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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000361/LER-1999-005-01, :on 990831,loss of Physical Separation in Control Room,Occurred.Caused by Personnel Error.Creacus Train a Was Returned to Standby on 9908311999-09-23023 September 1999
- on 990831,loss of Physical Separation in Control Room,Occurred.Caused by Personnel Error.Creacus Train a Was Returned to Standby on 990831
05000206/LER-1999-001-02, :on 990808,unattended Security Weapon Was Discovered Inside Pa.Caused by Posted Security Officer Falling Asleep.Officer Was Relieved of Duties,Pa Access Was Removed & Officer Was Placed on Investigatory Suspension1999-08-31031 August 1999
- on 990808,unattended Security Weapon Was Discovered Inside Pa.Caused by Posted Security Officer Falling Asleep.Officer Was Relieved of Duties,Pa Access Was Removed & Officer Was Placed on Investigatory Suspension
05000361/LER-1999-004-01, :on 990708,automatic Tgis Actuation Occurred. Caused by Small Leak in Suction Side of Tgis Train a Sample Pump.Small Leak Repaired1999-08-0606 August 1999
- on 990708,automatic Tgis Actuation Occurred. Caused by Small Leak in Suction Side of Tgis Train a Sample Pump.Small Leak Repaired
05000362/LER-1999-005, :on 990630,discovered LTOP Sys Relief Valve Setpoint Was Higher than Allowed by Ts.Cause Indeterminate. Subject Valve Will Be Disassembled & Inspected to Determine Caused of High Setpoint.With1999-07-28028 July 1999
- on 990630,discovered LTOP Sys Relief Valve Setpoint Was Higher than Allowed by Ts.Cause Indeterminate. Subject Valve Will Be Disassembled & Inspected to Determine Caused of High Setpoint.With
05000362/LER-1999-006, :on 990623,EDG 3G003 Was Inadvertently Made Inoperable.Caused by Operators Aligning EDG to Inoperable Automatic Voltage Regulator.Licensee Will Revise Process of Locating Tags.With1999-07-26026 July 1999
- on 990623,EDG 3G003 Was Inadvertently Made Inoperable.Caused by Operators Aligning EDG to Inoperable Automatic Voltage Regulator.Licensee Will Revise Process of Locating Tags.With
05000362/LER-1999-003-01, :on 990513,reactor Manually Tripped Due to Loss of Main Feedwater.Caused by Open Relay Contact in Output of Feedwater Regulation Control Sys.Faulty Relay Was Replaced1999-06-11011 June 1999
- on 990513,reactor Manually Tripped Due to Loss of Main Feedwater.Caused by Open Relay Contact in Output of Feedwater Regulation Control Sys.Faulty Relay Was Replaced
05000362/LER-1999-004, :on 990515,reactor Manually Tripped Due to Feedwater Control Valve Opening.Caused by Faulty Valve Positioner.Faulty Positioner Was Replaced1999-06-11011 June 1999
- on 990515,reactor Manually Tripped Due to Feedwater Control Valve Opening.Caused by Faulty Valve Positioner.Faulty Positioner Was Replaced
05000362/LER-1999-002-01, :on 990328,RWST Outlet Isolation Valve Failed to Open After Being Closed for Testing.Caused by Degradation of Valve.Rwst Oulet Valve Was Repaired.With1999-05-20020 May 1999
- on 990328,RWST Outlet Isolation Valve Failed to Open After Being Closed for Testing.Caused by Degradation of Valve.Rwst Oulet Valve Was Repaired.With
05000362/LER-1999-001-01, :on 990211,TS 3.0.3 Entered Due to Both Chilled Water Trains Being Inoperable.Warm Main Condenser Discharged Water Diverted in Salt Water Cooling (Swc)(Bs) Intake.With1999-03-12012 March 1999
- on 990211,TS 3.0.3 Entered Due to Both Chilled Water Trains Being Inoperable.Warm Main Condenser Discharged Water Diverted in Salt Water Cooling (Swc)(Bs) Intake.With
05000361/LER-1999-002, :on 990208,pressurizer Safety Valves Were Above TS Limit.Caused by Setpoint Drift.Sce Submitted License Amend Application on 980904 Requesting Tolerence Be Changed to +3/-2%.With1999-03-10010 March 1999
- on 990208,pressurizer Safety Valves Were Above TS Limit.Caused by Setpoint Drift.Sce Submitted License Amend Application on 980904 Requesting Tolerence Be Changed to +3/-2%.With
05000361/LER-1999-001, :on 990201,automatic Start of EDG Was Noted. Caused by Workers Closing Breaker 2A0418 by Discharging Closing Springs.Operators Restored SDC in Approx 26 Minutes. with1999-03-0303 March 1999
- on 990201,automatic Start of EDG Was Noted. Caused by Workers Closing Breaker 2A0418 by Discharging Closing Springs.Operators Restored SDC in Approx 26 Minutes. with
05000361/LER-1998-021, :on 980903,train B Ecw Chiller Failed to Start Using CR Start Push Button.Caused by Incorrect Wiring of Switch by Personnel.Wiring Was Corrected & Chiller Was Declared Operable on 9809261998-10-26026 October 1998
- on 980903,train B Ecw Chiller Failed to Start Using CR Start Push Button.Caused by Incorrect Wiring of Switch by Personnel.Wiring Was Corrected & Chiller Was Declared Operable on 980926
05000361/LER-1998-020, :on 980806,determined That Ecw Sys Was Inoperable.Caused by Faulty Temp Control Unit.Temp Control Unit Was Replaced & Chiller Performed Satisfactorily1998-10-26026 October 1998
- on 980806,determined That Ecw Sys Was Inoperable.Caused by Faulty Temp Control Unit.Temp Control Unit Was Replaced & Chiller Performed Satisfactorily
05000361/LER-1998-004-01, :on 980211,diesel Fuel Oil Particulates - ASTM Test Methods Yield Varying Results Were Received.Caused by Unexpected Variations Obtained from Different Test Methods. Fuel Oil Filtered & Confirmed by Reanalysis1998-09-0101 September 1998
- on 980211,diesel Fuel Oil Particulates - ASTM Test Methods Yield Varying Results Were Received.Caused by Unexpected Variations Obtained from Different Test Methods. Fuel Oil Filtered & Confirmed by Reanalysis
05000361/LER-1998-011, :on 980617,determined That Setpoints for High Log Power Bypass Automatic Removal Had Not Been Verified IAW Ts.Caused by Log Power Not Satisfying TS as Written.Utils Investigation If Ongoing & LER Will Be Revised by 9809301998-07-17017 July 1998
- on 980617,determined That Setpoints for High Log Power Bypass Automatic Removal Had Not Been Verified IAW Ts.Caused by Log Power Not Satisfying TS as Written.Utils Investigation If Ongoing & LER Will Be Revised by 980930
