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' fW1heast Naciea Energy Company (203)S65-5000 April 30, 1993 MP-93-349 Re: 10CFR50.73(a)(2)(iv)
U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 i
Reference:
Facility Operating License No. NPF-49 Docket No. 50-423 Licensee Event Report 93-004-00 l
Gentlemen:
This letter forwards Licensee Event Report 93-004-00 required to be submitted within thirty (30) days pursuant to 10CFR50.73(a)(2)(iv) any event or condition that resulted in manual or automauc actuation of any Encineered Safetv Feature (ESF) including the Reactor Protection System (RPS).
ll Very truly yours, NORTHEAST NUCLEAR ENERGY COMPANY
'h Stephen}E r mcv cace Vice President - Millstone Station i
i SES!JSY:ljs Attachment: LER 93-004-00 cc:
T. T. Martin, Region 1 Administrator P. D. Swetland, Senior Resident Inspector, Millstone Unit Nos.1, 2 and 3 V. L. Rooney, NRC Project Manager, Millstone Unit No. 3 050032 (2nd fff 9305060219 930430 I
PDR ADOCK 05000423 S
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NRC Fo*m 366 U E NUOLE AR RE Ggt ATORY C OUM;SstDN APPROVED oMD NO. 3150-0104 (649)
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ASSTR/ CT tum u 400 scates ie anoco mtet 1 **eer s ngte-s;. ace typewrtt:en imes) os 1 At 0103 on March 31, 1993. with the plant in Mode 1 at 100cc power, a turbine valve closure resulted in a reactor inp followed by a turbine inp.
Turbme rahe closure was the resuh of a faulty power supply in the Electro-Hydraulic Control (EHC) system.
With the exception of a steam generator code safety valve not completely reseaung, the plant responded normally to the transte,t.
Extensive trouble shooting determmed that a power supply m the EHC system was faulty and caused the turbine valves to close. The faulty power supply was replaced. As action to present recurrence, the power supphes in the EHC system will be replaced or refurbished on a 10 year perio.l.
Subsequent msesugation determmed that the steam generator safet z vahe which did not completely rescat had an incorrect lower adjustment rmg settmg. Additional inspection r.tvealed that 7 other safety valves also had inconect settings. Three of these valves mdicated that they hfied ; nd reseated during the transient. The other 4 vahes did not open.
The root cause of the improper settings has not been dm%ed Crosby Valve and Gage Company, who perfonned maintenance on the safeties, documented Troper settmgs and sne records do not show any work performed on the safenes after dehvery to the site.
NRC Form 306 (6-82)
NRC For'n a66 A U S. NUCLE AR REGULATORY CoMM:SSON APPROVED OMB NO 3150-0 44 T-SD)
EXPAE S a '30 42 Estimated burcen oe* resporme to compiy mtn 1Ns
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**'8 LICENSEE EVENT REPORT (LER) c"om'ments rega om'*g buro'e'n estmate to tne' Reco os TEXT CONTINUATION
..e Repons Manageme,t sranca (p-saor u s Nuc1ea-Repatory Comrmssion W ashington De 20555. anc to the Noerwom Re:Letton Pro <stt (3'50-0104L o*Lce of i
Managemerit and Bsopet. Waswgton DC 20503.
i F AclLf"Y' N AVE (li DoO*r,ET NUMBE R (2) t rce ytvrer ra (f;i P AGE (31 VEAR N
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Descrmnon of Es en' On March 31,1993, at 0103 wnh the plant m Mode 1 at 1009 power (566 degrees Fahrenheit and 2250 psia) a turbme load rejecuon alarm was recened as the turbine control vahes began to close. A normal response to tu bme vah'e closure occurred. This consisted of all steam dumps opening, atmosphene dumps on 3 steam generators opening, and 1 Pressunzer Power Operated Relief Valve (PORV) cychng open for 6 seconds. In addmon, mdicauon was received that several code safety valves on 2 steam generators hfted. Smeteen seconds after the turbine vahes began to clote, steam generator lesels shrank to the loa low seipoim which resulted m a reactor trip followed by a turbme trip. After the reactor and turbme trip, the atmospheric dumps on the fourth steam generator opened and indication was received that code safet es on a third steam generator htted. As steam pressure decreased, all atmosphen steam dumps and safeties reseated with the exception of I safety on the "D' steam generator.
