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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEARML20198Q4391997-11-0303 November 1997 LER 97-S001-00:on 971003,vital Area Barrier Gratings in Main Steam Valve Bldg Floor Not Secured.Caused by Inadequate Verification/Validation Process for Ensuring Vital Area Boundary Integrity.Security Instructions Will Be Revised ML20217F2321997-09-29029 September 1997 LER 970934-01:on 970918,RHR Pump Suction Relief Valve Setpoint Not IAW TS Was Determined.Caused by Insufficient Configuration Control.Declared B Train RHR Valve Inoperable, Recalibrated to Correct Setpoint & Declared Operable 05000336/LER-1997-003, Corrected Page One to LER 97-003-01:on 961216,discovered Discrepancy in Plant Procedure Utilized to Perform Periodic Insp of Fire Protection Sys Smoke Detectors.Caused by Failure to Properly Incorporate Ts.Ts Partially Revised1997-04-15015 April 1997 Corrected Page One to LER 97-003-01:on 961216,discovered Discrepancy in Plant Procedure Utilized to Perform Periodic Insp of Fire Protection Sys Smoke Detectors.Caused by Failure to Properly Incorporate Ts.Ts Partially Revised 05000336/LER-1993-0191993-09-10010 September 1993 LER 93-019-00:on 930812,reactor Trip Occurred Due to Low SG Level.Conducted Shift Briefing of Event to Operating Shift While Assuming Watch.Briefing Included Listed Requirements for Subsequent Specific start-up.W/930910 Ltr 05000423/LER-1993-0121993-09-0303 September 1993 LER 93-012-00:on 930805,piece of Plywood Discovered in Train a of Sws.Caused by Inadequate Work Control During 1991 Outage to Repair Sws.Plywood Removed & Increased Attention Being Paid to Matl Exclusion in Critical sys.W/930903 Ltr 05000336/LER-1993-0181993-09-0303 September 1993 LER 93-018-00:on 930805,letdown Manual Isolation Valve 2-CH-442 Developed Leak Which Exceeded TS Limits.Root Cause Has Not Been Determined.Valve Replaced & All Code Required Post Intallation Tests Successfully completed.W/930903 Ltr 05000336/LER-1993-0081993-09-0202 September 1993 LER 93-008-01:on 930505,declared Charging Pumps Inoperable Due to Low Control Power Voltage.Established Administrative Controls & Installed Interposing Relay within C Charging Pump Control circuit.W/930902 Ltr 05000423/LER-1993-0041993-08-31031 August 1993 LER 93-004-01:on 930331,RT Occurred Due to electro-hydraulic Control Power Supply Failure.Replaced Faulty Power Supply. W/930831 Ltr 05000423/LER-1993-0111993-08-30030 August 1993 LER 93-011-00:on 930731,MSSV Lift Setpoint Drift Occurred Due to Unknown Cause.Reduced Setpoint for Power Range Neutron Flux High Trip to 10%.W/930830 Ltr 05000336/LER-1993-0161993-08-27027 August 1993 LER 93-016-00:on 930729,reportability Determination Made Re Analysis for Boron Dilution Event.Caused by Inadequate Review of Results of Boron Dilution in Relation to Plant Operating Conditions.Boron Results revised.W/930827 Ltr 05000336/LER-1993-0141993-08-13013 August 1993 LER 93-014-00:on 930714,discovered Surveillances Procedures Had Not Been Performed within Specified Time Intervals Due to Insufficent Planning.Missed Surveillances Immediately performed.W/930813 Ltr 05000423/LER-1990-0261990-07-25025 July 1990 LER 90-026-00:on 900625,Train B Containment Hydrogen Monitor Failed Calibr Surveillance.Caused by Inadequate Engineering Interface Between Facilities Design Organization.Caution Tags Placed on Main Control Board indicators.W/900725 Ltr 05000423/LER-1990-0251990-07-20020 July 1990 LER 90-025-00:on 900616,hourly Vice Fire Watch Maintained During Condition That Required Continuous Fire Watch Be Established.Caused by Personnel Error.Continuous Fire Watch Established & Personnel Involved counseled.W/900720 Ltr 05000336/LER-1990-0101990-07-20020 July 1990 LER 90-010-00:on 900621,door Identified in Configuration Not Consistent W/Bechtel Design Drawings During High Energy Line Review.Caused by Lack of Knowledge of Requirements.Double Door reinforced.W/900720 Ltr 05000423/LER-1990-0241990-07-20020 July 1990 LER 90-024-00:on 900620,control Bldg Isolations Occurred Due to Radiation Monitor Detector