|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEARML20198Q4391997-11-0303 November 1997 LER 97-S001-00:on 971003,vital Area Barrier Gratings in Main Steam Valve Bldg Floor Not Secured.Caused by Inadequate Verification/Validation Process for Ensuring Vital Area Boundary Integrity.Security Instructions Will Be Revised ML20217F2321997-09-29029 September 1997 LER 970934-01:on 970918,RHR Pump Suction Relief Valve Setpoint Not IAW TS Was Determined.Caused by Insufficient Configuration Control.Declared B Train RHR Valve Inoperable, Recalibrated to Correct Setpoint & Declared Operable 05000336/LER-1997-003, Corrected Page One to LER 97-003-01:on 961216,discovered Discrepancy in Plant Procedure Utilized to Perform Periodic Insp of Fire Protection Sys Smoke Detectors.Caused by Failure to Properly Incorporate Ts.Ts Partially Revised1997-04-15015 April 1997 Corrected Page One to LER 97-003-01:on 961216,discovered Discrepancy in Plant Procedure Utilized to Perform Periodic Insp of Fire Protection Sys Smoke Detectors.Caused by Failure to Properly Incorporate Ts.Ts Partially Revised 05000336/LER-1993-0191993-09-10010 September 1993 LER 93-019-00:on 930812,reactor Trip Occurred Due to Low SG Level.Conducted Shift Briefing of Event to Operating Shift While Assuming Watch.Briefing Included Listed Requirements for Subsequent Specific start-up.W/930910 Ltr 05000423/LER-1993-0121993-09-0303 September 1993 LER 93-012-00:on 930805,piece of Plywood Discovered in Train a of Sws.Caused by Inadequate Work Control During 1991 Outage to Repair Sws.Plywood Removed & Increased Attention Being Paid to Matl Exclusion in Critical sys.W/930903 Ltr 05000336/LER-1993-0181993-09-0303 September 1993 LER 93-018-00:on 930805,letdown Manual Isolation Valve 2-CH-442 Developed Leak Which Exceeded TS Limits.Root Cause Has Not Been Determined.Valve Replaced & All Code Required Post Intallation Tests Successfully completed.W/930903 Ltr 05000336/LER-1993-0081993-09-0202 September 1993 LER 93-008-01:on 930505,declared Charging Pumps Inoperable Due to Low Control Power Voltage.Established Administrative Controls & Installed Interposing Relay within C Charging Pump Control circuit.W/930902 Ltr 05000423/LER-1993-0041993-08-31031 August 1993 LER 93-004-01:on 930331,RT Occurred Due to electro-hydraulic Control Power Supply Failure.Replaced Faulty Power Supply. W/930831 Ltr 05000423/LER-1993-0111993-08-30030 August 1993 LER 93-011-00:on 930731,MSSV Lift Setpoint Drift Occurred Due to Unknown Cause.Reduced Setpoint for Power Range Neutron Flux High Trip to 10%.W/930830 Ltr 05000336/LER-1993-0161993-08-27027 August 1993 LER 93-016-00:on 930729,reportability Determination Made Re Analysis for Boron Dilution Event.Caused by Inadequate Review of Results of Boron Dilution in Relation to Plant Operating Conditions.Boron Results revised.W/930827 Ltr 05000336/LER-1993-0141993-08-13013 August 1993 LER 93-014-00:on 930714,discovered Surveillances Procedures Had Not Been Performed within Specified Time Intervals Due to Insufficent Planning.Missed Surveillances Immediately performed.W/930813 Ltr 05000423/LER-1990-0261990-07-25025 July 1990 LER 90-026-00:on 900625,Train B Containment Hydrogen Monitor Failed Calibr Surveillance.Caused by Inadequate Engineering Interface Between Facilities Design Organization.Caution Tags Placed on Main Control Board indicators.W/900725 Ltr 05000423/LER-1990-0251990-07-20020 July 1990 LER 90-025-00:on 900616,hourly Vice Fire Watch Maintained During Condition That Required Continuous Fire Watch Be Established.Caused by Personnel Error.Continuous Fire Watch Established & Personnel Involved counseled.W/900720 Ltr 05000336/LER-1990-0101990-07-20020 July 1990 LER 90-010-00:on 900621,door Identified in Configuration Not Consistent W/Bechtel Design Drawings During High Energy Line Review.Caused by Lack of Knowledge of Requirements.Double Door reinforced.W/900720 Ltr 05000423/LER-1990-0241990-07-20020 July 1990 LER 90-024-00:on 900620,control Bldg Isolations Occurred Due to Radiation Monitor Detector Degradation.Other Equipment Not Affected.Degradation Caused Radiation Levels to Exceed High Alarm Setpoint.Detector replaced.W/900720 Ltr 05000336/LER-1990-0081990-07-18018 July 1990 LER 90-008-00:on 900620,determined That Grab Sample of Unit Stack Gas Not Taken.Caused by Lack of Communication Between Personnel.Grab Sample Obtained & analyzed.W/900718 Ltr 05000336/LER-1987-0091990-07-18018 July 1990 LER 87-009-02:on 870902,unit Experienced Automatic Reactor Trip Due to Low Steam Generator Level.Caused by Valve Stem Slightly Loose from Valve Plug.Damaged Stem/Plug Assembly replaced.W/900718 Ltr 05000423/LER-1990-0211990-07-16016 July 1990 LER 90-021-00:on 900607,integrated Leak Rate Test Supply & Exhaust Valve 3HVU*V5 Discovered Unlocked & Opened.Caused by Failure to Use Applicable Procedure for Nonroutine Evolution.Valve Closed & locked.W/900716 Ltr 05000336/LER-1990-0091990-07-16016 July 1990 LER 90-009-00:on 900617,inadvertent Partial Actuation of Train B of Enclosure Bldg Filtration Sys Occurred.Root Cause Not Determined.No Corrective