05000206/LER-1998-004, :on 980323,safeguards Drawing Was Inappropriately Decontrolled.Caused by Personnel Error. Revised Procedure for Decontrolling SI & Has Established New Detailed Process for SCE to More Effectively Control SI1998-07-10010 July 1998
- on 980323,safeguards Drawing Was Inappropriately Decontrolled.Caused by Personnel Error. Revised Procedure for Decontrolling SI & Has Established New Detailed Process for SCE to More Effectively Control SI
05000361/LER-1996-012, :on 960226,condensate Storage Tank Outside Design Basis Occurred.Caused by Several Mechanisms for Loss of Water Vol from T-120.Procedures Revised1998-06-29029 June 1998
- on 960226,condensate Storage Tank Outside Design Basis Occurred.Caused by Several Mechanisms for Loss of Water Vol from T-120.Procedures Revised
05000361/LER-1998-009, :on 980428,discovered That Steps in Aoi to Isolate Tank Following Operating Bases Earthquake Had Been Inadvertently Deleted in Aug 1996.Caused by Individual Error.Event Reviewed W/Individual Involved1998-06-29029 June 1998
- on 980428,discovered That Steps in Aoi to Isolate Tank Following Operating Bases Earthquake Had Been Inadvertently Deleted in Aug 1996.Caused by Individual Error.Event Reviewed W/Individual Involved
05000361/LER-1998-010, :on 980526,post-accident Cleanup Units Trains Were Declared Inoperable.Unit Concluded Condition May Be Reportable Under 10CFR50.73(a)(2)(i) for Operation During Past Refueling Outages.Ler Will Be Revised by 9808281998-06-29029 June 1998
- on 980526,post-accident Cleanup Units Trains Were Declared Inoperable.Unit Concluded Condition May Be Reportable Under 10CFR50.73(a)(2)(i) for Operation During Past Refueling Outages.Ler Will Be Revised by 980828
05000361/LER-1986-036, :on 860619,line Voltage Regulators Caused Vital Buses to Be Inoperable.Caused by Procedural Discrepancy. Revised Procedure SO23-II-11.1841998-06-0606 June 1998
- on 860619,line Voltage Regulators Caused Vital Buses to Be Inoperable.Caused by Procedural Discrepancy. Revised Procedure SO23-II-11.184
05000361/LER-1996-012, :on 960229,discovered That CST Was Outside Design Basis.Cause Under Investigation.Compensatory Measures Were Put in Place to Administratively Increase Tanks Water Volume & to Procedularize Operator Actions1998-05-29029 May 1998
- on 960229,discovered That CST Was Outside Design Basis.Cause Under Investigation.Compensatory Measures Were Put in Place to Administratively Increase Tanks Water Volume & to Procedularize Operator Actions
05000361/LER-1998-009, :on 980429,discovered That CST Was Outside Design Basis Due to Procedure Error.Caused by Individual Error.Replaced Steps That Had Been Inadvertently Deleted from Aoi1998-05-29029 May 1998
- on 980429,discovered That CST Was Outside Design Basis Due to Procedure Error.Caused by Individual Error.Replaced Steps That Had Been Inadvertently Deleted from Aoi
05000361/LER-1998-003, :on 980205,inoperable Valve Occurred Due to Grit in Linestarter Mechanism.Sce Has Been Programmatically Replacing Square D Linestarters1998-04-17017 April 1998
- on 980205,inoperable Valve Occurred Due to Grit in Linestarter Mechanism.Sce Has Been Programmatically Replacing Square D Linestarters
05000361/LER-1998-001, :on 980113,loose Collar Was Noted on Turbine Driven AFW Speed Circuit.Caused by Collar Not Properly Being Tightened at Last Documented Reassembly in 1993.Collar & Plug Were Reassembled1998-04-17017 April 1998
- on 980113,loose Collar Was Noted on Turbine Driven AFW Speed Circuit.Caused by Collar Not Properly Being Tightened at Last Documented Reassembly in 1993.Collar & Plug Were Reassembled
05000361/LER-1998-007, :on 980317,discovered Matl in Containment That Could Become Debris in Emergency Sumps.Caused by Ineffective Program Mgt.Removed Identified Matl & Will Issue Memo to Personnel Emphasizing Containment Cleanliness Maint1998-04-16016 April 1998
- on 980317,discovered Matl in Containment That Could Become Debris in Emergency Sumps.Caused by Ineffective Program Mgt.Removed Identified Matl & Will Issue Memo to Personnel Emphasizing Containment Cleanliness Maint
05000206/LER-1998-003-01, :on 980316,unauthorized Protected Entry Area Entry,Was Determined.Caused by Data Entry Error.Appropriate Collection Site Personnel Were Coached.Computer Data Base Modified1998-04-0808 April 1998
- on 980316,unauthorized Protected Entry Area Entry,Was Determined.Caused by Data Entry Error.Appropriate Collection Site Personnel Were Coached.Computer Data Base Modified
05000361/LER-1998-005, :on 980305,inadequate Voltage to 120 Vac Circuits Due to Calculation Error Occurred.Caused by Personnel Error.Sys Mods Made to Affected Sys to Correct Deficiencies1998-04-0606 April 1998
- on 980305,inadequate Voltage to 120 Vac Circuits Due to Calculation Error Occurred.Caused by Personnel Error.Sys Mods Made to Affected Sys to Correct Deficiencies
05000361/LER-1998-008, :on 980306,4160 Vac Supply Cable Exceeded Ampacity Rating.Caused by Error in Feeder Cable Sizing Calculation Completed by Plant Architect/Engineer. Administrative Restrictions Imposed1998-04-0606 April 1998
- on 980306,4160 Vac Supply Cable Exceeded Ampacity Rating.Caused by Error in Feeder Cable Sizing Calculation Completed by Plant Architect/Engineer. Administrative Restrictions Imposed
05000206/LER-1998-002-01, :on 980219,diesel Fuel Filtration Unit Access Was Not Controlled as Vital Area.Caused by Inadequate Training.Security Personnel Will Be Trained on Concept of Vital Matls1998-03-20020 March 1998
- on 980219,diesel Fuel Filtration Unit Access Was Not Controlled as Vital Area.Caused by Inadequate Training.Security Personnel Will Be Trained on Concept of Vital Matls
05000362/LER-1984-045-01, :on 840719,recognized That Four Iodine Transients Met Reporting Criteria of TS 3.4.7,but Had Not Been Reported.Cause Indeterminate.Nrc Approved TS Amend Which Deleted Reporting Requirement of TS 3.4.7.A1998-03-0303 March 1998