At the time of the inp, operators venfied that the Reactor Tnp and Bypass Breakers were open, that all control rods were fully mserted, and that neutron flux was decreasmg. An automatic start of the Auxihary Feedwater System occurred due to the 20w low water level in one steam generator and the turbme drnen Auxihary Feedwater Pump staned on low low water level m two steam generators. A Feedwater Isolation occurred due to the low average Reactor Coolant System temperature (564 degrees Fahrenheit) comeident with the reactor trip. Subsequently, the plant stabihzed at the no load temperature of 557 degrees Fahrenheit, These were expected system responses. No additional Engineered Safety Feature (ESF) actuations uere required or initiated.
Aher the plant had stabihzed, the safety was gagged but still did not close completely. A normal plant cooldown was performed and the safety reseated at approximately 1000 psig steam generator pressure.
Subsequent mvestiganon revealed that the lower adjustment ring of the malfunctioning safety valve was 4
inconect. When set properly. the lower nng insures a clean, forceful popping action when the safety lifts and a cushioned reseatmg when the safety c!oses. If this ring is set too high, steam cannot escape as rapidly when the vahe begms to close. As a resuh the blowdown is increased. The settings of the lower
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adjustment rings on 11 other safeties which h9 oeen worked on by Crosby Valve were checked. All 7 of the vahes which were installed were found to be set improperly. Of these, 3 indicated that they had hfted and reseated dunnp the transient and 4 did not open because their setpoints were not reached.
II.
Cause of Es ent The root cause of the turbine sahe closure was equipment failure. A capacitor failure m one of the EHC power supplies caused noise to EHC solenoids resulting in a slow closure of all turbine vahes with i
sersos The root cause of the safety vahe fathng to completely reseat has not been determmed. When the contractor performed malmenance on 4 safeties in 1957 and 1988, NNECO Ouahty Control performed I
an inspection of the work on 2 that required ring adjustment. No discrepancies uere noted and the rmg settings of these safeties were correct. Work on another group of 8 safeties was performed between 1989 and 1991. During this period, the ring settings were documented and a certification statement was inued; howeser, NNECO mspection was not requ red as the work was performed under Crosby Valve and Gage Company's Appendix B program. Since plant records indicate that no adjustments were made onsite, a dehmte cause for the improper adjustment has not been determined. NNECO will continue to work with the contractor to determine when and how the improper adjustments may have occurred.
III.
Apah* nf Es ent This esent is being reported in accordance with 10CFR50.73(a)(2)(iv) as any event or condition that resulted in automatic actuation of an ESF including the Reactor Protection System. An immediate nouhcation was made in accordance with 10CFR50.72(b)f 2)(ii).
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NRc Fort a66A U S. t#JcLE AR AE GuLAToRY CoMM.SSION ADPROVED oMB NO 3150-0104
@-69; EKRAES 4,30:92 Estwatec Durcer per response le comply eth tr s e
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' c" *'d LICENSEE EVENT REPORT (LER) c"em"ums wgaremp woen esamte to tw Reeves TEXT CONTINUATION ano Renons uanrgement emen +534 u s. Nxteme Regula17y Commst.on-W eshmpt an DC 2%55 and to 1% F aperwe Recxt on D oje-1 m50-0100. O' hee of Manageme
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All safety systems funcuaned as de.igned as a result of the reactor inp. The Auxihary Feeduater System started automancally due to the lov lou steam generator water les el. A Feeduater isolation occurred due to the lou Reactor Coolant Sysam aserage temperature coincident with the reactor inp. No other ESF signah were 1ruuated and the es ant posed no sigmficant hazard to the heahh and safety of the pabltc. Secondary plant equipment wa3 returned to normal operanon. and the unit was returned to power The :mproper 3etung of the louer adjustnient rmp or the safety vahes did not place the plant out side of the de-ign ba(n for a stuck open safet) ahe. i ne pLmt is analyzed for a flou of C~,200 lbm/hr for ihn accidem Each safety vahe o designed to pass 5G (970.000 lbm/hr) of total steam flow. Hou erer, parameter mdicauons showed that the af fected safety salve had not completely reseated but was not i
stuck full > open. The parually open safety did not resuh m an uncontrolled cooldown and the plant 5
operators were aHe to mamtam normal shutdou n plant temperature and pressure. Indicated proper operanon of ^ other safenes uhich had improper nng adjustment durmg the transient showed that improper setung of the louer adjustment nng doe ( not necessarily mean that a safety will not reseat.
