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Category:Letter
MONTHYEARIR 05000334/20240112024-10-17017 October 2024 License Renewal Phase IV Inspection Report 05000334/2024011 L-24-038, License Amendment Request to Remove the Expired One-Time Action for Valve Leak Repair in Technical Specification (TS) 3.5.2 and to Correct Core Operating Limits Rep Ort (COLR) References2024-09-17017 September 2024 License Amendment Request to Remove the Expired One-Time Action for Valve Leak Repair in Technical Specification (TS) 3.5.2 and to Correct Core Operating Limits Rep Ort (COLR) References L-24-015, Twenty-Ninth Refueling Outage Inservice Inspection Summary Report2024-09-17017 September 2024 Twenty-Ninth Refueling Outage Inservice Inspection Summary Report ML24134A1522024-09-17017 September 2024 Exemption from the Requirements of 10 CFR 50.71(e)(4) Final Safety Analysis Report Update Schedule (EPID L-2024-LLE-0005) - Letter ML24260A1912024-09-16016 September 2024 Operator Licensing Examination Approval IR 05000334/20240052024-08-29029 August 2024 Updated Inspection Plan for Beaver Valley Power Station, Units 1 and 2 (Reports 05000334/2024005 and 05000412/2024005) L-24-188, Submittal of Quality Assurance Program Manual, Revision 302024-08-27027 August 2024 Submittal of Quality Assurance Program Manual, Revision 30 L-24-199, Discharge Monitoring Report (NPDES) Permit No. PA00256152024-08-22022 August 2024 Discharge Monitoring Report (NPDES) Permit No. PA0025615 IR 05000334/20244022024-08-22022 August 2024 Security Baseline Inspection Report 05000334/2024402 and 05000412/2024402 (Cover Letter Only) L-24-186, Response to RAI for Exemption Request from 10 CFR 50.71(e)(4) Final Safety Analysis Update Schedule2024-08-15015 August 2024 Response to RAI for Exemption Request from 10 CFR 50.71(e)(4) Final Safety Analysis Update Schedule IR 05000334/20240022024-08-0505 August 2024 Integrated Inspection Report 05000334/2024002 and 05000412/2024002 ML24208A0462024-07-26026 July 2024 NRC Office of Investigations Case No. 1-2023-005 L-24-182, Discharge Monitoring Report (NPDES) Permit No. PA00256152024-07-23023 July 2024 Discharge Monitoring Report (NPDES) Permit No. PA0025615 L-24-161, Discharge Monitoring Report (NPDES) Permit No. PA00256152024-07-19019 July 2024 Discharge Monitoring Report (NPDES) Permit No. PA0025615 05000334/LER-2024-004, Reactor Trip Due to Bypass Feedwater Regulating Valve Failure to Control2024-07-17017 July 2024 Reactor Trip Due to Bypass Feedwater Regulating Valve Failure to Control L-24-014, Annual 10 CFR 50.46 Report of Changes to or Errors in Emergency Core Cooling Svstem Evaluation Models2024-07-16016 July 2024 Annual 10 CFR 50.46 Report of Changes to or Errors in Emergency Core Cooling Svstem Evaluation Models ML24193A2912024-07-16016 July 2024 Revision to Reactor Vessel Surveillance Capsule Withdrawal Schedule IR 05000334/20245012024-07-0808 July 2024 Emergency Preparedness Biennial Exercise Inspection Report 05000334/2024501 and 05000412/2024501 05000334/LER-2024-003, Unanalyzed Containment Bypass Condition Due to Degraded River Water Piping2024-07-0202 July 2024 Unanalyzed Containment Bypass Condition Due to Degraded River Water Piping L-24-164, BV-2, Post Accident Monitor Report2024-06-27027 June 2024 BV-2, Post Accident Monitor Report IR 05000334/20244012024-06-26026 June 2024 Material Control and Accounting Program Inspection Report 05000334/2024401 and 05000412/2024401 (Cover Letter Only) L-24-094, Reactor Vessel Surveillance Capsule Withdrawal Schedule2024-06-24024 June 2024 Reactor Vessel Surveillance Capsule Withdrawal Schedule L-24-152, Response to NRC Regulatory Issue Summary 2024-01 Preparation and Scheduling of Operator Licensing Examinations2024-06-17017 June 2024 Response to NRC Regulatory Issue Summary 2024-01 Preparation and Scheduling of Operator Licensing Examinations 05000334/LER-2024-002, Automatic Reactor Trip Due to Low Reactor Coolant Flow Caused by Transformer Overexcitation Protection Relay Actuation2024-06-11011 