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LER-1982-085, Forwards LER 82-085/03L-0.Detailed Event Analysis Encl |
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O PSEG Public Service Electric and Gas Company P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station September 3, 1982 Mr.
R.
C. Haynes Regional Administrator USNRC Region 1 631 Park Avenue King of Prussia,. Pennsylvania 19406
Dear Mr. Haynes:
LICENSE NO. DPR-75 DOCKET NO. 50-311 REPORTABLE OCCURRENCE 82-085/03L Pursuant to the requirements of Salem Generating Station Unit No.
2, Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for Reportable Occurrence 82-085/03L.
This report is required within thirty (30) days of the occurrence.
Sincerely yours,
/f
~
H.
J.
IIidura General Manager -
Salem Operations fdh RH:ks CC:
Distribution 8209220299 820903 PDR ADOCK 05000311 S
PDR The Energy Peopic p#
% 21M (20M) 118 9
gn Report Number:
82-085/03L Report Date:
09-03-82 Occurrence Date:
08-16-82 Facility:
Salem Generating Station, Unit 2 Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Reactor C ulant Loop Channel II Flow Indication -
Inoperable.
This report was initiated by Incident Reports82-235 and 82-237.
CONDITIONS PRIOR TO OCCURRENCE:
Mode 1 - Rx Power 82% - Unit Load 890 MWe.
DESCRIPTION OF OCCURRENCE:
At 1240 hours0.0144 days <br />0.344 hours <br />0.00205 weeks <br />4.7182e-4 months <br />, August 16, 1982, during routine operation, the Control Room Operator observed that No. 24 Reactor Coolant Loop Channel II indicated flow was reading high.
The channel was declared inoperable and the associated bistables were placed in a tripped condition.
Limiting Condition for Operation Action Statement'3.3.1 Action 7 was entered at 1245 hours0.0144 days <br />0.346 hours <br />0.00206 weeks <br />4.737225e-4 months <br />, August 16, 1982.
The signal isolation amplifier was replaced and a channel calibration was satisfactorily performed.
At 1407 hours0.0163 days <br />0.391 hours <br />0.00233 weeks <br />5.353635e-4 months <br />, August 16, 1982, No. 24 Reactor Coolant Loop Channel II Flow Indication was declared operable, and Limiting Condition for Operation Action Statement 3.3.1 Action 7 was terminated.
Later that day, at 2330 hours0.027 days <br />0.647 hours <br />0.00385 weeks <br />8.86565e-4 months <br />, the Control Room Operator again received indication of a malfunction of No. 24 Reactor Coolant Loop Channel II Flow Indication.
In this case, the channel was reading low.
The channel was declared inoperable and the asso-ciated bistables were placed in a tripped condition.
Limiting Condition for Operation Action Statement 3.3.1 Action 7'was entered at 2330 hours0.027 days <br />0.647 hours <br />0.00385 weeks <br />8.86565e-4 months <br />, August 16, 1982.
The signal isolation amplifier was replaced and a channel calibration check was satisfactorily performed.
At 0005 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />, August 17, 1982, No. 24 Reactor Coolant Loop Channel II Flow Indication was declared operable, and Limiting Condition for Operation Action Statement 3.3.1 Action 7 was terminated.
LER 82-085/03L 9p' DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
The cause of both occurrences was determined to be failure of the signal isolation amplifiers.
This caused an inaccurate signal to be sent to the channel flow meter.
Although both occurrences were on the same indication channel, investigation disclosed no common cause for the signal isolation amplifier failures.
The signal isolation amplifier currently installed, shows no indication of malfunction.
ANALYSIS OF OCCURRENCE:
The operability of the protective and Engineered Safety Feature (ESF) Instrumentation Systems and interlocks ensure that; l) the associated ESF action and or reactor trip will be initiated when the parameter monitored by each channel or combination thereof, reaches its setpoint, 2) the specified coincidence logic is maintained, 3) sufficient redundancy is maintained to permit a channel to be out of service for testing or maintenance, and 4) sufficient system functional capability is available for protective and ESF purposes from diverse parameters.
The operability of these systems is required to provide the overall reliability, redundancy and diversity assumed available in the faciltiy design for the protection and mitigation of accident and transient conditions.
The integrated operation of each of these systems is consistent with the assumptions used in the accident analysis.
Redundant Reactor Coolant Loop Flow Indication and trip capability is provided by two other independent channels per loop.
Therefore, this occurrence involved no risk to the health and safety of the general public.
