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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEARML20198Q4391997-11-0303 November 1997 LER 97-S001-00:on 971003,vital Area Barrier Gratings in Main Steam Valve Bldg Floor Not Secured.Caused by Inadequate Verification/Validation Process for Ensuring Vital Area Boundary Integrity.Security Instructions Will Be Revised ML20217F2321997-09-29029 September 1997 LER 970934-01:on 970918,RHR Pump Suction Relief Valve Setpoint Not IAW TS Was Determined.Caused by Insufficient Configuration Control.Declared B Train RHR Valve Inoperable, Recalibrated to Correct Setpoint & Declared Operable 05000336/LER-1997-003, Corrected Page One to LER 97-003-01:on 961216,discovered Discrepancy in Plant Procedure Utilized to Perform Periodic Insp of Fire Protection Sys Smoke Detectors.Caused by Failure to Properly Incorporate Ts.Ts Partially Revised1997-04-15015 April 1997 Corrected Page One to LER 97-003-01:on 961216,discovered Discrepancy in Plant Procedure Utilized to Perform Periodic Insp of Fire Protection Sys Smoke Detectors.Caused by Failure to Properly Incorporate Ts.Ts Partially Revised 05000336/LER-1993-0191993-09-10010 September 1993 LER 93-019-00:on 930812,reactor Trip Occurred Due to Low SG Level.Conducted Shift Briefing of Event to Operating Shift While Assuming Watch.Briefing Included Listed Requirements for Subsequent Specific start-up.W/930910 Ltr 05000423/LER-1993-0121993-09-0303 September 1993 LER 93-012-00:on 930805,piece of Plywood Discovered in Train a of Sws.Caused by Inadequate Work Control During 1991 Outage to Repair Sws.Plywood Removed & Increased Attention Being Paid to Matl Exclusion in Critical sys.W/930903 Ltr 05000336/LER-1993-0181993-09-0303 September 1993 LER 93-018-00:on 930805,letdown Manual Isolation Valve 2-CH-442 Developed Leak Which Exceeded TS Limits.Root Cause Has Not Been Determined.Valve Replaced & All Code Required Post Intallation Tests Successfully completed.W/930903 Ltr 05000336/LER-1993-0081993-09-0202 September 1993 LER 93-008-01:on 930505,declared Charging Pumps Inoperable Due to Low Control Power Voltage.Established Administrative Controls & Installed Interposing Relay within C Charging Pump Control circuit.W/930902 Ltr 05000423/LER-1993-0041993-08-31031 August 1993 LER 93-004-01:on 930331,RT Occurred Due to electro-hydraulic Control Power Supply Failure.Replaced Faulty Power Supply. W/930831 Ltr 05000423/LER-1993-0111993-08-30030 August 1993 LER 93-011-00:on 930731,MSSV Lift Setpoint Drift Occurred Due to Unknown Cause.Reduced Setpoint for Power Range Neutron Flux High Trip to 10%.W/930830 Ltr 05000336/LER-1993-0161993-08-27027 August 1993 LER 93-016-00:on 930729,reportability Determination Made Re Analysis for Boron Dilution Event.Caused by Inadequate Review of Results of Boron Dilution in Relation to Plant Operating Conditions.Boron Results revised.W/930827 Ltr 05000336/LER-1993-0141993-08-13013 August 1993 LER 93-014-00:on 930714,discovered Surveillances Procedures Had Not Been Performed within Specified Time Intervals Due to Insufficent Planning.Missed Surveillances Immediately performed.W/930813 Ltr 05000423/LER-1990-0261990-07-25025 July 1990 LER 90-026-00:on 900625,Train B Containment Hydrogen Monitor Failed Calibr Surveillance.Caused by Inadequate Engineering Interface Between Facilities Design Organization.Caution Tags Placed on Main Control Board indicators.W/900725 Ltr 05000423/LER-1990-0251990-07-20020 July 1990 LER 90-025-00:on 900616,hourly Vice Fire Watch Maintained During Condition That Required Continuous Fire Watch Be Established.Caused by Personnel Error.Continuous Fire Watch Established & Personnel Involved counseled.W/900720 Ltr 05000336/LER-1990-0101990-07-20020 July 1990 LER 90-010-00:on 900621,door Identified in Configuration Not Consistent W/Bechtel Design Drawings During High Energy Line Review.Caused by Lack of Knowledge of Requirements.Double Door reinforced.W/900720 Ltr 05000423/LER-1990-0241990-07-20020 July 