June 2024 Automatic Reactor Trip Due to Low Reactor Coolant Flow Caused by Transformer Overexcitation Protection Relay Actuation 05000334/LER-2024-001, Offsite AC Power Source Inoperable Due to Breaker Failure Resulting in Condition Prohibited by Technical Specification2024-06-0606 June 2024 Offsite AC Power Source Inoperable Due to Breaker Failure Resulting in Condition Prohibited by Technical Specification ML24135A2282024-05-29029 May 2024 Review of the Spring 2023 Outage Generic Letter 95-05 Voltage-Based Alternate Repair Criteria and Steam Generator F Star Reports ML24135A1702024-05-29029 May 2024 – Steam Generator Tube Inspection - Review of the Spring 2023 Tube Inspection Reports L-24-021, Cycle 30 Core Operating Limits Report2024-05-23023 May 2024 Cycle 30 Core Operating Limits Report L-24-121, Discharge Monitoring Report (NPDES) Permit No. PA00256152024-05-23023 May 2024 Discharge Monitoring Report (NPDES) Permit No. PA0025615 ML24141A1052024-05-20020 May 2024 Senior Reactor and Reactor Operator Initial License Examinations IR 05000334/20240102024-05-15015 May 2024 Information Request for Quadrennial Baseline Comprehensive Engineering Team Inspection; Notification to Perform Inspection 05000334/2024010 and 05000412/2024010 L-24-107, CFR 50.55a Request 1-TYP-5-RRP-l, for Alternative Method of Nondestructive Examination for River Water Outlet Piping Weld Repair2024-05-13013 May 2024 CFR 50.55a Request 1-TYP-5-RRP-l, for Alternative Method of Nondestructive Examination for River Water Outlet Piping Weld Repair IR 05000334/20240012024-05-0808 May 2024 Integrated Inspection Report 05000334/2024001 and 05000412/2024001 L-23-269, Application to Revise Technical Specifications to Adopt TSTF-569, Revision of Response Time Testing Definitions2024-05-0707 May 2024 Application to Revise Technical Specifications to Adopt TSTF-569, Revision of Response Time Testing Definitions L-24-054, Submittal of 2023 Annual Radioactive Effluent Release Report 2023 Annual Radiological Environmental Operating Report and 2023 Annual Environmental Operating Report (Non-Radiological)2024-04-29029 April 2024 Submittal of 2023 Annual Radioactive Effluent Release Report 2023 Annual Radiological Environmental Operating Report and 2023 Annual Environmental Operating Report (Non-Radiological) L-24-089, Emergency Preparedness Plan2024-04-23023 April 2024 Emergency Preparedness Plan L-24-088, Discharge Monitoring Report (NPDES) Permit No. PA0025615 for March 20242024-04-22022 April 2024 Discharge Monitoring Report (NPDES) Permit No. PA0025615 for March 2024 ML24101A2752024-04-10010 April 2024 Response to Request for Additional Information Regarding Spring 2023 180-Day Steam Generator Tube Inspection Report L-24-082, Withdrawal of Exemption Request2024-04-0303 April 2024 Withdrawal of Exemption Request L-24-013, Annual Notification of Property Insurance Coverage2024-03-26026 March 2024 Annual Notification of Property Insurance Coverage L-24-064, Submittal of Discharge Monitoring Report (NPDES) Permit No. PA00256152024-03-13013 March 2024 Submittal of Discharge Monitoring Report (NPDES) Permit No. PA0025615 ML24044A0662024-03-0404 March 2024 Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0083 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting ML24057A0752024-03-0101 March 2024 The Associated Independent Spent Fuel Storage Installations IR 05000334/20230062024-02-28028 February 2024 Annual Assessment Letter for Beaver Valley Power Station, Units 1 and 2 (Reports 05000334/2023006 and 05000412/2023006) L-23-264, Request for Exemption from 10 CFR 50.71(e)(4) Final Safety Analysis Report Update Schedule2024-02-23023 February 2024 Request for Exemption from 10 CFR 50.71(e)(4) Final Safety Analysis Report Update Schedule CP-202300502, Notice of Planned Closing of Transaction and Provision of Documents to Satisfy Order Conditions2024-02-23023 February 2024 Notice of Planned Closing of Transaction and Provision of Documents to Satisfy Order Conditions L-24-050, Retrospective Premium Guarantee2024-02-22022 February 2024 Retrospective Premium Guarantee 05000412/LER-2023-003-01, Missile Barrier Door Left Open Resulting in a Loss of Safety Function2024-02-20020 February 2024 Missile Barrier Door Left Open Resulting in a Loss of Safety Function IR 05000334/20230042024-02-12012 February 2024 Integrated Inspection Report 05000334/2023004 and 05000412/2023004 ML24025A0922024-01-25025 January 2024 Requalification Program Inspection 2024-09-17
