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Category:Letter
MONTHYEARML25013A3062025-01-23023 January 2025 Independent Spent Fuel Storage Installation Security Inspection Plan ML24366A0332024-12-31031 December 2024 Documentary Evidence of Performance Bond IR 05000302/20240012024-09-23023 September 2024 Accelerated Decommissioning Partners (ADP) CR3, LLC, Crystal River Unit 3, NRC Inspection Report No. 05000302/2024001 ML24240A1692024-09-18018 September 2024 Cy 2023 Summary of Decommissioning Trust Fund Status ML24226B2392024-08-27027 August 2024 Application for License Amendment Request to Add License Condition to Include License Termination Plan Requirements – Acknowledgement of Withdrawal ML24179A0702024-07-26026 July 2024 SHPO S106 Completion Crystal River Unit 3 ML24205A2202024-07-24024 July 2024 Tribal S106 Completion Crystal River Unit 3_Miccosukee Tribe of Florida ML24179A0912024-07-24024 July 2024 Tribal S106 Completion Crystal River Unit 3: Seminole Tribe of Florida ML24205A2192024-07-24024 July 2024 Tribal S106 Completion Crystal River Unit 3: Muscogee Nation ML24205A2182024-07-24024 July 2024 Tribal S106 Completion Crystal River Unit 3: Seminole Nation of Oklahoma ML24190A1912024-07-0808 July 2024 Fws Concurrence for Crystal River Unit 3 ML24172A2552024-06-20020 June 2024 Fws to NRC Species List: Florida Ecological Services Field Office 06/20/2024 ML24170A9242024-06-18018 June 2024 024-0023697 Crystal River License Termination Plan Unit 3 ML24151A6482024-06-0303 June 2024 Changes in Reactor Decommissioning Branch Project Management Assignments for Some Decommissioning Facilities ML24114A2262024-04-24024 April 2024 Amended Special Package Authorization for the Cr3 Middle Package (Crystal River 3 Middle Package - Docket No. 71-9393) IR 05000302/20230022024-04-17017 April 2024 Accelerated Decommissioning Partners (ADP) CR3, LLC, Crystal River Unit 3 - NRC Inspection Report No. 05000302/2023002 ML24054A0812024-04-0202 April 2024 Tribal S106 Initiation Crystal River Unit 3-Osceola, Marcellus ML24054A0582024-04-0202 April 2024 Achp S106 Initiation Crystal River Unit 3 - Letter 1 ML24079A2482024-04-0202 April 2024 Tribal S106 Initiation Crystal River Unit 3-Hill, David Hill ML24079A2492024-04-0202 April 2024 Tribal S106 Initiation Crystal River Unit 3-Johnson, Lewis Johnson ML24079A2472024-04-0202 April 2024 Tribal S106 Initiation Crystal River Unit 3-Cypress, Talbert ML24054A0612024-04-0202 April 2024 Request to Initiate Section 106 Consultation Regarding the License Termination Plan for Crystal River Unit 3 in Citrus County, Florida ML24089A0362024-03-29029 March 2024 Response to Audit Plan in Support of Accelerated Decommissioning Partners and Request to Add License Condition to Include License Termination Plan Requirements. W/Enclosures 1 to 5 ML24073A1922024-03-11011 March 2024 Fws to NRC, List of Threatened and Endangered Species That May Occur in Your Proposed Project Location or May Be Affected by Your Proposed Project ML24054A6452024-02-29029 February 2024 Letter - Reply to Request for RAI Extension Related to the Crystal River License Termination Plan ML24030A7482024-02-12012 February 2024 Audit Report Cover Letter and Report - Crystal River Unit 3 Nuclear Generating Plant LTP ML23342A0942024-01-0909 January 2024 – Independent Spent Fuel Storage Installation Security Inspection Plan ML23354A0632023-12-22022 December 2023 Cover Letter - Crystal River License Termination Plan Request for Additional Information ML23345A1882023-12-0606 December 2023 Fws to NRC Crystal River Species