1990 LER 90-024-00:on 900620,control Bldg Isolations Occurred Due to Radiation Monitor Detector Degradation.Other Equipment Not Affected.Degradation Caused Radiation Levels to Exceed High Alarm Setpoint.Detector replaced.W/900720 Ltr 05000336/LER-1990-0081990-07-18018 July 1990 LER 90-008-00:on 900620,determined That Grab Sample of Unit Stack Gas Not Taken.Caused by Lack of Communication Between Personnel.Grab Sample Obtained & analyzed.W/900718 Ltr 05000336/LER-1987-0091990-07-18018 July 1990 LER 87-009-02:on 870902,unit Experienced Automatic Reactor Trip Due to Low Steam Generator Level.Caused by Valve Stem Slightly Loose from Valve Plug.Damaged Stem/Plug Assembly replaced.W/900718 Ltr 05000423/LER-1990-0211990-07-16016 July 1990 LER 90-021-00:on 900607,integrated Leak Rate Test Supply & Exhaust Valve 3HVU*V5 Discovered Unlocked & Opened.Caused by Failure to Use Applicable Procedure for Nonroutine Evolution.Valve Closed & locked.W/900716 Ltr 05000336/LER-1990-0091990-07-16016 July 1990 LER 90-009-00:on 900617,inadvertent Partial Actuation of Train B of Enclosure Bldg Filtration Sys Occurred.Root Cause Not Determined.No Corrective Actions Recommended Until Further Testing & Troubleshooting performed.W/900716 Ltr 05000423/LER-1990-0221990-07-16016 July 1990 LER 90-022-00:on 900618,discovered That Hourly Fire Watch Patrol Had Not Been Established in Battery 4 Inverter Room. Caused by Procedural Deficiency.Hourly Fire Watch Established.Procedures revised.W/900716 Ltr 05000423/LER-1990-0191990-07-0303 July 1990 LER 90-019-00:on 900606,automatic Reactor Trip from Negative Flux Rate Signal Occurred Due to Dropped Control Rod.Caused by Broken Connection in Stationary Coil Power Cable for Rod. Special EOP Performed & Connector replaced.W/900703 Ltr 05000000/LER-1986-022, Partially Deleted LER 86-022-02:on 861018,potential Undetected Access Into Vital Area Discovered.Caused by Use of Incorrect Procedure.Card Reader Replaced & Tested to Ensure Proper Operation1987-02-20020 February 1987 Partially Deleted LER 86-022-02:on 861018,potential Undetected Access Into Vital Area Discovered.Caused by Use of Incorrect Procedure.Card Reader Replaced & Tested to Ensure Proper Operation 05000000/LER-1986-030, Partially Deleted LER 86-030-00:on 861211,unauthorized Opening Into Protected Area Discovered.Caused by Area Not Properly Identified as Area for Security Concern.Signs Posted1986-12-16016 December 1986 Partially Deleted LER 86-030-00:on 861211,unauthorized Opening Into Protected Area Discovered.Caused by Area Not Properly Identified as Area for Security Concern.Signs Posted 05000000/LER-1986-026, Partially Deleted LER 86-026-00:on 861124,vital Area Door Discovered W/O Alarm Capability.Caused by Personnel Error. Secutiry Officer in Question Terminated & Function of Administrative Sergeant Reviewed1986-12-0101 December 1986 Partially Deleted LER 86-026-00:on 861124,vital Area Door Discovered W/O Alarm Capability.Caused by Personnel Error. Secutiry Officer in Question Terminated & Function of Administrative Sergeant Reviewed 05000000/LER-1986-023, Partially Deleted LER 86-023-01:on 861023,unauthorized Access Into Vital Area Door Discovered.Caused by Card Reader Malfunction.Malfunctioning Card Reader Replaced.Cause Still Under Investigation1986-11-21021 November 1986 Partially Deleted LER 86-023-01:on 861023,unauthorized Access Into Vital Area Door Discovered.Caused by Card Reader Malfunction.Malfunctioning Card Reader Replaced.Cause Still Under Investigation 05000000/LER-1986-024, Partially Deleted LER 86-024-00:on 861113,attempted Introduction of Unauthorized Weapon Into Protected Area Discovered.Caused by Personnel Attempt to Enter Plant W/ Concealed Gun.Personnel Denied Facility Access1986-11-18018 November 1986 Partially Deleted LER 86-024-00:on 861113,attempted Introduction of Unauthorized Weapon Into Protected Area Discovered.Caused by Personnel Attempt to Enter Plant W/ Concealed Gun.Personnel Denied Facility Access 