1
Unit 2 LPCI and CCSW Electrical Checklist
DOP 1500-M1
Unit 2 LPCI and Containment Cooling Valve Checklist
Work Orders
U2 CRD System Parameters Minor Fluctuations at Steady
State
71111.05Q Corrective Action
Documents
4106319
Rain Water Leaking into Turb Bldg Behind Bus 31
2/21/2018
237828
NRC Identified Issues
04/09/2019
238193
NRC Walkdown 2/3 Cable Tunnel
04/10/2019
Procedures
Plant Barrier Control Program
DFPS 4175-02
Operating Fire Stop/Break Surveillance
Fire Protection System Impairment Control
OP-DR-201-
2-1001
21, RMA Checklist #21 U3 Turbine Bldg, Cable
Tunnel EL 502 Feet
Corrective Action
Documents
250565
Penetration MK 856 Found Above 200 scfh During DOS
1500-20
05/21/2019
251243
Penetration Seal Bolt Broken during Maintenance of CCSW
Seal
05/23/2019
252333
U3 CCSW Vault Penetrations Removal
05/28/2019
Procedures
DOS 1500-20
CCSW Pump Vault Penetration Surveillance Testing
DTP 70
Evaluation of CCSW Pump Vault Flooding Protection
Leakage Test
Work Orders
D3 18M TSTR CCSW Pump Vault Penetration Seal Testing
06/07/2019
Replace Seal in Penetration
5/21/2019
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
71111.11Q Corrective Action
Documents
247664
Condensate Min Flow FCV Will Not Open
05/09/2019
248231
CRD J-6 Double Notched
05/11/2019
248262
IRM 18 Spike Results in 1/2 Scram on Unit 2 During S/U
05/11/2019
248264
IRM 15 Downscale When Ranging 6 to 7
05/11/2019
248266
U2 CRD L-12 (42-47) Rod Drift, 902-5 A-3 Alarm
05/11/2019
248293
CRD HCU L-13 Movement from Position 04 to 08
05/11/2019
248358
High Vibes Cause U2 Turbine Trip
05/12/2019
248407
Unexpected U2 Hydrogen Seal Oil Emergency Pump
Auto-Start
05/13/2019
248666
2-5 A-3, Rod Drift from HCU F-2
05/13/2019
248927
U2 Rod Drift Alarm Actuated With no Drifting Control Rods
05/14/2019
250988
4.0 Critique - U2 Main Turbine Trip Due to High Vibrations
05/12/2019
Procedures
DGP 01-01
Unit Startup
196
DGP 02-01
Unit Shutdown
169
DOS 5600-11
Testing the Main Turbine Overspeed Trip System
Corrective Action
Documents
2508639
2-2099-969A, Unit 2 East LPCI/CS Corner Room 'A' Sump
Pump Discharge Check Valve, is Stuck in its Current
Position
06/01/2015
4049215
Unexpected Alarm for Unit 3 West LPCI/CS Sump Level Hi
09/05/2017
230383
2C RBFDS Check Valve Sticking Open
03/18/2019
243959
3B RBFDS Sump Pump Tripped on Thermal Overload
04/27/2019
251847
Unexpected Trip of MCC Breaker on 39-3 During Testing of
3A/3B RBFDS Hi Level Alarms and Pump Start Switches
05/26/2019
251920
Unit 3 East Reactor Building Floor Drain System Hi-Hi Level
Alarm Not Functioning
05/26/2019
261506
2A RBFDS Pump Motor Coupling Sheared
07/02/2019
261507
2C RBFDS Pump Degraded and Not Pumping Effectively
07/02/2019
261508
Suspected Leak Past 2D RBFDS Check Valve
07/02/2019
Miscellaneous
Maintenance Rule System Basis Document for
Miscellaneous Sumps and Drains
Procedures
Structures Monitoring
ER-DR-450-1001
Dresden Structures Monitoring Instructions
Corrective Action
237979
U3 DEHC
04/09/2019
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Documents
238358
Work Orders Needed for Unit 2 UCVF Jumper Configuration