List of Threatened and Endangered Species That May Occur in Your Proposed Project Location or May Be Affected by Your Proposed Project ML23313A1322023-11-15015 November 2023 Request for Additional Information for the Environmental Assessment of the License Termination Plan for Crystal River Unit 3 Nuclear Generating Plant ML23310A0712023-11-0707 November 2023 Audit Plan Cover Letter - Crystal River Unit 3 Nuclear Generating Plant LTP ML23187A1112023-07-25025 July 2023 Acceptance of Requested Licensing Action License Request to Add License Condition to Include License Termination Plan Requirements ML23107A2722023-06-13013 June 2023 Letter Transmitting NRC Survey Results for East Settling Pond ML23160A2962023-06-0909 June 2023 Response to Crystal River, Unit 3 – Supplemental Information Needed for Acceptance on the Application for a License Amendment Regarding Approval of the License Termination Plan ML23107A2732023-06-0707 June 2023 Orise Independent Survey Report Dcn 5366-SR-01-0 IR 05000302/20220032023-05-25025 May 2023 Accelerated Decommissioning Partners (ADP) CR3, LLC, Crystal River Unit 3 - NRC Inspection Report No. 05000302/2022003 ML23103A1902023-04-19019 April 2023 Request for Supplemental Information Cover Letter ML23058A2532023-03-22022 March 2023 Accelerated Decommissioning Partners (ADP) CR3, LLC, Crystal River, Unit 3 - NRC Inspection Report No. 05000302/2022003 ML22361A1022023-02-24024 February 2023 Reactor Decommissioning Branch Project Management Changes for Some Decommissioning Facilities and Establishment of Backup Project Manager for All Decommissioning Facilities ML22265A0192022-09-26026 September 2022 Nuclear Generating Plant - U.S. Nuclear Regulatory Commissions Analysis of ADP CR3, LLCs Decommissioning Funding Status Report (License No. DPR-72, Docket Nos. 50-302 and 72-1035) IR 05000302/20220022022-08-0909 August 2022 Accelerated Decommissioning Partners (ADP) CR3, LLC, Crystal River Unit 3 - NRC Inspection Report 05000302/2022002 IR 05000302/20220012022-05-0303 May 2022 Accelerated Decommissioning Partners (ADP) CR3, LLC, Crystal River Unit 3 - NRC Inspection Report 05000302/2022001 ML22116A1752022-04-27027 April 2022 Accelerated Decommissioning Partners (ADP) CR3, LLC, Crystal River Unit 3- Independent Spent Fuel Storage Installation Security Inspection Report 07201035/2022401 ML22105A3992022-04-18018 April 2022 Nuclear Generating Plant - Change in NRC Project Manager ML22011A1362022-01-31031 January 2022 Independent Spent Fuel Storage Installation Security Inspection Plan IR 05000302/20210042022-01-24024 January 2022 Accelerated Decommissioning Partners (ADP) CR3, LLC, Crystal River Unit 3 - NRC Inspection Report No. 05000302/2021004 ML22024A2142022-01-24024 January 2022 Nuclear Generating Plant - NMFS NRC Letter - Crystal River Energy Complex Biological Opinion Status (License No. DPR-72, Docket Nos. 50-302 and 72-1035) ML21351A0052021-12-20020 December 2021 NRC Analysis of ADP CR3, LLC Decommissioning Funding Status Report for the Crystal River Unit 3 Nuclear Generating Plant (License No. DPR-72, Docket Nos. 50-302 and 72-1035) ML21322A2702021-11-24024 November 2021 Nuclear Generating Plant - Issuance of Amendment No. 260 Approving the Independent Spent Fuel Storage Installation Only Security Plan, Rev 3 IR 05000302/20210032021-11-0909 November 2021 Accelerated Decommissioning Partners (ADP) CR3, LLC, Crystal River Unit 3 - NRC Inspection Report Nos. 05000302/2021003 and 07201035/2021001 2025-01-23
