Similar Documents at Salem |
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LER-1982-129, Forwards LER 82-129/03L-0.Detailed Event Analysis Encl |
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D >SEG Public Service Electric and Gas Company P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station November 10, 1982 Mr.
R. C.
Ilaynes Regional Administrator USNRC Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406 I
Dear Mr. Ilaynes :
LICENSE NO. DPR-7 5 DOCKET NO. 50-311 REPORTABLE OCCURRENCE 82-129/03L 1
Pursuant.to the
- -inirements of Salem Generating Station Unit No.
2, Technical Specifications, Section 6.9.1.9.b, we are. submitting Licensee Event Report for Reportable Occurrence 82-129/03L.
This report is required within thirty (30) days of the occurrence.
Sincerely yours,
/bf YY II. J. Midura j
i General Manager -
(
Salem Operations
'RF:ks 9.d CC:
Distribution
- , w 8211290547 821110 PDR ADOCK 05000311 s
PDR The Energy People pW wam oun n ei
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Report Number:
82-129/03L Report Date:
11-10-82 Occurrence Date:
10-24-82 Facility:
Salem Generating Station, Unit 2 Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Containment Air Locks - Inoperable.
This report was initiated by Incident Reports82-386 and 82-394.
CONDITIONS PRIOR TO OCCURRENCE:
Mode 1 - Rx Power 82% - Unit Load 910 MWe.
DESCRIPTION OF OCCURREUCE:
At 1415 hours0.0164 days <br />0.393 hours <br />0.00234 weeks <br />5.384075e-4 months <br />, October 24, 1982, during routine surveillance of the 130' Elevation Containment Air Lock, an operator observed that there was excessive leakage on the inner door seals.
The air lock was declared inoperable and Action State-ment 3.6.1.3.a was entered.
The air lock outer door was maintained closed to provide for centainment integrity.
Later that day the latch rollers on the inner door were adjusted, and the air ~ock was satisfactorily tested.
The 130' Elevation Air Lock was declared operable and at 2130 hours0.0247 days <br />0.592 hours <br />0.00352 weeks <br />8.10465e-4 months <br />, Action State-ment 3.6.1.3.a was terminated.
At 2210 hours0.0256 days <br />0.614 hours <br />0.00365 weeks <br />8.40905e-4 months <br />, October 26, 1982, during similar surveillance on the 100' Elevation Air Lock seals, the leakage on the interior door seals was found to be greater than the test specification.
The air lock was declared inoperable and Action Statement 3.6.1.3.a was entered for a second time.
Containment integrity was again maintained by insuring the outer door was closed.
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
In the first case, the excessive seal leakage was due to the air lock door latch linkage being out of adjustment.
Personnel operating the door handwheels too rapidly impose unnecessary force on the linkage and cause it to prematurely go out of adjustment.
Some shift in the adjustment is likely to occur with the frequent operation of the doors.
LER 82-129/03L.
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:In the second instance, the excessive leakage was due to a damaged inner door seal.
Opening of the door before the i
pressure across the seals was fully equalized apparently resulted in the seal being forced out of the seal groove; subsequent closure of the door with the seal out of the groove resulted in the seal being damaged by the knife edges.
ANALYSIS OF OCCURRENC'.
The containment air lock doors allow for personnel access to the Containment Building while providing a redundant boundary as part of overall containment integrity.
This barrier prevents the release of radioactive contamination to the environment in the event of a design basis accident.
Since one door was main-tained closed, providing containment integrity, no risk to the health and safety of the public was involved.
Therefore, this event constituted operation in a degraded mode permitted by a limiting condition for operation, and is reportable in accordance with Technical Specification 6.9.1.9.b.
Action Statement 3.6.1.3.a requires:
With one containment air lock door inoperable, maintain at least the operable air lock door closed and either restore the inoperable door to operable status within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, or lock the operable air lock door closed.
CORRECTIVE ACTION
As noted, in both instances an operable air lock door was main-tained closed, in compliance with the action statement.
In the first case, as mentioned, the air lock tested satisfactorily, was declared operable and the action statement terminated.
On the second occasion, the failed seal was replaced, and the air lock was satisfactorily tested.
It was declared operable at 0310 hours0.00359 days <br />0.0861 hours <br />5.125661e-4 weeks <br />1.17955e-4 months <br />, October 27, 1982, and Action Statement 3.6.1.3.a was terminated for the second time.
