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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEARML20198Q4391997-11-0303 November 1997 LER 97-S001-00:on 971003,vital Area Barrier Gratings in Main Steam Valve Bldg Floor Not Secured.Caused by Inadequate Verification/Validation Process for Ensuring Vital Area Boundary Integrity.Security Instructions Will Be Revised ML20217F2321997-09-29029 September 1997 LER 970934-01:on 970918,RHR Pump Suction Relief Valve Setpoint Not IAW TS Was Determined.Caused by Insufficient Configuration Control.Declared B Train RHR Valve Inoperable, Recalibrated to Correct Setpoint & Declared Operable 05000336/LER-1997-003, Corrected Page One to LER 97-003-01:on 961216,discovered Discrepancy in Plant Procedure Utilized to Perform Periodic Insp of Fire Protection Sys Smoke Detectors.Caused by Failure to Properly Incorporate Ts.Ts Partially Revised1997-04-15015 April 1997 Corrected Page One to LER 97-003-01:on 961216,discovered Discrepancy in Plant Procedure Utilized to Perform Periodic Insp of Fire Protection Sys Smoke Detectors.Caused by Failure to Properly Incorporate Ts.Ts Partially Revised 05000336/LER-1993-0191993-09-10010 September 1993 LER 93-019-00:on 930812,reactor Trip Occurred Due to Low SG Level.Conducted Shift Briefing of Event to Operating Shift While Assuming Watch.Briefing Included Listed Requirements for Subsequent Specific start-up.W/930910 Ltr 05000423/LER-1993-0121993-09-0303 September 1993 LER 93-012-00:on 930805,piece of Plywood Discovered in Train a of Sws.Caused by Inadequate Work Control During 1991 Outage to Repair Sws.Plywood Removed & Increased Attention Being Paid to Matl Exclusion in Critical sys.W/930903 Ltr 05000336/LER-1993-0181993-09-0303 September 1993 LER 93-018-00:on 930805,letdown Manual Isolation Valve 2-CH-442 Developed Leak Which Exceeded TS Limits.Root Cause Has Not Been Determined.Valve Replaced & All Code Required Post Intallation Tests Successfully completed.W/930903 Ltr 05000336/LER-1993-0081993-09-0202 September 1993 LER 93-008-01:on 930505,declared Charging Pumps Inoperable Due to Low Control Power Voltage.Established Administrative Controls & Installed Interposing Relay within C Charging Pump Control circuit.W/930902 Ltr 05000423/LER-1993-0041993-08-31031 August 1993 LER 93-004-01:on 930331,RT Occurred Due to electro-hydraulic Control Power Supply Failure.Replaced Faulty Power Supply. W/930831 Ltr 05000423/LER-1993-0111993-08-30030 August 1993 LER 93-011-00:on 930731,MSSV Lift Setpoint Drift Occurred Due to Unknown Cause.Reduced Setpoint for Power Range Neutron Flux High Trip to 10%.W/930830 Ltr 05000336/LER-1993-0161993-08-27027 August 1993 LER 93-016-00:on 930729,reportability Determination Made Re Analysis for Boron Dilution Event.Caused by Inadequate Review of Results of Boron Dilution in Relation to Plant Operating Conditions.Boron Results revised.W/930827 Ltr 05000336/LER-1993-0141993-08-13013 August 1993 LER 93-014-00:on 930714,discovered Surveillances Procedures Had Not Been Performed within Specified Time Intervals Due to Insufficent Planning.Missed Surveillances Immediately performed.W/930813 Ltr 05000423/LER-1990-0261990-07-25025 July 1990 LER 90-026-00:on 900625,Train B Containment Hydrogen Monitor Failed Calibr Surveillance.Caused by Inadequate Engineering Interface Between Facilities Design Organization.Caution Tags Placed on Main Control Board indicators.W/900725 Ltr 05000423/LER-1990-0251990-07-20020 July 1990 LER 90-025-00:on 900616,hourly Vice Fire Watch Maintained During Condition That Required Continuous Fire Watch Be Established.Caused by Personnel Error.Continuous Fire Watch Established & Personnel Involved counseled.W/900720 Ltr 05000336/LER-1990-0101990-07-20020 July 1990 LER 90-010-00:on 900621,door Identified in Configuration Not Consistent W/Bechtel Design Drawings During High Energy Line Review.Caused by Lack of Knowledge of Requirements.Double Door reinforced.W/900720 Ltr 05000423/LER-1990-0241990-07-20020 July 1990 LER 90-024-00:on 900620,control Bldg Isolations Occurred Due to Radiation Monitor