04/11/2019
244414
Unexpected Alarm 903-4 C-22 Due to 3-2301-14 Opening
04/29/2019
244414
Unexpected Alarm 903-4 C-22 Due to 3-2301-14 Opening
04/29/2019
244503
3-3933-502 Packing Leak
04/29/2019
244988
Crew 6 Clock Reset
04/29/2019
245899
U3 Main Turb CV #4 LVDT Fault
05/03/2019
247719
D2F57: 2A FWP Min Flow Line Pipe Support 121 Degraded
05/09/2019
248786
D2F57 Startup Monitoring: Elevated Off Gas Flow
05/13/2019
249040
U2 Main Condenser Vacuum
05/14/2019
249543
Crack on 2A RFP Min Flow Line Seal Weld to Condenser
Wall
05/16/2019
249607
Entered DOA 0010-02
05/16/2019
249815
4.0 Critique on Helium Testing
05/17/2019
250565
Penetration MK 856 found above schf during DOS 1500-20
05/21/2019
Drawings
M-12
Diagram of Steam Piping, Sheet 2
ABT
M-14
Diagram of Reactor Feed Piping
MB
M-40
Diagram of Turbine Building Piping
ZK
Miscellaneous
74-1
Analysis of Effects of Piping Break Outside Containment,
Dresden Station Units 2 and 3, Special Report 37,
Revision 1, February 1975
December
1973
Procedures
DAN 902(3)-4 C-
Torus Narrow Range Wtr Lvl Hi
DAN 902(3)-7 B-
W Air Eject Suct Vlv Closed
DAP 07-44
Control of Temporary Openings in Secondary Containment
During Performance of Work Packages, Surveillances, or
Other Procedures
DGP 03-01
136
DOA 0010-02
Tornado Warning/Severe Winds,
DOA 3300-02
DOA 5650-02
Pressure Regulator Failure
DOP 5400-24
2B Steam Jet Air Ejector/Recombiner Combined Startup,
Operation and Shutdown
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Pre-Job Briefings
OP-AA-108-111-
1001
Severe Weather and Natural Disaster Guidelines
OP-DR-108-111-
1002
Main Condenser Air In-Leakage Troubleshooting
Work Orders
01592255
Replace HPCI Room Cooler Cooling Coil
04/29/2019
01841713
U3 DEHC S1 UCVF Card Replacement
04/10/2019
04921978
Install Temp Leak Repair on 2-3205-A-6"-F
05/16/2019
Corrective Action
Documents
4187100
Containment Spray Interlock Vulnerability
10/24/2018
29611
Indications found in Legacy 3A RBCCW HX Tube Sheet
03/14/2019
29613
Rejectable NDE Indications Identified on 3A RBCCW Welds
03/14/2019
29618
NDE Rejectable Indication Identified on New 3A RBCCW
03/14/2019
232113
PS 2-0263-52A Circuit 2 found OOT
03/22/2019
246780
Historical Operability Evaluation of PS 2-0263-52A
05/06/2019
252166
NRC ID: Pre-lube Oil Line Support Clamp Not Fully
Engaged
05/28/2019
255271
U1 DFP Capacity Test Unsatisfactory Results
06/07/2019
27307
Unit 3 EDG Lube Oil Gallery Site Glass is Empty
01/26/2008
Drawings
2E-2437, Sheets
and 2
Schematic Diagram LPCI/Containment Cooling System 1
AZ
LPCI Loop Select Logic
LPCI Loop Select Logic
Schematic Diagram LPCI/Containment Cooling System
Motor Operated Valves 2-1501-18A/18B/38A/38B
AG
M-23 sh 5
Diagram of Fire Protection Piping
U
Engineering
Changes
U1 DFP Operability per DFPS 4123-07
10/05/2017
NDE Reports19-037, 19-038,19-039
Operability
Evaluations08-001
Unit 3 EDG Pre-Lubrication System
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Procedures
DEOP 200-1
Primary Containment Control
DIS 1500-04
Containment Spray Interlock, Containment High Pressure