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000302/LER-2013-001, Regarding Valid Actuation of an Emergency Diesel Generator Due to a Spurious Fault on a Breaker Non-Segregated Bus Duct2013-07-25025 July 2013 Regarding Valid Actuation of an Emergency Diesel Generator Due to a Spurious Fault on a Breaker Non-Segregated Bus Duct 05000302/LER-2010-001-01, For Crystal River, Unit 3 Re As-Found Cycle 16 Pressurizer Code Safety Valve Setpoints Outside Improved Technical Specification Limit2011-01-17017 January 2011 For Crystal River, Unit 3 Re As-Found Cycle 16 Pressurizer Code Safety Valve Setpoints Outside Improved Technical Specification Limit 05000302/LER-2009-004, Regarding Main Steam Safety Valve Setpoints Outside Required Tolerance Longer than Allowed by Technical Specifications2009-11-20020 November 2009 Regarding Main Steam Safety Valve Setpoints Outside Required Tolerance Longer than Allowed by Technical Specifications 05000302/LER-2009-003, Regarding Manual Reactor Trip Due to Group 7 Control Rods Insertion Caused by Inadequately Protected Test Jumper2009-10-21021 October 2009 Regarding Manual Reactor Trip Due to Group 7 Control Rods Insertion Caused by Inadequately Protected Test Jumper ML1010603452009-10-0707 October 2009 Event Number 45416, Crystal River, Regarding Discovery of a Containment Separation 05000302/LER-2009-002, Regarding in Technical Specification 3.0.3 Greater than One Hour Due to Loss of Motor Control Center During Testing2009-06-22022 June 2009 Regarding in Technical Specification 3.0.3 Greater than One Hour Due to Loss of Motor Control Center During Testing 05000302/LER-2009-001, Re Manual Reactor Trip Due to Loss of a 4160V Unit Bus Loads Caused by Incorrectly Connected Test Leads2009-03-20020 March 2009 Re Manual Reactor Trip Due to Loss of a 4160V Unit Bus Loads Caused by Incorrectly Connected Test Leads 05000302/LER-2008-004, Regarding Motor-Operated Main Feedwater Isolation Valve Inoperable Due to Motor Rotor Oxidation/Corrosion2009-01-28028 January 2009 Regarding Motor-Operated Main Feedwater Isolation Valve Inoperable Due to Motor Rotor Oxidation/Corrosion 05000302/LER-2008-003, Manual Reactor Trip Due to Main Feedwater System Oscillations Caused by an Inconsistent Procedure2008-10-21021 October 2008 Manual Reactor Trip Due to Main Feedwater System Oscillations Caused by an Inconsistent Procedure 05000302/LER-2008-002, Emergency Feedwater Actuation on Low Steam Generator Level Due to Feedwater Pump Speed Tuning2008-04-29029 April 2008 Emergency Feedwater Actuation on Low Steam Generator Level Due to Feedwater Pump Speed Tuning 05000302/LER-2008-001, Regarding Software Change Causes Inoperability of Redundant Core Subcooling Monitors for Longer than TS Allowable2008-03-20020 March 2008 Regarding Software Change Causes Inoperability of Redundant Core Subcooling Monitors for Longer than TS Allowable 05000302/LER-2007-002, Regarding Reactor Trip Caused by Failed Circuit Board in the Main Feedwater Integrated Control System2007-04-19019 April 2007 Regarding Reactor Trip Caused by Failed Circuit Board in the Main Feedwater Integrated Control System 05000302/LER-2007-001, Re Design Oversight Results in 10 CFR 50, Appendix R, Cable Separation Criteria Not Being Met2007-03-0909 March 2007 Re Design Oversight Results in 10 CFR 50, Appendix R, Cable Separation Criteria Not Being Met 05000302/LER-2006-002, Regarding Emergency Diesel Generator in a Condition Prohibited by Technical Specifications Due to Mispositioning2006-12-14014 December 2006 Regarding Emergency Diesel Generator in a Condition Prohibited by Technical Specifications Due to