Detector Degradation.Other Equipment Not Affected.Degradation Caused Radiation Levels to Exceed High Alarm Setpoint.Detector replaced.W/900720 Ltr 05000336/LER-1990-0081990-07-18018 July 1990 LER 90-008-00:on 900620,determined That Grab Sample of Unit Stack Gas Not Taken.Caused by Lack of Communication Between Personnel.Grab Sample Obtained & analyzed.W/900718 Ltr 05000336/LER-1987-0091990-07-18018 July 1990 LER 87-009-02:on 870902,unit Experienced Automatic Reactor Trip Due to Low Steam Generator Level.Caused by Valve Stem Slightly Loose from Valve Plug.Damaged Stem/Plug Assembly replaced.W/900718 Ltr 05000423/LER-1990-0211990-07-16016 July 1990 LER 90-021-00:on 900607,integrated Leak Rate Test Supply & Exhaust Valve 3HVU*V5 Discovered Unlocked & Opened.Caused by Failure to Use Applicable Procedure for Nonroutine Evolution.Valve Closed & locked.W/900716 Ltr 05000336/LER-1990-0091990-07-16016 July 1990 LER 90-009-00:on 900617,inadvertent Partial Actuation of Train B of Enclosure Bldg Filtration Sys Occurred.Root Cause Not Determined.No Corrective Actions Recommended Until Further Testing & Troubleshooting performed.W/900716 Ltr 05000423/LER-1990-0221990-07-16016 July 1990 LER 90-022-00:on 900618,discovered That Hourly Fire Watch Patrol Had Not Been Established in Battery 4 Inverter Room. Caused by Procedural Deficiency.Hourly Fire Watch Established.Procedures revised.W/900716 Ltr 05000423/LER-1990-0191990-07-0303 July 1990 LER 90-019-00:on 900606,automatic Reactor Trip from Negative Flux Rate Signal Occurred Due to Dropped Control Rod.Caused by Broken Connection in Stationary Coil Power Cable for Rod. Special EOP Performed & Connector replaced.W/900703 Ltr 05000000/LER-1986-022, Partially Deleted LER 86-022-02:on 861018,potential Undetected Access Into Vital Area Discovered.Caused by Use of Incorrect Procedure.Card Reader Replaced & Tested to Ensure Proper Operation1987-02-20020 February 1987 Partially Deleted LER 86-022-02:on 861018,potential Undetected Access Into Vital Area Discovered.Caused by Use of Incorrect Procedure.Card Reader Replaced & Tested to Ensure Proper Operation 05000000/LER-1986-030, Partially Deleted LER 86-030-00:on 861211,unauthorized Opening Into Protected Area Discovered.Caused by Area Not Properly Identified as Area for Security Concern.Signs Posted1986-12-16016 December 1986 Partially Deleted LER 86-030-00:on 861211,unauthorized Opening Into Protected Area Discovered.Caused by Area Not Properly Identified as Area for Security Concern.Signs Posted 05000000/LER-1986-026, Partially Deleted LER 86-026-00:on 861124,vital Area Door Discovered W/O Alarm Capability.Caused by Personnel Error. Secutiry Officer in Question Terminated & Function of Administrative Sergeant Reviewed1986-12-0101 December 1986 Partially Deleted LER 86-026-00:on 861124,vital Area Door Discovered W/O Alarm Capability.Caused by Personnel Error. Secutiry Officer in Question Terminated & Function of Administrative Sergeant Reviewed 05000000/LER-1986-023, Partially Deleted LER 86-023-01:on 861023,unauthorized Access Into Vital Area Door Discovered.Caused by Card Reader Malfunction.Malfunctioning Card Reader Replaced.Cause Still Under Investigation1986-11-21021 November 1986 Partially Deleted LER 86-023-01:on 861023,unauthorized Access Into Vital Area Door Discovered.Caused by Card Reader Malfunction.Malfunctioning Card Reader Replaced.Cause Still Under Investigation 05000000/LER-1986-024, Partially Deleted LER 86-024-00:on 861113,attempted Introduction of Unauthorized Weapon Into Protected Area Discovered.Caused by Personnel Attempt to Enter Plant W/ Concealed Gun.Personnel Denied Facility Access1986-11-18018 November 1986 Partially Deleted LER 86-024-00:on 861113,attempted Introduction of Unauthorized Weapon Into Protected Area Discovered.Caused by Personnel Attempt to Enter Plant W/ Concealed Gun.Personnel Denied Facility Access 05000000/LER-1986-007, Partially Deleted LER 86-007-01:on 860218,loss of Alarm Surveillance Occurred.Caused by Water Leaking Into Cable Due to Heavy Rain.Cable Dried,Leak Repaired & Design