Action Statement 3.3.1 Action 7 requires:
With the number of operable channels one less than the total number of channels, startup and/or power operation may proceed until performance of the next required channel functional test, provided that the inoperable channel is placed in the tripped condition within one hour.
Inoperability of one reactor coolant loop flow channel, therefore, constitutes operation in a degraded mode permitted by a limiting condition for operation, and is reportable in accordance with Technical Specification 6.9.1.9.b.
CORRECTIVE ACTION
As noted, the signal isolation amplifiers were replaced and channel calibrations were satisfactorily performed.
An investi-gation was conducted, however, no common cause of the amplifier failures was discovered.
LER 82-085/03L i FAILURE DATA:
Hagan Corporation Signal Isolation Amplifier Model 110 Prepared By R.
Heller
/
b e
.A General Manager -
Salem Operations SORC Meeting No.
82-80
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| 05000311/LER-1982-001, Supplemental LER 82-001/03X-1:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Stuck Open,Freezing Pressure Sensing Line.Damper Freed, Exercised & Closed | Supplemental LER 82-001/03X-1:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Stuck Open,Freezing Pressure Sensing Line.Damper Freed, Exercised & Closed | | | 05000272/LER-1982-001-03, Pressurizer Overprotection Sys Valve 1PR1 Was Isolated Due to Leakage. on 820107,while Draining Rcs,Valve 1RP2 Would Not Open. Caused by Generic Problem.Reactor Vessel Head Removed | Pressurizer Overprotection Sys Valve 1PR1 Was Isolated Due to Leakage. on 820107,while Draining Rcs,Valve 1RP2 Would Not Open. Caused by Generic Problem.Reactor Vessel Head Removed | | | 05000311/LER-1982-001-03, /03L-0:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Sticking Open,Freezing Pressure Sensing Line.Damper Freed & Closed. Line Thawed | /03L-0:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Sticking Open,Freezing Pressure Sensing Line.Damper Freed & Closed. Line Thawed | | | 05000272/LER-1982-001, Forwards Revised LER 82-001/03X-1.Detailed Event Analysis Encl | Forwards Revised LER 82-001/03X-1.Detailed Event Analysis Encl | | | 05000272/LER-1982-002-01, /01T-0:on 820119,indications of Tube Thinning Were Detected by Eddy Current Exam.Steam Generators 12 & 14 Required Two & Three Sample Insp,Respectively.All Defective Tubes & Tubes Degraded Above 30& Plugged | /01T-0:on 820119,indications of Tube Thinning Were Detected by Eddy Current Exam.Steam Generators 12 & 14 Required Two & Three Sample Insp,Respectively.All Defective Tubes & Tubes Degraded Above 30& Plugged | | | 05000311/LER-1982-002-03, /03L-0:on 820111,2A1 Battery Charger Tripped, Was Reset & Tripped Again.No Problem Found.Subsequent Trip Caused by Difference Between Battery Voltage & Battery Charger Voltage Setting.Personnel Instructed | /03L-0:on 820111,2A1 Battery Charger Tripped, Was Reset & Tripped Again.No Problem Found.Subsequent Trip Caused by Difference Between Battery Voltage & Battery Charger Voltage Setting.Personnel Instructed | | | 05000272/LER-1982-002, Supplemental LER 82-002/01X-2:on 820119,during Surveillance, Indications of Tube Thinning Detected by Eddy Current Exam. Tubes Above 30% Degradation Plugged.Tube R44C62 Sent to Westinghouse for Chemical & Metallurgical Testing | Supplemental LER 82-002/01X-2:on 820119,during Surveillance, Indications of Tube Thinning Detected by Eddy Current Exam. Tubes Above 30% Degradation Plugged.Tube R44C62 Sent to Westinghouse for Chemical & Metallurgical Testing | | | 05000311/LER-1982-002, Supplemental LER 82-002/03X-1:on 820111,battery Charger 2A1 Tripped.Charger Tripped Again Upon Resetting Breaker.Caused by Difference Between Battery & Battery Charger Voltages. Operating Instructions Revised to Adjust Float Vo | Supplemental LER 82-002/03X-1:on 820111,battery Charger 2A1 Tripped.Charger Tripped Again Upon Resetting Breaker.Caused by Difference Between Battery & Battery Charger Voltages. Operating Instructions Revised