Degradation.Other Equipment Not Affected.Degradation Caused Radiation Levels to Exceed High Alarm Setpoint.Detector replaced.W/900720 Ltr 05000336/LER-1990-0081990-07-18018 July 1990 LER 90-008-00:on 900620,determined That Grab Sample of Unit Stack Gas Not Taken.Caused by Lack of Communication Between Personnel.Grab Sample Obtained & analyzed.W/900718 Ltr 05000336/LER-1987-0091990-07-18018 July 1990 LER 87-009-02:on 870902,unit Experienced Automatic Reactor Trip Due to Low Steam Generator Level.Caused by Valve Stem Slightly Loose from Valve Plug.Damaged Stem/Plug Assembly replaced.W/900718 Ltr 05000423/LER-1990-0211990-07-16016 July 1990 LER 90-021-00:on 900607,integrated Leak Rate Test Supply & Exhaust Valve 3HVU*V5 Discovered Unlocked & Opened.Caused by Failure to Use Applicable Procedure for Nonroutine Evolution.Valve Closed & locked.W/900716 Ltr 05000336/LER-1990-0091990-07-16016 July 1990 LER 90-009-00:on 900617,inadvertent Partial Actuation of Train B of Enclosure Bldg Filtration Sys Occurred.Root Cause Not Determined.No Corrective Actions Recommended Until Further Testing & Troubleshooting performed.W/900716 Ltr 05000423/LER-1990-0221990-07-16016 July 1990 LER 90-022-00:on 900618,discovered That Hourly Fire Watch Patrol Had Not Been Established in Battery 4 Inverter Room. Caused by Procedural Deficiency.Hourly Fire Watch Established.Procedures revised.W/900716 Ltr 05000423/LER-1990-0191990-07-0303 July 1990 LER 90-019-00:on 900606,automatic Reactor Trip from Negative Flux Rate Signal Occurred Due to Dropped Control Rod.Caused by Broken Connection in Stationary Coil Power Cable for Rod. Special EOP Performed & Connector replaced.W/900703 Ltr 05000000/LER-1986-022, Partially Deleted LER 86-022-02:on 861018,potential Undetected Access Into Vital Area Discovered.Caused by Use of Incorrect Procedure.Card Reader Replaced & Tested to Ensure Proper Operation1987-02-20020 February 1987 Partially Deleted LER 86-022-02:on 861018,potential Undetected Access Into Vital Area Discovered.Caused by Use of Incorrect Procedure.Card Reader Replaced & Tested to Ensure Proper Operation 05000000/LER-1986-030, Partially Deleted LER 86-030-00:on 861211,unauthorized Opening Into Protected Area Discovered.Caused by Area Not Properly Identified as Area for Security Concern.Signs Posted1986-12-16016 December 1986 Partially Deleted LER 86-030-00:on 861211,unauthorized Opening Into Protected Area Discovered.Caused by Area Not Properly Identified as Area for Security Concern.Signs Posted 05000000/LER-1986-026, Partially Deleted LER 86-026-00:on 861124,vital Area Door Discovered W/O Alarm Capability.Caused by Personnel Error. Secutiry Officer in Question Terminated & Function of Administrative Sergeant Reviewed1986-12-0101 December 1986 Partially Deleted LER 86-026-00:on 861124,vital Area Door Discovered W/O Alarm Capability.Caused by Personnel Error. Secutiry Officer in Question Terminated & Function of Administrative Sergeant Reviewed 05000000/LER-1986-023, Partially Deleted LER 86-023-01:on 861023,unauthorized Access Into Vital Area Door Discovered.Caused by Card Reader Malfunction.Malfunctioning Card Reader Replaced.Cause Still Under Investigation1986-11-21021 November 1986 Partially Deleted LER 86-023-01:on 861023,unauthorized Access Into Vital Area Door Discovered.Caused by Card Reader Malfunction.Malfunctioning Card Reader Replaced.Cause Still Under Investigation 05000000/LER-1986-024, Partially Deleted LER 86-024-00:on 861113,attempted Introduction of Unauthorized Weapon Into Protected Area Discovered.Caused by Personnel Attempt to Enter Plant W/ Concealed Gun.Personnel Denied Facility Access1986-11-18018 November 1986 Partially Deleted LER 86-024-00:on 861113,attempted Introduction of Unauthorized Weapon Into Protected Area Discovered.Caused by Personnel Attempt to Enter Plant W/ Concealed Gun.Personnel Denied Facility Access 05000000/LER-1986-007, Partially Deleted LER 86-007-01:on 860218,loss of Alarm Surveillance Occurred.Caused by Water Leaking Into Cable Due to Heavy Rain.Cable Dried,Leak Repaired & Design Corrected1986-10-0606 