While actual operanon and subsequent tesung of the malfuncuan:ng safety (see below) shoved that it reseated at lower Pressures, these pressures are normally reached seseral hours after plant shutdown.
Therefore, any other vahe which did not fully resea would esentually close by itself.
Test Number Ghe Reseated Reseat Pressure Dunny Test (PSIG) 1 No
< 1055 2
Yes 10M 3
Yes 1062 4
No
< 1065 Therefore, the 4 sahes that did not open may have reseated properly if they had opened. In addition, they would not hate stuck fulh open if they had failed to receat and would have closed completely by themsehes after a controlled plant cooldoun to approximately 530 degrees Fahrenheit.
Because there is no mea urable onmary to secondary leakage in the "D" steam generator, there was no release of radioacute matenal as a resuh of the parually open safety valve.
The imphtations of the improperly set safety vahes on other postulated accidents base not been determmed A review of these impbcations will be completed and reported in a supplement to this report.
IV.
Correcme Action As immediate correcthe action for the inp, the faulty power supply was replaced. As action to prevent recurrence, the power supph will be replaced or refurbished on a 10 year period. Due to replacement unavailabihty, the other power supphes in the EHC system will be replaced during the upcoming refuelmg i
outage.
As immediate corrective action for the improper ring settings, the 11 other safety vahes which had been refurbished, repaired or set by Crosby Whe were examined for proper ring settings. The 7 (excluding the malfunctioning one) which were improperly set were adjusted as necessary to their proper ring settmgs. All Fpare safeties currentl3 out for mamtenance at any comractor will be venfied before return to the site.
I-
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NAO. Fo-n 366A U S. NUCLE ACI REGULATORY COMM1SStON APPROVED OMB NO 3150-0104 (6-6 0 )
gxpAES 4 /30 $2 i
Estimated baroen per response to compiy witn in.s LICENSEE EVENT REPORT (LER)
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.ement Br Repwatery Commesson. Wasn.ngton. DC P0555. ano to the Paperworm Resacuen Prmeet (315D-0104). office of Management and Badge. W ashmgton. DC. 20503 FACfLrTY NAME tij DOC #.ET NUMBE A (2) i F A Mupr n; #4, F AGE (3.-
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Additional Information
No other Licensee Esent Reports (LERs) have been submined for reactor trips resulung from a failed power suppl 3 in the EHC system _
+
This LER also satisfies NNECO's ecaluauon, nonficanon and reporting obligation to repon defects under 10CFR21. In addition, a copy of this LER will be sent to Crosby Valve and Gage Company.
No simibt power supply malfuncuens were found in a renew of NPRDS.
Ells codet i
4 cem Comnonent Nain Turbine Control Power Supply, Electric - JX Fluid Sy stem - TG Main / Reheat Steam Relief Valve - RV System - SB l
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P YY Wm hh (6-89)
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| 05000245/LER-1993-001-01, :on 930108,determined That Previous Snubber Failure of HSS-018 B SRV Discharge Line Resulted in Failure to Meet TS LCO for Section 3.6.I.4.Caused by Use of Incorrect Bleed Rate.Snubber Rebuilt |
- on 930108,determined That Previous Snubber Failure of HSS-018 B SRV Discharge Line Resulted in Failure to Meet TS LCO for Section 3.6.I.4.Caused by Use of Incorrect Bleed Rate.Snubber Rebuilt
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000336/LER-1993-001, :on 921227,weekly TS Surveillance in Modes 5 & 6 Not Performed within Specified Time Interval.Caused by Lack of Procedural Detail & Administrative Error.Flowpath Instruction Revised & Personnel Counseled |
- on 921227,weekly TS Surveillance in Modes 5 & 6 Not Performed within Specified Time Interval.Caused by Lack of Procedural Detail & Administrative Error.Flowpath Instruction Revised & Personnel Counseled
| 10 CFR 50.73(a)(2)(i) | | 05000423/LER-1993-001-02, :on 930126,discovered That Signal Path from Nis Axial Flux Circuit Input Into Westinghouse 7300 Process Control Sys Not Periodically Tested.Caused by Procedure Deficiency.Test Changes Incorporated |