to Adjust Float Voltage | | | 05000311/LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1982-003-03, /03L-0:on 820106,1B & 1C Diesels Locked Out, Rendering Diesels Inoperable at Same Time.On 820106,diesel Generator 1C Declared Inoperable While Diesel 1B Out of Svc for Maint.Caused by Misinterpretation of Lockout Switch Tag | /03L-0:on 820106,1B & 1C Diesels Locked Out, Rendering Diesels Inoperable at Same Time.On 820106,diesel Generator 1C Declared Inoperable While Diesel 1B Out of Svc for Maint.Caused by Misinterpretation of Lockout Switch Tag | | | 05000311/LER-1982-003-03, /03L-0:on 820112,during Routine Calibr Testing, Radiation Monitor 2R11A Found Out of Calibr.Caused by Instrument Drift.Monitor Recalibr & Tested Satisfactorily | /03L-0:on 820112,during Routine Calibr Testing, Radiation Monitor 2R11A Found Out of Calibr.Caused by Instrument Drift.Monitor Recalibr & Tested Satisfactorily | | | 05000272/LER-1982-004-03, /03L-0:on 820109,primary Coolant Water Sample Results Indicated Excessive Boron Concentration,Constituting Positive Reactivity Change.Caused by Water Draining Out of Steam Generator Tubes.Rcs Rapid Boration Initiated | /03L-0:on 820109,primary Coolant Water Sample Results Indicated Excessive Boron Concentration,Constituting Positive Reactivity Change.Caused by Water Draining Out of Steam Generator Tubes.Rcs Rapid Boration Initiated | | | 05000272/LER-1982-004, Supplemental LER 82-004/03X-1:on 820108,charging Pump 13 Declared Inoperable Due to Component Cooling Water Sys Being Tagged Out for Planned Maint.On 820109,positive Reactivity Change Found in RCS Boron Concentration | Supplemental LER 82-004/03X-1:on 820108,charging Pump 13 Declared Inoperable Due to Component Cooling Water Sys Being Tagged Out for Planned Maint.On 820109,positive Reactivity Change Found in RCS Boron Concentration | | | 05000311/LER-1982-004, Forwards LER 82-004/03X-1.Detailed Event Analysis Encl | Forwards LER 82-004/03X-1.Detailed Event Analysis Encl | | | 05000272/LER-1982-005-01, /01X-1:on 820131,degradation of Fuel Cladding on Fuel Assembly C-04 Discovered.Caused by Fuel Lockup Due to Wedged Fuel Pellet.Fuel Assembly Placed in Spent Fuel Pit. All C Assemblies Scheduled for Reuse in Core | /01X-1:on 820131,degradation of Fuel Cladding on Fuel Assembly C-04 Discovered.Caused by Fuel Lockup Due to Wedged Fuel Pellet.Fuel Assembly Placed in Spent Fuel Pit. All C Assemblies Scheduled for Reuse in Core | | | 05000272/LER-1982-005, Forwards LER 82-005/01X-1.Detailed Event Analysis Encl | Forwards LER 82-005/01X-1.Detailed Event Analysis Encl | | | 05000311/LER-1982-005, Forwards LER 82-005/03L-0.Detailed Event Analysis Encl | Forwards LER 82-005/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-005-03, /03L-0:on 820121,during Performance of M3T Maint Surveillance Test Undervoltage Relay on 2C Vital Bus Actuated at 5.5 Volts Instead of 77.3 Volt Trip Setpoint Value.No Defects Found.Relay Recalibr | /03L-0:on 820121,during Performance of M3T Maint Surveillance Test Undervoltage Relay on 2C Vital Bus Actuated at 5.5 Volts Instead of 77.3 Volt Trip Setpoint Value.No Defects Found.Relay Recalibr | | | 05000272/LER-1982-006-03, /03L-0:on 820113,air Particulate Detector Failed. Cause Not Stated.All Required Containment Purge & Pressure Vacuum Relief Penetrations Isolated.High & Low Speed Filter Paper Drives Replaced | /03L-0:on 820113,air Particulate Detector Failed. Cause Not Stated.All Required Containment Purge & Pressure Vacuum Relief Penetrations Isolated.High & Low Speed Filter Paper Drives Replaced | | | 05000272/LER-1982-006, Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-006, Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-006-03, /03L-0:on 820128,svc Water Flow Indicator Indicated No Flow Condition.Caused by Svc Water Discharge Valve 22SW223 Being Stuck Shut.Valve Opened,Locally Tested & Returned to Svc | /03L-0:on 820128,svc Water Flow Indicator Indicated No Flow Condition.Caused by Svc Water Discharge Valve 22SW223 Being Stuck Shut.Valve Opened,Locally Tested & Returned