October 1986 Partially Deleted LER 86-007-01:on 860218,loss of Alarm Surveillance Occurred.Caused by Water Leaking Into Cable Due to Heavy Rain.Cable Dried,Leak Repaired & Design Corrected 05000000/LER-1986-021, Partially Deleted LER 86-021-00:on 860911,vital Area Doors Failed to Alarm When Tested During Surveillance.Caused by Failure to Report Door Transactions to Host Computer.Central Procesing Unit Board Replaced1986-09-15015 September 1986 Partially Deleted LER 86-021-00:on 860911,vital Area Doors Failed to Alarm When Tested During Surveillance.Caused by Failure to Report Door Transactions to Host Computer.Central Procesing Unit Board Replaced 05000000/LER-1986-020, Partially Deleted LER 86-020-00:on 860812,security Sys Experienced Loss of Power.Caused Withheld.Numerous Failures Experienced Until Machine a Designated as Prime.Procedures to Reboot Computers Revised1986-08-15015 August 1986 Partially Deleted LER 86-020-00:on 860812,security Sys Experienced Loss of Power.Caused Withheld.Numerous Failures Experienced Until Machine a Designated as Prime.Procedures to Reboot Computers Revised 05000000/LER-1986-004, Partially Deleted LER 86-004-01:on 860204,loss of Dynamic Reporting of Alarm Surveillance Occurred.Cause Withheld. Computer Svcs Personnel Will Continue to Monitor Sys for Indicators of Cause1986-06-11011 June 1986 Partially Deleted LER 86-004-01:on 860204,loss of Dynamic Reporting of Alarm Surveillance Occurred.Cause Withheld. Computer Svcs Personnel Will Continue to Monitor Sys for Indicators of Cause 05000000/LER-1986-016, Partially Deleted LER 86-016-00:on 860501,vital Area Door Discovered W/O Alarm Capabilities.Caused by Access Control Security Officer Asleep at Post.Determination to Suspend or Discontinue Employment Being Made1986-05-0606 May 1986 Partially Deleted LER 86-016-00:on 860501,vital Area Door Discovered W/O Alarm Capabilities.Caused by Access Control Security Officer Asleep at Post.Determination to Suspend or Discontinue Employment Being Made 05000000/LER-1986-015, Partially Deleted LER 86-015-00:on 860428,stationary Side of Door Failed to Alarm When Tested.Cause Withheld.Alarm Repaired1986-05-0202 May 1986 Partially Deleted LER 86-015-00:on 860428,stationary Side of Door Failed to Alarm When Tested.Cause Withheld.Alarm Repaired 05000000/LER-1986-014, Partially Deleted LER 86-014-00:on 860421,bomb Threat Received by Security Officer in Security Assembly Room. Cause Not Applicable.Actions Taken to Minimize Station Threat & Investigation Underway1986-04-25025 April 1986 Partially Deleted LER 86-014-00:on 860421,bomb Threat Received by Security Officer in Security Assembly Room. Cause Not Applicable.Actions Taken to Minimize Station Threat & Investigation Underway 05000000/LER-1986-013, Partially Deleted LER 86-013-00:on 860414,vital Area Door W/O Alarm Capability Discovered.Caused by Personnel Error. Personnel Removed from Shift & Vital Area Checked for Unauthorized Personnel W/None Being Found1986-04-18018 April 1986 Partially Deleted LER 86-013-00:on 860414,vital Area Door W/O Alarm Capability Discovered.Caused by Personnel Error. Personnel Removed from Shift & Vital Area Checked for Unauthorized Personnel W/None Being Found 05000000/LER-1986-012, Partially Deleted LER 86-012-00:on 860412,breach Discovered in Protected Area Barrier.Caused by Personnel Error. Personnel Counseled1986-04-17017 April 1986 Partially Deleted LER 86-012-00:on 860412,breach Discovered in Protected Area Barrier.Caused by Personnel Error. Personnel Counseled 05000000/LER-1986-011, Partially Deleted LER 86-011-00:on 860410,vital Area Intrusion Alarm Failure Occurred.Cause of Event Deleted. Alarm & Door Tested Satisfactorily1986-04-15015 April 1986 Partially Deleted LER 86-011-00:on 860410,vital Area Intrusion Alarm Failure Occurred.Cause of Event Deleted. Alarm & Door Tested Satisfactorily 05000000/LER-1986-003, Partially Deleted LER 86-003-00:on 860125,loss of Dynamic Reporting of Vital Area Door Activity Occurred.Caused by Equipment Malfunction.Corrective Action Withheld1986-01-29029 January 1986 