05000361/LER-1986-001, :on 860102 & 04,inoperable & Degraded Snubbers Found on Main Steam Line to Auxiliary Feedwater Pump Turbine.Caused by Hydraulic Transient.Snubbers Replaced & Engineering Analysis Performed
ML20137R985 | |
Person / Time | |
---|---|
Site: | San Onofre |
Issue date: | 02/03/1986 |
From: | Morgan H SOUTHERN CALIFORNIA EDISON CO. |
To: | NRC OFFICE OF ADMINISTRATION (ADM) |
References | |
LER-86-001, LER-86-1, NUDOCS 8602130525 | |
Download: ML20137R985 (4) | |
Event date: | |
---|---|
Report date: | |
Reporting criterion: | 10 CFR 50.73(a)(2)(1) 10 CFR 50.73(a)(2) |
3611986001R00 - NRC Website | |
text
r- -
N 1 Form 366 LA S$ NUCLEAR REGULATORY COMMISSION p
APPROVED OMO NO, 31540104 LICENSEE EVENT REPORT (LER)
Em aE5' 84'85 j
u m.,..-- (. i
.....,.....(,)
,AOEin SAN ON0FRE NUCLEAR GENERATING STATION, UNIT 2 ol51010101 136l 1lorl0 p i
ve,o (.)
INOPERABLE SNUBBERS - MAIN STEAM TO AUXILIARY FEEDWATER PUMP TURBINE CVENT DATE (5)
LER NUMBER (4)
REPORT D ATE (7)
OTHER F ACILITIES INVOLVED (8)
.=~,,a.-==
a.< a =, a = = = = = (. i
,, n.
1,, n.......
. a,-
l SONGS, UNIT 3 o [5 l0 lo 10 l3 f) l2 00 0 12 0 13 81 6 o 15 lolo 10 l l l 01 1 01 2 86 816 0l0l1 1
THIS REPORT IS SUOMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR, (Ch.cis on. or mor. of th. following) (11 )
g-g pg ggy,gg
" " t'8 1
20.402(on 20.405(ci 50.73(.ii2)(iv) 73.7 (o)
W st 20.405(a)(1)(i) 50.36(c)(1) 50.7 3(a)(2)(v)
- 72. 7) (c)
T 50.3.(cn2 50.73(a n2n.,o OgR (sgc g A,ou,aci (1el 110l0 20.405(ani mo 20.405(a)(1)(eu)
T 50.73(a)(2)(1) 50.7 3(a)(2)(viii)( A)
Form 366A) 20.405(a)(i)(tv) 50.73(a)(2)(in 50.73(an2nviu)(B) 20.405(a)(I n v) 50.73(a)(2)(ui) 50.7 3(a)(2)(.)
LICENSEE CONT ACT FOR THIS LER (12)
"'"2 TELEPHONE NUM BER
.... coo.
3 6l8l-1 l2l4 1 1
6 1
7 1 l4 H. E. MORGAN, STATION MANAGER 1
COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRe9ED IN THt$ REPORT (13)
- c-
=l,:::::
- ac-
=l,=:::::
. c....
ca.m C
I l l [
III I
III i l1 1
1II III SUPPLEMENT AL REPORT EXPECTED (14) an.m,-
.a, lYES M MOMD$*TE E
^
l 83 NO g
g l
Ao.,xi (Lim,i io i 400...c... l...
a,0,o..mai.,,,,,i..n
......ac.
.,,,,.o 1,n..) i i.)
On January 2,1986, with Unit 2 at 100% power, a Pacific Scientific Mechanical Snubber was found disconnected and hanging free. The snubber was located on the Main Steam line to the Auxiliary Feedwater Pump Turbine (AFWPT). The snubber was manually stroked and found frozen due to transient damage. Pursuant to Technical Specification 4.7.6 additional potentially affected snubbers were manually stroked, identifying two additional failures.
. On January 4,1986, with Unit 3 in Hot Standby, the snubbers on the similar line in Unit 3 were inspected. As a result, seven degraded snubbers were identified.
All of the degraded snubbers on both units were replaced and engineering analyses were performed to determine their effect on the supported systems. The analysis determined that both systems remained capable of performing their safety functions under all cperating conditions.
As corrective action, design studies of the system configuration have been initiated.
In the interim, after every operation of the AFWPT of each unit, snubber surveillance has been increased by inspecting and manually stroking the snubbers, which are most susceptible to transient damage, to assure operability.
Since both systems remained functionally operable under all operating conditions, including a Design Basis Earthquake, there was no safety significance to these events.
0602130525 060203 (c,, Form 3*6 gDR ADOCK 0500 1
[a
~
N83N LICENSEE EVENT REPORT (LER)
ArmYd "N
a TEXT CONTINUATION EXPT RES: 8/31/85 P,h4877 N AMElt)
DOCMET NWMSE. (3)
LER NUM BE R (6)
PAGE (3)
.:::6.
u:::6.
SAN ON0FRE NUCLEAR GENERATING STATION,
- - NcIdr..u. a r.auir.a3Wtion.i KRc%,m ise A,i '<i7:
1 8.B
.0 b h 0 D O b. F 0 b
~~
On January 2,1986, with Unit 2 at 100% power, a Nuclear Regulatory Comission (NRC) resident inspector, during a random walkdown, identified a Pacific Scientific flechanical Snubber (EIIS Component Code SNB) that was disconnected and was hanging free. The snubber was located on the Itain Steam line (EIIS System Code SB) to the Auxiliary Feedwater Pump Turbine (AFWPT)(EIIS Component Code TRB)(EIIS System Code BA). This snubber was manually stroked and found frozen. A failure analysis was performed, which determined the cause to be due to hydraulic transient. Pursuant to Tcchnical Specification 4.7.6 all additional snubbers which may have been subjected to this transient were manually stroked. A total of seventeen snubbers were stroked, of which a total of three were found degraded. Two failures were caused by transients and one was due to environmental degradation.