to Svc | | | 05000272/LER-1982-007-01, /01X-2:on 820211,during Design Review,Discovered That Check Valves 1AF71 & 1AF72 & Associated Piping Not Seismically Analyzed & Protected.Protective Steel Structures Provided Off Seismic Wall | /01X-2:on 820211,during Design Review,Discovered That Check Valves 1AF71 & 1AF72 & Associated Piping Not Seismically Analyzed & Protected.Protective Steel Structures Provided Off Seismic Wall | | | 05000272/LER-1982-007, Forwards LER 82-007/01X-2 | Forwards LER 82-007/01X-2 | | | 05000272/LER-1982-008, Supplemental LER 82-008/03X-1:on 820126,boric Acid Concentrations in Boric Acid Storage Tanks 11 & 12 Found Below Tech Spec Limit.Caused by Dilution of Concentration by Flushing Water in Tank Following Maint.Boric Acid Added | Supplemental LER 82-008/03X-1:on 820126,boric Acid Concentrations in Boric Acid Storage Tanks 11 & 12 Found Below Tech Spec Limit.Caused by Dilution of Concentration by Flushing Water in Tank Following Maint.Boric Acid Added | | | 05000272/LER-1982-008-03, /03L-0:on 820126,sample Results from Boric Acid Tanks Indicated Boric Acid Concentration Below Tech Specs. Refueling Water Storage Tank Low.Core Alterations & Positive Reactivity Changes Suspended.Level Adjusted | /03L-0:on 820126,sample Results from Boric Acid Tanks Indicated Boric Acid Concentration Below Tech Specs. Refueling Water Storage Tank Low.Core Alterations & Positive Reactivity Changes Suspended.Level Adjusted | | | 05000311/LER-1982-008, Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-008-03, /03L-0:on 820128,overpower Delta T Indication for Channel 21 Failed High.Caused by Signal Summator 2T-M412E Having No Output Due to Failed Capacitors. Five Capacitors Replaced | /03L-0:on 820128,overpower Delta T Indication for Channel 21 Failed High.Caused by Signal Summator 2T-M412E Having No Output Due to Failed Capacitors. Five Capacitors Replaced | | | 05000311/LER-1982-009, Forwards LER 82-009/03L-0.Detailed Event Analysis Encl | Forwards LER 82-009/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1982-009, Supplemental LER 82-009/03X-1:on 820118 & 25,Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Area 12 Inoperable for More than 14 Days.Caused by Sys in Manual Mode Due to Maint Outage | Supplemental LER 82-009/03X-1:on 820118 & 25,Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Area 12 Inoperable for More than 14 Days.Caused by Sys in Manual Mode Due to Maint Outage | | | 05000272/LER-1982-009-03, /03L-0:on 820118 & 25,switches for Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Tank Area 12 Had Been in Manual Position for Greater than 14 Days Due to Maint Outage | /03L-0:on 820118 & 25,switches for Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Tank Area 12 Had Been in Manual Position for Greater than 14 Days Due to Maint Outage | | | 05000311/LER-1982-009-03, /03L-0:on 820129,air Particulate Detector Pump Low Flow Alarm Annuniciated.Caused by Incorrect Normal Flow Valve Lineup to Pump.Pump Removed from Normal Flow & Placed in Backup Flow Lineup | /03L-0:on 820129,air Particulate Detector Pump Low Flow Alarm Annuniciated.Caused by Incorrect Normal Flow Valve Lineup to Pump.Pump Removed from Normal Flow & Placed in Backup Flow Lineup | | | 05000311/LER-1982-010-03, /03L-0:on 820201,discrepancy Between Individual Rod Position Indicator (Irpi) & Control Rod Bank Demand Indicator for Rod 2C2 Exceeded 12 Steps in Either Direction. Caused by Incorrect Calibr of Irpi.Irpi Calibr | /03L-0:on 820201,discrepancy Between Individual Rod Position Indicator (Irpi) & Control Rod Bank Demand Indicator for Rod 2C2 Exceeded 12 Steps in Either Direction. Caused by Incorrect Calibr of Irpi.Irpi Calibr | | | 05000272/LER-1982-010-03, /03X-1:on 820201,temporary Hose Connection from Unit 1 Spent Fuel Pool to Unit 2 Exchanger Found Leaking on Auxiliary Bldg 84-ft Elevation.Caused by Improper Clamp Installation.Hose Disconnected | /03X-1:on 820201,temporary Hose Connection from Unit 1 Spent Fuel Pool to Unit 2 Exchanger Found Leaking on Auxiliary Bldg 84-ft Elevation.Caused