Partially Deleted LER 86-003-00:on 860125,loss of Dynamic Reporting of Vital Area Door Activity Occurred.Caused by Equipment Malfunction.Corrective Action Withheld 05000000/LER-1986-002, Partially Deleted LER 86-002-00:on 860117,loss of Alarm Surveillance on Doors Occurred.Caused by Erroneously Listing Officer as Being Posted on Door 398.Processing of Rev to Physical Security Plan Initiated1986-01-23023 January 1986 Partially Deleted LER 86-002-00:on 860117,loss of Alarm Surveillance on Doors Occurred.Caused by Erroneously Listing Officer as Being Posted on Door 398.Processing of Rev to Physical Security Plan Initiated 05000000/LER-1986-001, Partially Deleted LER 86-001-00:on 860105,loss of Dynamic Reporting of Vital Door Activity Occurred.Cause & Corrective Action Completely Deleted1986-01-10010 January 1986 Partially Deleted LER 86-001-00:on 860105,loss of Dynamic Reporting of Vital Door Activity Occurred.Cause & Corrective Action Completely Deleted 05000336/LER-1983-012, Updated LER 83-012/03X-1:on 830322 & 26,charging Pump C Shut Down Due to Lost Oil Pressure.Caused by Failed Integral Oil Pump Drive Coupling.Coupling Repaired1984-03-12012 March 1984 Updated LER 83-012/03X-1:on 830322 & 26,charging Pump C Shut Down Due to Lost Oil Pressure.Caused by Failed Integral Oil Pump Drive Coupling.Coupling Repaired 05000336/LER-1983-020, Updated LER 83-020/01X-1:on 830613,2,557 Degraded Tubes Discovered on Steam Generator Tubing.Cause Undetermined. Tubes W/Flaws Less than + or - 40% Through Wall or Eddy Current Probe Restrications repaired.W/840213 Ltr1984-02-13013 February 1984 Updated LER 83-020/01X-1:on 830613,2,557 Degraded Tubes Discovered on Steam Generator Tubing.Cause Undetermined. Tubes W/Flaws Less than + or - 40% Through Wall or Eddy Current Probe Restrications repaired.W/840213 Ltr 05000336/LER-1983-007, Updated LER 83-007/01T-1:on 830318,nonconservative Safety Analysis Assumption Discovered in Steam Generator Tube Rupture Analysis.Radiological Consequences of Reanalysis Being Analyzed1983-12-0909 December 1983 Updated LER 83-007/01T-1:on 830318,nonconservative Safety Analysis Assumption Discovered in Steam Generator Tube Rupture Analysis.Radiological Consequences of Reanalysis Being Analyzed ML20064F8591978-11-28028 November 1978 /03L-0 on 781115:spent Fuel Pool(Sfp)Ventilation Particulate & Gaseous Setpoints Exceeded Tech Specs Setpoints of Table 3.3-6,items 2.c & 2.d.Caused by Monitor Recalibr W/O Taking Into Account Tech Spec Limit ML20064F1651978-11-21021 November 1978 /03L-0 on 781025:during Oper,Surveillance Test on Channel a Reactor Protec Sys Core Protec Calculator Reveated Sys Ground Traced to Signal for Pressurizer Pressure W/In Containment Boundary.Source Not Known at This Time ML20064E6611978-11-16016 November 1978 /03L-0 on 781024:plant Computer Malfunction Caused CEA Pulse Counting Position to Be in Oper.Cause of Computer Failure Could Not Be Traced ML20064E1501978-11-0606 November 1978 /03L-0 on 781007:daily Tech Spec 4.3.1.1.1.,Table 4.3-1,items 2.a & 2.b,Nuc Pwr Surveillance & Delta-T Pwr Channel Calibr Not Performed Due to Personnel Error. Supervisors Told to Perform Req Surveillance ML20064D6131978-11-0303 November 1978 /03L-0 on 781025:Analysis of Instru Installations Revealed That Two Transmitters Assoc W/Channel a Steam Generator Low Water Lever Were non-seismically Mounted. Channel a SG Was Bypassed.Seismic Brackets Will Be Used ML20064D6011978-11-0101 November 1978 /03L-0 on 781004:during Surveillance Testing, Setpoint for Reactor Protec Sys Reactor Coolant Low Flow Trip on Channel B Was Out of Spec.Setpoint Was Readjusted. Rev Will Req Low Flow Trip Unit Setpoint Be Reset ML20064B8171978-10-0202 October 1978 /03L-0 on 780906:Loss of Methyl Iodide Removal Efficiency for a Ebfs Train. Cause Unknown 1997-09-29