A number of previous problems with air lock operating linkage and door seals have been encountered (see LER's 32-055/03L, 82-056/03L, and 82-090/03L).
Efforts are presently underway to correct the problems including improved personnel training, installation of snubbers on the doors, relocation of test air supply isolation valves and revision of the surveillance test to more accurately simulate desired air lock performance.
Final evaluation of the effectiveness of the measures is pending full implementation.
LER 82-129/03L.
EAILURE DATA:
Not Applicable.
Prepared By R.
Frahm
//7 M,'
Gerferal Manager -
Salem Operations SORC Meeting No.82-101
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| 05000311/LER-1982-001, Supplemental LER 82-001/03X-1:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Stuck Open,Freezing Pressure Sensing Line.Damper Freed, Exercised & Closed | Supplemental LER 82-001/03X-1:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Stuck Open,Freezing Pressure Sensing Line.Damper Freed, Exercised & Closed | | | 05000272/LER-1982-001-03, Pressurizer Overprotection Sys Valve 1PR1 Was Isolated Due to Leakage. on 820107,while Draining Rcs,Valve 1RP2 Would Not Open. Caused by Generic Problem.Reactor Vessel Head Removed | Pressurizer Overprotection Sys Valve 1PR1 Was Isolated Due to Leakage. on 820107,while Draining Rcs,Valve 1RP2 Would Not Open. Caused by Generic Problem.Reactor Vessel Head Removed | | | 05000311/LER-1982-001-03, /03L-0:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Sticking Open,Freezing Pressure Sensing Line.Damper Freed & Closed. Line Thawed | /03L-0:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Sticking Open,Freezing Pressure Sensing Line.Damper Freed & Closed. Line Thawed | | | 05000272/LER-1982-001, Forwards Revised LER 82-001/03X-1.Detailed Event Analysis Encl | Forwards Revised LER 82-001/03X-1.Detailed Event Analysis Encl | | | 05000272/LER-1982-002-01, /01T-0:on 820119,indications of Tube Thinning Were Detected by Eddy Current Exam.Steam Generators 12 & 14 Required Two & Three Sample Insp,Respectively.All Defective Tubes & Tubes Degraded Above 30& Plugged | /01T-0:on 820119,indications of Tube Thinning Were Detected by Eddy Current Exam.Steam Generators 12 & 14 Required Two & Three Sample Insp,Respectively.All Defective Tubes & Tubes Degraded Above 30& Plugged | | | 05000311/LER-1982-002-03, /03L-0:on 820111,2A1 Battery Charger Tripped, Was Reset & Tripped Again.No Problem Found.Subsequent Trip Caused by Difference Between Battery Voltage & Battery Charger Voltage Setting.Personnel Instructed | /03L-0:on 820111,2A1 Battery Charger Tripped, Was Reset & Tripped Again.No Problem Found.Subsequent Trip Caused by Difference Between Battery Voltage & Battery Charger Voltage Setting.Personnel Instructed | | | 05000272/LER-1982-002, Supplemental LER 82-002/01X-2:on 820119,during Surveillance, Indications of Tube Thinning Detected by Eddy Current Exam. Tubes Above 30% Degradation Plugged.Tube R44C62 Sent to Westinghouse for Chemical & Metallurgical Testing | Supplemental LER 82-002/01X-2:on 820119,during Surveillance, Indications of Tube Thinning Detected by Eddy Current Exam. Tubes Above 30% Degradation Plugged.Tube R44C62 Sent to Westinghouse for Chemical & Metallurgical Testing | | | 05000311/LER-1982-002, Supplemental LER 82-002/03X-1:on 820111,battery Charger 2A1 Tripped.Charger Tripped Again Upon Resetting Breaker.Caused by Difference Between Battery & Battery Charger Voltages. Operating Instructions Revised to Adjust Float Vo | Supplemental LER 82-002/03X-1:on 820111,battery Charger 2A1 Tripped.Charger Tripped Again Upon Resetting Breaker.Caused by Difference Between Battery & Battery Charger Voltages. Operating Instructions Revised to Adjust Float Voltage | | | 05000311/LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1982-003-03, /03L-0:on 820106,1B & 1C Diesels Locked Out, Rendering Diesels Inoperable at Same Time.On 820106,diesel Generator 1C Declared