Corrected1986-10-0606 October 1986 Partially Deleted LER 86-007-01:on 860218,loss of Alarm Surveillance Occurred.Caused by Water Leaking Into Cable Due to Heavy Rain.Cable Dried,Leak Repaired & Design Corrected 05000000/LER-1986-021, Partially Deleted LER 86-021-00:on 860911,vital Area Doors Failed to Alarm When Tested During Surveillance.Caused by Failure to Report Door Transactions to Host Computer.Central Procesing Unit Board Replaced1986-09-15015 September 1986 Partially Deleted LER 86-021-00:on 860911,vital Area Doors Failed to Alarm When Tested During Surveillance.Caused by Failure to Report Door Transactions to Host Computer.Central Procesing Unit Board Replaced 05000000/LER-1986-020, Partially Deleted LER 86-020-00:on 860812,security Sys Experienced Loss of Power.Caused Withheld.Numerous Failures Experienced Until Machine a Designated as Prime.Procedures to Reboot Computers Revised1986-08-15015 August 1986 Partially Deleted LER 86-020-00:on 860812,security Sys Experienced Loss of Power.Caused Withheld.Numerous Failures Experienced Until Machine a Designated as Prime.Procedures to Reboot Computers Revised 05000000/LER-1986-004, Partially Deleted LER 86-004-01:on 860204,loss of Dynamic Reporting of Alarm Surveillance Occurred.Cause Withheld. Computer Svcs Personnel Will Continue to Monitor Sys for Indicators of Cause1986-06-11011 June 1986 Partially Deleted LER 86-004-01:on 860204,loss of Dynamic Reporting of Alarm Surveillance Occurred.Cause Withheld. Computer Svcs Personnel Will Continue to Monitor Sys for Indicators of Cause 05000000/LER-1986-016, Partially Deleted LER 86-016-00:on 860501,vital Area Door Discovered W/O Alarm Capabilities.Caused by Access Control Security Officer Asleep at Post.Determination to Suspend or Discontinue Employment Being Made1986-05-0606 May 1986 Partially Deleted LER 86-016-00:on 860501,vital Area Door Discovered W/O Alarm Capabilities.Caused by Access Control Security Officer Asleep at Post.Determination to Suspend or Discontinue Employment Being Made 05000000/LER-1986-015, Partially Deleted LER 86-015-00:on 860428,stationary Side of Door Failed to Alarm When Tested.Cause Withheld.Alarm Repaired1986-05-0202 May 1986 Partially Deleted LER 86-015-00:on 860428,stationary Side of Door Failed to Alarm When Tested.Cause Withheld.Alarm Repaired 05000000/LER-1986-014, Partially Deleted LER 86-014-00:on 860421,bomb Threat Received by Security Officer in Security Assembly Room. Cause Not Applicable.Actions Taken to Minimize Station Threat & Investigation Underway1986-04-25025 April 1986 Partially Deleted LER 86-014-00:on 860421,bomb Threat Received by Security Officer in Security Assembly Room. Cause Not Applicable.Actions Taken to Minimize Station Threat & Investigation Underway 05000000/LER-1986-013, Partially Deleted LER 86-013-00:on 860414,vital Area Door W/O Alarm Capability Discovered.Caused by Personnel Error. Personnel Removed from Shift & Vital Area Checked for Unauthorized Personnel W/None Being Found1986-04-18018 April 1986 Partially Deleted LER 86-013-00:on 860414,vital Area Door W/O Alarm Capability Discovered.Caused by Personnel Error. Personnel Removed from Shift & Vital Area Checked for Unauthorized Personnel W/None Being Found 05000000/LER-1986-012, Partially Deleted LER 86-012-00:on 860412,breach Discovered in Protected Area Barrier.Caused by Personnel Error. Personnel Counseled1986-04-17017 April 1986 Partially Deleted LER 86-012-00:on 860412,breach Discovered in Protected Area Barrier.Caused by Personnel Error. Personnel Counseled 05000000/LER-1986-011, Partially Deleted LER 86-011-00:on 860410,vital Area Intrusion Alarm Failure Occurred.Cause of Event Deleted. Alarm & Door Tested Satisfactorily1986-04-15015 April 1986 Partially Deleted LER 86-011-00:on 860410,vital Area Intrusion Alarm Failure Occurred.Cause of Event Deleted. Alarm & Door Tested Satisfactorily 05000000/LER-1986-003, Partially Deleted LER 86-003-00:on 860125,loss of Dynamic Reporting of Vital Area Door Activity Occurred.Caused by Equipment Malfunction.Corrective Action Withheld1986-01-29029 January 1986 