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217P5391999-10-25025 October 1999 Rev 0,Change 1 to Millstone Unit 1 Northeast Utils QA Program ML20217C8721999-10-0606 October 1999 Rev 21,change 3 to MP-02-OST-BAP01, Nuqap Topical Rept, App F & G Only B17896, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With B17894, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With B17898, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216J4341999-09-24024 September 1999 Mnps Unit 3 ISI Summary Rept,Cycle 6 ML20211N8401999-09-0202 September 1999 Rev 21,change 1 to Northeast Utils QA TR, Including Changes Incorporated Into Rev 20,changes 9 & 10 B17878, Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With B17874, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 B17879, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With ML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20211A6561999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2 B17858, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With B17856, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With ML20210J0311999-07-21021 July 1999 Rev 20,Change 10 to QAP 1.0, Organization ML20210E5931999-07-19019 July 1999 Revised Page 16 of 21,to App F of Northeast Util QA Program Plan ML20210C5911999-07-15015 July 1999 Revised Rev 20,change 10 to Northeast Util QA Program TR, Replacing Summary of Changes ML20210A0411999-07-15015 July 1999 Rev 20,change 10 to Northeast Util QA Program Tr B17814, Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start1999-07-12012 July 1999 Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start ML20209D1881999-07-0101 July 1999 Rev 20,change 9 to Northeast Util QA Program Tr ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20211A6751999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level & Operating Data Rept ML20196A8451999-06-30030 June 1999 Post Shutdown Decommissioning Activities Rept ML20209J0541999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Unit 2 B17830, Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With ML20196K1791999-06-30030 June 1999 Addendum 6 to Millstone Unit 2 Annual Rept, ML20196J1821999-06-30030 June 1999 Rev 21,Change 0 to Northeast Utilities QAP (Nuqap) Tr B17833, Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With ML20195H1011999-06-11011 June 1999 Rev 20,change 8 to Northeast Utilities QAP (Nuqap) TR ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20211A6631999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level,Operating Data Rept & Unit Shutdowns & Power Reductions B17808, Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With ML20211B7351999-05-31031 May 1999 Cycle 7 Colr B17804, Monthly Operating Rept for May 1999 for Mnps,Unit 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 2.With B17807, Monthly Operating Rept for May 1999 for Mnps,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 1.With ML20209J0661999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Unit 2 ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206J8351999-05-0707 May 1999 Rev 20,Change 7 to QAP-1.0, Northeast Utls QA Program (Nuqap) Tr ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 B17782, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With ML20205R3531999-04-30030 April 1999 Addendum 4 to Annual Rept, B17775, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With ML20205K6141999-04-30030 April 1999 Non-proprietary Version of Rev 2 to Holtec Rept HI-971843, Licensing Rept for Reclassification of Discharge in Millstone Unit 3 Spent Fuel Pool ML20206E2971999-04-30030 April 1999 Rev 1 to Millstone Nuclear Power Station,Unit 2 COLR - Cycle 13 B17777, Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with ML20205Q5891999-04-0909 April 1999 Rev 20,change 6 to QAP-1.0,Northeast Utils QA Program TR ML20205R8751999-04-0909 April 1999 Provides Commission with Staff Assessment of Issues Related to Restart of Millstone Unit 2 & Staff Recommendations Re Restart Authorization for Millstone Unit 2 ML20206T3991999-03-31031 March 1999 First Quarter 1999 Performance Rept, Dtd May 1999 B17747, Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With 1999-09-30
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text
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g General Offices'Selden Street.' Berhn Connecticut .- !