Inoperable While Diesel 1B Out of Svc for Maint.Caused by Misinterpretation of Lockout Switch Tag | /03L-0:on 820106,1B & 1C Diesels Locked Out, Rendering Diesels Inoperable at Same Time.On 820106,diesel Generator 1C Declared Inoperable While Diesel 1B Out of Svc for Maint.Caused by Misinterpretation of Lockout Switch Tag | | | 05000311/LER-1982-003-03, /03L-0:on 820112,during Routine Calibr Testing, Radiation Monitor 2R11A Found Out of Calibr.Caused by Instrument Drift.Monitor Recalibr & Tested Satisfactorily | /03L-0:on 820112,during Routine Calibr Testing, Radiation Monitor 2R11A Found Out of Calibr.Caused by Instrument Drift.Monitor Recalibr & Tested Satisfactorily | | | 05000272/LER-1982-004-03, /03L-0:on 820109,primary Coolant Water Sample Results Indicated Excessive Boron Concentration,Constituting Positive Reactivity Change.Caused by Water Draining Out of Steam Generator Tubes.Rcs Rapid Boration Initiated | /03L-0:on 820109,primary Coolant Water Sample Results Indicated Excessive Boron Concentration,Constituting Positive Reactivity Change.Caused by Water Draining Out of Steam Generator Tubes.Rcs Rapid Boration Initiated | | | 05000272/LER-1982-004, Supplemental LER 82-004/03X-1:on 820108,charging Pump 13 Declared Inoperable Due to Component Cooling Water Sys Being Tagged Out for Planned Maint.On 820109,positive Reactivity Change Found in RCS Boron Concentration | Supplemental LER 82-004/03X-1:on 820108,charging Pump 13 Declared Inoperable Due to Component Cooling Water Sys Being Tagged Out for Planned Maint.On 820109,positive Reactivity Change Found in RCS Boron Concentration | | | 05000311/LER-1982-004, Forwards LER 82-004/03X-1.Detailed Event Analysis Encl | Forwards LER 82-004/03X-1.Detailed Event Analysis Encl | | | 05000272/LER-1982-005-01, /01X-1:on 820131,degradation of Fuel Cladding on Fuel Assembly C-04 Discovered.Caused by Fuel Lockup Due to Wedged Fuel Pellet.Fuel Assembly Placed in Spent Fuel Pit. All C Assemblies Scheduled for Reuse in Core | /01X-1:on 820131,degradation of Fuel Cladding on Fuel Assembly C-04 Discovered.Caused by Fuel Lockup Due to Wedged Fuel Pellet.Fuel Assembly Placed in Spent Fuel Pit. All C Assemblies Scheduled for Reuse in Core | | | 05000272/LER-1982-005, Forwards LER 82-005/01X-1.Detailed Event Analysis Encl | Forwards LER 82-005/01X-1.Detailed Event Analysis Encl | | | 05000311/LER-1982-005, Forwards LER 82-005/03L-0.Detailed Event Analysis Encl | Forwards LER 82-005/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-005-03, /03L-0:on 820121,during Performance of M3T Maint Surveillance Test Undervoltage Relay on 2C Vital Bus Actuated at 5.5 Volts Instead of 77.3 Volt Trip Setpoint Value.No Defects Found.Relay Recalibr | /03L-0:on 820121,during Performance of M3T Maint Surveillance Test Undervoltage Relay on 2C Vital Bus Actuated at 5.5 Volts Instead of 77.3 Volt Trip Setpoint Value.No Defects Found.Relay Recalibr | | | 05000272/LER-1982-006-03, /03L-0:on 820113,air Particulate Detector Failed. Cause Not Stated.All Required Containment Purge & Pressure Vacuum Relief Penetrations Isolated.High & Low Speed Filter Paper Drives Replaced | /03L-0:on 820113,air Particulate Detector Failed. Cause Not Stated.All Required Containment Purge & Pressure Vacuum Relief Penetrations Isolated.High & Low Speed Filter Paper Drives Replaced | | | 05000272/LER-1982-006, Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-006, Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-006-03, /03L-0:on 820128,svc Water Flow Indicator Indicated No Flow Condition.Caused by Svc Water Discharge Valve 22SW223 Being Stuck Shut.Valve Opened,Locally Tested & Returned to Svc | /03L-0:on 820128,svc Water Flow Indicator Indicated No Flow Condition.Caused by Svc Water Discharge Valve 22SW223 Being Stuck Shut.Valve Opened,Locally Tested & Returned to Svc | | | 05000272/LER-1982-007-01, /01X-2:on 820211,during Design Review,Discovered That Check Valves 1AF71 & 1AF72 & Associated Piping Not Seismically