Partially Deleted LER 86-003-00:on 860125,loss of Dynamic Reporting of Vital Area Door Activity Occurred.Caused by Equipment Malfunction.Corrective Action Withheld 05000000/LER-1986-002, Partially Deleted LER 86-002-00:on 860117,loss of Alarm Surveillance on Doors Occurred.Caused by Erroneously Listing Officer as Being Posted on Door 398.Processing of Rev to Physical Security Plan Initiated1986-01-23023 January 1986 Partially Deleted LER 86-002-00:on 860117,loss of Alarm Surveillance on Doors Occurred.Caused by Erroneously Listing Officer as Being Posted on Door 398.Processing of Rev to Physical Security Plan Initiated 05000000/LER-1986-001, Partially Deleted LER 86-001-00:on 860105,loss of Dynamic Reporting of Vital Door Activity Occurred.Cause & Corrective Action Completely Deleted1986-01-10010 January 1986 Partially Deleted LER 86-001-00:on 860105,loss of Dynamic Reporting of Vital Door Activity Occurred.Cause & Corrective Action Completely Deleted 05000336/LER-1983-012, Updated LER 83-012/03X-1:on 830322 & 26,charging Pump C Shut Down Due to Lost Oil Pressure.Caused by Failed Integral Oil Pump Drive Coupling.Coupling Repaired1984-03-12012 March 1984 Updated LER 83-012/03X-1:on 830322 & 26,charging Pump C Shut Down Due to Lost Oil Pressure.Caused by Failed Integral Oil Pump Drive Coupling.Coupling Repaired 05000336/LER-1983-020, Updated LER 83-020/01X-1:on 830613,2,557 Degraded Tubes Discovered on Steam Generator Tubing.Cause Undetermined. Tubes W/Flaws Less than + or - 40% Through Wall or Eddy Current Probe Restrications repaired.W/840213 Ltr1984-02-13013 February 1984 Updated LER 83-020/01X-1:on 830613,2,557 Degraded Tubes Discovered on Steam Generator Tubing.Cause Undetermined. Tubes W/Flaws Less than + or - 40% Through Wall or Eddy Current Probe Restrications repaired.W/840213 Ltr 05000336/LER-1983-007, Updated LER 83-007/01T-1:on 830318,nonconservative Safety Analysis Assumption Discovered in Steam Generator Tube Rupture Analysis.Radiological Consequences of Reanalysis Being Analyzed1983-12-0909 December 1983 Updated LER 83-007/01T-1:on 830318,nonconservative Safety Analysis Assumption Discovered in Steam Generator Tube Rupture Analysis.Radiological Consequences of Reanalysis Being Analyzed ML20064F8591978-11-28028 November 1978 /03L-0 on 781115:spent Fuel Pool(Sfp)Ventilation Particulate & Gaseous Setpoints Exceeded Tech Specs Setpoints of Table 3.3-6,items 2.c & 2.d.Caused by Monitor Recalibr W/O Taking Into Account Tech Spec Limit ML20064F1651978-11-21021 November 1978 /03L-0 on 781025:during Oper,Surveillance Test on Channel a Reactor Protec Sys Core Protec Calculator Reveated Sys Ground Traced to Signal for Pressurizer Pressure W/In Containment Boundary.Source Not Known at This Time ML20064E6611978-11-16016 November 1978 /03L-0 on 781024:plant Computer Malfunction Caused CEA Pulse Counting Position to Be in Oper.Cause of Computer Failure Could Not Be Traced ML20064E1501978-11-0606 November 1978 /03L-0 on 781007:daily Tech Spec 4.3.1.1.1.,Table 4.3-1,items 2.a & 2.b,Nuc Pwr Surveillance & Delta-T Pwr Channel Calibr Not Performed Due to Personnel Error. Supervisors Told to Perform Req Surveillance ML20064D6131978-11-0303 November 1978 /03L-0 on 781025:Analysis of Instru Installations Revealed That Two Transmitters Assoc W/Channel a Steam Generator Low Water Lever Were non-seismically Mounted. Channel a SG Was Bypassed.Seismic Brackets Will Be Used ML20064D6011978-11-0101 November 1978 /03L-0 on 781004:during Surveillance Testing, Setpoint for Reactor Protec Sys Reactor Coolant Low Flow Trip on Channel B Was Out of Spec.Setpoint Was Readjusted. Rev Will Req Low Flow Trip Unit Setpoint Be Reset ML20064B8171978-10-0202 October 1978 /03L-0 on 780906:Loss of Methyl Iodide Removal Efficiency for a Ebfs Train. Cause Unknown 1997-09-29