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wYsfe"rnYa's*sIeNttNac CMny P.O. BOX 270 f g '
, Ene*a:YEt enc'Eany - HARTFORD. CoNNECTioVT 06414 4 270 ' I Nortnoast Nuclear Energy Company r,
.(203)665-5000 J
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< July'18,.1990 MP-90-717.
Re: 10CFR50.73(a)(2)(iv) ,
1 l
U.S. Nuclear Regulatory Commission Document Control Desk o Washington, 'D.C; '20555 P-
Reference:
Facility Operating License No' DPR-65 Docket No. 50-336 Licensee Event Report 87-009-02 ;
i Gent l emen:
l1This11etter- forwards Licensee Event Report 87-009-02 required' to be submitted pursuant to paragraph 50.73(a)(2)(iv). l 4
Very truly yours, 1
NORTHEAST NUCLEAR ENERGY COMPANY l
FOR: Stephen E. Scace j Director, Millstone Station l ]
L !
L -BY:
k n P. Stetz Millstone Unit 1 Director SES/JMB:mo l
L
Attachment:
LER 87-009-02 1,
L cc: T. T. Martin, Recion 1 Administrator l: W. -J. Raymond,' Senior Resident inspector, Millstone Unit Nos.1, 2 and 3 G. S. Vissing, NRC Project Mar.ager, Millstone Unit No. 2 L
0[71+50Bllf 90d7$5 $49 900718 PDR S
ADOCK 05000336 PDC
[M MM
/[/
.NRC Form 366 U.S. NUCLE AR REGULATORY COMMISSION APPROVED OMB NO. 3160-0104 (6-89)* EXPERE S: 4/30/02
'a Estimated buroen per respons2 to comply witn this Information cohection teovest: 50.0 hrs Forward LICENSEE EVENT REPORT (LER) ' Me"cUtEflNeNint B .NE*2 ')"*uIS 30 Uu'cioar Regulatory Commission, Washington. DC 20555. and to f the Paperwork Reduction Protect (3150-0104). Office of Management and Buopet Washington. DC 20503.