- on 930126,discovered That Signal Path from Nis Axial Flux Circuit Input Into Westinghouse 7300 Process Control Sys Not Periodically Tested.Caused by Procedure Deficiency.Test Changes Incorporated
| 10 CFR 50.73(a)(2)(i) | | 05000336/LER-1993-002, :on 930107,determined That LCO, Accident Monitoring Not Entered Upon Entry Into Mode 3.Caused by Incomplete Application of Change to Ts.Event Will Be Reviewed by All Licensed Operators |
- on 930107,determined That LCO, Accident Monitoring Not Entered Upon Entry Into Mode 3.Caused by Incomplete Application of Change to Ts.Event Will Be Reviewed by All Licensed Operators
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000423/LER-1993-002, :on 930206 & 07,Train a & Train B CR Pressurization Sys Failed 18-month Surveillance Test, Respectively.Caused by Moisture in Air Banks & Pressure Oscillations.Air Banks Purged |
- on 930206 & 07,Train a & Train B CR Pressurization Sys Failed 18-month Surveillance Test, Respectively.Caused by Moisture in Air Banks & Pressure Oscillations.Air Banks Purged
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2) | | 05000423/LER-1993-002-01, :on 930207,train a CR Pressurization Sys Failed 18 Month Pressurization Surveillance Test.Caused by Moisture in Air Banks.Cr Placed in Filtered Recirculation & Air Banks Refilled W/Dry Air |
- on 930207,train a CR Pressurization Sys Failed 18 Month Pressurization Surveillance Test.Caused by Moisture in Air Banks.Cr Placed in Filtered Recirculation & Air Banks Refilled W/Dry Air
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000245/LER-1993-002, Corrected Cover Sheet to LER 93-002,correcting Administrative Error.First Sentence of Cover Sheet Should Be Corrected to Read as Stated | Corrected Cover Sheet to LER 93-002,correcting Administrative Error.First Sentence of Cover Sheet Should Be Corrected to Read as Stated | 10 CFR 50.73(a)(2)(i) | | 05000245/LER-1993-002-02, :on 930314,declared Secondary Containment Inoperable & Commenced an Orderly Shutdown.Caused by Operation of Two Redundant RB Supply Fans.Rb Supply Fans Will Be Modified |
- on 930314,declared Secondary Containment Inoperable & Commenced an Orderly Shutdown.Caused by Operation of Two Redundant RB Supply Fans.Rb Supply Fans Will Be Modified
| 10 CFR 50.73(a)(2) | | 05000423/LER-1993-003-01, :on 930329,discovered That Slave Relay Testing of air-operated Valves for Auxiliary Feedwater Pump Alternate Suction Inadequate.Caused by Mfg Deficiency.Lco Entered & Task Force Formed to Review Relays |
- on 930329,discovered That Slave Relay Testing of air-operated Valves for Auxiliary Feedwater Pump Alternate Suction Inadequate.Caused by Mfg Deficiency.Lco Entered & Task Force Formed to Review Relays
| 10 CFR 50.73(a)(2)(i) | | 05000245/LER-1993-003-02, :on 930426,discovered That Primary Containment Penetration X-25/202D Exceeded Max Allowed TS Leakage.Caused by Slightly Worn Seat Ring & Plug in Valve Not Fully Seating.Seat Ring Replaced |
- on 930426,discovered That Primary Containment Penetration X-25/202D Exceeded Max Allowed TS Leakage.Caused by Slightly Worn Seat Ring & Plug in Valve Not Fully Seating.Seat Ring Replaced
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | | 05000336/LER-1993-003, :on 930217,discovered That Mispositioned HPSI Valve Would Have Rendered Facility 1 HPSI Sys Inoperable Due to Inadequate Procedural Guidance.Affected Valve Returned to Correct Position & Appropriate Sps Revised |
- on 930217,discovered That Mispositioned HPSI Valve Would Have Rendered Facility 1 HPSI Sys Inoperable Due to Inadequate Procedural Guidance.Affected Valve Returned to Correct Position & Appropriate Sps Revised
| | | 05000423/LER-1993-004, :on 930331,turbine Valve Closure Resulted in Reactor Trip Followed by Turbine Trip.Caused by Faulty Power Supply in electro-hydraulic Control Sys Mfg by Crosby Valve & Gauge Co.Also Reported Per Part 21 |
- on 930331,turbine Valve Closure Resulted in Reactor Trip Followed by Turbine Trip.Caused by Faulty Power Supply in electro-hydraulic Control Sys Mfg by Crosby Valve & Gauge Co.Also Reported Per Part 21