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217P5391999-10-25025 October 1999 Rev 0,Change 1 to Millstone Unit 1 Northeast Utils QA Program ML20217C8721999-10-0606 October 1999 Rev 21,change 3 to MP-02-OST-BAP01, Nuqap Topical Rept, App F & G Only B17896, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With B17894, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With B17898, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216J4341999-09-24024 September 1999 Mnps Unit 3 ISI Summary Rept,Cycle 6 ML20211N8401999-09-0202 September 1999 Rev 21,change 1 to Northeast Utils QA TR, Including Changes Incorporated Into Rev 20,changes 9 & 10 B17878, Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With B17874, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 B17879, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With ML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20211A6561999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2 B17858, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With B17856, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With ML20210J0311999-07-21021 July 1999 Rev 20,Change 10 to QAP 1.0, Organization ML20210E5931999-07-19019 July 1999 Revised Page 16 of 21,to App F of Northeast Util QA Program Plan ML20210C5911999-07-15015 July 1999 Revised Rev 20,change 10 to Northeast Util QA Program TR, Replacing Summary of Changes ML20210A0411999-07-15015 July 1999 Rev 20,change 10 to Northeast Util QA Program Tr B17814, Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start1999-07-12012 July 1999 Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start ML20209D1881999-07-0101 July 1999 Rev 20,change 9 to Northeast Util QA Program Tr ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20211A6751999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level & Operating Data Rept ML20196A8451999-06-30030 June 1999 Post Shutdown Decommissioning Activities Rept ML20209J0541999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Unit 2 B17830, Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With ML20196K1791999-06-30030 June 1999 Addendum 6 to Millstone Unit 2 Annual Rept, ML20196J1821999-06-30030 June 1999 Rev 21,Change 0 to Northeast Utilities QAP (Nuqap) Tr B17833, Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With ML20195H1011999-06-11011 June 1999 Rev 20,change 8 to Northeast Utilities QAP (Nuqap) TR ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20211A6631999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level,Operating Data Rept & Unit Shutdowns & Power Reductions B17808, Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With ML20211B7351999-05-31031 May 1999 Cycle 7 Colr B17804, Monthly Operating Rept for May 1999 for Mnps,Unit 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 2.With B17807, Monthly Operating Rept for May 1999 for Mnps,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 1.With ML20209J0661999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Unit 2 ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206J8351999-05-0707 May 1999 Rev 20,Change 7 to QAP-1.0, Northeast Utls QA Program (Nuqap) Tr ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 B17782, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With ML20205R3531999-04-30030 April 1999 Addendum 4 to Annual Rept, B17775, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With ML20205K6141999-04-30030 April 1999 Non-proprietary Version of Rev 2 to Holtec Rept HI-971843, Licensing Rept for Reclassification of Discharge in Millstone Unit 3 Spent Fuel Pool ML20206E2971999-04-30030 April 1999 Rev 1 to Millstone Nuclear Power Station,Unit 2 COLR - Cycle 13 B17777, Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with ML20205Q5891999-04-0909 April 1999 Rev 20,change 6 to QAP-1.0,Northeast Utils QA Program TR ML20205R8751999-04-0909 April 1999 Provides Commission with Staff Assessment of Issues Related to Restart of Millstone Unit 2 & Staff Recommendations Re Restart Authorization for Millstone Unit 2 ML20206T3991999-03-31031 March 1999 First Quarter 1999 Performance Rept, Dtd May 1999 B17747, Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With 1999-09-30
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- EN'a:NIn[ed IEc'Eany _ HAR1 FORD. CONNECTICUT 06414-0270 t*vineast Nue=ar Erwegy company (203)665-6000 W[ .