FACILITY NAME (1) DOCF.E I NUMBEH (2) 8%M Millstone Nuclear Power Station Unit 2 ol sl ol ol ol3 l3 ls i lod 0l3 TITLE (4)
Reactor Trip on Low #1 Steam Generator Level EVENT DATE (51 LFA NUMPF A #61 AFPORT D ATE t71 OTHFA F ACrtl TIFS INVOLVED (Si MONTF- DAY YEAR YEAR MONTH DAY YEAR FAOldTY NAMES olslofofof I I 0 9 0l2 8 7 8 l7 0l0l9 0l 2 0l7j1l8 9l0 01610l o1 ol l l OPERATINo THIS REPORT IS BEINo SUBMITTED PURSUANT TO THE AEOtrREMENTS OF 10 CFR $ ICneck one or more of the followingH11) 20 402(b) _
20 402(cl J 50.73(a)(2)(ev) _
73.7 t (b) i po a 20.405(a)(1)(0 50.36(C)(1) 50.73(a)(2)(v) 73.71(c)
(10s l9l} 20.405(a)(1)(iu 50.36(c)(2) 50 73.ta)(2Hviu _ {THER (goecit 20 405(a)D)(ii0 50.73(a)(2)(0 50.73(a)(2)(vi 0 ( A) Text. NRC Form 366A) 20 405(aH1)(w) 50.73(aH2)(10 50 73(a)(2)(viiO(B) 20 405 tan tifw) 50.73f a)(2Hil0 50 73 tail 2)fx) j LICENSEE CONTACT FOR THS LEA (121 NAME TELEDHONE NUMBER ARcA CQDi Joseph M. Bergin. Engineer, Ext. 5352 2l0j3 4]4l7]-l1l7l9]1 COMPLETE ONE LINE FOR E ACH COMPONENT F AILURE DESCA! BED IN THS REPORT (131 CAUSE SYSTEU COMPONEMr hhhh' 7d CAUSE SYSTEM COMPONENT hhE ~
X SlJ LlClVl Cl6l3l5 -
l l l l l l l I II I I I I I II I I I I SUDPLEMENTAL AEPOAT EXPECTED (14r MONTH DAY YEAR SUBVIS$10N
] YES fit yes. comp <ete EXPECTED SUBMLSSION DATE) A US)
NO l l l AssTRACT (Limit to 1400 spaces. e e . amoroximateiy titteen singie-space typewntion nresi (i6; While operating at 91re power on September 2,1987 at 2015 the unit experienced an automatic reactor trip due to low steam generator level in the #1 steam generator. The operation's staff was performing a routine reduction in power level from 100re to 90Fe. Dunng this evolution the secondary plant operator observed the feed flow to the #1 steam generator less than the steam flow. The operator took manual control of the feedwater regulating valve, 2-FW-51 A, and the feedwater regulating bypass valve, 2-FW-41 A, in an attempt to l restore level in the #1 steam generator. Level continued to decrease in the #1 steam generator and the unit tnpped. Operations responded to the trip by performing EOP 2525, " Standard Post Trip Actions" and EOP i 2526 " Reactor Trip Recovery" No other systems were affected and the unit was placed in a stable condition.
The #1 feedwater regulating valve, 2-FW-51 A, was disassembled and repaired. Dunng the disassembly it was l discovered that the stem had separated from the plug. This event is being reported pursuant to the requirements of paragraph 5L.73(a)(2)(iv) due to the automatic reactor trip on low steam generator level.
Similar LER's: None.
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k e NRc form 3660 ' U.S MJCLEAR REGULATORY COMMISSION APPROVED OMB No 3150-0104 (6-60) EXPIRE 6: G30/02 Estimateo t>uroen per response to comply witn inis '
LICENSEE EVENT REPORT (LER) 'ajgga gg',gg5h,5,0f,,"'4,,F
, g rwa nc s TEXT CONTINUATION ano neoorts uanagemeni eranen ip-Sao). u o Nucies, F Regulatory Commission. Wasnington DC 20565. and to the Paperwork Recuction Project (31s0-0104). ofisce of Management and Buocet. Wasnington. Do 20503-FActuTY NAME (t) DOCKET NUMBER (2) un NipBEn m PAGE f3:
YEAR N Millstone Nuclear Power Station Unit 2 OF 0l 5l ol ol 0l3 l's l 6 8l7 0l 0l 9 0l2 0) 0l3 TEXT pf more space is requeroc. use moditional NRc Form 366A s) (17)
- 1. Descrintion of Event While operating at 91rc power on September 2,1987 at 2015 the unit experienced an automatic reactor trip due to low steam generator level in the #1 steam generator. The operation's staff was performing a-routine reduction in power level from 100rc to 90re. The power reduction was in response to fouling of-the B condenser waterbox, requiring it's removal from service. During this evolution the secondary plant operator observed the feedflow to the #1 steam generator to be less than the steam flow. The operator took manual control of the feedwater regulating valve, 2-FW-5' A and the feedwater regulating bypass valve, 2-FW-41 A, in an attempt to restore level in the #1 s'erm generator, i.evel continued to decrease '
in the #1 steam generator. Plant Equipment Cperators were dispatched to the feedwater regulating valve, ,
2-FW-51 A, to take local manual control. The Unit tripped prior to the Plant Equipment Operators i arriving at the valves. The licensed operators responded to the trip by performing EOP 2525, " Standard 5 Post Trip Actions" and EOP 2526, " Reactor Trip Recovery" No other systems were affected and the unit was placed in a stable condition.