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000423/LER-1993-004-01, :on 930331,RT Occurred Due to electro-hydraulic Control Power Supply Failure.Replaced Faulty Power Supply |
- on 930331,RT Occurred Due to electro-hydraulic Control Power Supply Failure.Replaced Faulty Power Supply
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000245/LER-1993-004-01, :on 930430,1-inch Instrument Lines from Main Steam Line Flow Venturis Found to Be Missing Pipe Restraints in Several Locations.Possibly Caused by Improper Maint &/Or Vibration.Missing Restraints Reinstalled |
- on 930430,1-inch Instrument Lines from Main Steam Line Flow Venturis Found to Be Missing Pipe Restraints in Several Locations.Possibly Caused by Improper Maint &/Or Vibration.Missing Restraints Reinstalled
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000336/LER-1993-004, :on 930222,reactor Trips on SG Low Water Level Occurred.Caused by Automatic Trip of MFW Pump B on Low Suction Pressure Due to High FW Flow Rates.Classroom Training on Main & Afwc Received by Licensed Operators |
- on 930222,reactor Trips on SG Low Water Level Occurred.Caused by Automatic Trip of MFW Pump B on Low Suction Pressure Due to High FW Flow Rates.Classroom Training on Main & Afwc Received by Licensed Operators
| | | 05000336/LER-1993-004-02, Forwards LER 93-004-02,updating Corrective Actions Identified in LER 93-004-01,submitted Per 10CFR50.73(a)(2)(iv),reporting Any Event or Condition That Resulted in Manual or Automatic Actuation of ESF Sys | Forwards LER 93-004-02,updating Corrective Actions Identified in LER 93-004-01,submitted Per 10CFR50.73(a)(2)(iv),reporting Any Event or Condition That Resulted in Manual or Automatic Actuation of ESF Sys | 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000245/LER-1993-005-01, :on 930429,hydraulic Snubber HSS-039 Identifed W/Unacceptable End Attachment to Recirculation Pump Motor Due to Missing Cotter Pin.Snubber Replaced W/Rebuilt Spare & Load Pin Installed Correctly |
- on 930429,hydraulic Snubber HSS-039 Identifed W/Unacceptable End Attachment to Recirculation Pump Motor Due to Missing Cotter Pin.Snubber Replaced W/Rebuilt Spare & Load Pin Installed Correctly
| 10 CFR 50.73(a)(2)(i) | | 05000423/LER-1993-005-02, :on 930520,cold Over Pressure Protection Sys Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Mgt Deficiency.Overlap Task Force Will Continue to Review Procedures Associated W/Reactor Trip |
- on 930520,cold Over Pressure Protection Sys Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Mgt Deficiency.Overlap Task Force Will Continue to Review Procedures Associated W/Reactor Trip
| 10 CFR 50.73(a)(2)(i) | | 05000336/LER-1993-005, :on 930311,discovered That Automatic RPS Actuation Occurred on 930222 & Not Immediately Reported to Nrc.Caused by Personnel Error.Memo Sent to All Licensed Operators/Personnel Re Reporting Requirements |
- on 930311,discovered That Automatic RPS Actuation Occurred on 930222 & Not Immediately Reported to Nrc.Caused by Personnel Error.Memo Sent to All Licensed Operators/Personnel Re Reporting Requirements
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000336/LER-1993-006, Corrected LER 93-006-00:on 930324,determined That Svc Water Supply Piping to Switchgear Room Coolers X-181A & X-181B Did Not Meet TS Structural Integrity Requirements.Caused by Personnel Error.Clamp Installed | Corrected LER 93-006-00:on 930324,determined That Svc Water Supply Piping to Switchgear Room Coolers X-181A & X-181B Did Not Meet TS Structural Integrity Requirements.Caused by Personnel Error.Clamp Installed | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000245/LER-1993-006-01, Forwards Updated LER 93-006-01 Which Was Previously Submitted W/O Rev Bars | Forwards Updated LER 93-006-01 Which Was Previously Submitted W/O Rev Bars | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000245/LER-1993-006, :on 930604,dicovered Unsealed Fire Barrier Penetration in TS Fire Wall Due to Lack of Detailed Guidance Re Procedure Used in Insp.Established Fire Watch to Compensate for Unsealed Penetrations |
- on 930604,dicovered Unsealed Fire Barrier Penetration in TS Fire Wall Due to Lack of Detailed Guidance Re Procedure Used in Insp.Established Fire Watch to Compensate for Unsealed Penetrations