Switches Calibration
DIS 1500-29
Division I Low Pressure Coolant Injection/Containment
Spray, Torus Cooling, and 2/3 Core Coverage Logic System
Functional Test
Code Acceptance & Recording Criteria for Nondestructive
(NDE) Surface Examination
Work Orders
00023998
Perform Weld Repairs on Partition Plate
04/02/2001
00364132
RBCCW 'A' HX Cleaning and Inspection
2/09/2005
00894244
RBCCW 'A' HX Cleaning and Inspection
2/02/2008
01506091
RBCCW 'A' HX Clean, Insp, Eddy Current Test 33-1/3
percent
01/09/2017
04866870-01
Quarterly Technical Specification Reactor Low Pressure
(350 PSIG) ECCS Permissive Calibration
03/22/2019
22057
Upgrade to 3A RBCCW HX Partition Plate
03/15/2019
Corrective Action
Documents
4106195
Plunger Nut Missing on Removed Check Valve
2/20/2018
4157872
U3 Diesel Generator Cylinder #10 Temp Reading High
07/23/2018
238755
Incorrect Stuffing Box for 3A Service Water Pump
04/11/2019
239228
A Chip Approx.125 Inches x.125 Inches Along the Seal
Face
04/13/2019
242034
TI 3-6641-500 Showing Signs of Degradation
04/22/2019
242485
Discharge Hose off of Turbo Pump Piping Offset
04/22/2019
242736
Minor Air Leak on Unit 3 EDG Starting Air Filter B
04/23/2019
242841
U3 EDG Lube Oil Check Valve Sticking
04/23/2019
246339
2-2001-5 Dual Indication While Opening
05/04/2019
247652
U2 SRM 23 Will Not Insert
05/09/2019
248278
APRM 6 High and Downscale
05/11/2019
257607
U2 HPCI AOV 2-2301-29 Fails to Open
06/18/2019
Engineering
Changes
2555
Install 3A Service Water Pump Open Line Shaft Design with
Greene Tweed AR-HT Bearings - 3-3901-A
000
23191
Foreign Material Evaluation: U3 Emergency Diesel
Generator (EDG) 3-6699-114 Check Valve/Lost Disc
2/21/2018
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Retaining Nut
Operability
Evaluations08-001
IR 727307, EC 369166
Procedures
Rigging Evaluation Form
DIS 0700-05
APRM Setdown Calibration
DIS 0700-06
Average Power Range Monitor (APRM) Flow Biased
SCRAM, Rod Block, and Downscale Calibrations
DIS 0700-09
Preventive Maintenance and Calibration of RBM, LPRM,
DMP 3900-02
Service Water Pump (With Lube Water Strainers) Removal
and Installation
DMP 3900-06
Upgraded Service Water Pump (With Process Lubed
Bearings) Removal and Installation
DOS 0700-01
SRM Functional Test
DOS 0700-03
SRM Detector Position Rod Block Functional Test
DOS 0700-12
Determining Source Range Monitor Signal to Noise (S/N)
Ratio and Minimum SRM Count Rate
DOS 2300-01
High Pressure Coolant Injection Valve Operability and
Timing
DOS 6600-01
Diesel Generator Surveillance Tests
2
Lost Parts Evaluations
Conduct of Troubleshooting
Rigging and Lifting Program
Work Orders
271972
D3 10Y Com Service Water PP 3A Overhaul (3-3901A)
08/09/2017
01401688-20
Replace SRM Drive Motor
05/12/2019
04790382
U3 EDG Lube Oil Lower Sightgass Empty
04/23/2019
04790382
PMT U3 EDG Oil Check Valve Repairs
04/24/2019
04895330
HPCI Motor Operated Valve Operability
05/06/2019
04918104
2-2001-5 Dual Indication While Opening
05/07/2019
20619
APRM 6 High and Downscale
05/11/2019
Corrective Action
Documents
247644
U2 Control Rod L-6 Indicating Orange '00'
05/09/2019