05000000/LER-1986-007, Partially Deleted LER 86-007-01:on 860218,loss of Alarm Surveillance Occurred.Caused by Water Leaking Into Cable Due to Heavy Rain.Cable Dried,Leak Repaired & Design Corrected1986-10-0606 October 1986 Partially Deleted LER 86-007-01:on 860218,loss of Alarm Surveillance Occurred.Caused by Water Leaking Into Cable Due to Heavy Rain.Cable Dried,Leak Repaired & Design Corrected 05000000/LER-1986-021, Partially Deleted LER 86-021-00:on 860911,vital Area Doors Failed to Alarm When Tested During Surveillance.Caused by Failure to Report Door Transactions to Host Computer.Central Procesing Unit Board Replaced1986-09-15015 September 1986 Partially Deleted LER 86-021-00:on 860911,vital Area Doors Failed to Alarm When Tested During Surveillance.Caused by Failure to Report Door Transactions to Host Computer.Central Procesing Unit Board Replaced 05000000/LER-1986-020, Partially Deleted LER 86-020-00:on 860812,security Sys Experienced Loss of Power.Caused Withheld.Numerous Failures Experienced Until Machine a Designated as Prime.Procedures to Reboot Computers Revised1986-08-15015 August 1986 Partially Deleted LER 86-020-00:on 860812,security Sys Experienced Loss of Power.Caused Withheld.Numerous Failures Experienced Until Machine a Designated as Prime.Procedures to Reboot Computers Revised 05000000/LER-1986-004, Partially Deleted LER 86-004-01:on 860204,loss of Dynamic Reporting of Alarm Surveillance Occurred.Cause Withheld. Computer Svcs Personnel Will Continue to Monitor Sys for Indicators of Cause1986-06-11011 June 1986 Partially Deleted LER 86-004-01:on 860204,loss of Dynamic Reporting of Alarm Surveillance Occurred.Cause Withheld. Computer Svcs Personnel Will Continue to Monitor Sys for Indicators of Cause 05000000/LER-1986-016, Partially Deleted LER 86-016-00:on 860501,vital Area Door Discovered W/O Alarm Capabilities.Caused by Access Control Security Officer Asleep at Post.Determination to Suspend or Discontinue Employment Being Made1986-05-0606 May 1986 Partially Deleted LER 86-016-00:on 860501,vital Area Door Discovered W/O Alarm Capabilities.Caused by Access Control Security Officer Asleep at Post.Determination to Suspend or Discontinue Employment Being Made 05000000/LER-1986-015, Partially Deleted LER 86-015-00:on 860428,stationary Side of Door Failed to Alarm When Tested.Cause Withheld.Alarm Repaired1986-05-0202 May 1986 Partially Deleted LER 86-015-00:on 860428,stationary Side of Door Failed to Alarm When Tested.Cause Withheld.Alarm Repaired 05000000/LER-1986-014, Partially Deleted LER 86-014-00:on 860421,bomb Threat Received by Security Officer in Security Assembly Room. Cause Not Applicable.Actions Taken to Minimize Station Threat & Investigation Underway1986-04-25025 April 1986 Partially Deleted LER 86-014-00:on 860421,bomb Threat Received by Security Officer in Security Assembly Room. Cause Not Applicable.Actions Taken to Minimize Station Threat & Investigation Underway 05000000/LER-1986-013, Partially Deleted LER 86-013-00:on 860414,vital Area Door W/O Alarm Capability Discovered.Caused by Personnel Error. Personnel Removed from Shift & Vital Area Checked for Unauthorized Personnel W/None Being Found1986-04-18018 April 1986 Partially Deleted LER 86-013-00:on 860414,vital Area Door W/O Alarm Capability Discovered.Caused by Personnel Error. Personnel Removed from Shift & Vital Area Checked for Unauthorized Personnel W/None Being Found 05000000/LER-1986-012, Partially Deleted LER 86-012-00:on 860412,breach Discovered in Protected Area Barrier.Caused by Personnel Error. Personnel Counseled1986-04-17017 April 1986 Partially Deleted LER 86-012-00:on 860412,breach Discovered in Protected Area Barrier.Caused by Personnel Error. Personnel Counseled 05000000/LER-1986-011, Partially Deleted LER 86-011-00:on 860410,vital Area Intrusion Alarm Failure Occurred.Cause of Event Deleted. Alarm & Door Tested Satisfactorily1986-04-15015 April 1986 Partially Deleted LER 86-011-00:on 860410,vital Area Intrusion Alarm Failure