Actions Recommended Until Further Testing & Troubleshooting performed.W/900716 Ltr 05000423/LER-1990-0221990-07-16016 July 1990 LER 90-022-00:on 900618,discovered That Hourly Fire Watch Patrol Had Not Been Established in Battery 4 Inverter Room. Caused by Procedural Deficiency.Hourly Fire Watch Established.Procedures revised.W/900716 Ltr 05000423/LER-1990-0191990-07-0303 July 1990 LER 90-019-00:on 900606,automatic Reactor Trip from Negative Flux Rate Signal Occurred Due to Dropped Control Rod.Caused by Broken Connection in Stationary Coil Power Cable for Rod. Special EOP Performed & Connector replaced.W/900703 Ltr 05000000/LER-1986-022, Partially Deleted LER 86-022-02:on 861018,potential Undetected Access Into Vital Area Discovered.Caused by Use of Incorrect Procedure.Card Reader Replaced & Tested to Ensure Proper Operation1987-02-20020 February 1987 Partially Deleted LER 86-022-02:on 861018,potential Undetected Access Into Vital Area Discovered.Caused by Use of Incorrect Procedure.Card Reader Replaced & Tested to Ensure Proper Operation 05000000/LER-1986-030, Partially Deleted LER 86-030-00:on 861211,unauthorized Opening Into Protected Area Discovered.Caused by Area Not Properly Identified as Area for Security Concern.Signs Posted1986-12-16016 December 1986 Partially Deleted LER 86-030-00:on 861211,unauthorized Opening Into Protected Area Discovered.Caused by Area Not Properly Identified as Area for Security Concern.Signs Posted 05000000/LER-1986-026, Partially Deleted LER 86-026-00:on 861124,vital Area Door Discovered W/O Alarm Capability.Caused by Personnel Error. Secutiry Officer in Question Terminated & Function of Administrative Sergeant Reviewed1986-12-0101 December 1986 Partially Deleted LER 86-026-00:on 861124,vital Area Door Discovered W/O Alarm Capability.Caused by Personnel Error. Secutiry Officer in Question Terminated & Function of Administrative Sergeant Reviewed 05000000/LER-1986-023, Partially Deleted LER 86-023-01:on 861023,unauthorized Access Into Vital Area Door Discovered.Caused by Card Reader Malfunction.Malfunctioning Card Reader Replaced.Cause Still Under Investigation1986-11-21021 November 1986 Partially Deleted LER 86-023-01:on 861023,unauthorized Access Into Vital Area Door Discovered.Caused by Card Reader Malfunction.Malfunctioning Card Reader Replaced.Cause Still Under Investigation 05000000/LER-1986-024, Partially Deleted LER 86-024-00:on 861113,attempted Introduction of Unauthorized Weapon Into Protected Area Discovered.Caused by Personnel Attempt to Enter Plant W/ Concealed Gun.Personnel Denied Facility Access1986-11-18018 November 1986 Partially Deleted LER 86-024-00:on 861113,attempted Introduction of Unauthorized Weapon Into Protected Area Discovered.Caused by Personnel Attempt to Enter Plant W/ Concealed Gun.Personnel Denied Facility Access 05000000/LER-1986-007, Partially Deleted LER 86-007-01:on 860218,loss of Alarm Surveillance Occurred.Caused by Water Leaking Into Cable Due to Heavy Rain.Cable Dried,Leak Repaired & Design Corrected1986-10-0606 October 1986 Partially Deleted LER 86-007-01:on 860218,loss of Alarm Surveillance Occurred.Caused by Water Leaking Into Cable Due to Heavy Rain.Cable Dried,Leak Repaired & Design Corrected 05000000/LER-1986-021, Partially Deleted LER 86-021-00:on 860911,vital Area Doors Failed to Alarm When Tested During Surveillance.Caused by Failure to Report Door Transactions to Host Computer.Central Procesing Unit Board Replaced1986-09-15015 September 1986 Partially Deleted LER 86-021-00:on 860911,vital Area Doors Failed to Alarm When Tested During Surveillance.Caused by Failure to Report Door Transactions to Host Computer.Central Procesing Unit Board Replaced 05000000/LER-1986-020, Partially Deleted LER 86-020-00:on 860812,security Sys Experienced Loss of Power.Caused Withheld.Numerous Failures Experienced Until Machine a Designated as Prime.Procedures to Reboot Computers Revised1986-08-15015 August 1986 Partially Deleted LER 86-020-00:on 860812,security Sys Experienced Loss of Power.Caused Withheld.Numerous Failures Experienced Until Machine a Designated as Prime.Procedures to Reboot Computers Revised 05000000/LER-1986-004, Partially Deleted LER 86-004-01:on 860204,loss of Dynamic Reporting of Alarm Surveillance Occurred.Cause Withheld. Computer Svcs Personnel Will Continue to Monitor Sys for Indicators of Cause1986-06-11011 June 1986 Partially Deleted LER 86-004-01:on 860204,loss of Dynamic Reporting of Alarm Surveillance Occurred.Cause Withheld. Computer Svcs Personnel Will Continue to Monitor Sys for Indicators of Cause 05000000/LER-1986-016, Partially Deleted LER 86-016-00:on 860501,vital Area Door Discovered W/O Alarm Capabilities.Caused by Access Control Security Officer Asleep at Post.Determination to Suspend or Discontinue Employment Being Made1986-05-0606 May 1986 Partially Deleted LER 86-016-00:on 860501,vital Area Door Discovered W/O Alarm Capabilities.Caused by Access Control Security Officer Asleep at Post.Determination to Suspend or Discontinue Employment Being Made 05000000/LER-1986-015, Partially Deleted