July 3. 1990 MP-90-653 i
, - Re:' 10CFR50.73(a)(2)(iv) .
' U.S. Nuclear Regulato'ry Commission Document Control Desk -
Washington, D.C. 20555
Reference:
Facility Operating License No. NPF-49
- Docket No. 50-423 .
Licensee Event Report 90-019-00
- Gentlemen: 1
- This letter forwards Licensee' Event Report 90-019-00 required to be submitted n'ithinL 3~
. thirty _(30) days pursuant to 10CFR50.73(a)(2)(iv), any event or condition that resulted .
in automatic actuation of the Reactor Protection System (RPS). .
Very truly yours, NORTHEAST NUCLEAR ENERGY COMPANY h
Stephen . Scace cale. -
Director, Millstone Station e
SES/KHJ:ljs .
Attachment:
LER 90-019-00 m ;
cc: T. T. Martin, Region 1 Administrator .
l' W. J. Raymond,- Senior Resident las 3ector, Millstone Unit-Nos.1, 2 and 3 '
D. H.:Jaffe, NRC Project Manager, vlillstone Unit No. 3
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f f-e NRC Form 366 U,$, NUCLEAR REGULATORY COMMISSION APPROVED OMb NO. 3160-0104
,t6-89) q;. : EXPtRE S: 4/30/92 Estemsted buroen per rosconsi to comply with this 3
' information ooiection reauest 60.0 hrs.- Forwarc
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7'iear Regulatory Commission. Washington. Oc 20666. and te -
the Paperwork Reouction P o#ect (3160-0104). Office of Management anc Esuaget. Washington. DC 20503 F ACILITY NAME (1) DMl NWUEh (2) W --*
Millstone Nuclear Power Station Unit 3 ol 61 of 01014 l213 1lOFl0l3 T!TLE (4) .
Reactor Trip Due to Dropped Rod Due to Broken Cable to Stationary Gripper EVENT DATE (51 L E A NUMBF A e64 AFPOAT DATF f 71 OTHER F AClllTIES INVOLVED fbi MONTF DAY YEAR YEAR > MONT H DAY YEAR F ACILITY NAMES 0lslololol l l
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0 6 0l6 9 0 9 l0 0l1l9 0l 0 0l 7 0l3 9l 0 ol sl ol ol ol l l ODERATING THIS REPORT IS BEING SUEtMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR i: (Check one or more of the followino)Dil MODI # 20 40210) 20.402(c) v 60.73 t a)(2 Hiv) 73 7t(b) po R 20 406f aH1)D) 60.36tcH1) -
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LICENSEE CONT ACT FOR THIS LE A (121 TELEPHONE NUMBER l NAME AREA CODt Keith Jensen, Engineer, Ext. 5496 2l0l3 4l4l7l-l1l7l9l1 COMPLETE ONE LINE FOR E ACH COMPONENT F AILURF DESCA6 BED IN THfS REPORT (13i .i 1
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SUPPLEMENTAL AEPORT EXPECTED (141 p MONTH DAY YEAf4 f SUB SiON YES (if yes. compiete EXPECTED SUBMISSION DATE) ] NO DA E 06) 1l2 2l8 9l0 ABSTRACT (Limit to 1400 spaces. i.e...approximately fifteen single-space typewntion 1:nes) 06)
On June 6,1990, at 0618 hours0.00715 days <br />0.172 hours <br />0.00102 weeks <br />2.35149e-4 months <br /> with the plant in Mode I at 100% power,587 degrees Fahrenheit and 2250 -l psia, an automatic reactor trip from a negative flux rate signal occurred due to a dropped control rod, l The cause of this event was a broken connection in the stationary pripper coil power cable for rod G13. This' o single dropped rod resulted in a negative flux rate signal on two Power Range Detectors, thereby resulting in a reactor trip signal. The root cause of the broken connection could not be immediately determined, independent evaluation by a material testing facility is in progress to ascertain the failure mechanism. When the .i root cause is positively determined, a supplemental report will be issued.