Analyzed & Protected.Protective Steel Structures Provided Off Seismic Wall | /01X-2:on 820211,during Design Review,Discovered That Check Valves 1AF71 & 1AF72 & Associated Piping Not Seismically Analyzed & Protected.Protective Steel Structures Provided Off Seismic Wall | | | 05000272/LER-1982-007, Forwards LER 82-007/01X-2 | Forwards LER 82-007/01X-2 | | | 05000272/LER-1982-008, Supplemental LER 82-008/03X-1:on 820126,boric Acid Concentrations in Boric Acid Storage Tanks 11 & 12 Found Below Tech Spec Limit.Caused by Dilution of Concentration by Flushing Water in Tank Following Maint.Boric Acid Added | Supplemental LER 82-008/03X-1:on 820126,boric Acid Concentrations in Boric Acid Storage Tanks 11 & 12 Found Below Tech Spec Limit.Caused by Dilution of Concentration by Flushing Water in Tank Following Maint.Boric Acid Added | | | 05000272/LER-1982-008-03, /03L-0:on 820126,sample Results from Boric Acid Tanks Indicated Boric Acid Concentration Below Tech Specs. Refueling Water Storage Tank Low.Core Alterations & Positive Reactivity Changes Suspended.Level Adjusted | /03L-0:on 820126,sample Results from Boric Acid Tanks Indicated Boric Acid Concentration Below Tech Specs. Refueling Water Storage Tank Low.Core Alterations & Positive Reactivity Changes Suspended.Level Adjusted | | | 05000311/LER-1982-008, Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-008-03, /03L-0:on 820128,overpower Delta T Indication for Channel 21 Failed High.Caused by Signal Summator 2T-M412E Having No Output Due to Failed Capacitors. Five Capacitors Replaced | /03L-0:on 820128,overpower Delta T Indication for Channel 21 Failed High.Caused by Signal Summator 2T-M412E Having No Output Due to Failed Capacitors. Five Capacitors Replaced | | | 05000311/LER-1982-009, Forwards LER 82-009/03L-0.Detailed Event Analysis Encl | Forwards LER 82-009/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1982-009, Supplemental LER 82-009/03X-1:on 820118 & 25,Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Area 12 Inoperable for More than 14 Days.Caused by Sys in Manual Mode Due to Maint Outage | Supplemental LER 82-009/03X-1:on 820118 & 25,Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Area 12 Inoperable for More than 14 Days.Caused by Sys in Manual Mode Due to Maint Outage | | | 05000272/LER-1982-009-03, /03L-0:on 820118 & 25,switches for Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Tank Area 12 Had Been in Manual Position for Greater than 14 Days Due to Maint Outage | /03L-0:on 820118 & 25,switches for Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Tank Area 12 Had Been in Manual Position for Greater than 14 Days Due to Maint Outage | | | 05000311/LER-1982-009-03, /03L-0:on 820129,air Particulate Detector Pump Low Flow Alarm Annuniciated.Caused by Incorrect Normal Flow Valve Lineup to Pump.Pump Removed from Normal Flow & Placed in Backup Flow Lineup | /03L-0:on 820129,air Particulate Detector Pump Low Flow Alarm Annuniciated.Caused by Incorrect Normal Flow Valve Lineup to Pump.Pump Removed from Normal Flow & Placed in Backup Flow Lineup | | | 05000311/LER-1982-010-03, /03L-0:on 820201,discrepancy Between Individual Rod Position Indicator (Irpi) & Control Rod Bank Demand Indicator for Rod 2C2 Exceeded 12 Steps in Either Direction. Caused by Incorrect Calibr of Irpi.Irpi Calibr | /03L-0:on 820201,discrepancy Between Individual Rod Position Indicator (Irpi) & Control Rod Bank Demand Indicator for Rod 2C2 Exceeded 12 Steps in Either Direction. Caused by Incorrect Calibr of Irpi.Irpi Calibr | | | 05000272/LER-1982-010-03, /03X-1:on 820201,temporary Hose Connection from Unit 1 Spent Fuel Pool to Unit 2 Exchanger Found Leaking on Auxiliary Bldg 84-ft Elevation.Caused by Improper Clamp Installation.Hose Disconnected | /03X-1:on 820201,temporary Hose Connection from Unit 1 Spent Fuel Pool to Unit 2 Exchanger Found Leaking on Auxiliary Bldg 84-ft Elevation.Caused by Improper Clamp Installation.Hose Disconnected | | | 05000311/LER-1982-010, Forwards