LER 86-015-00:on 860428,stationary Side of Door Failed to Alarm When Tested.Cause Withheld.Alarm Repaired1986-05-0202 May 1986 Partially Deleted LER 86-015-00:on 860428,stationary Side of Door Failed to Alarm When Tested.Cause Withheld.Alarm Repaired 05000000/LER-1986-014, Partially Deleted LER 86-014-00:on 860421,bomb Threat Received by Security Officer in Security Assembly Room. Cause Not Applicable.Actions Taken to Minimize Station Threat & Investigation Underway1986-04-25025 April 1986 Partially Deleted LER 86-014-00:on 860421,bomb Threat Received by Security Officer in Security Assembly Room. Cause Not Applicable.Actions Taken to Minimize Station Threat & Investigation Underway 05000000/LER-1986-013, Partially Deleted LER 86-013-00:on 860414,vital Area Door W/O Alarm Capability Discovered.Caused by Personnel Error. Personnel Removed from Shift & Vital Area Checked for Unauthorized Personnel W/None Being Found1986-04-18018 April 1986 Partially Deleted LER 86-013-00:on 860414,vital Area Door W/O Alarm Capability Discovered.Caused by Personnel Error. Personnel Removed from Shift & Vital Area Checked for Unauthorized Personnel W/None Being Found 05000000/LER-1986-012, Partially Deleted LER 86-012-00:on 860412,breach Discovered in Protected Area Barrier.Caused by Personnel Error. Personnel Counseled1986-04-17017 April 1986 Partially Deleted LER 86-012-00:on 860412,breach Discovered in Protected Area Barrier.Caused by Personnel Error. Personnel Counseled 05000000/LER-1986-011, Partially Deleted LER 86-011-00:on 860410,vital Area Intrusion Alarm Failure Occurred.Cause of Event Deleted. Alarm & Door Tested Satisfactorily1986-04-15015 April 1986 Partially Deleted LER 86-011-00:on 860410,vital Area Intrusion Alarm Failure Occurred.Cause of Event Deleted. Alarm & Door Tested Satisfactorily 05000000/LER-1986-003, Partially Deleted LER 86-003-00:on 860125,loss of Dynamic Reporting of Vital Area Door Activity Occurred.Caused by Equipment Malfunction.Corrective Action Withheld1986-01-29029 January 1986 Partially Deleted LER 86-003-00:on 860125,loss of Dynamic Reporting of Vital Area Door Activity Occurred.Caused by Equipment Malfunction.Corrective Action Withheld 05000000/LER-1986-002, Partially Deleted LER 86-002-00:on 860117,loss of Alarm Surveillance on Doors Occurred.Caused by Erroneously Listing Officer as Being Posted on Door 398.Processing of Rev to Physical Security Plan Initiated1986-01-23023 January 1986 Partially Deleted LER 86-002-00:on 860117,loss of Alarm Surveillance on Doors Occurred.Caused by Erroneously Listing Officer as Being Posted on Door 398.Processing of Rev to Physical Security Plan Initiated 05000000/LER-1986-001, Partially Deleted LER 86-001-00:on 860105,loss of Dynamic Reporting of Vital Door Activity Occurred.Cause & Corrective Action Completely Deleted1986-01-10010 January 1986 Partially Deleted LER 86-001-00:on 860105,loss of Dynamic Reporting of Vital Door Activity Occurred.Cause & Corrective Action Completely Deleted 05000336/LER-1983-012, Updated LER 83-012/03X-1:on 830322 & 26,charging Pump C Shut Down Due to Lost Oil Pressure.Caused by Failed Integral Oil Pump Drive Coupling.Coupling Repaired1984-03-12012 March 1984 Updated LER 83-012/03X-1:on 830322 & 26,charging Pump C Shut Down Due to Lost Oil Pressure.Caused by Failed Integral Oil Pump Drive Coupling.Coupling Repaired 05000336/LER-1983-020, Updated LER 83-020/01X-1:on 830613,2,557 Degraded Tubes Discovered on Steam Generator Tubing.Cause Undetermined. Tubes W/Flaws Less than + or - 40% Through Wall or Eddy Current Probe Restrications repaired.W/840213 Ltr1984-02-13013 February 1984 Updated LER 83-020/01X-1:on 830613,2,557 Degraded Tubes Discovered on Steam Generator Tubing.Cause Undetermined. Tubes W/Flaws Less than + or - 40% Through Wall or Eddy Current Probe Restrications repaired.W/840213 Ltr 05000336/LER-1983-007, Updated LER 83-007/01T-1:on 830318,nonconservative Safety Analysis Assumption Discovered in Steam Generator Tube Rupture Analysis.Radiological Consequences of Reanalysis Being Analyzed1983-12-0909 December 1983 Updated LER 83-007/01T-1:on 830318,nonconservative Safety Analysis Assumption Discovered in Steam Generator Tube Rupture Analysis.Radiological Consequences of Reanalysis Being Analyzed ML20064F8591978-11-28028 November 1978 /03L-0 on 781115:spent Fuel Pool(Sfp)Ventilation Particulate & Gaseous Setpoints Exceeded Tech Specs Setpoints of Table 3.3-6,items 2.c & 2.d.Caused by Monitor Recalibr W/O Taking Into Account Tech Spec Limit ML20064F1651978-11-21021 November 1978 /03L-0 on 781025:during Oper,Surveillance Test on Channel a Reactor Protec Sys Core Protec Calculator Reveated Sys Ground Traced to Signal for Pressurizer Pressure W/In Containment Boundary.Source Not Known at This Time ML20064E6611978-11-16016 November 1978 /03L-0 on 781024:plant Computer Malfunction Caused CEA Pulse Counting Position to Be in Oper.Cause of Computer Failure Could Not Be Traced ML20064E1501978-11-0606 November 1978 /03L-0 on 781007:daily Tech Spec 4.3.1.1.1.,Table 4.3-1,items 2.a & 2.b,Nuc Pwr Surveillance & Delta-T Pwr Channel Calibr Not Performed Due to Personnel Error. Supervisors Told to Perform Req Surveillance ML20064D6131978-11-0303 November 1978 /03L-0 on 781025:Analysis of Instru Installations Revealed That Two Transmitters Assoc W/Channel a Steam Generator Low Water Lever Were non-seismically Mounted. Channel a SG Was Bypassed.Seismic Brackets Will Be Used ML20064D6011978-11-0101 November 1978 /03L-0 on 781004:during Surveillance Testing, Setpoint for Reactor Protec Sys Reactor Coolant Low Flow Trip on Channel B Was Out of Spec.Setpoint Was Readjusted. Rev Will Req Low Flow Trip Unit Setpoint Be Reset ML20064B8171978-10-0202 October 1978 /03L-0 on 780906:Loss of Methyl Iodide Removal Efficiency for a Ebfs Train. Cause Unknown 1997-09-29