247711
05/09/2019
247719
D2F57: 2A FWP Min Flow Line Pipe Support 121 Degraded
05/09/2019
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
247728
D2F57: FW Insulation Pulled Away From Wall
05/09/2019
247761
D2F57: Very Small U2 EHC Leak Found
05/09/2019
247762
IRM 16 Mode Switch 125 Position Not Working
05/09/2019
247795
U2 Turbine Bearing #3 Metal Temperature Failed Downscale 05/09/2019
247854
Received Unplanned 'B' RPS 1/2 SCRAM
05/09/2019
247868
IRM 15 Spike Results in 1/2 SCRAM on Unit 2
05/09/2019
247869
IRM 16 Drawer Internal Sig Generator Position 40 Output
Low
05/09/2019
247907
IRM 14 Inoperable Due to Inability to Perform Channel
Check
05/10/2019
247927
U2 CRD G-12 Difficult to Unlatch
05/10/2019
247931
RPIS Problem U2 R-6 (No Zero in One's Column)
05/10/2019
247936
RPIS Problem U2 C-8 (No One in Ten's Column)
05/10/2019
248196
U2 CRD J-5 Difficult to Unlatch
05/11/2019
248208
DOS 0300-08 Not Completed
05/11/2019
248361
U2 Turbine Bearing Lift Pump #1 Discharge Isolation Vlv
Leak
05/12/2019
248666
2-5 A-3, Rod Drift From HCU F-2
05/13/2019
248989
Unacceptable Post Maintenance Vibration Levels
05/14/2019
249019
CRD F-2 Fast Insert Speed During PMT
05/14/2019
249097
U2 Turbine Oil Temp Controller Not Controlling at Setpoint
05/15/2019
249775
Nights OCC: 4.0 Critique of D2F57
05/17/2019
249851
EMD: 4.0 Critique of D2F47
05/17/2019
249898
Engineering 4.0 Critique D2F57
05/17/2019
249902
RP 4.0 Critique
05/17/2019
249923
Engineering Star-Up Monitoring 4.0 Critique
05/17/2019
249924
Days OCC: 4.0 Critique D2F57
05/17/2019
250069
Fatigue Assessment Performed
05/18/2019
Procedures
DAN 902(3)-5 A-
Rod Drift
DGP 01-S1
Start-Up Checklist
101
DGP 01-S5
Mode 3 to Mode 2 Restart Checklist
DOA 0300-05
Inoperable or Failed Control Rod Drives
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
DOA 0300-12
Mispositioned Control Rod,
DOP 0202-04
Reactor Recirculation System Shutdown
DOS 1600-10
Drywell Closeout Inspection Plan
Unit Restart Review
Shutdown Safety Management Program
Work Orders
01693647-01
Unit 2 Turbine Front Standard Mechanical
Inspect/Maintenance
05/12/2019
Corrective Action
Documents
259261
FLEX Diesel Flood Pump 'A' Unavailable
06/25/2019
259730
Low Coolant on FLEX Barge Diesel Flood Pump 'B'
06/26/2019
Procedures
DIS 1500-32
Division I & II Low Pressure Coolant Injection ECCS LOOP
Selection Circuitry Logic System Functional Test
DOS 1100-04
Standby Liquid Control System Quarterly/Comprehensive
Pump Test for The Inservice Testing (IST) System
DOS 7000-03
Local Leak Rate Testing of Primary Containment Airlock
DTP 47
Leak Rate Testing Program
FSG-60
FLEX Flood Pump Deployment and Operation
Work Orders
01580095-22
Perform Final As Left LLRT Personnel Air Lock
05/14/2019
04570953-01
Unit 2 Technical Specification Division 1 & 2 LPCI ECCS
04/17/2019
4882157
Annual FLEX Barge Pump/Motor 'A' Operation Test
06/25/2019
4882158
Annual FLEX Barge Pump/Motor 'B' Operations Test
06/26/2019
Procedures
Radiological Emergency Plan Annex for Dresden Station
Emergency Classification and Protective Action
Recommendations