Occurred.Cause of Event Deleted. Alarm & Door Tested Satisfactorily 05000000/LER-1986-003, Partially Deleted LER 86-003-00:on 860125,loss of Dynamic Reporting of Vital Area Door Activity Occurred.Caused by Equipment Malfunction.Corrective Action Withheld1986-01-29029 January 1986 Partially Deleted LER 86-003-00:on 860125,loss of Dynamic Reporting of Vital Area Door Activity Occurred.Caused by Equipment Malfunction.Corrective Action Withheld 05000000/LER-1986-002, Partially Deleted LER 86-002-00:on 860117,loss of Alarm Surveillance on Doors Occurred.Caused by Erroneously Listing Officer as Being Posted on Door 398.Processing of Rev to Physical Security Plan Initiated1986-01-23023 January 1986 Partially Deleted LER 86-002-00:on 860117,loss of Alarm Surveillance on Doors Occurred.Caused by Erroneously Listing Officer as Being Posted on Door 398.Processing of Rev to Physical Security Plan Initiated 05000000/LER-1986-001, Partially Deleted LER 86-001-00:on 860105,loss of Dynamic Reporting of Vital Door Activity Occurred.Cause & Corrective Action Completely Deleted1986-01-10010 January 1986 Partially Deleted LER 86-001-00:on 860105,loss of Dynamic Reporting of Vital Door Activity Occurred.Cause & Corrective Action Completely Deleted 05000336/LER-1983-012, Updated LER 83-012/03X-1:on 830322 & 26,charging Pump C Shut Down Due to Lost Oil Pressure.Caused by Failed Integral Oil Pump Drive Coupling.Coupling Repaired1984-03-12012 March 1984 Updated LER 83-012/03X-1:on 830322 & 26,charging Pump C Shut Down Due to Lost Oil Pressure.Caused by Failed Integral Oil Pump Drive Coupling.Coupling Repaired 05000336/LER-1983-020, Updated LER 83-020/01X-1:on 830613,2,557 Degraded Tubes Discovered on Steam Generator Tubing.Cause Undetermined. Tubes W/Flaws Less than + or - 40% Through Wall or Eddy Current Probe Restrications repaired.W/840213 Ltr1984-02-13013 February 1984 Updated LER 83-020/01X-1:on 830613,2,557 Degraded Tubes Discovered on Steam Generator Tubing.Cause Undetermined. Tubes W/Flaws Less than + or - 40% Through Wall or Eddy Current Probe Restrications repaired.W/840213 Ltr 05000336/LER-1983-007, Updated LER 83-007/01T-1:on 830318,nonconservative Safety Analysis Assumption Discovered in Steam Generator Tube Rupture Analysis.Radiological Consequences of Reanalysis Being Analyzed1983-12-0909 December 1983 Updated LER 83-007/01T-1:on 830318,nonconservative Safety Analysis Assumption Discovered in Steam Generator Tube Rupture Analysis.Radiological Consequences of Reanalysis Being Analyzed ML20064F8591978-11-28028 November 1978 /03L-0 on 781115:spent Fuel Pool(Sfp)Ventilation Particulate & Gaseous Setpoints Exceeded Tech Specs Setpoints of Table 3.3-6,items 2.c & 2.d.Caused by Monitor Recalibr W/O Taking Into Account Tech Spec Limit ML20064F1651978-11-21021 November 1978 /03L-0 on 781025:during Oper,Surveillance Test on Channel a Reactor Protec Sys Core Protec Calculator Reveated Sys Ground Traced to Signal for Pressurizer Pressure W/In Containment Boundary.Source Not Known at This Time ML20064E6611978-11-16016 November 1978 /03L-0 on 781024:plant Computer Malfunction Caused CEA Pulse Counting Position to Be in Oper.Cause of Computer Failure Could Not Be Traced ML20064E1501978-11-0606 November 1978 /03L-0 on 781007:daily Tech Spec 4.3.1.1.1.,Table 4.3-1,items 2.a & 2.b,Nuc Pwr Surveillance & Delta-T Pwr Channel Calibr Not Performed Due to Personnel Error. Supervisors Told to Perform Req Surveillance ML20064D6131978-11-0303 November 1978 /03L-0 on 781025:Analysis of Instru Installations Revealed That Two Transmitters Assoc W/Channel a Steam Generator Low Water Lever Were non-seismically Mounted. Channel a SG Was Bypassed.Seismic Brackets Will Be Used ML20064D6011978-11-0101 November 1978 /03L-0 on 781004:during Surveillance Testing, Setpoint for Reactor Protec Sys Reactor Coolant Low Flow Trip on Channel B Was Out of Spec.Setpoint Was Readjusted. Rev Will Req Low Flow Trip Unit Setpoint Be Reset ML20064B8171978-10-0202 October 1978 /03L-0 on 780906:Loss of Methyl Iodide Removal Efficiency for a Ebfs Train. Cause Unknown 1997-09-29