| 10 CFR 50.73(a)(2) | | 05000423/LER-1993-006-02, :on 930525,two HPSI Discharge Check Valves Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Personnel Error.Test Written & Performed to Demonstrate Valve Operability |
- on 930525,two HPSI Discharge Check Valves Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Personnel Error.Test Written & Performed to Demonstrate Valve Operability
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) | | 05000245/LER-1993-006-03, :on 930604,unsealed Fire Barrier Penetration Discovered in TS Fire Wall Between Auxiliary Boiler Room & Maint Shop.Caused by Lack of Detailed Procedural Guidance. Fire Watch Established & Penetration Sealed |
- on 930604,unsealed Fire Barrier Penetration Discovered in TS Fire Wall Between Auxiliary Boiler Room & Maint Shop.Caused by Lack of Detailed Procedural Guidance. Fire Watch Established & Penetration Sealed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000336/LER-1993-007, Incorporates NRC Comments Discussed During 940324 Telcon Into 931217 Application for Amend to License DPR-65,revising TS 3.8.1.1,as Result of LER 93-007-00,dtd 930428 & Util 930726 Response to NOV from Insp Rept 50-336/93-81 | Incorporates NRC Comments Discussed During 940324 Telcon Into 931217 Application for Amend to License DPR-65,revising TS 3.8.1.1,as Result of LER 93-007-00,dtd 930428 & Util 930726 Response to NOV from Insp Rept 50-336/93-81 | | | 05000245/LER-1993-007, :on 930623,discovered Potential for Loss of Tbsccw Sys Due to Incomplete Review of safety-related/non- safety-related Sys Interface.Scope of Seismic Piping Reviews Expanded |
- on 930623,discovered Potential for Loss of Tbsccw Sys Due to Incomplete Review of safety-related/non- safety-related Sys Interface.Scope of Seismic Piping Reviews Expanded
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000423/LER-1993-007-01, :on 930611,plant Mgt Discovered Reduction in EDG Fuel Oil Storage Capacity Per SER & Fsar,Constituting Event Outside Design Basis of Plant.Caused by Inadequate Design Interface.Temporary Tanker Utilized |
- on 930611,plant Mgt Discovered Reduction in EDG Fuel Oil Storage Capacity Per SER & Fsar,Constituting Event Outside Design Basis of Plant.Caused by Inadequate Design Interface.Temporary Tanker Utilized
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000245/LER-1993-007-02, :on 930623,TBSCCW Sys Pressure Boundary Integrity Failed Due to Incomplete Review of Safety & non-safety-related Sys Interface.Isolation Valve (1-SC-184) 3/4-SC-105 Closed |
- on 930623,TBSCCW Sys Pressure Boundary Integrity Failed Due to Incomplete Review of Safety & non-safety-related Sys Interface.Isolation Valve (1-SC-184) 3/4-SC-105 Closed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | | 05000336/LER-1993-008, :on 930505,declared Charging Pumps Inoperable Due to Low Control Power Voltage.Established Administrative Controls & Installed Interposing Relay within C Charging Pump Control Circuit |
- on 930505,declared Charging Pumps Inoperable Due to Low Control Power Voltage.Established Administrative Controls & Installed Interposing Relay within C Charging Pump Control Circuit
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000423/LER-1993-008-01, :on 930614,one Channel of Electrical Environmentally Qualified Temp Monitor for Main Steam Valve Bldg Found Indicating Improperly.Caused by Personnel Error. Manual Logging of Temp Initiated |
- on 930614,one Channel of Electrical Environmentally Qualified Temp Monitor for Main Steam Valve Bldg Found Indicating Improperly.Caused by Personnel Error. Manual Logging of Temp Initiated
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | | 05000423/LER-1993-009, :on 930617,determined That SLCRS May Have Been Inoperable During Certain Cold Weather Period.Caused by Failure to Account for Chimney Effect in Encl Bldg.Design Change Implemented to Increase SLCRS Capacity |
- on 930617,determined That SLCRS May Have Been Inoperable During Certain Cold Weather Period.Caused by Failure to Account for Chimney Effect in Encl Bldg.Design Change Implemented to Increase SLCRS Capacity