Personnel Protective Actions
Notifications
EP-AA-114-F-02
BWR Release in Progress Determination Guidance
A
Calibration
Records
Calibration
Number:
0011072436
Certificate of Calibration Eberline RO-20AA; Serial Number,
292
05/01/2018
Certificate
Number:
0011074275
Certificate of Calibration Frisker Ludlum Model 3; Serial
Number, 298171
01/05/2018
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Work Order:
01968474 01
D3 24M/RFL TS COM Drywell Hi Rad Monitor Functional Cal 08/28/2018
Corrective Action
Documents
226328
ARM 22 Repeated Down-Scale Alarms
03/05/2019
236816
ARM Box Calibrator Source Certificates Not Found on
04/05/2019
248415
Accuscan II (WBC) Out of Service
05/13/2019
Miscellaneous
1; Out of Tolerance Report; MGP AMP-100;
Instrument ID, 0020787
01/25/2019
Procedures
Calibration Verification of Whole Body Counting Systems
Using Apex In-Vivo
Calibration of Shepherd Box Irradiators
Operation and Calibration of IPM Whole Body Frisking
Monitor
Operation and Calibration of PCM-2 Whole Body Frisking
Monitor
Operation and Calibration of the PM-12 Gamma Portal
Monitor
Operation and Calibration of The Canberra ARGOS-5
Personal Contamination Monitor
Calibration, Source Check, Operation and Set-Up of The
Eberline Beta Air Monitor, Model AMS-4
Self-Assessments AR 04201673
SA (RP): Instrumentation (NRC IP 71124.05)
01/04/2019
Miscellaneous
CY-DR-170-301
Offsite Dose Calculation Manual Dresden 1, 2, 3
G-20170801-586-
C
Gas Permit Post-Release Data
09/12/2017
G-20170801-587-
C
Gas Permit Post-Release Data
09/12/2017
L-20170801-221-
C
Liquid Permit Post-Release Data
09/12/2017
LS-AA-2150-
Monthly Data Elements for RETS/ODCM Radiological
Effluent Occurrences
10/01/2018 -
03/31/2019
SVPLTR: #18-
20
Corrected Dresden Nuclear Power Station 2017 Radioactive
Effluent Release Report
06/26/2018
SVPLTR: #19-
Dresden Nuclear Power Station 2018 Radioactive Effluent
04/15/2019
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
20
Release Report
Procedures
CY-DR-170-213
Dresden Potentially Contaminated System Controls Program
CY-DR-170-215
Unit 2/3 Main Chimney Sampling
CY-DR-170-220
Reactor Building Vent
CY-DR-170-400
Tritium Remediation at 2/3 CSTS
Self-Assessments 4099712
Radioactive Gaseous & Liquid Effluent Treatment IP 71124.06
2/20/2019
Work Orders
04618727-01
EWP IM 2/3 Quarterly Chimney SPING Functional Test
07/20/2017
04669719-01
EWP IM D2/3 Quarterly Reactor Building Functional Test
10/25/2017
04676705-01
Perform Appendix I Calculation
09/11/2017
Corrective Action
Documents
AR 040009983
Untimely Evaluation of Potential Abnormal Release From
OGFB
05/12/2017
REMP Program - Degradation of Air Sampling Stations
10/18/2017
Low Level Nickel 63 Nuclide Detected in GW at MW-DN-
119I
01/08/2018
IR Initiated for REMP Sampling Issues
2/27/2019
Miscellaneous
Dresden Nuclear Power Station 2017 Annual Radiological
Environmental Operating Report
05/10/2018
Monthly Report on the Meteorological Monitoring Program at
the Dresden Nuclear Generating Station
2/2018
Monthly Report on the Meteorological Monitoring Program at