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217P5391999-10-25025 October 1999 Rev 0,Change 1 to Millstone Unit 1 Northeast Utils QA Program ML20217C8721999-10-0606 October 1999 Rev 21,change 3 to MP-02-OST-BAP01, Nuqap Topical Rept, App F & G Only B17896, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With B17894, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With B17898, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216J4341999-09-24024 September 1999 Mnps Unit 3 ISI Summary Rept,Cycle 6 ML20211N8401999-09-0202 September 1999 Rev 21,change 1 to Northeast Utils QA TR, Including Changes Incorporated Into Rev 20,changes 9 & 10 B17878, Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With B17874, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 B17879, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With ML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20211A6561999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2 B17858, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With B17856, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With ML20210J0311999-07-21021 July 1999 Rev 20,Change 10 to QAP 1.0, Organization ML20210E5931999-07-19019 July 1999 Revised Page 16 of 21,to App F of Northeast Util QA Program Plan ML20210C5911999-07-15015 July 1999 Revised Rev 20,change 10 to Northeast Util QA Program TR, Replacing Summary of Changes ML20210A0411999-07-15015 July 1999 Rev 20,change 10 to Northeast Util QA Program Tr B17814, Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start1999-07-12012 July 1999 Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start ML20209D1881999-07-0101 July 1999 Rev 20,change 9 to Northeast Util QA Program Tr ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20211A6751999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level & Operating Data Rept ML20196A8451999-06-30030 June 1999 Post Shutdown Decommissioning Activities Rept ML20209J0541999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Unit 2 B17830, Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With ML20196K1791999-06-30030 June 1999 Addendum 6 to Millstone Unit 2 Annual Rept, ML20196J1821999-06-30030 June 1999 Rev 21,Change 0 to Northeast Utilities QAP (Nuqap) Tr B17833, Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With ML20195H1011999-06-11011 June 1999 Rev 20,change 8 to Northeast Utilities QAP (Nuqap) TR ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20211A6631999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level,Operating Data Rept & Unit Shutdowns & Power Reductions B17808, Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With ML20211B7351999-05-31031 May 1999 Cycle 7 Colr B17804, Monthly Operating Rept for May 1999 for Mnps,Unit 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 2.With B17807, Monthly Operating Rept for May 1999 for Mnps,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 1.With ML20209J0661999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Unit 2 ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206J8351999-05-0707 May 1999 Rev 20,Change 7 to QAP-1.0, Northeast Utls QA Program (Nuqap) Tr ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 B17782, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With ML20205R3531999-04-30030 April 1999 Addendum 4 to Annual Rept, B17775, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With ML20205K6141999-04-30030 April 1999 Non-proprietary Version of Rev 2 to Holtec Rept HI-971843, Licensing Rept for Reclassification of Discharge in Millstone Unit 3 Spent Fuel Pool ML20206E2971999-04-30030 April 1999 Rev 1 to Millstone Nuclear Power Station,Unit 2 COLR - Cycle 13 B17777, Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with ML20205Q5891999-04-0909 April 1999 Rev 20,change 6 to QAP-1.0,Northeast Utils QA Program TR ML20205R8751999-04-0909 April 1999 Provides Commission with Staff Assessment of Issues Related to Restart of Millstone Unit 2 & Staff Recommendations Re Restart Authorization for Millstone Unit 2 ML20206T3991999-03-31031 March 1999 First Quarter 1999 Performance Rept, Dtd May 1999 B17747, Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With 1999-09-30
[Table view] |
LER-2093-004, |
Event date: |
|
---|
Report date: |
|
---|
4232093004R00 - NRC Website |
|
text
. . .__ _ _. ._ _ _ _ _ . _ _ _.