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000336/LER-1993-009, :on 930506,inlet & Outlet skid-mounted Isolation Valves to Radiation Monitor Found Shut.Caused by Procedure Noncompliance by I&C Personnel.Personnel Will Review & Edit Radiation Procedures |
- on 930506,inlet & Outlet skid-mounted Isolation Valves to Radiation Monitor Found Shut.Caused by Procedure Noncompliance by I&C Personnel.Personnel Will Review & Edit Radiation Procedures
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | | 05000423/LER-1993-009-01, :on 930617,determined That Suppl Leak Collection & Release Sys May Have Been Inoperable During Certain Weather Periods in Past.Caused by Failure to Account for Chimney Effect.Suppl Will Be Sent |
- on 930617,determined That Suppl Leak Collection & Release Sys May Have Been Inoperable During Certain Weather Periods in Past.Caused by Failure to Account for Chimney Effect.Suppl Will Be Sent
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2) | | 05000245/LER-1993-009-02, :on 930706,inoperability of LPCI Sys Due to Outboard LPCI to Recirculation Loop Valve 1-LP-9B Failed to Open Electrically After Being Manually Opened.Declutch Fork & Clutch Repositioned |
- on 930706,inoperability of LPCI Sys Due to Outboard LPCI to Recirculation Loop Valve 1-LP-9B Failed to Open Electrically After Being Manually Opened.Declutch Fork & Clutch Repositioned
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000245/LER-1993-010-01, :on 930917,determined Unit 1 Has No Automatic Reactor Recirculation Pump Runback Circuitry in Place.Caused by Incorrect Analysis Assumption in Original Plant Accident analysis.Re-analysis Performed |
- on 930917,determined Unit 1 Has No Automatic Reactor Recirculation Pump Runback Circuitry in Place.Caused by Incorrect Analysis Assumption in Original Plant Accident analysis.Re-analysis Performed
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000336/LER-1993-010-02, :on 931029,unit Failed to Perform post-work ASME Leakage Test on Valve 2-CH-223.Caused by Personnel Error.Leakage Test Repeated & Found Satisfactory |
- on 931029,unit Failed to Perform post-work ASME Leakage Test on Valve 2-CH-223.Caused by Personnel Error.Leakage Test Repeated & Found Satisfactory
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000423/LER-1993-010, :on 930707,reactor Trip Input to Turbine Trip Portion of ESFAS Declared Inoperable Due to Inadequate Surveillance Testing.Test to Verify Operability Written & Performed |
- on 930707,reactor Trip Input to Turbine Trip Portion of ESFAS Declared Inoperable Due to Inadequate Surveillance Testing.Test to Verify Operability Written & Performed
| 10 CFR 50.73(a)(2)(i) | | 05000245/LER-1993-011, Responds to NRC 981002 Request to Counsel That NNECO Waive Any Assertion of Statue of Limitations for 60-90 Days with Respect to NRC Ability to Initiate Civil Penalty Action Based on Apparent Violation of 10CFR50.59 Re LER 93-0 | Responds to NRC 981002 Request to Counsel That NNECO Waive Any Assertion of Statue of Limitations for 60-90 Days with Respect to NRC Ability to Initiate Civil Penalty Action Based on Apparent Violation of 10CFR50.59 Re LER 93-011-00 | | | 05000336/LER-1993-011-02, :on 931007,EDG B Declared Inoperable Due to Underrated Air Start Solenoid.Caused by Design Replacement Error.Underrated Solenoid Replaced on 931008 W/Solenoid Model 212-630-1F |
- on 931007,EDG B Declared Inoperable Due to Underrated Air Start Solenoid.Caused by Design Replacement Error.Underrated Solenoid Replaced on 931008 W/Solenoid Model 212-630-1F
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000245/LER-1993-011-01, :on 930917,determined That Conditions May Have Existed Where Sfpcs May Have Been Incapable of Maintaining Pool Temp.Caused by Inappropriate Assumptions in Support of SFP Project.Design Basis Documents Revised |
- on 930917,determined That Conditions May Have Existed Where Sfpcs May Have Been Incapable of Maintaining Pool Temp.Caused by Inappropriate Assumptions in Support of SFP Project.Design Basis Documents Revised
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1993-011, :on 930731,MSSV Lift Setpoint Drift Occurred Due to Unknown Cause.Reduced Setpoint for Power Range Neutron Flux High Trip to 10% |