the Dresden Nuclear Generating Station
11/2018
Procedures
EIML-SPM-1
Sampling Procedures Manual Environmental Incorporated
Midwest Laboratory
Radiological Groundwater Protection Program
Radiological Groundwater Protection Program
Implementation
EN-DR-408-4160
Dresden RGPP Reference Material
Underground (Buried) Piping and Raw Water Integrity
Management Programs Guide
71151
Corrective Action
Documents
204527
Change Needed for EDG SSPI Hours for October and
November 2018
2/19/2018
Engineering
Evaluations
DR-MSPI-01
Dresden MSPI Basis Document
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Miscellaneous
Unit 2 and Unit 3 MSPI Validation Packages for High
Pressure Injection Systems
04/01/2018-
03/31/2019
Unit 2 and Unit 3 MSPI Validation Packages for Emergency
AC Power Systems
04/01/2018-
03/31/2019
Monthly Elements for NRC Occupational Exposure Control
Effectiveness
05/01/2018 -
05/01/2019
Procedures
Monthly Data Elements for RETS/ODCM Radiological
Effluent Occurrences
Corrective Action
Documents
4110251
Half SCRAM Due to RPS Contactor Failure
03/01/2018
4114024
DOA 0500-02 Entry for Unit 3 Channel 'B' RPS Half SCRAM
03/12/2018
209752
FIN Crew Clock Reset
01/09/2019
218143
Work Not Completed Due to Risk Intervention
2/07/2019
219113
IMD Human Performance Trend
2/11/2019
219125
Decline in Human Performance NCAP CAPE
03/22/2019
24931
Improper Maintenance on Oil Pump
2/27/2019
230493
Pack Revision Incomplete for Scheduled Work
03/18/2019
243105
Engineering Critique of Instrument Air Dryer Replacement
04/08/2019
244894
U3 EDG LCO Fragnet Critique
04/30/2019
247317
Trend IR: Control Valve LVDT Cable Performance
05/08/2019
249933
Trend IR: Adverse Trend in Equipment Performance Since
D3R25
05/17/2019
250801
Half SCRAM Due to RPS 'B' Contactor Failure
05/21/2019
251371
Trend IR: Operations HURBs Completed between
December 2018 and May 2019
05/23/2019
253250
Trend IR: Crew Clock Resets in Last 30 Days
05/31/2019
256344
Operations Crew 6 Clock Reset
06/06/2019
257253
4.0 Critique for Unit 3 ECCS Surveillances
06/16/2019
258384
Crew 1 Clock Reset
06/17/2019
258569
Trend IR: Declining Trend in Procedure Use and Adherence
06/21/2019
Drawings
Schematic Diagram Reactor Protection System Channel 'B'
SCRAM and Auxiliary Trip Relays
AK
Procedures
DAN 902(3)-5 D-
Channel B Reactor SCRAM
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
DOA 0500-02
Partial Half or Full SCRAM Actuation
Work Orders
1434796
Troubleshooting for IR 4250801 (Unit 3 Half SCRAM)
05/22/2019
23862
Monitor Voltage on Unit 2 and Unit 3 RPS Logic Strings
05/22/2019
Corrective Action
Documents
23885
Secondary Containment dP Transient
2/09/2016
215383
North RB DP Local Indication On 613' Not Accurate
01/30/2019
249997
4.0 Critique 5.9.19 Turbine Trip and SCRAM
05/10/2019
Procedures
Post Transient or SCRAM Walkdown
DAN 902(3)-7 B-7 Turb Shaft BRG Oil PP Disch Press Lo
DAN 923-5 C-1
Rx Bldg DP LO
DGP 02-03
Reactor Scram
114
DOA 0600-01
Transient Level Control
DOA 5600-01
DOA 5700-01
Loss of Heating Boilers
DOA 6000-01
Main Generator Trip
Post Transient Review - BWR (For IR 4247636)
13