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000334/LER-2024-004, Reactor Trip Due to Bypass Feedwater Regulating Valve Failure to Control2024-07-17017 July 2024 Reactor Trip Due to Bypass Feedwater Regulating Valve Failure to Control 05000334/LER-2024-003, Unanalyzed Containment Bypass Condition Due to Degraded River Water Piping2024-07-0202 July 2024 Unanalyzed Containment Bypass Condition Due to Degraded River Water Piping 05000334/LER-2024-002, Automatic Reactor Trip Due to Low Reactor Coolant Flow Caused by Transformer Overexcitation Protection Relay Actuation2024-06-11011 June 2024 Automatic Reactor Trip Due to Low Reactor Coolant Flow Caused by Transformer Overexcitation Protection Relay Actuation 05000334/LER-2024-001, Offsite AC Power Source Inoperable Due to Breaker Failure Resulting in Condition Prohibited by Technical Specification2024-06-0606 June 2024 Offsite AC Power Source Inoperable Due to Breaker Failure Resulting in Condition Prohibited by Technical Specification 05000412/LER-2023-003-01, Missile Barrier Door Left Open Resulting in a Loss of Safety Function2024-02-20020 February 2024 Missile Barrier Door Left Open Resulting in a Loss of Safety Function 05000412/LER-2023-004, Condition Prohibited by Technical Specification and Loss of Safety Function Due to Emergency Diesel Generator Lube Oil Contamination by Fuel Oil2023-09-0808 September 2023 Condition Prohibited by Technical Specification and Loss of Safety Function Due to Emergency Diesel Generator Lube Oil Contamination by Fuel Oil 05000412/LER-2023-003, Missile Barrier Door Left Open Resulting in a Loss of Safety Function2023-08-0808 August 2023 Missile Barrier Door Left Open Resulting in a Loss of Safety Function 05000412/LER-2023-002, Automatic Actuation of Auxiliary Feedwater System2023-07-12012 July 2023 Automatic Actuation of Auxiliary Feedwater System 05000412/LER-2023-001, Indications Identified During Reactor Vessel Head Inspection2023-06-16016 June 2023 Indications Identified During Reactor Vessel Head Inspection 05000412/LER-2022-001, Operation or Condition Prohibited by Technical Specification and Loss of Safety Function Due to Emergency Diesel Generator Fuel Oil Intrusion Into Lube Oil2022-09-0808 September 2022 Operation or Condition Prohibited by Technical Specification and Loss of Safety Function Due to Emergency Diesel Generator Fuel Oil Intrusion Into Lube Oil 05000334/LER-2022-001, Manual Reactor Trip and Auxiliary Feedwater Actuation Due to Heater Drain System Valve Failure2022-08-10010 August 2022 Manual Reactor Trip and Auxiliary Feedwater Actuation Due to Heater Drain System Valve Failure 05000412/LER-2021-005, Manual Reactor Trip and Auxiliary Feedwater Actuation Due to Trip of a Main Feedwater Pump2022-01-17017 January 2022 Manual Reactor Trip and Auxiliary Feedwater Actuation Due to Trip of a Main Feedwater Pump 05000412/LER-2021-004, Manual Reactor Trip2022-01-11011 January 2022 Manual Reactor Trip 05000412/LER-2021-003, Indications Identified During Reactor Vessel Head Inspection2021-12-17017 December 2021 Indications Identified During Reactor Vessel Head Inspection 05000412/LER-2021-002, Unit 2, Automatic Reactor Trip and Automatic Actuation of the Auxiliary Feedwater System2021-12-0303 December 2021 Unit 2, Automatic Reactor Trip and Automatic Actuation of the Auxiliary Feedwater System 05000334/LER-2017-0032018-01-0404 January 2018 Beaver Valley Power Station Unit 1 Reactor Trip due to Turbine Trip and Automatic Initiation of the Auxiliary Feedwater System, LER 17-003-00 for Beaver Valley, Unit 