- on 930731,MSSV Lift Setpoint Drift Occurred Due to Unknown Cause.Reduced Setpoint for Power Range Neutron Flux High Trip to 10%
| 10 CFR 50.73(a)(2)(i) | | 05000336/LER-1993-012, :on 930524,turbine & Reactor Tripped During Mussel Cook (Thermal Backwash) Due to Lack of Heat Removal Capabilities from Main Generator Stator Water Cooling Sys. Installed Thermoconductivity Filler |
- on 930524,turbine & Reactor Tripped During Mussel Cook (Thermal Backwash) Due to Lack of Heat Removal Capabilities from Main Generator Stator Water Cooling Sys. Installed Thermoconductivity Filler
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000245/LER-1993-012-02, :on 930917,components Supporting Safety Related Function of FWCI Sys Were Not Category 1 or Seismically Qualified.Caused by Failure to Incorporate Sep. Upgrade Mepl for Millstone Unit 1 |
- on 930917,components Supporting Safety Related Function of FWCI Sys Were Not Category 1 or Seismically Qualified.Caused by Failure to Incorporate Sep. Upgrade Mepl for Millstone Unit 1
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1993-012-01, :on 930805,discovered Train a of SWS Inoperable Due to Inadequate Work Planning by Const Dept.Removed Plywood & Performed Evaluation |
- on 930805,discovered Train a of SWS Inoperable Due to Inadequate Work Planning by Const Dept.Removed Plywood & Performed Evaluation
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | | 05000423/LER-1993-013-01, :on 930901,determined Reactor at Power Permissive Bistable Set to Incorrect Value.Caused by TS W/ Mutually Exclusive Conditions for P-10 Interlock.Tss Revised |
- on 930901,determined Reactor at Power Permissive Bistable Set to Incorrect Value.Caused by TS W/ Mutually Exclusive Conditions for P-10 Interlock.Tss Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | | 05000336/LER-1993-013, :on 930603,noted That Main Turbine Generator EHC Sys Caused an Increase in Pressurizer Pressure,Resulting in Reactor Trip,Due to Closing of Intercept & Cv.Operators Performed EOP & Sys Performed as Expected |
- on 930603,noted That Main Turbine Generator EHC Sys Caused an Increase in Pressurizer Pressure,Resulting in Reactor Trip,Due to Closing of Intercept & Cv.Operators Performed EOP & Sys Performed as Expected
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000245/LER-1993-013, :on 920330,discovered That One of Two RB Ventilation Exhaust Isolation Valves Failed to Go Fully Closed When Given Isolation Signal.Caused by Minor Valve Misalignment.Valve Realigned |
- on 920330,discovered That One of Two RB Ventilation Exhaust Isolation Valves Failed to Go Fully Closed When Given Isolation Signal.Caused by Minor Valve Misalignment.Valve Realigned
| 10 CFR 50.73(a)(2)(i) | | 05000245/LER-1993-014-02, :on 930923,potential Uninhabitability of Control Room Occurred.Caused by Deficiency in Standby Gas Treatment.Openings Plugged to Preclude Potential Discharge of Radioactivity |
- on 930923,potential Uninhabitability of Control Room Occurred.Caused by Deficiency in Standby Gas Treatment.Openings Plugged to Preclude Potential Discharge of Radioactivity
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1993-014-01, :on 930903,determined That Delayed Start of Train a Auxiliary Bldg Fan During Testing Due to Inherent Design Characteristics of Flow Switch.Design Changed to Provide Uninterruptible Source of Power |
- on 930903,determined That Delayed Start of Train a Auxiliary Bldg Fan During Testing Due to Inherent Design Characteristics of Flow Switch.Design Changed to Provide Uninterruptible Source of Power
| 10 CFR 50.73(a)(2)(i) | | 05000423/LER-1993-014, :on 930903,train a of Supplemental Leak Collection & Release Sys Was Inoperable Due to Lack of Understanding of Flow Switch Response to Loss of Power Event.Formed Task Force & Design Changed |
- on 930903,train a of Supplemental Leak Collection & Release Sys Was Inoperable Due to Lack of Understanding of Flow Switch Response to Loss of Power Event.Formed Task Force & Design Changed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) |
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