i EORTHEAST UTILITIES a = S = ces s a en street Beran connecocut 1 I*cif NaY,$ dtN EIC ah
( 'I o/'[$s't [d e EcScany
' rwineast Noea Erew comran, HARTFORD. CONNECTICUT 06141-0270 (203)665-5000 August 31, 1993 MP-93-687 Re: 10CFR50.73('a)(2)(iv) 1 l U.S. Nuclear Reculatorv Commission Document Control Desk l Washington, D.C. 20555 1
Reference:
Facility Operating License No. NPF-49 Docket No. 50-423 Licensee Event Report 93-004-01 Gentlemen:
1 This letter forwards Licensee Event Report 93-004-01 which is being submitted to report on root cause and revise the analysis of event. Licensee Event Report 93-004-00 was l
- submitted pursuant to 10CFR50.73(a)(2)(iv). any event or condition that resulted in l
manual or automatic actuation of any Engineered Safety Feature (ESF), including the l
Reactor Protection System (RPS).
I Very truly yours, NORTHEAST NUCLEAR ENERGY COh1PAhT ephen .
Vice President - hiillstone Station SES/JSY:ljs
Attachment:
LER 93-004-01 cc: T. T. h1artin, Region 1 Administrator P. D. Swetland, Senior Resident inspector, hiillstone Unit Nos.1, 2 and 3 )
V. L Rooney, NRC Project hianager, hiillstone Unit No. 3 l
l 08007" 9309090435 930831 P 1 PDR ADOCK 05000423 i I S PDR L I f
aW4 P 7 as U 71s & '
APPROVED BY OMB NO. 3150-0104 i F AC Nm 3M U.S. NUCLEAR REGULATORY COMMISSION '
es-921 EXPIRES: 5/31/95 ESTMATED Bu:(DEN PER RE SPONFE TO COVEY WTH TW$
PFC+W ATON COLLECTON PEOvE 5' 50t HAS F ORA ARD CMEM RE GWNC, BJRDEN E STMAT E 'O T HE LICENSEE EVENT REPORT (LER) INF ORV AT CN AND RECORDS M AN A GE ME NT fBRAN;H (MNBB 7714 ; US NJOLEAA RE GJL 4 7 DPY COMMSEON W ASH:NGTON DO PI.M S-ODD'. AND TO THE P ADE 4W DAx (See reverse ter recured number cf digitsechwacters for each block) REDUCTON PROJE C' 0150-c 041 DrFICE Oc MANAGE MEN' ANO BUDGr? V. ASHfNGTON DC 2$03 F ACILIN NAME 0; DOCKET NUMBER (21 PAGE13.
Mmstone Nuclear Power Station Untt 3 05000423 1 OF 4 T1TLE 14 Reactor Tno Due to Electro-Hydrauhc Contro! Power Sucoty Failure Tvf NT DATE r5) LE A NUMEE4 m RE DOMT DATE f71 OTHE A F ACILITIE S INVOLVED (6)
VDNTH LAv TEAA N E. A R bEh! f-A JM M ONT
- On YEAR FACfLNY NAME DOCKET NUMBER 05000 08 31 93 rAc m NAVE ocesET NsMBER 03 31 93 93 - 004 - 01 , 05000 ;
OPE RATING T M:S REPORT 15 EiEING SUBMlTTED PUR$UANT TO THE PEOUIREMENTS OF 10 CFR $: (Oneca one or more) 01)
MODI
- pt 4 2 . , 2C ALc Y F4 73'a';D ov 72 7D' POWE R X s'5 a : r 50 30 r ' ' 60 73 a t f 2 + f v 73 71ic '
WEL DN 100 2 srs a. m s.. C3 c.- SC 73's:re-w . CTHEA 2c 405 ai n ), <
i 50 73.a , W i 50 73 + a l (2 H vi A: (5pec% m Arme twow ev n 7 ext. NGC 2C 4?5 elrt, ~ ED 73:e 20.o 50 73:aH2 m !E':
K 4 M ' air s s0 73.e,71ro 60 73<str?:.m ]
L.CENSEE CONTACT FOR THIS LER (12) )
NAVE r. r o-eNr u tvP c. nne w Aee, c me.
1 Jettrey S. Young. Engineer. 6442 (203) 447-1791 COMPLETE ONE LINE FOR E ACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
- E occtT As.E , PE DORT ABLE CAUSE D STEU CE'P ONEN' P/ANUCAO'UCEE 'O 'FAC S CAJSE fv5'EV OOMPONENT MANLC ACTURER T O N
- 'ROS a
SUPPLEMENTAL REPORT EXPECTED (14) E xPE CTED YES SUBM:ESION No NE W f4 ses com.e'e E ADE CTED SJBM SSON L ATE. X ABSTRACT um.t tc 60; antes . e. , an ycea:e'.15 s mo e-u.a:*c tgw mea res)06)
At 0103 on March 31. 1943. wnh the plant in Mode i at 1009 pouer, a turbine vahe closure resulted in a )'
reactor inn fol! owed by a turbme inp.