- on 840719,recognized That Four Iodine Transients Met Reporting Criteria of TS 3.4.7,but Had Not Been Reported.Cause Indeterminate.Nrc Approved TS Amend Which Deleted Reporting Requirement of TS 3.4.7.A
05000361/LER-1998-002, :on 980126,reactor Coolant Sys Boundary Leakage Occurred.Caused by Cracking of Inconel 600 Nozzle.Four Nozzles (2TW0139B,2TE0122-4,2PDT0978-1 & 2PDT0978-2) Were Repaired1998-02-25025 February 1998
- on 980126,reactor Coolant Sys Boundary Leakage Occurred.Caused by Cracking of Inconel 600 Nozzle.Four Nozzles (2TW0139B,2TE0122-4,2PDT0978-1 & 2PDT0978-2) Were Repaired
05000361/LER-1998-001-01, :on 980113,turbine Driven Auxiliary Feedwater Pump Speed Circuit Collar Loose Were Noted.Caused by vibration-induced Loosening During Periodic Pump Test Runs. Collar & Plug Were Reassembled1998-02-12012 February 1998
- on 980113,turbine Driven Auxiliary Feedwater Pump Speed Circuit Collar Loose Were Noted.Caused by vibration-induced Loosening During Periodic Pump Test Runs. Collar & Plug Were Reassembled
05000362/LER-1997-003-02, :on 971218,determined That Pressurizer Safety Valve Setpoints Were Out of Tolerance.Caused by Setpoint Drift.Valves Will Be Disassembled,Inspected,Reassembled & Reset by Proper Personnel1998-01-19019 January 1998
- on 971218,determined That Pressurizer Safety Valve Setpoints Were Out of Tolerance.Caused by Setpoint Drift.Valves Will Be Disassembled,Inspected,Reassembled & Reset by Proper Personnel
05000362/LER-1997-004-01, :on 971205,typo in TS Was Found.Caused by Personnel Error.Tendon Surveillance Procedure Correctly Referenced Tendon 88-154 & Not 38-1541998-01-0505 January 1998
- on 971205,typo in TS Was Found.Caused by Personnel Error.Tendon Surveillance Procedure Correctly Referenced Tendon 88-154 & Not 38-154
05000361/LER-1997-016, :on 971202,SONGS Personnel Recognized That Fire Damper SARW504165001FD Was Not in Licensee Controlled Specification Surveillance Procedure.Caused by Cognitive Personnel Error.Occurrence Reviewed W/Appropriate Personnel1998-01-0202 January 1998
- on 971202,SONGS Personnel Recognized That Fire Damper SARW504165001FD Was Not in Licensee Controlled Specification Surveillance Procedure.Caused by Cognitive Personnel Error.Occurrence Reviewed W/Appropriate Personnel
05000206/LER-1997-003-01, :on 970520,SCE Discovered Security Computer Sys Was Out of Svc.Caused by Unit 1 Permanently Shutdown,Unit 2 at 100% Full Power & Unit 3 Shutdown.Computer Sys Was Restored1997-12-22022 December 1997
- on 970520,SCE Discovered Security Computer Sys Was Out of Svc.Caused by Unit 1 Permanently Shutdown,Unit 2 at 100% Full Power & Unit 3 Shutdown.Computer Sys Was Restored
05000206/LER-1997-002-02, :on 971027,discovered That Single Copy of Security Contingency Plan Was Missing.Cause Indeterminate. Revised LER Will Be Submitted by 971219 to Provide Results of Investigation1997-11-25025 November 1997
- on 971027,discovered That Single Copy of Security Contingency Plan Was Missing.Cause Indeterminate. Revised LER Will Be Submitted by 971219 to Provide Results of Investigation
05000361/LER-1997-011, :on 970704,instrumentation Channel 1 Declared Inoperable.Caused by Cognitive Personnel Error.Operator Was Coached in Need for Attention to Detail & Util Revised Procedures1997-08-0505 August 1997
- on 970704,instrumentation Channel 1 Declared Inoperable.Caused by Cognitive Personnel Error.Operator Was Coached in Need for Attention to Detail & Util Revised Procedures
05000361/LER-1997-011, :on 970704,wrong B Sample Was Used for Shutdown Margin Surveillance.Caused by Personnel Error.Revised Procedures for Performing SDM Calculations1997-07-30030 July 1997
- on 970704,wrong B Sample Was Used for Shutdown Margin Surveillance.Caused by Personnel Error.Revised Procedures for Performing SDM Calculations
05000362/LER-1997-002-01, :on 970703,RCS Leakage Occurred in Instrument Thermowell Nozzles.Caused by Primary Water Stress Corrosion Cracking of Alloy 600 Type Matls.Replaced Outer Half of Nozzles W/Inconel 690 Matl1997-07-30030 July 1997
- on 970703,RCS Leakage Occurred in Instrument Thermowell Nozzles.Caused by Primary Water Stress Corrosion Cracking of Alloy 600 Type Matls.Replaced Outer Half of Nozzles W/Inconel 690 Matl
05000361/LER-1997-010, :on 970626,check Valve in Charging Subsystem Failed to Open Completely.Caused by Design Defect.Replaced Faulty Design Valves.Rept Includes 10CFR21 Info1997-07-28028 July 1997
- on 970626,check Valve in Charging Subsystem Failed to Open Completely.Caused by Design Defect.Replaced Faulty Design Valves.Rept Includes 10CFR21 Info
05000361/LER-1997-009, :on 970509,class IE 125 Vdc Battery Surveillance Testing Was Completed on 3 Replaced Batteries, Indicating Apparent Drop in Capacity of Two.Caused by No Requirement to Test.Revised TS Bases1997-06-0505 June 1997
- on 970509,class IE 125 Vdc Battery Surveillance Testing Was Completed on 3 Replaced Batteries, Indicating Apparent Drop in Capacity of Two.Caused by No Requirement to Test.Revised TS Bases
05000362/LER-1997-001-02, :on 970412,four Out of Five RCS Nozzles Leaked During Plant Operation & Fifth Suspected of Leaking.Caused by Crack Through Nozzle in Heat Affected Zone of Partial Penetration Weld.Completed Required Welding1997-05-0909 May 1997
- on 970412,four Out of Five RCS Nozzles Leaked During Plant Operation & Fifth Suspected of Leaking.Caused by Crack Through Nozzle in Heat Affected Zone of Partial Penetration Weld.Completed Required Welding
05000361/LER-1997-006, :on 970319,NRC Noted Some Utils Had Not Been Fully Complying W/Requirements of TS Re Surveillance Testing of Electronic Circuits,Per GL 96-01.Specific Cause of Omission Not Known.Procedures Revised1997-04-18018 April 1997
- on 970319,NRC Noted Some Utils Had Not Been Fully Complying W/Requirements of TS Re Surveillance Testing of Electronic Circuits,Per GL 96-01.Specific Cause of Omission Not Known.Procedures Revised
05000361/LER-1997-008, :on 970304,TS Surveillance of Pressurizer Cooldown Rate Was Missed Because Operator Did Not Recognize That real-time Evaluation Plant Data Was Required.Cooldown Transient Terminated1997-04-18018 April 1997