by Improper Clamp Installation.Hose Disconnected | | | 05000311/LER-1982-010, Forwards LER 82-010/03L-0.Detailed Event Analysis Encl | Forwards LER 82-010/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1982-010, Forwards LER 82-010/03X-1.Detailed Event Analysis Encl | Forwards LER 82-010/03X-1.Detailed Event Analysis Encl | | | 05000311/LER-1982-011, Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-011-03, /03L-0:on 820205,during Radiological Survey of Hot Laundry Trailer Area,Technician Discovered Lint from Dryer Exhaust of Trailer B Revealing Traces of Cs-137,Co-60 & Co-58.New Trailer & Lint Collector Installed | /03L-0:on 820205,during Radiological Survey of Hot Laundry Trailer Area,Technician Discovered Lint from Dryer Exhaust of Trailer B Revealing Traces of Cs-137,Co-60 & Co-58.New Trailer & Lint Collector Installed | | | 05000272/LER-1982-011, Forwards LER 82-011/03X-1.Detailed Event Analysis Encl | Forwards LER 82-011/03X-1.Detailed Event Analysis Encl | | | 05000272/LER-1982-012, Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-012, Forwards LER 82-012/03X-1.Detailed Event Analysis Encl | Forwards LER 82-012/03X-1.Detailed Event Analysis Encl | | | 05000311/LER-1982-012-03, /03X-1:on 820209,steam Generator Level Channel 2 Displayed Erratic Behavior,Indicating Drift.Apparently Caused by Intermittent Ground on Signal Lead.Ground Eliminated by Lifting Leads While Troubleshooting Problem | /03X-1:on 820209,steam Generator Level Channel 2 Displayed Erratic Behavior,Indicating Drift.Apparently Caused by Intermittent Ground on Signal Lead.Ground Eliminated by Lifting Leads While Troubleshooting Problem | | | 05000272/LER-1982-012-03, /03L-0:on 820223,operator Found Significant Amount of Chromated Water on Floor in Diesel Generator 1B Cubicle. Caused by Leakage on Right Side Jacket Water Heater.Jacket Water Heaters Replaced | /03L-0:on 820223,operator Found Significant Amount of Chromated Water on Floor in Diesel Generator 1B Cubicle. Caused by Leakage on Right Side Jacket Water Heater.Jacket Water Heaters Replaced | | | 05000272/LER-1982-013-03, /03L-0:on 820301,control Room Operator Closed Pressurizer Relief Valve 1PR1 When Valve 1PR2 Was Still Closed.Caused by Operator Error.Operator Counseled by Senior Shift Supervisor | /03L-0:on 820301,control Room Operator Closed Pressurizer Relief Valve 1PR1 When Valve 1PR2 Was Still Closed.Caused by Operator Error.Operator Counseled by Senior Shift Supervisor | | | 05000311/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-013-03, L-0:on 820215,shift Supervisor Informed That Two 4-inch Core Bores Opened on 78-ft Elevation Between Mechanical & Electrical Penetration Areas.No Fire Watch Posted.Caused by Inadvertently Posting Watch on Wrong Unit | L-0:on 820215,shift Supervisor Informed That Two 4-inch Core Bores Opened on 78-ft Elevation Between Mechanical & Electrical Penetration Areas.No Fire Watch Posted.Caused by Inadvertently Posting Watch on Wrong Unit | | | 05000272/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-014-03, /03L-0:on 820219,steam Generator 21 Level Channel 2 Read 20% Higher than Channels 3 & 4.Channel 2 Declared Inoperable.Cause Unknown.Transmitter Tested & Found Satisfactory.Sensing Lines Blown Down to Remove Solids | /03L-0:on 820219,steam Generator 21 Level Channel 2 Read 20% Higher than Channels 3 & 4.Channel 2 Declared Inoperable.Cause Unknown.Transmitter Tested & Found Satisfactory.Sensing Lines Blown Down to Remove Solids | | | 05000272/LER-1982-014-03, /03L-0:on 820306,wind Speed Indications for 150 & 300-ft Elevations Failed.Local Indications Also Failed. Caused by iced-up Anemometers.Anemometers Thawed & Declared Operable | /03L-0:on 820306,wind Speed Indications for 150 & 300-ft Elevations Failed.Local Indications Also Failed. Caused by iced-up Anemometers.Anemometers Thawed & Declared Operable | | | 05000311/LER-1982-014, Forwards LER 82-014/03L-0.Detailed Event Analysis Encl | Forwards LER 82-014/03L-0.Detailed Event Analysis Encl | |
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