1, Regarding Reactor Trip due to Turbine Trip and Automatic Initiation of the Auxiliary Feedwater System 05000334/LER-2017-0022017-09-13013 September 2017 1 OF 4, LER 17-002-00 for Beaver Valley Power Station, Unit No. 1 Regarding Inadequate Emergency Diesel Generator (EOG) Tornado Missile Protection Identified Due to Non-conforming Design Conditions 05000412/LER-2017-0012017-05-0202 May 2017 Surveillance Testing Rendered Service Water System Inoperable Due to the Coupling of Seismic Category 1 Piping to Not Seismic Category 1 Piping, LER 17-001-00 For Beaver Valley Power Station, Unit No. 2 Re: Surveillance Testing Rendered Service Water System Inoperable Due to the Coupling of Seismic Category l Piping to Not Seismic Category 1 Piping 05000334/LER-2017-0012017-04-18018 April 2017 Inadequate Tornado Missile Protection Identified Due to Non-Conforming Design Conditions, LER 17-001-00 for Beaver Valley Power Station, Unit Nos. 1 and 2 Regarding Inadequate Tornado Missile Protection Identified Due to Nonconforming Design Conditions L-08-222, LER 08-01-00 for Beaver Valley, Unit 2, Regarding Unplanned Actuation of the Auxiliary Feedwater System During Plant Startup2008-07-23023 July 2008 LER 08-01-00 for Beaver Valley, Unit 2, Regarding Unplanned Actuation of the Auxiliary Feedwater System During Plant Startup 2024-07-02
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Beaver Valley Power Station energy P.O. Box4 Shippingport, PA 15077 harbor
John J. Grabnar 724-682-5234 Site Vice President Fax: 724-643-8069
August 10, 2022 L-22-186 10 CFR 50.73
ATTN: Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555-0001
SUBJECT:
Beaver Valley Power Station, Unit No. 1 Docket No. 50-334, License No. DPR-66 LER 2022-001-00
Enclosed is Licensee Event Report (LER) 2022-001-00, "Manual Reactor Trip and Auxiliary Feedwater Actuation due to Heater Drain System Valve Failure". This event is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A).
There are no regulatory commitments contained in this submittal. Any actions described in this document represent intended or planned actions and are described for information only.
If there are any questions or if additional information is required, please contact Mr. Steve Sawtschenko, Manager, Regulatory Compliance and Emergency Response, at 724-682-4284.
Sincerely,
John J. Grabnar
Enclosure: Beaver Valley Power Station, Unit 1 LER 2022-001-00
cc: Mr. D. C. Lew, NRC Region I Administrator NRC Senior Resident Inspector Mr. B. Ballard, NRC Project Manager INPO Records Center (via INPO Industry Reporting and Information System)
Mr. L. Winker (BRP/DEP)
Enclosure L-22-186
Beaver Valley Power Station, Unit 1 LER 2022-001-00
Abstract
At 0724 on June 15, 2022 while at approximately 100 percent power, the Beaver Valley Power Station, Unit No. 1 (BVPS-1) reactor was manually tripped due to lowering steam generator water levels. This was due to reduced heater drain flow from the heater drain system (HDS) to the main feedwater pumps (MFPs) when the heater drain receiver normal level control valve, LCV-1SD-106B, experienced a valve plug to stem separation. The Operators manually tripped the reactor as required per the predefined trip criteria for low steam generator water level.
This event is being reported pursuant to 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in a manual actuation of the Reactor Protection System, 10 CFR 50.73(a)(2)(iv)(B)(1), and the automatic actuation of the Auxiliary Feedwater System, 10 CFR 50.73(a)(2)(iv)(B)(6). Corrective actions include replacing the plug, stem, and pin (trim) of LCV-1SD-106B with an enhanced design during the next refueling outage (Fall 2022).
Energy Industry Identification System (EIIS) codes are identified in the text as [XX].
BACKGROUND
The Unit 1 Heater Drains System (HDS) [SN] is designed to collect drains from the feedwater heaters, main turbine reheater steam coils, and moisture separators and deliver the condensate to the Main Feedwater Pumps (MFPs) [SJ] as steam generator feedwater.