All three snubbers were replaced and an engineering analysis was performed to determine their effect on the supported system. During the Cycle 1 Refueling in November 1984, these same snubbers, along with others on this line, were found degraded. The engineering analysis performed for those failures bounds these recent-failures. The results of the Cycle 1 analysis determined that the supported system remained capable of performing its safety function in all modes of operation and to remain functional during a Design Basis Earthquake (DBE).
The depinning of the snubber is believed to have been caused by a combination of effects. First, during the transients which caused the snubber to become frozen, the C-clip which holds the clevis pin in place probably fell off. Second, over tine, n:rmal vibration of the system may have caused the pin to work loose and disengage the snubber. The cause of this vibration is likely due to the flow of steam through the orifices (EIIS Component Code OR), which were added as part of the corrective action taken following the snubber failures found during the Cycle 1 Refueling 18-itonth Surveillance Testing, reported in LER-84-079R1 (Docket No. 50-361). The orifices were added in place of the existing steam traps to allow a continued flow of steam through the Itain Steam line to the AFWPT to help maintain temperature in the line and to provide a continuous drain, which would reduce the accumulation of condensation, reducing the chances of water hamer and turbine overspeed trips. These orifices are performing as expected, although, during heatup from Shutdown, they appear to be inadequate to handle the large amounts of water which result frca this evolution.
On January 4,1986, with Unit 3 in Hot Standby, the corresponding Unit 3 snubbers were inspected. The need for the Unit 3 inspection was based on the failures on Unit 2, the similarity of the Unit 2 and Unit 3 pf aing (although Unit 3 has more snubbers on this line than Unit 2), and since during tie Unit 3 Cycle 1 Refueling Outage in S:ptember 1985, the same type of orifice system was installed. In addition, Unit 3 had gone through a heatup evolution and the AFWPT had been operated after the Cycle 1 18-!1onth snubber surveillance. A total of twenty five snubbers were manually stroked, which identified seven failures.
It was determined that all seven failures were transient related and the seven snubbers were replaced. An engineering analysis was performed to determine their effect on the supported system. The results of.this analysis determined that the affected system remained capable of performing its safety function in all modes of operations and would have renained functionally operable in a DBE.
C orm 366A
?
ion erm men us Nucuan nemuterony c-W8M" LICENSEE EVENT REPORT (LER) mRoveo oue Na 31socio4 TEXT CONTINUATlON NRES: 8/31/95 raiskety seanseln).
secess? ~weems. (e)
LER NUMBER (4)
PAGE l3)
.w'::..
v :::6.
v.
SAN ON0FRE NUCLEAR GEllERATIflG STATION, UNIT 2 015Iglo10131611_ 816_
0J0_l1_10j0_.0j3 0F.0j3
\\ TEXT (If more Space IS required. Use additional NRC Form 366A's) (17)
As corrective action for both units, additional design studies have been initiated.
If any required design changes result from these studies they will be implemented during the next outage of sufficient duration for each unit. In the interim, in addition to the continuing program of system blowdown and draining, reported in LER 84-079Rl.(Docket No. 50-361) for Unit 2 and in LER 85-017R1 (Docket No. 50-362) for Unit 3, after every operation of the AFWPT, snubber surveillance has been increased by inspecting and manually stroking the snubbers, which are the most susceptible to-transient danage, to assure operability. These interim corrective actions will continue until the frequency of snubber failures decrease significantly.
Al} hough'thereweresnubberfailuresonbothUnits2and3,nodamagetoanyother supports, piaing or the AFWPT's was observed. Analyses of these systems for both units have slown that the affected systems have been functionally operable under all c'perating conditions, including a DBE. Therefore, there was no safety significance to these events.
f'
$~
.L;f -
l.*
i F
i A
C orm 366A
.?
m pggr Southem Callfamia Edlaon Company 7;
SAN ONOFRE NUCLEAR GENERATING STATION P. O BOX 128 SAN CLEMENTE. CAL 6FORNIA 92672
.'H.E, MORGAN TELEPHONE
- * ~ ~ ~ "
February 3, 1986~
.U.-S.' Nuclear Regulatory Commission Document Control Desk Washington, D.C.
20555
~
Subject:
Docket No. 50-361
~-30-Day Report
- - Licensee Event Report No.86-001
~
San Onofre Nuclear Generating Station,-Units 2 and 3
' Pursuant to 10 CFR 50.36(c)(2) and 10 CFR 50.73(a)(2)(i.), this submittal
- provides:the required 30-day written Licensee Event Report (LER) for two
- occurrences involving inoperable snubbers; on the Main Steam Line to the
- Auxiliary Feedwater Pump Turbine. Since these events involved similar
. systems;.causes and corrective actions on both Units 2 and 3, a single report Lis'being_ filed in accordance with NUREG-1022. Neither the health and sa'fety
.of plant personnel nor the health and safety of'the public was
.'fected by this event.
' If you require any additional.information, please so advise.
Sincerely,
&EW
^
=
- Enciosure:
LER No.86-001 cc:
F. R. Huey-(USNRC Senior Resident Inspector, Units 1, 2 and 3)
J. B. Martin-(Regional Administrator, USNRC Region V)
Institute of~ Nuclear Power Operations (INPO) 8
'/'