- on 970304,TS Surveillance of Pressurizer Cooldown Rate Was Missed Because Operator Did Not Recognize That real-time Evaluation Plant Data Was Required.Cooldown Transient Terminated
05000361/LER-1997-005, :on 970319,determined That RCS Leakage Was Through Body of Valve Packing Leakoff Plug Caused by Defect. Defective Plug Confirmed to Be Free of Similar Defects, Removed Head & Ground Smooth1997-04-15015 April 1997
- on 970319,determined That RCS Leakage Was Through Body of Valve Packing Leakoff Plug Caused by Defect. Defective Plug Confirmed to Be Free of Similar Defects, Removed Head & Ground Smooth
05000361/LER-1997-004, :on 970303,discovered Steam Leakage from Reactor Coolant Sys Pressurizer Thermowell.Caused by Primary Water Stress Corrosion Cracking of Alloy 600 Type Materials. Removed & Replaced Nozzle W/Inconel 6901997-04-0202 April 1997
- on 970303,discovered Steam Leakage from Reactor Coolant Sys Pressurizer Thermowell.Caused by Primary Water Stress Corrosion Cracking of Alloy 600 Type Materials. Removed & Replaced Nozzle W/Inconel 690
05000361/LER-1997-003, :on 970225,out of Tolerance Condition Identified During Testing of Pressurizer Safety Valve Setpoints.Caused by Setpoints Drift.Setpoints Bounded by Analysis1997-03-18018 March 1997
- on 970225,out of Tolerance Condition Identified During Testing of Pressurizer Safety Valve Setpoints.Caused by Setpoints Drift.Setpoints Bounded by Analysis
05000361/LER-1997-002, :on 970128,increase in Pressurizer Level Occurred Due to Valve Alignment Error.Npeo Was Temporarily Removed from Duties & Counseled by Mgt1997-03-0707 March 1997
- on 970128,increase in Pressurizer Level Occurred Due to Valve Alignment Error.Npeo Was Temporarily Removed from Duties & Counseled by Mgt
05000206/LER-1997-001-01, :on 970107,security Test/Insp Was Missed.Caused by Individual Responsible for Security Sys Tests/Insp Failing to Ensure Tests Completed.Implemented Required Compensatory Actions1997-03-0606 March 1997
- on 970107,security Test/Insp Was Missed.Caused by Individual Responsible for Security Sys Tests/Insp Failing to Ensure Tests Completed.Implemented Required Compensatory Actions
1999-09-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217B4471999-10-0707 October 1999 Safety Evaluation Supporting Amends 159 & 150 to Licenses NPF-10 & NPF-15,respectively ML20217E3381999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Songs,Units 2 & 3 05000361/LER-1999-005-01, :on 990831,loss of Physical Separation in Control Room,Occurred.Caused by Personnel Error.Creacus Train a Was Returned to Standby on 9908311999-09-23023 September 1999
- on 990831,loss of Physical Separation in Control Room,Occurred.Caused by Personnel Error.Creacus Train a Was Returned to Standby on 990831
ML20212A1471999-09-13013 September 1999 Special Rept:On 990904,condenser Monitor Was Declared Inoperable.Difficulties Encountered During Component Replacement Precluded SCE from Restoring Monitor to Service within 72 H.Alternate Method of Monitoring Was Established ML20211R0571999-09-0909 September 1999 Safety Evaluation Supporting Amends 158 & 149 to Licenses NPF-10 & NPF-15,respectively ML20212A2391999-09-0707 September 1999 Safety Evaluation Supporting Amends 157 & 148 to Licenses NPF-10 & NPF-15,respectively ML20211N0511999-09-0303 September 1999 SER Approving Exemption from Certain Requirements of 10CFR50.44 & 10CFR50 App A,General Design Criterion 41 to Remove Requirements from Hydrogen Control Systems from SONGS Units 2 & 3 Design Basis ML20211Q8201999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Songs,Units 2 & 3. with 05000206/LER-1999-001-02, :on 990808,unattended Security Weapon Was Discovered Inside Pa.Caused by Posted Security Officer Falling Asleep.Officer Was Relieved of Duties,Pa Access Was Removed & Officer Was Placed on Investigatory Suspension1999-08-31031 August 1999
- on 990808,unattended Security Weapon Was Discovered Inside Pa.Caused by Posted Security Officer Falling Asleep.Officer Was Relieved of Duties,Pa Access Was Removed & Officer Was Placed on Investigatory Suspension
ML20211H8621999-08-23023 August 1999 Safety Evaluation Accepting Licensee Requests for Relief RR-E-2-03 - RR-E-2-08 from Exam Requirements of Applicable ASME Code,Section Xi,For First Containment ISI Interval ML20211E9441999-08-19019 August 1999 Safety Evaluation Supporting Amends 156 & 147 to Licenses NPF-10 & NPF-15,respectively ML20211F2211999-08-19019 August 1999 Safety Evaluation Supporting Amends 155 & 146 to Licenses NPF-10 & NPF-15,respectively ML20210P4791999-08-11011 August 1999 COLR Cycle 10 Songs,Unit 3 ML20210P4731999-08-11011 August 1999 COLR Cycle 10 Songs,Unit 2 05000361/LER-1999-004-01, :on 990708,automatic Tgis Actuation Occurred. Caused by Small Leak in Suction Side of Tgis Train a Sample Pump.Small Leak Repaired1999-08-0606 August 1999
- on 990708,automatic Tgis Actuation Occurred. Caused by Small Leak in Suction Side of Tgis Train a Sample Pump.Small Leak Repaired
ML20210Q6521999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Songs,Units 2 & 3 ML20210L2771999-07-30030 July 1999 SONGS Unit 3 ISI Summary Rept 2nd Interval,2nd Period Cycle 10 Refueling Outage U3C10 Site Technical Services 05000362/LER-1999-005, :on 990630,discovered LTOP Sys Relief Valve Setpoint Was Higher than Allowed by Ts.Cause Indeterminate. Subject Valve Will Be Disassembled & Inspected to Determine Caused of High Setpoint.With1999-07-28028 July 1999
- on 990630,discovered LTOP Sys Relief Valve Setpoint Was Higher than Allowed by Ts.Cause Indeterminate. Subject Valve Will Be Disassembled & Inspected to Determine Caused of High Setpoint.With
05000362/LER-1999-006, :on 990623,EDG 3G003 Was Inadvertently Made Inoperable.Caused by Operators Aligning EDG to Inoperable Automatic Voltage Regulator.Licensee Will Revise Process of Locating Tags.With1999-07-26026 July 1999