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217P5391999-10-25025 October 1999 Rev 0,Change 1 to Millstone Unit 1 Northeast Utils QA Program ML20217C8721999-10-0606 October 1999 Rev 21,change 3 to MP-02-OST-BAP01, Nuqap Topical Rept, App F & G Only B17896, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With B17894, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With B17898, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216J4341999-09-24024 September 1999 Mnps Unit 3 ISI Summary Rept,Cycle 6 ML20211N8401999-09-0202 September 1999 Rev 21,change 1 to Northeast Utils QA TR, Including Changes Incorporated Into Rev 20,changes 9 & 10 B17878, Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With B17874, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 B17879, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With ML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20211A6561999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2 B17858, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With B17856, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With ML20210J0311999-07-21021 July 1999 Rev 20,Change 10 to QAP 1.0, Organization ML20210E5931999-07-19019 July 1999 Revised Page 16 of 21,to App F of Northeast Util QA Program Plan ML20210C5911999-07-15015 July 1999 Revised Rev 20,change 10 to Northeast Util QA Program TR, Replacing Summary of Changes ML20210A0411999-07-15015 July 1999 Rev 20,change 10 to Northeast Util QA Program Tr B17814, Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start1999-07-12012 July 1999 Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start ML20209D1881999-07-0101 July 1999 Rev 20,change 9 to Northeast Util QA Program Tr ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20211A6751999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level & Operating Data Rept ML20196A8451999-06-30030 June 1999 Post Shutdown Decommissioning Activities Rept ML20209J0541999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Unit 2 B17830, Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With ML20196K1791999-06-30030 June 1999 Addendum 6 to Millstone Unit 2 Annual Rept, ML20196J1821999-06-30030 June 1999 Rev 21,Change 0 to Northeast Utilities QAP (Nuqap) Tr B17833, Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With ML20195H1011999-06-11011 June 1999 Rev 20,change 8 to Northeast Utilities QAP (Nuqap) TR ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20211A6631999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level,Operating Data Rept & Unit Shutdowns & Power Reductions B17808, Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With ML20211B7351999-05-31031 May 1999 Cycle 7 Colr B17804, Monthly Operating Rept for May 1999 for Mnps,Unit 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 2.With B17807, Monthly Operating Rept for May 1999 for Mnps,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 1.With ML20209J0661999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Unit 2 ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206J8351999-05-0707 May 1999 Rev 20,Change 7 to QAP-1.0, Northeast Utls QA Program (Nuqap) Tr ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 B17782, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With ML20205R3531999-04-30030 April 1999 Addendum 4 to Annual Rept, B17775, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With ML20205K6141999-04-30030 April 1999 Non-proprietary Version of Rev 2 to Holtec Rept HI-971843, Licensing Rept for Reclassification of Discharge in Millstone Unit 3 Spent Fuel Pool ML20206E2971999-04-30030 April 1999 Rev 1 to Millstone Nuclear Power Station,Unit 2 COLR - Cycle 13 B17777, Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with ML20205Q5891999-04-0909 April 1999 Rev 20,change 6 to QAP-1.0,Northeast Utils QA Program TR ML20205R8751999-04-0909 April 1999 Provides Commission with Staff Assessment of Issues Related to Restart of Millstone Unit 2 & Staff Recommendations Re Restart Authorization for Millstone Unit 2 ML20206T3991999-03-31031 March 1999 First Quarter 1999 Performance Rept, Dtd May 1999 B17747, Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With 1999-09-30