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- l. As immediate corrective action control room operators performed the actions required by the applicable .
j emergency operating procedure. The broken connector was replaced. A functional test was performed by fully }
l- withdrawing and then inserting the affected rod. Potential long term corrective actions will be evaluated when ;
the root cause analysis is complete.
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, FAcMTY NAME (1) DOCKET NUMBER (2). (Em NUMBFA #9 PAGEf31 YEAR W .
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- 1. Descrintion of Event On June 6,1990, at 0618 hours0.00715 days <br />0.172 hours <br />0.00102 weeks <br />2.35149e-4 months <br /> with .the plant in Mode 1 at 100re power, 587 degrees Fahrenheit and 2250 psia, an automatic reactor tnp from a negative flux rate signal occurred due to a dropped control rod.
At the time of the tnp, operators verified that the reactor trip and bypass breakers were open, that all control rods were fully inserted, and that neutron flux was decreasing. A Feedwater Isolation signal was :
received due to low Reactor Coolant System Average Temperature following the trip. An Auxihary Feedwater actuation. occurred as a result of a steam generator low-low level signal. These are normal- ,
9: plant responses following a trip from 1007c power. No additional engineered safety features were required or initiated. . There were no operational, maintenance, or construction activities in progress at - l the time which affected the event. Plant stabihty, based on Reactor Coolant System Average Temperature, was achieved at approximately 0638 hours0.00738 days <br />0.177 hours <br />0.00105 weeks <br />2.42759e-4 months <br /> on June 6,1990.
L II. Cnnse of Event ;
The cause of the dropped rod was a broken connection in the stationary gripper coil p9wer cable for rod {
G13 in Shutdown Bank B. The single dropped rod resulted in a negative flux rate signal on two out of q four Power Range Channels, thereby meeting the required logic for a reactor trip signal, j The root cause of the broken connection could not be positively determined. The cable and connector
, assembly were sent to an independent materials testing facility to ascertain the failure mechanism. When this information is available, and the root cause has been positively determined, a supplemental report j will be issued. I The connector cable failure affected the Rod Control System in the following manner. To hold a control rod in a given position, a holding current is applied to the stationary gripper coil. This coil is mounted outside the Control Rod Drive Mechanism (CRDM) pressure housing. The coil is magnetically coupled i to the stationary gripper arm assembhes, which are inside the CRDM pressure housing. The gripper arms 0 engage with circumferercial grooves on the drive rod assembly, which is in turn connected to the affected control rod. If power to the stationary pripper coil is lost, the magnetic flux holding the gripper arms'in .
place will be interrupted. The gripper arms will disengage from the drive rod, and the control rod will be j released. Thus, when the G13 stationary gripper coil connector broke, power to the coll'was lost, and !
the rod fell from its fully withdrawn position. I 1
Because rod G13 is located on the core periphery, excore Power Range Channels 42 and 44 detected the j rapid drop in nuclear power due to the falling rod. A reactor trip signal will be generated when two out i
l' of four Power Range channels generate a rate trip. As a result, a high negative flux rate trip signal was ;
generated on both of these channels. The setpoint for this signal is a change of less than or equal to SFc ,
rated thermal power with a time' constant of greater than or equal to 2 seconds. :I N 111, : Annivsis of Event
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] This event is being reported in accordance with 10CFR50.73(a)(2)(iv) as an event or condition that resulted in automatic actuation of any Engineered Safety Feature, including the Reactor Protection System. Immediate notifications were made in accordance with 10CFR50.72(b)(2)(ii).
There were no significant safety consequences due to this event. The intended design function of the negative rate trip is to mitigate the effects of a multiple rod drop event at high power. Multiple dropped rods, without a subsequent reactor trip, could cause local flux peaking. resulting in a localized, ,
non-conservative Departure from Nucleate Boiling Ratio (DNBR) values. By mitiating a reactor trip, and 4 thereby causing full insertion of all control rods, the negauve rate inp prevents these hmiting DNBR values from occurrir.g.
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Text o, mor in.c. is reaver.o. u.. aoii onei NRc Form assA si or) o Although this inp signal protecte against multiple dropped rods, discussions with the fuel vendor indicated that untier certain ecnditions, a single dropped rod could cause a reactor trip. Based on the reactivity worth of rod 013 and its geometrical relation to Power Range Channels 42 and 44, receipt of two negative rate signals upon the rod drop is a valid assumption. Further discussion.with the fuel vendor indicated that there have been several instances at similar plants where a single dropped rod caused a reactur trip. The response of the Reactor Protection System in generating a reactor trip signal due to rod 013 dropping is therefore conservative with respect to its design basis.