- on 990623,EDG 3G003 Was Inadvertently Made Inoperable.Caused by Operators Aligning EDG to Inoperable Automatic Voltage Regulator.Licensee Will Revise Process of Locating Tags.With
ML20209G8991999-07-12012 July 1999 Safety Evaluation Supporting Amends 154 & 145 to Licenses NPF-10 & NPF-15,respectively ML20209C9281999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Songs,Units 2 & 3. with 05000362/LER-1999-003-01, :on 990513,reactor Manually Tripped Due to Loss of Main Feedwater.Caused by Open Relay Contact in Output of Feedwater Regulation Control Sys.Faulty Relay Was Replaced1999-06-11011 June 1999
- on 990513,reactor Manually Tripped Due to Loss of Main Feedwater.Caused by Open Relay Contact in Output of Feedwater Regulation Control Sys.Faulty Relay Was Replaced
05000362/LER-1999-004, :on 990515,reactor Manually Tripped Due to Feedwater Control Valve Opening.Caused by Faulty Valve Positioner.Faulty Positioner Was Replaced1999-06-11011 June 1999
- on 990515,reactor Manually Tripped Due to Feedwater Control Valve Opening.Caused by Faulty Valve Positioner.Faulty Positioner Was Replaced
ML20195D3061999-06-0202 June 1999 Safety Evaluation of TR SCE-9801-P, Reload Analysis Methodology for San Onofre Nuclear Generating Station,Units 2 & 3. Rept Acceptable ML20195H5491999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Songs,Units 2 & 3 05000362/LER-1999-002-01, :on 990328,RWST Outlet Isolation Valve Failed to Open After Being Closed for Testing.Caused by Degradation of Valve.Rwst Oulet Valve Was Repaired.With1999-05-20020 May 1999
- on 990328,RWST Outlet Isolation Valve Failed to Open After Being Closed for Testing.Caused by Degradation of Valve.Rwst Oulet Valve Was Repaired.With
ML20207A0211999-05-13013 May 1999 Safety Evaluation Supporting Amends 153 & 144 to Licenses NPF-10 & NPF-15,respectively ML20196L3221999-05-11011 May 1999 SONGS Unit 2 ISI Summary Rept 2nd Interval,2nd Period Cycle-10 Refueling Outage ML20206H2611999-05-0505 May 1999 Part 21 Rept Re Defect Found in Potter & Brumfield Relays. Sixteen Relays Supplied in Lot 913501 by Vendor as Commercial Grade Items.Caused by Insufficient Contact Pad Welding.Relays Replaced with New Relays ML20206S7281999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Songs,Units 2 & 3 ML20206G6561999-04-27027 April 1999 SER Accepting Proposed Exemption from 10CFR50.71(e)(4) for SONGS Units 2 & 3 ML20206D1461999-04-26026 April 1999 Safety Evaluation Supporting Amend 152 to License NPF-10 ML20205Q6221999-04-19019 April 1999 Safety Evaluation Authorizing Proposed Alternative to Use Wire Penetrameters for ISI Radiography in Place of ASME Code Requirement ML20205R0371999-04-16016 April 1999 SER Approving Proposed Deviation from Approved Fire Protection Program Incorporating Technical Requirements of 10CFR50,App R,Section III.0 That Applies to RCP Oil Fill Piping ML20205N2691999-04-0909 April 1999 Safety Evaluation Supporting Amends 151 & 143 to Licenses NPF-10 & NPF-15,respectively ML20205G2611999-04-0101 April 1999 Special Rept:On 990328,3RT-7865 Was Removed from Service. Monitor Is Scheduled to Be Returned to Service Prior to Mode 4 Entry (Early May 1999) Which Will Exceed 72 H Allowed by LCS 3.3.102.Alternate Method of Monitoring Will Be Used ML20205Q0981999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Songs,Units 2 & 3 05000362/LER-1999-001-01, :on 990211,TS 3.0.3 Entered Due to Both Chilled Water Trains Being Inoperable.Warm Main Condenser Discharged Water Diverted in Salt Water Cooling (Swc)(Bs) Intake.With1999-03-12012 March 1999
- on 990211,TS 3.0.3 Entered Due to Both Chilled Water Trains Being Inoperable.Warm Main Condenser Discharged Water Diverted in Salt Water Cooling (Swc)(Bs) Intake.With
05000361/LER-1999-002, :on 990208,pressurizer Safety Valves Were Above TS Limit.Caused by Setpoint Drift.Sce Submitted License Amend Application on 980904 Requesting Tolerence Be Changed to +3/-2%.With1999-03-10010 March 1999
- on 990208,pressurizer Safety Valves Were Above TS Limit.Caused by Setpoint Drift.Sce Submitted License Amend Application on 980904 Requesting Tolerence Be Changed to +3/-2%.With
05000361/LER-1999-001, :on 990201,automatic Start of EDG Was Noted. Caused by Workers Closing Breaker 2A0418 by Discharging Closing Springs.Operators Restored SDC in Approx 26 Minutes. with1999-03-0303 March 1999
- on 990201,automatic Start of EDG Was Noted. Caused by Workers Closing Breaker 2A0418 by Discharging Closing Springs.Operators Restored SDC in Approx 26 Minutes. with
ML20204F8101999-02-28028 February 1999 Monthly Operating Repts for Songs,Units 2 & 3.With ML20203J1981999-02-12012 February 1999 Safety Evaluation Supporting Amends 149 & 141 to Licenses NPF-10 & NPF-15,respectively ML20203J1131999-02-12012 February 1999 Safety Evaluation Supporting Amends 150 & 142 to Licenses NPF-10 & NPF-15,respectively ML20202F7041999-01-21021 January 1999 Special Rept:On 990106,SCE Began to Modify 2RT-7865.2RT-7865 to Allow Monitor to Provide Input to New Radiation Monitoring Data Acquisition Sys.Monitor Found to Exceeds 72 H Allowed Bt LCS 3.3.102.Alternate Monitoring Established ML20199F0771998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Songs,Units 2 & 3 ML20206H2101998-12-31031 December 1998 SCE 1998 Annual Rept ML20206N6281998-12-16016 December 1998 Safety Evaluation Supporting Amends 145 & 137 to Licenses NPF-10 & NPF-15,respectively ML20198A6731998-12-11011 December 1998 Special Rept:On 981124,meteorological Sys Wind Direction Sensor Was Observed to Be Inoperable.Caused by Loss of Communication from Tower to Cr.Sensor Was Replaced & Sys Was Declared Operable on 981204 ML20198C3471998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Songs,Units 2 & 3 ML20196D8901998-11-30030 November 1998 Non-proprietary Reload Analysis Methodology for Songs,Units 2 & 3 1999-09-09
[Table view] |
text
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Southem Califomia Edison Company P. O. BOX 128 SAN CLEMENTE, CALWORNIA 92674 0t28
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January 17, 1994 w u.....