LER 82-010/03L-0.Detailed Event Analysis Encl | Forwards LER 82-010/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1982-010, Forwards LER 82-010/03X-1.Detailed Event Analysis Encl | Forwards LER 82-010/03X-1.Detailed Event Analysis Encl | | | 05000311/LER-1982-011, Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-011-03, /03L-0:on 820205,during Radiological Survey of Hot Laundry Trailer Area,Technician Discovered Lint from Dryer Exhaust of Trailer B Revealing Traces of Cs-137,Co-60 & Co-58.New Trailer & Lint Collector Installed | /03L-0:on 820205,during Radiological Survey of Hot Laundry Trailer Area,Technician Discovered Lint from Dryer Exhaust of Trailer B Revealing Traces of Cs-137,Co-60 & Co-58.New Trailer & Lint Collector Installed | | | 05000272/LER-1982-011, Forwards LER 82-011/03X-1.Detailed Event Analysis Encl | Forwards LER 82-011/03X-1.Detailed Event Analysis Encl | | | 05000272/LER-1982-012, Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-012, Forwards LER 82-012/03X-1.Detailed Event Analysis Encl | Forwards LER 82-012/03X-1.Detailed Event Analysis Encl | | | 05000311/LER-1982-012-03, /03X-1:on 820209,steam Generator Level Channel 2 Displayed Erratic Behavior,Indicating Drift.Apparently Caused by Intermittent Ground on Signal Lead.Ground Eliminated by Lifting Leads While Troubleshooting Problem | /03X-1:on 820209,steam Generator Level Channel 2 Displayed Erratic Behavior,Indicating Drift.Apparently Caused by Intermittent Ground on Signal Lead.Ground Eliminated by Lifting Leads While Troubleshooting Problem | | | 05000272/LER-1982-012-03, /03L-0:on 820223,operator Found Significant Amount of Chromated Water on Floor in Diesel Generator 1B Cubicle. Caused by Leakage on Right Side Jacket Water Heater.Jacket Water Heaters Replaced | /03L-0:on 820223,operator Found Significant Amount of Chromated Water on Floor in Diesel Generator 1B Cubicle. Caused by Leakage on Right Side Jacket Water Heater.Jacket Water Heaters Replaced | | | 05000272/LER-1982-013-03, /03L-0:on 820301,control Room Operator Closed Pressurizer Relief Valve 1PR1 When Valve 1PR2 Was Still Closed.Caused by Operator Error.Operator Counseled by Senior Shift Supervisor | /03L-0:on 820301,control Room Operator Closed Pressurizer Relief Valve 1PR1 When Valve 1PR2 Was Still Closed.Caused by Operator Error.Operator Counseled by Senior Shift Supervisor | | | 05000311/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-013-03, L-0:on 820215,shift Supervisor Informed That Two 4-inch Core Bores Opened on 78-ft Elevation Between Mechanical & Electrical Penetration Areas.No Fire Watch Posted.Caused by Inadvertently Posting Watch on Wrong Unit | L-0:on 820215,shift Supervisor Informed That Two 4-inch Core Bores Opened on 78-ft Elevation Between Mechanical & Electrical Penetration Areas.No Fire Watch Posted.Caused by Inadvertently Posting Watch on Wrong Unit | | | 05000272/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-014-03, /03L-0:on 820219,steam Generator 21 Level Channel 2 Read 20% Higher than Channels 3 & 4.Channel 2 Declared Inoperable.Cause Unknown.Transmitter Tested & Found Satisfactory.Sensing Lines Blown Down to Remove Solids | /03L-0:on 820219,steam Generator 21 Level Channel 2 Read 20% Higher than Channels 3 & 4.Channel 2 Declared Inoperable.Cause Unknown.Transmitter Tested & Found Satisfactory.Sensing Lines Blown Down to Remove Solids | | | 05000272/LER-1982-014-03, /03L-0:on 820306,wind Speed Indications for 150 & 300-ft Elevations Failed.Local Indications Also Failed. Caused by iced-up Anemometers.Anemometers Thawed & Declared Operable | /03L-0:on 820306,wind Speed Indications for 150 & 300-ft Elevations Failed.Local Indications Also Failed. Caused by iced-up Anemometers.Anemometers Thawed & Declared Operable | | | 05000311/LER-1982-014, Forwards LER 82-014/03L-0.Detailed Event Analysis Encl | Forwards LER 82-014/03L-0.Detailed Event Analysis Encl | |
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