IV. Corrective Action in order to determine which control rods had dropped, a special procedure was performed in which each control rod was individually latched and withdrawn approximately 6 inches off the bottom.- Rod 013 in Shutdown Bank B was the only rod that would not move. Subsequent continuity checking from the Rod Control cabinets to the CRDM coil indicated an electrical fault in a section of cable inside Containment.
A Containment entry was made, and the faulted section was identified and removed. Bench testing and 1 inspection revealed that a stationary gripper coil power cable had broken in the connector. = The
- connector was replaced, the cable was continuity checked, and the cable =was then reinstalled. The entire power loop,"from the Rod Control Cabinets to the CRDM coil stack, was then continuity checked.
As a final functional test, rod 013 was latched and withdrawn to its fully withdrawn position and then reinserted. No problems with rod 013 were experienced. As an additional test, the continuity of all d.
other control rods, from the Rod Control cabinets to the CRDM coil stacks, was verified to be l satisfactory. Furthermore, potential long term corrective actions will be evaluated when the root cause aneysis is complete. A supplemental report will be submitted by December 28, 1990, detailing the results of the root cause analysis and any additional corrective action deemed necessary.
V, ' Additionni Information .
x There have been no similar events with the same root cause and sequence of events.
Ells Codes -
System j i Control' Rod Drive System - AA L Reactor Coolant System - AB- 1 Auxiliary Feedwater System -BA j Plant Protection System - JC 1 Excore . Monitoring System - IG j f
Comnonent l
.i Cable, Low Voltage - Power - CBL4 Coll - CL-Rod - ROD ~
. Detector - DET go,m 3 6 4
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05000336/LER-1990-008 | LER 90-008-00:on 900620,determined That Grab Sample of Unit Stack Gas Not Taken.Caused by Lack of Communication Between Personnel.Grab Sample Obtained & analyzed.W/900718 Ltr | | 05000336/LER-1990-009 | LER 90-009-00:on 900617,inadvertent Partial Actuation of Train B of Enclosure Bldg Filtration Sys Occurred.Root Cause Not Determined.No Corrective Actions Recommended Until Further Testing & Troubleshooting performed.W/900716 Ltr | | 05000336/LER-1990-010 | LER 90-010-00:on 900621,door Identified in Configuration Not Consistent W/Bechtel Design Drawings During High Energy Line Review.Caused by Lack of Knowledge of Requirements.Double Door reinforced.W/900720 Ltr | | 05000423/LER-1990-019 | LER 90-019-00:on 900606,automatic Reactor Trip from Negative Flux Rate Signal Occurred Due to Dropped Control Rod.Caused by Broken Connection in Stationary Coil Power Cable for Rod. Special EOP Performed & Connector replaced.W/900703 Ltr | | 05000423/LER-1990-021 | LER 90-021-00:on 900607,integrated Leak Rate Test Supply & Exhaust Valve 3HVU*V5 Discovered Unlocked & Opened.Caused by Failure to Use Applicable Procedure for Nonroutine Evolution.Valve Closed & locked.W/900716 Ltr | | 05000423/LER-1990-022 | LER 90-022-00:on 900618,discovered That Hourly Fire Watch Patrol Had Not Been Established in Battery 4 Inverter Room. Caused by Procedural Deficiency.Hourly Fire Watch Established.Procedures revised.W/900716 Ltr | | 05000423/LER-1990-024 | LER 90-024-00:on 900620,control Bldg Isolations Occurred Due to Radiation Monitor Detector Degradation.Other Equipment Not Affected.Degradation Caused Radiation Levels to Exceed High Alarm Setpoint.Detector replaced.W/900720 Ltr | | 05000423/LER-1990-025 | LER 90-025-00:on 900616,hourly Vice Fire Watch Maintained During Condition That Required Continuous Fire Watch Be Established.Caused by Personnel Error.Continuous Fire Watch Established & Personnel Involved counseled.W/900720 Ltr | | 05000423/LER-1990-026 | LER 90-026-00:on 900625,Train B Containment Hydrogen Monitor Failed Calibr Surveillance.Caused by Inadequate Engineering Interface Between Facilities Design Organization.Caution Tags Placed on Main Control Board indicators.W/900725 Ltr | |
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