- 11. Cante of Event Investigation of this event included the disassembly of the #1 feedwater regulating valve, 2-FW-51A, to l determine the cause of the lack of. response to automatic or manual level control signals. During the disassembly the valves bonnet stem and p!ug were removed from the valve body. Further investigation revealed that the valve stem was slightly loose from the valve's plug. The stem was then torqued in an -
attempt to tighten the stem to the plug. The stem then became loose enough to remove the stem from the plug by pulling it out of the plug by hand. The threads on the stem were rolled over and were not applying the required connection between the plug and the stem. The threads on the plug are also in a
- similar condition. Proper connection between the stem and the plug for this valve requires the stem to be threaded into the plug so that a tapered portion of the stem makes contact with a tapered fit on the plug. Rotation of the stem with respect to plug is resisted by the friction forces in the threads and a roll pin which is installed through the stem and plug assembly. Examination of the valve body and the stem / plug assembly did not reveal the existence of the roll pin. The Unit staff has concluded that the root cause of the transient was the loss or the lack of this roll pin in the stem plug assembly initiated the degradation of the stem / plug assembly which eventually resulted m the loss of feed water flow control and steam generator level.
l 111. Analysis of Event l This event is being reported pursuant to the requirements of paragraph 50.73(a)(2)(iv) due to the I automatic reactor trip on low steam generator level.
There were no safety consequences resulting from this reactor trip since all safety systems functioned to restore the Unit to a stable condition. Aher the reactor trip the damaged valve received a signal to close I with the feedwater regulating bypass valve receiving a signal to open. The bypass valve supplied enough
- flow to recover level in the al steam generator. The introduction of the rolled pin into the steam generator has been reviewed to evaluate its affect on the integrity of the steam generator tubing. This l condition has been found acceptable due to the slignt mass of the pin involved. Since it cannot be i determined if the rolled pin was installed by the valve's manufacturer a shght potential may exist that this same condition may occur in the #2 steam generator feed water regulating valve. This condition has been determined to be acceptable based on the low probabihties of occurrence and the ability to provide an adequate heat sink to the affected steam generator via the feedwater regulating bypass valve for removal of decay heat. The Unit was shutdown for 21 hours2.430556e-4 days <br />0.00583 hours <br />3.472222e-5 weeks <br />7.9905e-6 months <br /> 20 minutes.
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' Estimated buroen per response to comply witn this 4~ **
LICENSEE EVENT REPORT (LER) ,";o"",',,",glgg,%q'g,6g,"',*g ,,',n*,8,'d,,,
o TEXT CONTINUATION ano n.corts Managem.. Brenen ip-sso). u.s Nuclear Regulatory Commission Washington. DC 20655- and to tne PSDerWork Reduction Proiect (31604104L Office of Management and Bucost. Washin0 ton DC 20603-
, F ACILITY NAME (1) DOCKET NUMBER (2)- t FR NUMPF A (Fi PAGE(31 YEAR @ N Millstone Nuclear Power Station '
UDil 2 0l 5l 0l 0l 0l3 l3 l6 8l7 0l0l9 0l2 0l 3 OF 0[3 TEXT (it more space is reawrec, use edditional NRC Form 366A's) (17)
-IV. Corrective Action The damaged stem / plug assembly was replaced, the valve was assembled and tested. The Unit was then returned to service. This valve and the #2 feedwater regulating valve have been inspected during the End of Cycle 09 refuel outage, no problems of a similar nature were found in these valves. The appropriate valve preventative maintenance procedure has been revised to inspect for the proper installation of this roll pin.
.V. Additional Information
. The Main Feedwater Regulating valve, 2-FW-51 A, is a Copes - Vulcan 12" 900# angle style valve ~ l assembly with a P-200-12 operator. '
Similar LERs: None l-l l
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05000336/LER-1987-009 | LER 87-009-02:on 870902,unit Experienced Automatic Reactor Trip Due to Low Steam Generator Level.Caused by Valve Stem Slightly Loose from Valve Plug.Damaged Stem/Plug Assembly replaced.W/900718 Ltr | |
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