MVCot An Ge he matsow U. S. Nuclear Regulatory Commission Document Control Desk Washington, D.C.
20555
Subject:
Docket No. 50-361 Supplemental Report Licensee Event Report No.90-001, Revision 1 San Onofre Nuclear Generating Station, Unit 2
Reference:
Letter, H. E. Morgan (Edison) to USNRC Document Control Desk, dated March 22, 1990 The referenced letter provided Licensee Event Report (LER) No.90-001 for an occurrence involving a missed fire watch due to a procedural inadequacy.
The enclosed supplemental LER provides~
additional information regarding the schedule for completion of
planned corrective actions
Neither the health nor the safety-
- - i of plant personnel or the public was affected by this occurrence.
l If you require any additional information, please so advise.
4 Sincerely, ll.! GW[/
U
}
L,
Enclosure:
LER No.90-001, Rev. 1 cc:
K. E. Perkins, Jr., Acting Regional Administrator, NRC Region V J.-Sloan, Senior Resident Inspector, San Onofre Units 1, 2&3 3
M. B. Fields, NRC Project Manager, San Onofre Units 2&3 1
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LICENSEE EVENT REPORT (LET) f firacility rjame (1)
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I TECHNICAL SPECIFICATION VIOLATION INVOLVING A MISSED FIRE WATCH DUE TO A PROCEDURAL INADEQUACY l.
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ITHIS REPORT IS SUBMJTTED PURSUANT TO THE hEQUIREMENTS OF 10CFR I
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J At 1552 on 2/20/90 with Unit 2 operating at 100% power, Technical' Specification (TS) fire door DG2201 located in the Unit 2 Diesca Generator (DG) building was determined to be impaired-due to a sticky-door' latch.
At 1656, in accordance with TS 3.7.9, Action "a",
an' hourly fire watch was posted in two fire areas- (2-DG-30-156, room 101 and 2-DG-30-158, room 103) which were located on either side of the fire door,'according to the fire protection system computer data base.
During a review on 2/22/90 at 1328, it was determined that a TS-violation had occurred because the rooms identified to be protected by.
fire door DG2201 were determined to be incorrect.
The correct' rooms were rooms 201 and 202 located in fire areas 2-DG-30-156 and 2-DG 158, respectively.
Since these rooms'do not contain any' fire detection' or suppression systems,'a continuous fire watch should have been q
posted.
As required by TS 3.7. 9, Action "a",
a continuous fire watch 1
was posted in Room 201 on 2/22/90 at 1352.
j The root cause of this event was procedural inadequacy, in that the J
- - fire protection procedures do not provide sufficient guidance-to identify the correct data needed to properly establish the required compensatory measures for this fire door impairment.
q 1
1 Fire protection procedures have been revised to provide the guidance
]
required to properly identify the necessary compensatory measures for 1
impaired fire protection equipment.
This event has been discussed with appropriate EP personnel.
The rooms-which are protected by fire door-DG2201 have been corrected in the fire protection equipment computer data base.
An audit of the fire protection equipment data base will be~
performed and any errors found will be corrected.
The computerized Fire Protection Impairment Program will be upgraded so that it can be used to make fire equipment impairment evaluations without requiring reference to other controlled documents.
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TEXT-CONTINUATION-y
- - LICENSEE EVENT REPORT - (LER)
LS1W ONOFRE NUCLEAR GENERATION STATION DOCKET NUMBER
- - LER NUMBER.
PAGE' I
s
- UNIT'2 05000361 90-001-01 l2 OF 6--
H cPlant: San Onofre Nuclear Generating Station-Unit: Two Reactor; Vendor:
Comuustion Engineering Event Date:. 02-20-90 Time: 1656 i
5 A.
CONDITIONS AT TIME OFLTHE EVENT:
Mode:
1, Power Operation at 100% Power 1
~ B.
BACKGROUND INFORMATION
At San Onofre Units 1, 2, and 3, when inoperable fire protection equipment [KP, KQ)-is identified, the Emergency: Service Officers-(ESO), who are part of the Emergency Preparedness (EP) 1 organization,-are responsible for-the establishment.of appropr'iate
.i compensatory measures required by th'e Technical Specifications-
.i
~
(TS).
Upon notification of a' failed surveillance, the ESOs'use.
impairment evaluation procedures to identify the= inoperable-fire protection equipment and to establish'the appropriate compensatory
.l measures pursuant to the TS Action requirements.~ Based ontthe;
- j ESO's evaluation, a Fire Impairment Form isninitiatedi to-document
't and track the establishment and termination of the compensatory measures such as firewatches.
~
j The Fire Protection-Information System.(FPIS) is aJcomputer [ CPU) based data management system designed to provide-for tracking'of
' fire protection. equipment status -and associated compensatory measures.
Also, FPIS is a secondary tool for ESO.s to uselin-evaluating impairments and. determining the required compensatory measures.' In.this capacity,~FPIS is to be used in. conjunction with' impairment evaluation procedures.
The Plant and Equipment Data Management. System'(PEDMS) is'the-l centralized information data base reflecting plant. configuration in accordance with SONGS Design Documentation (with associated-changes) and other associated field information.
The Updated Fire Hazards Analysis (UFHA) describes the capability-of the plant to achieve safe shutdown in the eventJof a fire.
The UFHA divides the plant into fire area / zones and a fire area / zone may be further divided into rooms.
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LICENSEE. EVENT REPORT (LER)- TEXTLCONTINUATION SAN ONOFRE NUCLEAR GENERATION STATION DOCKET NUMBER LER NUMBER 1
- PAGE UNIT'2 05000361
'90-001-01 3 OF 6 C.
DESCRIPTION OF THE EVENT:
1.