Either of two full size heater drain pumps take suction from the heater drain receiver and discharge into the MFP suction header. The MFPs deliver the feedwater to the steam generators.
Normal level is maintained in the heater drain receiver by modulation of the level control valve, LCV-1SD-106B [LCV], at the discharge of the heater drain pumps.
HDS flow rates are based upon supplying sufficient heater drain flow, together with the condensate system [SG], to satisfy the operational requirements of the steam generator MFPs. The HDS is designed to supply 25 percent of full feed flow required for operation of the steam generator MFPs.
DESCRIPTION OF EVENT
At 0100 on June 13, 2022 while at full power operation, heater drain pump flow oscillations were identified with indications that LCV-1SD-106B was binding. An action plan was developed if the LCV were to fail and operators were briefed for a potential controlled down power.
At 0724 on June 15, 2022 while at approximately 100 percent power, the BVPS-1 reactor was manually tripped due to lowering steam generator water levels. This was due to reduced condensate flow from the HDS to the MFPs when LCV-1SD-106B experienced a valve plug to stem separation.
The trip was not complicated and the plant was stabilized in Mode 3. All control rods [AA] fully inserted into the reactor core. The Auxiliary Feedwater System (AFW) [BA] automatically actuated on low steam generator water level as expected, and the AFW system performed as designed. There was no safety-related equipment inoperable at the start of the event that contributed to the event.
CAUSE OF EVENT
The direct cause of the need to perform the manual reactor trip was the lowering steam generator levels due to reduced heater drain flow from the HDS to the MFPs. This was the result of LCV-1SD-106B experiencing a valve pin failure and plug to stem separation.
The apparent cause is that the design of the valve assembly is less than adequate due to lack of pre-load on the threaded connection at the stem and plug making this connection prone to loosening and separating. Stress and fatigue from system flow induced vibration with this condition led to the wearing away of the stem threads and eventual failure of the locking pin which allowed the stem/plug separation. The pin is intended to only be a locking device and is not designed to support the load applied to the stem. To ensure the pin is not overloaded, the stem must be properly torqued to the valve plug.
A contributing cause is the organization did not have an adequate consequence bias for risk from a previous similar event in May 2021. In May 2021, LCV-1SD-106B also experienced a pin failure and plug/stem separation that resulted in a controlled down power to repair the valve. The valve was repaired by replacing the pin and stem, however the existing plug was reinstalled due to parts availability. It was perceived that the used plug would allow the valve to operate reliably to the next refueling outage and that the organization could predict and control the plant should the valve exhibit degradation. The valve was not classified or evaluated as a single point vulnerability (SPV) to a reactor shutdown.
ANALYSIS OF EVENT
The event was reported per Event Notification 55943 as an event that resulted in the actuation of the reactor protection system, 10 CFR 50.72(b)(2)(iv)(B), and a specific system actuation, 10 CFR 50.72(b)(3)(iv)(A). This event is reportable pursuant to 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in a manual actuation of the Reactor Protection System, 10 CFR 50.73(a)(2)(iv)(B)(1), and the automatic actuation of the Auxiliary Feedwater System, 10 CFR 50.73(a)(2)(iv)(B)
(6).
The plant risk associated with the BVPS-1 reactor trip on June 15, 2022, is considered to be very low. This is based on the change in average core damage frequency derived using the conditional core damage probability and change in average large early release frequency derived using conditional large early release probability for the event. Therefore, this event had very low safety significance.
CORRECTIVE ACTIONS
Completed Actions:
- 1) The level control valve, LCV-1SD-106B, was repaired with a new trim. BVPS-1 was returned to service and synchronized to the grid on June 17, 2022.
Planned Actions:
- 1) Replace the trim of LCV-1SD-106B with an enhanced design during the next refueling outage (Fall 2022). The new valve assembly will have an improved shouldered stem design, a hardened stem pin, and a hardened stainless-steel stem to resolve the potential for loosening.
- 2) Evaluate whether LCV-1SD-106B should be classified as a SPV.
PREVIOUS SIMILAR EVENTS
A review of the previous three years was performed. A previous event occurred in May 2021 when LCV-1SD-106B failed due to a plug/stem separation. The valve was repaired by replacing the stem and pin, however the existing plug was reinstalled due to parts availability. The organization did not have an adequate consequence bias for risk as it was perceived that the used plug would allow the valve to operate reliably to the next refueling outage, and that the organization could predict and control the plant should the valve exhibit degradation.