Turbme vahe closure was the result of a faut > power supply m the Electo-Hydraunc Control (EHC) system.
With the excepuon of a (team generator code safety sahe not completely reseatmc the plant responded normall> to the tr2nuent Extenme uou& shooung determmed that a power supply in the EHC system was fauhy arid caused the turbine sahes to close. The faulty power supph was replaced. At action to present recurrence, the power supplies m the EHC system mll be replaced or refurbnhed on a 10 year penod.
Subsequent mvesugation determmed that the steam generator safety vahe which did not completely re> eat had i an mcorrect lower adjustrnent rmg setung. Addiuonal mtpect on revealed that other safety sahes also had i mcorrect setungs Three of these vahes mdnated that they hited and reseated durmg the transient. The other four vahes d:d not open.
The root cause of the improper setungs was madequate work control b3 the sendor Crosby Yahe and Gage Compans, who performed rnamtenance on the saieues. conducted an mvesupuon and determmed that their personnel madvertent!) used the wrong procedure to set the lower adrustment rmgs.
l NRO 6m 3M (5-GD
I P*c % 3MA U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104
" 2' EXPIRES: S /31/95 EstruATED eunDr N prn AEspow io coupuy wcw Tes l
1 LICENSEE EVENT REPORT (LER) acc=xw cemtenoN nrour s1 e o +s , oumo ;
- TEXT CONTINUATION OcWE NT E RWRDim BMN ES ATE T c' THr :
w oau Avion AND ntcows u ANAGE MENT en Auc., 1 fMNBB 77141 U f. fJUcLE. AA CiEGAAioRY C of.M SSf 0N l WASWNGT ON DO 20s%-0301 Af C T o '! HE PAPt twob REDucTtoN PROJE CT (3 M-01r* oMCE C# MAAAGEMENT AND BJDGET, A AWGTON Dc 206%
FAc W v NAME11: TDec.ET NOMEE 4 2, tfn Nuuetnit; P AGE r3 VE AR e , r Mustone Nuclear Power Staton Umt 3 05000423 93 - 004 - D1 02 OF 04 T EXT m m u. ace .s w. a an w r w ase NacS w ano nn ,
I Dt& tion of Fa,w t
On March 31,1993 at 0103 wnh the plant m Mode 1 at 1009 pouer (M6 degrees Fahrenhen and 2250 psta) a turbme load teJection alarm was recened as the turbine control vahes began to close. A normal response to turbme valve closure occurred. This conusted of all steam dumps opemng, atmosphenc durnps on 3 steam generators opening, and 1 Pressunzer Power Operated Rehef Yahe (PORY) cythng ,
open for 6 seconds. In add: tion. mdicauon was recen ed that several code safet) vahes on 2 steam generators hhed. 19 seconds aber the turbme vahes began to close, steam generator levels shrank to the low low setpomt which resulted m a reactor tnp followed by a turbme tnp. After the reactor and turbme inp, the atmosphenc dumps on the fourth steam generator opened and mdicahon was recened that code safeues on a 'htrd steam generator hfted. At steam pressure decreased. all dumps and safenes rescated with the excepuon of I safety on the "D" steam generator.
At the ume of the inp. operaton venhed that the Reactor Tnp and Bypass Breakers were open, that ali i
control roos uere fvlh inserted. and that neutron flux was decreasmc. An automatic start of the Auuhan f eeduater System occuned due to the low low water lesel'm one steam generator and the ;
turbme drnen Auxihart Feedwater Pump staned on low low water level in two steam generators. A Fteawater holanon occurred due to the lov average Reactor Coolant System temperature (564 degrees Fatuenheiy comtidem with the reactor tnp Subsequentiv, the plant stabihzed at the no load temperatore of 557 ceprees Fahrenheit. Thece were expected sptem responses. No addinonal Engmeered Safet3 Feature (ESF) actuanons were required or irnuated.
Aher the plant had stabihred, the salen was gagged but still did not close completeh' A normal plant cooldown was performed and the safety reseated at approximately 1000 psig steam generator pressure, Subsequent irnesuganon resealed that the louer adjustment rmg of the malfunctiomng safety vahe was i mc ot r ect. When set properly, the louer nng insures a clean forceful popping action when the safety lifts ,
and a cushioned rescating when the safety closes. If this nng is set 100 h:ph, steam cannot escape as i rapidh> u hen the vahe bepms to close. As a result the blowdown is mereased. The settings of the lower adlustment rmps on 11 other safeties which had been worked on by Crosby Vahe were checked. All 7 of the vahes which were mstalled were found to be set mtproperly. Of these, 3 mdicated that the3 had hfted and restated dunng the transient and 4 did not open because their setpomts were not reached.
- 11. Caute of Esent I l
The root cau*e of the turhme vahe closure was equipment failure. A capacnor failure m one of the EHC power rupphes caused noise to EHC solenoids resulting m a slow closure of all turbme vahes with servos.