Event:
At 1552 on 2/20/90, with Unit 2 operating'at.100% power',.TS:
E Fire Door DG2201 [DR], located-in the. Unit 2 Diesel Generator (DG) building, was discovered by EP personnel to be impaired' as the result of a sticking door latch. -At 1606, the ESOsi initiated an unanticipated. fire impairment -(Impairment Number:
90020331-00) and an impairment' analysis. form for the fire.
door.
The impairment evaluation determined that an hoarly fire watch should be posted in fire area / zone.2-DG-30-156, 1
room 101, and fire area / zone'2-DG-30-158, room'103,'which according to PEDMS were located on: either side of fire ~ door.
DG2201.
This evaluation was based on information' contained in PEDMS and a determination that fire detection and suppression-was operable in fire area / zone 2-DG-30-158, Room ^103.
As required by TS 3.7.9, an hourly fire watch was posted:in Rooms 101 and 103 on 2/20/90 at 1656.
During a review of impairment 90020331-00' by Fire' Protection Engineering (FPE) on 2/22/90 at 1328, it was determined that the PEDMS identified room numbers protected by fire door-DG2201 were~ incorrect.
The correct rooms separated by fire door DG2201 were determined to be-Rooms 201' and:202 located irn UFHA area / zones 2-DG-30-156.and,2-DG-30-158,Erespectively.
The rooms in these fire area / zones do not.contain~any fireL detection ~or suppression systems. _As requiredcby TS 3.7.9,.
Action "a",
continuous fire. watch ~was posted:in Room 201 en
~
2/22/90 at 5 2.'
2.
Inoperable Structures, Systems or Components that-Contributed.
to the Event:
Not applicable.
3.
Sequence of Events:
DATE TIME ACTION 2/20/90 1552 Fire Door DG2201 failed TS surveillance..
2/20/90 1656 Hourly fire watch set in Rooms 101 and-103 of Unit 2 DG building.
~
2/22/90 1328 FPE determined that the~ original' fire impairment for fire door DG2201 was incorrect.
2/22/90 1352 A continuous fire watch was posted.in Room 201 for' fire door DG2201.
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LICENSEE' EVENT REPORT (LER) TEXT CONTINUATION:
- SAN ONOFRE NUCLEAR GENERATION STATION
' DOCKET NUMBER.
LER NUMBER.
PAGE
? UNIT 2-05000361 90-001-01 c4 OF 6 4.
_-Method of Discovery:
During an operability evaluation of'the fire door,-FPE determined.that an incorrect fire watch-had been established' for fire door DG2201.
h fi 5.
Personnel Actions and Analysis of. Actions:
Upon identification that the fire watch"had'been incorrectly established, action was initiated to establish'the correct-fire watch.
6.
Safety System Responses:
Not applicable.
D.
CAUSE OF THE EVENT
1.
Root Cause:
The root cause of this_ event was procedural inadequacy in that-the fire protection impairment evaluation-procedures-do-not' provide sufficient guidance to the ESO personnel.to identify' the correct data needed to properly establish the required' compensatory measures for:this fire door impairment.
Specifically, the UFHA fire area / zone inLthe.DG building.
covers two elevations and is divided into1several' rooms.
The room' numbers were not identified in the station' procedures or in the UFHA, so the ESOs' relied on the infonnation supplied by' PEDMS~to FPIS and, because it wasLincorrect,'twere unable to' correctly. evaluate the-impaired fire _ door-andLimplement:the:
correct type of fire watch.
2.
Contributing Cause
The PEDMS data base information identifying the rooms that were on either-side of the impaired fire door was: incorrect.
This information was'used to determine the compensatory; measures required for the impaired fire door and caused the ESOs to post an hourly fire watch 1in the-wrong room.insteadLof a continuous fire watch in the correct room.
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LICENSEE EVENT REPORT (LER) TEXT CONTINUATION y
SAN ONOFRE NUCLEAR GENERATION STATION DOCKET NUMBER LER NUMBER
.PAGE-j
= UNIT 2 05000361 90-001-01 5~OF-6~
j E.
CORRECTIVE ACTIONS
- 1 3
1.
Corrective Actions Taken:
j y
a.
This~ event has been discussed with appropriate EP l
?
personnel, emphasizing that the PEDMS data base may be 1
incorrect and that the information provided by1 EDMS.to.
P FPIS must be verified in station procedures or other~-
i controlled documents prior to.use.
If this informationi l
cannot be verified prior to implementing:the TS; required compensatory measures within the one hour' time Li constraint,.the most restrictive compensatory-measure j
will be implemented in all affected' fire area / zones.
1 until the information provided by PEDMS has=been'
]l verified by the means stated above. 'This. practice will be discontinued once the planned corrective. actions 1
discussed in Sections E.2.c and E.2.d are_ complete..
j b.
The room numbers of the rooms associated with fire door I
DG2201 have been corrected in the PEDMS data base.
The PEDMS data base was reviewed to determine 'that the UFHA fire area / zones and rooms. protected by each fire door i
were correctly identified for all other fire doors in
- j the Units 2 and 3 DG buildings.
Other discrepancies 1
were noted and corrected.'
i I
c.
Fire protection. impairment evaluation procedures have 1
been revised to include a cross-reference of TS fire
'j i
doors with associated fire area / zones and rooms.
1 l
d.
Limitations on the use of FPIS, as' discussed in I
corrective action a above, have been incorporated fut the 1) 1 fire-protection impairment evaluation procedures.
l!
i 2.
Planned Corrective Actions
'l
'l a.
The PEDMS data base for fire protection equipment and other data files relied upon by'FPIS will be completely audited to determine if other incomplete or incorrect i
'i UFHA area / zone and/or room information exists.
July
- - incomplete or incorrect information discovered will be corrected.
I b.
The computerized Fire Protection Impairment. Program will-I be upgraded so it will befable to.belused to provide 1the!
-)
necessary data to EP personnel making. fire equipment impairment evaluations without requiring reference to y
the UFHA and/or-other controlled documents.
1 These planned corrective actions will be completed during-g I
normal TS surveillance 4.7.9.2.c, which requires visual
.. inspection.of 10% of the fire rated penetration sealing.
I devices at least once per 18 months and 100% at~1 east once.per-l 15 years.
The inspection cycle will be completed by the,end-il of 1997.
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i LICENSEE EVENT REPORT ~ (LER)-TEXT CONTINUATION i-~ tSAN ONOFRE NUCLEAR GENERATION STATION-DOCKET-NUMBER
.LER. NUMBER PAGE LUNIT:2'
'05000361 90-001-01<
6 OF'6 l
4 1
1 F.
SAFETY SIGNIFICANCE OF ' THE EVENT
'The-TS-basis for_ operability requirements of fire' barriers:ensuresi
.that fire damage will;be limited.