[Table view] |
Text
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NRcf oRM 366' U.S. NUCLEAR RLGuLAloRY CoMMibsloN Arraovto DV owe too stbo ono4 le 96) B AP'RE8 04!80'88 l '
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'l"g.,M.',l?t',, n LICENSEE EVENT REPORT (LER)
(See reverse for required number of L mw=mmm,a'I"b'd'Nd g,'t 'cJ' lt,",*,','g.m,a na* eg-
, gag digits / characters for each block)
PCCaLifV hAME (1) DOCktiNUMetHth PAQt(M
- Millstone Nuclear Power Station Unit 3 05000423 1 of 4 l
l 11f4E 64) l Residual Heat Removat Pump Suction Relief Valve Sotpoint Not in Accordance With Technical Specifications EVENT DATE (s) LLR NUMBER (6) REPORT DATE 17) o THER F ACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR stouENTIAL Revision MONTH DAY YEAR # Aclu 1Y NAME DOC &$ 1 NVMatM NUMBER NUMDER 09 18 90 96 - 034 - 01 09 29 97 l oPERATINo D THis REPORT IS SUDMITTED PURSUANT to THE REQUIREMENTSoF lu cFR 61 (CheCit one or more) (11)
I MODE (9) 20.2201(ts) 20.2203(aH2Hv) X; 60.73(aH2HI) bO.73(aH2Hvhi)
POWER. 000 20.2203(aH1) 20.2203(aH3Hil 60.73(aH2Hii) 60,73(aH2Hz)
~"
LEVEL (10) 20.2203(sH2Hil 20.2203(aH3Hn) bM3(aH2Hin) 73.71 20.2203(eH2Hn) 20.2203(aH4) 60.73(aH2Hiv) OTHER 20.2203(aH2 Haul 60.36(CH1) 60.73(aH2Hv) 20.2203(aH_2Hev) bO 36(cH2) 60.73(aH2Hvia) l gPgcg6n,Atget bei6w
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LICENSEE CONTACT FoR THIS LERi12)
NAMt TitlPHONE NUMatR sttictuce Ases Codel David A. Smith, MP3 Nuclear Licensing Manager (860)437 6840 COMPLETE ONE LINE FOR EACH COMPONENT FAILURF DESCltl8ED IN THis REPORT (13)
COUSE BY51EM COMPONt N T MANUf ACTURER HLPOH1 ABLE CAU$t $YSTEM COMPONt NT MANUF ACTURt R ht PQHI AHtt TO NPROS 10 NPRDS SUPPLEMENTAL REPORT EXPECTEDl14) EXPECTED MONTH DAY YEAR i X YES (if yes, complete EXPECTED sVBMISsioN DATL),
No suSMISSloN 11 22 97 DATE (15)
ADETRAct (L6mit to 1400 spaces,6.e., appromlmately16 single.spacedtypewnttenhnes) (16)
On September 18,1996 with the plant in Mode 5, during a review conducted by plant engineering pers0nnel, it was dCtermined that the actual setpoint for the Residual Heat Removal (RHR) pump suction relief valves was not in accordance with the requirements of Technical Specifications (TS). Contrary to the TS limit of 450 psig, the actuallift pressure for the RHR pump suction relief had been set at 440 psig. This condition was reported on October 18,1996 pursuant to 10CFR50.73(a)(2)(1)(B) as an operation or condition prohibited by the plant's TS, On August 29,1997 with the plant in Modo 5, while performing a review of RHR suction relief valve surveillance test procedures, it was discovered that previous RHR relief va've calibrations may have been performed improperly resulting in the B train RHR relief valve setpoint being outside the tolerance specified within the TS Limiting Condition for Operation. Consequently, this condition is being reported pursuant to 10CFR50.73(a)(2)(i)(B) as any operation or condition prohibited by the plant's TS.
The cause of the September 1996 event was attributed to insufficient configuration control within the design control program. The apparent cause of the August 29,1997, event was inadequate review of test procedures.
As an immediate corrective action for the August 29,1997 event, the B train RHR valve was declared inoperable, recalibrated to the correct setpoint and declared operable. Investigation into the cause of this event is ongoing. The RHR setpoint calculation will be revised to properly incorporate the RHR pump suction relief valve temperature correction for the full temperature range. An evaluation of the RHR relief valve setpoint effect on the RHR piping stress analyses will be performed.