The root cause of the safety vahe fathng to completeh reseat was madequate work control by the l t endor. When the contractor performed mamtenance on 4 safeties in 19S7 and 19%, NNECO Quahty I Control perforrned an mtpecuon of the uork on 2 that required ring adjustment. No discrepancies were noted and the nng setungs of these safenes were correct. Work on another group of b safenes was performed between 19E9 and 1991. Dunng this penod, the ring settings were documented and a certihcanon statement was issued. Investiganon by the vendor after the event revealed that a procedure +
for Crosby salen salves was inachenently u'ed m setting the lower adjustment rmg instead of the procedure specihed b) Nonheast Etihues. Northeast Cuhties performed a surveillance of Crotby and found no d:screpancies. An mdustry aud t team who had previously scheduled an audn of Crosb3's l Append:x B program was informed of this event and the results of the surveillrnce. This auda team had i no Upmhcam Endmgs and reported only a mmor order entry discrepanc3 Ill. Analvm ollvent Nac wmanA wo
s Nac ro m 36EA U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 1542 a EXPIRES: 5731/95 ESTNATED BURDEN PEA RES:CNSE TO CoMRv WITH TH:5
, LICENSEE EVENT REPOR (LER) wasuATON coaEcTCN nEcuEsT w e sns ro% AnD TEXT CONTINUATION C OMMET E RE G ARD'NG BJRDEN E ST'M A TE To '-E M oAM ATON AND AEcORDS M ANA GE MET BRANCH (MNBE 77 M; . US NUCLEAR PEGULAToAv CoMMSSCN }
AAEMNGioN De 2D5Lb-0D07. AND To THE FADERWorm i AEDucTON PROJECT i3150-0% 03CE 05 M ANAGEMET AND BUDGET W A SHN3T ON De cD503 j FAc0TvNAME0; JDcNE' trJM6E; 22: LE ri NUVEE% <6, P A GE f3 +
YEA 4 NTk[' DN Mmstone Nuciear Power Staton iJnit -0 05000423 93 - 004 - 01 03 OF 04 TEXT w mo e sme is re=wree use ax+oma cwes c' unc r om asc A: ti7)
This esent is bemp reponed m accordance with 10CFR50.73faH2Hn9 as any esent or condinon that resulted m automauc actuauon of an ESF meludme the Reactor Protecuon System. An immediate nonficauon was made m accordance with 10CFR50.72(bH2Hii). ;
All safet3 systems funcuoned as designed as a result of the reactor inp. The Auxthary Feedy ater System started automancally due to the low low steam generator water level. A Feedwater Isolauen occurred due to the low Reactor Coolant System aserage temperature comcident urh the reactor inp. No other 6 E5F signals were initiated and the esent posed no signif cant hazard to the health and safety of the public. Sc ondary plant equipment was returned to normal operation. and the unn was returned to pow er ;
The improper setung of the louer adiustment rings on the safety vahes did not place the plant out side of the design basis for a stuck open safen vahe. The plant is analyzed for a flow of 97'.200 lbm'hr for this accidem Each safety vahe is destgned to pass f r~r (970.000 lbm'hr) of total steam flow. How ever, parameter mdicauens shoued that the affected safet3 vahe had not completely reseated but was not !
stuck fully open The partially open safety did not result m an uncontrolled cooldown and the plant ;
operators were able to mamtam normal shutdown plant temperature and pressure. Indicated proper operanon of 3 other safeues which had improper nng adjustment durmg the transient showed that ,
~
improper setimg of the lower adiustment nng does not necessarily mean that a safety will not reseat.
4 While actual operanon and subsequent testmg of the malfunctionmp safety (see below) showed that n re'eated at lower pressures. these pressures are normall3 reached several hours aher p! ant shutdown. l Theref ore, arn. other vahe which did not fully reseat would eventualh. close by uself.
l W yle Valve Reteated Reseat Pressure {
Test No. Durmg Test (PSIG) 1 No < 1055 a 2 Yes 1068 i I
3 Yes 1062 4 No < 1065 I Therefore. the 4 vahes that did not open may hase rescated properly if they had opened. In addition. l I
they would not have stuck fully open if they had failed to reseat and would hase closed completely by
- t hemseh e3 after a controlled plant cooldown to approximatelv 530 decrees Fahre1 hen i
Because there is no measurable pnmarv to secondary leakace m the "D" steam generator, there was no .,
release of radioactne matenal as a result of the partially open safety vahe. l l
A review of the impact of an extended blowdown of a main steam safety vahe on other postulated accidents has been completed. This review concluded that the consequences o.f a main steam safety failmg to reseat properly are bounded by the assumptions and results of the accident analysis for ifnit 3 This completes review of this erem as a 10CFR21 concern.
IV. Correctn e Action ;
As immediate correcure action for the tr p, the fauhy power supply was replaced. As action to prevent !
recurrence. the power supply will be replaced or refurcished on a 10 year period. Due to replacement j unavailabihty. the other power supplies m the EHC system will be replaced durmg the upcoming refuelmg j outa ge , i Nec s o-m awA 15-923 4
i l
t*<C So m 36tA U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 l I6-Sh EXPIRES; 5/31/95 l
E STiMATED tauRDEN PER RE SPCNEE TO COM%v W TH MS
- LICENSEE EVENT REPORT (LER) m O=ucoN cOaEc, cN SE OuE sT Ee o Has re,naARD COMvENTS- RE G ARD!NG Ev4 DEN E ST M A' E TO T HE
- TEXT CONTINUATION v Damn cN ec PE:On;s us.w GEMENT r>nANcH fM NEE ??ia: US N A EAR RE GJi. AT OA V OOMMSScN 6ASMN3 TON OC MLE5MIOT ANO iC *HE PAPER A'ORF AEDuC
- cN PRO.;E CT (3* fG-CDa i OrFICE OF MANAGEMENT l ANC E'UDGET W ASMNGTON DC 20003 r 5 Acta NAME is 3DCVE T NJMSEE ;2) LE A ?LMEif R IU FAGEf3 I vrAn TXUfi^- 7J8Oh Mhstone Nuclear Power Station Un"~ 3 05000423 ;
93 - 004 -
01 04 OF 04 ;
. TEXT m m sme a rewee aeax: v a: era e N;; 4> m ace A: 07)
At ammed: ate correctne action for the 'mproper ring setungs, the 11 other safet3 vahes which had been r refurbnhed. repaired or set by Crosby \ ahe were examined for proper rmg setungs. The 7 (excludmg !