These design features minimizef I
the possibility of a single fire affecting'more than one' fire area.
prior to detection and extinguishment.
The safety. significance 3of
]
1 this event'is minimized by the fact that.an hourly' fire watch was-posted in the fire area / zones located on both sides of the-fire.
i door, even though it was not in-the~ correct' rooms within'the fire area / zones.
This is because fire area / zone 2-DG-30-156,;which isca t
staircase that interfaces with fire area / zone 2-DG-30-158, consists.
of two rooms (Rooms 101 and 201) that are physically open to each other.
Thus the' development of a' fire in either fire' area / zone.
a most likely would have been detected by the hourly-fire watch thatL r
was posted in tire area / zones 2-DG-30-156, room 101, and 2-DG :
158, room 103.
Therefore, the likelihood ofia single' fire affecting more than'one fire area prior'to detection'and controllof-this fire was minimal.
.q
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G.
ADDITIONAL INFORMATION
1.
Component Failure Information
')
Not applicable.:
2.
Previous LERs for Similar Events:
LER 89-003 (Docket No. 50-362) reported an event involving a:
j missed fire watch caused by a procedural inadequacy,;which-y resulted in'a-failure by Operations' personnel to notify the-ESOs of.a failed' fire protection surveillance.
This-event did not preclude the event being reported.in this LER since it involved an inadequacycin an Operations procedure.
3.
Results of NPRDS search:
3 Not applicable.
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05000361/LER-1990-001, :on 900220,TS Violation Involving Missed Fire Watch Occurred.Caused by Procedural Inadequacy.Fire Protection Procedures Revised |
- on 900220,TS Violation Involving Missed Fire Watch Occurred.Caused by Procedural Inadequacy.Fire Protection Procedures Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(viii)(B) | 05000361/LER-1990-011-02, :on 900601,pipe Wall Thinning Caused by Erosion/Corrosion Processes.Reevaluation Program Ongoing & Targeted for Completion in Spring 1991 |
- on 900601,pipe Wall Thinning Caused by Erosion/Corrosion Processes.Reevaluation Program Ongoing & Targeted for Completion in Spring 1991
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000361/LER-1990-011-01, Corrected LER 90-011-01:on 900722,AFW Bypass Control Valve 3HV-4763 Declared Inoperable After Failing to Close Due to Mechanical Failure of Solenoid Valve.Valve Manually Isolated & Solenoid Valve Replaced | Corrected LER 90-011-01:on 900722,AFW Bypass Control Valve 3HV-4763 Declared Inoperable After Failing to Close Due to Mechanical Failure of Solenoid Valve.Valve Manually Isolated & Solenoid Valve Replaced | | 05000361/LER-1990-013-02, :on 901107,delinquent Waste Gas Decay Tank Surveillance Interval Exceeded.W/Undated Ltr |
- on 901107,delinquent Waste Gas Decay Tank Surveillance Interval Exceeded.W/Undated Ltr
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000362/LER-1990-014, :on 901223,CSS Train B Pressure Indicator Determined Inoperable Due to Failure of Pressure Transmitter.Caused by Small Metallic Particle Jamming Feedback Coil.Transmitter Replaced |
- on 901223,CSS Train B Pressure Indicator Determined Inoperable Due to Failure of Pressure Transmitter.Caused by Small Metallic Particle Jamming Feedback Coil.Transmitter Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000361/LER-1990-014-01, :on 901120,safety Injection Sys,Containment Cooling Sys & Containment Spray Sys Inadvertently Actuated While Performing 31-day Interval Surveillance of Sys.Caused by Personnel Error |
- on 901120,safety Injection Sys,Containment Cooling Sys & Containment Spray Sys Inadvertently Actuated While Performing 31-day Interval Surveillance of Sys.Caused by Personnel Error
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000362/LER-1990-014-02, :on 901223,containment Spray Sys Train B Pump Discharge Pressure Indicator 3PI-0303-2 Did Not Display Correct Pressure Reading.Caused by Metallic Particle Near Feedback Coil.Transmitter Replaced |
- on 901223,containment Spray Sys Train B Pump Discharge Pressure Indicator 3PI-0303-2 Did Not Display Correct Pressure Reading.Caused by Metallic Particle Near Feedback Coil.Transmitter Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000361/LER-1990-015-01, Forwards LER 90-015-01 Re Auxiliary Feedwater Pump Support Sys Piping Misassembly.Operation of Support Sys Not Required to Meet Design Basis Requirements | Forwards LER 90-015-01 Re Auxiliary Feedwater Pump Support Sys Piping Misassembly.Operation of Support Sys Not Required to Meet Design Basis Requirements | | 05000361/LER-1990-016-02, :on 901206,automatic Reactor Trip Occurred Due to non-1E Uninterruptible Power Sys Failure.Preventive Maint Program Modified to Require Periodic Cleaning of non-1E UPS Cabinet Internals During Refueling Outages |
- on 901206,automatic Reactor Trip Occurred Due to non-1E Uninterruptible Power Sys Failure.Preventive Maint Program Modified to Require Periodic Cleaning of non-1E UPS Cabinet Internals During Refueling Outages
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | 05000361/LER-1990-016, :on 901206,unit Automatically Tripped from 100% Power on RPS Loss of Load Signal Due to non-1E Uninterruptible Power Sys Failure.Failed Capacitor Replaced W/Capacitor of Improved Design |
- on 901206,unit Automatically Tripped from 100% Power on RPS Loss of Load Signal Due to non-1E Uninterruptible Power Sys Failure.Failed Capacitor Replaced W/Capacitor of Improved Design
| 10 CFR 50.73(e)(2) | 05000206/LER-1990-017, :on 900716,several Equipment Qualification Discrepancies Noted During Thermal Shield Repair.Caused by Weaknesses in Implementation of EQ Program.Field Verification Walkdowns Conducted |
- on 900716,several Equipment Qualification Discrepancies Noted During Thermal Shield Repair.Caused by Weaknesses in Implementation of EQ Program.Field Verification Walkdowns Conducted
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000206/LER-1990-018, :on 900920 & 25,concluded That Testing for 10 Main Steam ASME Code Class Valves Had Not Been Performed Per Unit 1 TS 4.7 IST Requirements.Caused by Failure to Update Program Correctly.Ist Program Updated |
- on 900920 & 25,concluded That Testing for 10 Main Steam ASME Code Class Valves Had Not Been Performed Per Unit 1 TS 4.7 IST Requirements.Caused by Failure to Update Program Correctly.Ist Program Updated
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) |
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