9710090022 970929 PDR ADOCK 05000423; 6 PM l
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NRc f ORM 366A U.s. NUCLEAR REluLAToRY Commission i LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION P ACILITY NAME 11) DOCKET NUMBER (2) LER NVMSER ts) PAoE 13)
YEAR SEQUENTIAL Revision Millstona Nuclear Power Station Unit 3 05000423 NUMBE1 NUMBE R 2 of 4 96 - 034 -
01 1LXT lit more space is newted, vse ed&tionalcopies of NRC form 366A) l1 n
- 1. Descriptlon of Event On September 18,1990 with the plant in Mode 5, during a review conducted by plant engineering personnel, it was det:rmined that the actual setpoint for the Residual Heat Removal (RHRt pump suction relief valves was net in accordance with the requirements of Technical Specii'ication 3 4.9.3 a.2 and 3.4.9.3 a 3. Technical Specifications (TS) require that the RHR pump suction relief be set at 450 pounds per square inch gauge (psig)in order to provide adequate over pressure p'rotection when the temperature of any Reactor Coolant System (RCS) cold leg is less than
< 350 degrees Fahrenheit ( F). Contrary to this requirement the actuallift pressure for the RHR pump suction relief had been set at 440 psig. This condition was reported on October 18,1990 pursuant to 10CFR50.73(a)(2)(i)(B) as an operation or condition prohibited by the plant's Technical Specifications.
On July 10,1997. License Amendment 143 was incort wated resulting in an RHR relief valve satpoint of 2 426.8 psig and s 453.2 psig. On August 29,1997, with the pl% in Mode 5, while performing a review of RHR suction relief valve surveillance test procedures, it was discovered that previous RHR relief valve calibrations may have been performed improperl,. This condition was not identified during reviews performed in conjunction with implementation of the license amendment.
Th3 valve vendor requires a setpoint temperature correction factor of +3% when valves are used in 250' F or higher r,cryice and tested / set at ambient temperatures. This is to compensate for changes in spring loading. At MP3, the valves have always been tested and calibrated in this manner. At cold conditions (<250* F), the vendor's +3%
t:mperature correction factor no longer applies. Since this relief valve must serve in both temperature ranges, this 3 cffectively narrows the setpoint acceptance tolerance to 0%, +3% or (440 to 453.2 psig). The actual B train RHR relief valve setpoint was 455 psig and not within the Limiting Condition for Operation (LCO) tolerance. Consequently, this condition is being reported pursuant to 10CFR50.73(a)(2)p)(B) as any operation or condition prohibited by the plant's Technical Specifications.
II, Cause of Event On March 26,1985 during the construction of the unit, the Architect / Engineer (A/E) issued a design change, which lowered the setpoint for the RHR suction relief valve from 450 psig to 440 ps:g. This design change did not specify that a technical specification change was required. The design change also resulted in the issuance of a setpoint calculation change on April 29,1985 which confirmed the change from 450 psig to 440 psig. Subsequently, the plant M:intenance Department established the relief valve test program in accordance V,lth the requirements imposed by American Society Of Mechanical Engineers (ASME). In implementing the relief valve test program, reliance was placed on the information contained in setpoint calculations and design changes when establishing the appropriate values for t; sting of valves contained within the program.
The apparent cause of the August 29,1097, event involving the identification of incorrect previous RHR suction relief valve calibrations is inadequate review of test procedures. This condition was not identified during the reviews performed in conjunction with implementation of a TS license amendment to revise the RHR relief valve setpoint.
NRC FORM 366A 44-95)
NRc f ORM 366A U.s. NUCLEAR RE LUL AToHY COMMISSION UCENSEE EVENT REPORT (LER)
TEXT CONTINUATION 7 AclLITV NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAoE (3)
YLAH SLoulNTIAL ftLVISloN Millstone Nuclear Power Station Unit 3 05000423 wtaer 1 NUMBER 3 of 4 90 -
034 -
01 TLKT (11more space os required use additionnicopies of NRC form 366M (11) 111. Analysis of Event The unit has operated using the 440 psig setpoint as required by the original A/E design change and the associated setpoint calculation. The 440 psig setpoint is the fechnically correct setpoint for the RHR suction relief valves to ensure cv;r pressure protection for the RHR piping in accordance with /sSME requirements. Subsequent relief valve capacity calculations were based on the 440 psig setpoint. Over pressure protection of RHR piping and Low Temperature Over j pressure / Cold Over Pressure Protection System (LTOP/COPPS) requirements also f at i utilized the 440 psig setpoint for calculations performed following the initial design change.