the ma!!uncuonmp onel which were improperly set were adjusted as necessary to their proper nng -
setungs All spare safeues currentl3 out for mamtenance at any contractor will be serihed before return to the ute.
i V. Minonn! inf r rrv ati;/n No other Licensee Event Reports (LER31 hase been submitted for reactor inps resulung from a f atied ;
power supph in use EHC synem. [
Tlus LER also satishes NNECO's evaluation. nou6 cation and reporung obhrauon to report defects under 10CFR21. In addition, a copy 0.1 this LER was sent to the contractor that performed mamienance on l ,
the mam steam safeues. I i No sirmlar pouer supply malfuncuons were found m a renew of NPRDS. t Ells codn hm Egg,nnyn, Mam Turbine Control power Supply, Electric - JX I
- Flmd 53 stem - TG hn' Reheat Steam Rehe! Vahe - RV l Sutem - SB !
1 I
Mbb7 T M4 A 'D*h4j
_ , - . _ .
|
---|
|
|
| | Reporting criterion |
---|
05000423/LER-1993-004 | LER 93-004-01:on 930331,RT Occurred Due to electro-hydraulic Control Power Supply Failure.Replaced Faulty Power Supply. W/930831 Ltr | | 05000245/LER-1993-006, Forwards Updated LER 93-006-01 Which Was Previously Submitted W/O Rev Bars | Forwards Updated LER 93-006-01 Which Was Previously Submitted W/O Rev Bars | | 05000336/LER-1993-007, Incorporates NRC Comments Discussed During 940324 Telcon Into 931217 Application for Amend to License DPR-65,revising TS 3.8.1.1,as Result of LER 93-007-00,dtd 930428 & Util 930726 Response to NOV from Insp Rept 50-336/93-81 | Incorporates NRC Comments Discussed During 940324 Telcon Into 931217 Application for Amend to License DPR-65,revising TS 3.8.1.1,as Result of LER 93-007-00,dtd 930428 & Util 930726 Response to NOV from Insp Rept 50-336/93-81 | | 05000336/LER-1993-008 | LER 93-008-01:on 930505,declared Charging Pumps Inoperable Due to Low Control Power Voltage.Established Administrative Controls & Installed Interposing Relay within C Charging Pump Control circuit.W/930902 Ltr | | 05000423/LER-1993-011 | LER 93-011-00:on 930731,MSSV Lift Setpoint Drift Occurred Due to Unknown Cause.Reduced Setpoint for Power Range Neutron Flux High Trip to 10%.W/930830 Ltr | | 05000245/LER-1993-011, Responds to NRC 981002 Request to Counsel That NNECO Waive Any Assertion of Statue of Limitations for 60-90 Days with Respect to NRC Ability to Initiate Civil Penalty Action Based on Apparent Violation of 10CFR50.59 Re LER 93-0 | Responds to NRC 981002 Request to Counsel That NNECO Waive Any Assertion of Statue of Limitations for 60-90 Days with Respect to NRC Ability to Initiate Civil Penalty Action Based on Apparent Violation of 10CFR50.59 Re LER 93-011-00 | | 05000423/LER-1993-012 | LER 93-012-00:on 930805,piece of Plywood Discovered in Train a of Sws.Caused by Inadequate Work Control During 1991 Outage to Repair Sws.Plywood Removed & Increased Attention Being Paid to Matl Exclusion in Critical sys.W/930903 Ltr | | 05000336/LER-1993-014 | LER 93-014-00:on 930714,discovered Surveillances Procedures Had Not Been Performed within Specified Time Intervals Due to Insufficent Planning.Missed Surveillances Immediately performed.W/930813 Ltr | | 05000336/LER-1993-016 | LER 93-016-00:on 930729,reportability Determination Made Re Analysis for Boron Dilution Event.Caused by Inadequate Review of Results of Boron Dilution in Relation to Plant Operating Conditions.Boron Results revised.W/930827 Ltr | | 05000336/LER-1993-018 | LER 93-018-00:on 930805,letdown Manual Isolation Valve 2-CH-442 Developed Leak Which Exceeded TS Limits.Root Cause Has Not Been Determined.Valve Replaced & All Code Required Post Intallation Tests Successfully completed.W/930903 Ltr | | 05000336/LER-1993-019 | LER 93-019-00:on 930812,reactor Trip Occurred Due to Low SG Level.Conducted Shift Briefing of Event to Operating Shift While Assuming Watch.Briefing Included Listed Requirements for Subsequent Specific start-up.W/930910 Ltr | | 05000336/LER-1993-023, Forwards LER 93-023-02,documenting Event Occurred at Unit 2 on 930622.Commitments Made within Ltr Listed | Forwards LER 93-023-02,documenting Event Occurred at Unit 2 on 930622.Commitments Made within Ltr Listed | |
|