Fcr the Augus' 1997 event, the ability of the RHR relief valves to function as a Cold Over Pressure Protection (COPPs) r:12f valve % demonstrated in an engineering calculation. With the relief valves set to the TS values the maximum I
reactor csolant system pressure is $47 psig which is below the Appendix G overpressure limit of 558 psig.
Consequently, the maximum pressure limit of the reactor vessel was not challenged as a result of the TS setpoint being exceeded by 2 psig. Preliminary evaluation indicates that the pipe stresses within the RHR System are acceptable.
This report will be supplemented based on the results of the final evaluation.
Based on the preliminary evaluation, the over pressure protection functions were not compromised as a result of the reIZf valve exceeding the TS setpoint, the safety significance was minimal and there were no adverse safety consequences as a result of the event.
IV. Corrective Action As a result of the September 18,1996 event, a Technical Specifications Change was implemented on July 10,1997 that revised the setpoint value identified in Technical Specifications 3.4 9.3.a 2 and 3.4.9.3 a.3 from 450 psig to 2 426.8 psig and s 453.2 psig.
As an immediate corrective action for the August 29,1997 event, the B train HHR was declared inoperable. After correcting the surveillance testing procedure to take into account the valve's hot / cold settings (-0%, +3%) and gauge accuracies the valve was calibrated to the correct setpoint.
The following corrective actions will be performed:
- 1. Investigation into the cause of this event is ongoing. A supplement to this report will be submitted based on the results of this investigation prior to entry into Mode 4.
- 2. The setpoint calculation will be revised to properly incorporate the RHR pump suction relief valve temperature correction for the full temperature range prior to entry into Mode 4.
3, An evaluation of the RHR relief valve setpoint effect on the RHR piping stress analyses will be performed prior to entry into Mode 4.
V. Additional Information None NRC FOS 360A (4-95)
wnc fonwi[shA U.s. NUCLEAR REIULATcRY Commission LICENSEE EVENT REPORT (LER) )
TEXT CONTINUATION l FAclLITY NAME 11) DOCKET NUMsER (2) LER NUMBER (6) PAGE (3)
YEAR SEQUENilAL RLvlSION Millstone Nuclear Power Station Unit 3 05000423 NUMBH NUMBER 4 of 4 96 - 034 -
01 ,
TEKT illmore spaceis required. use addalonalcopies of NRC /orm .166As t11)
Similar Events Listed below are historical LERs whose causes can be attributed to insufficient configuration control within the design control program. Many of these events were identified as a result of the Configuration Management Review Process.
LER 96-007-00 Containment Recirculation Spray, Quench Spray, and Safety injection System Outside Design Basis Due to Design Errors LER 96-009-02 Inoperable Shutdown Margin Monitors from Low Count Rate, Due to inadequate Design Control LER 06-013-00 Residual Heat Removal System Design Deficiency Due to Non-conservative Original Design Assumption LER 96-026-02 Non-Conservative Primary Grade Water Flow Rates Used in Boron Dilution Safety Analysis LER 97-003 00- Potential For Recirculation Spray System (RSS) Piping Failure Due To RSS Pump Stopping And Restarting During Accident Conditions LER 97-015-00 Potential Vortexing of Recirculation Spray System Pumps LER 97-02100 Defective Design of RSS Expansion Joint Tie Rod Assembly LER 97 028-00 PotentialLoss of Net Positive Suction Head for Recirculation Spray System Pumps LER 97-029-00 Design Basis Concern on SGTR Analysis for MSPRBV .
LER 97-03100 RHR Valve Low Pressure Open Permissive Bistable Setting Set Non-Conservatively LER 97 035-00 Potential Nonconservatismfor Steam GeneratorWater Level Low Low Trip Setpoint Due to PMA Term Uncertainties LER 97 046-00 Containment Recirculation Spray System Cubicle Flood Potential Manuf acturer Data Ells System Code R Isid ual H e at Removal (PWR) . .... .. ... .. .. . . ... . .. . . ....... . . .... ... ... ..B P 4
Ells Component Code V ci v e , R e li e f . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . R V I
l NGC FORM 366A 14 9H -
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