Mispositioning 05000302/LER-2006-001, Re Train B Raw Water System in a Condition Prohibited by Technical Specifications Due to Equipment Failure2006-12-11011 December 2006 Re Train B Raw Water System in a Condition Prohibited by Technical Specifications Due to Equipment Failure 05000302/LER-2005-005, Inadvertent B Train Engineered Safeguards Actuation Due to Inadequate Procedure Guidance2006-01-11011 January 2006 Inadvertent B Train Engineered Safeguards Actuation Due to Inadequate Procedure Guidance 05000302/LER-2005-004, Re Motor-Operated Main Feedwater Isolation Valve Inoperable Due to Motor Rotor Oxidation/Corrosion2005-12-14014 December 2005 Re Motor-Operated Main Feedwater Isolation Valve Inoperable Due to Motor Rotor Oxidation/Corrosion 05000302/LER-2005-003, Re Manual Reactor Trip and Subsequent Emergency Feedwater Actuation Due to Condensate Pump Loss2005-11-30030 November 2005 Re Manual Reactor Trip and Subsequent Emergency Feedwater Actuation Due to Condensate Pump Loss 05000302/LER-2005-002, Regarding Emergency Diesel Generator EDGD-1A Inoperability for Period Longer than Permitted2005-05-16016 May 2005 Regarding Emergency Diesel Generator EDGD-1A Inoperability for Period Longer than Permitted 05000302/LER-2005-001, Regarding Design Change Creates Engineered Safeguards Bus Protective Relay Scheme Single Failure Vulnerability2005-03-23023 March 2005 Regarding Design Change Creates Engineered Safeguards Bus Protective Relay Scheme Single Failure Vulnerability 05000302/LER-2004-004, Regarding NUREG-1022 Clarification Required Reporting of Previous Steam Generator Tube Inspection Results2004-11-22022 November 2004 Regarding NUREG-1022 Clarification Required Reporting of Previous Steam Generator Tube Inspection Results 05000302/LER-2004-003, Re Reactor Trip and Emergency Feedwater Actuation Caused by 230 Kilovolt Switchyard/Transmission Faults2004-10-29029 October 2004 Re Reactor Trip and Emergency Feedwater Actuation Caused by 230 Kilovolt Switchyard/Transmission Faults 05000302/LER-2004-001, Regarding Actuation of the Reactor Protection System and Emergency Feedwater System Caused by a Failed Circuit Board within the Main Feedwater Integrated Control System on March 24, 20042004-05-18018 May 2004 Regarding Actuation of the Reactor Protection System and Emergency Feedwater System Caused by a Failed Circuit Board within the Main Feedwater Integrated Control System on March 24, 2004 05000302/LER-2003-005, Regarding Reactor Trip Caused by Loss of Feedwater While Troubleshooting Feedwater Pump Control Problems2004-03-22022 March 2004 Regarding Reactor Trip Caused by Loss of Feedwater While Troubleshooting Feedwater Pump Control Problems 05000302/LER-2001-005-01, Regarding Loss of Steam to the Operating Main Feedwater Pump Results in Actuation of the Emergency Feedwater System2004-02-26026 February 2004 Regarding Loss of Steam to the Operating Main Feedwater Pump Results in Actuation of the Emergency Feedwater System 05000302/LER-2003-004, Regarding Redundant Channels of a Post-Accident Monitoring Function Not Operable Due to Reversed Power Supplies2003-12-0808 December 2003 Regarding Redundant Channels of a Post-Accident Monitoring Function Not Operable Due to Reversed Power Supplies 05000302/LER-2003-002, Regarding Main Steam Safety Valve Setpoints Below Required Tolerance Longer than Allowed by Technical Specifications2003-11-20020 November 2003 Regarding Main Steam Safety Valve Setpoints Below Required Tolerance Longer than Allowed by Technical Specifications 05000302/LER-2003-003, Regarding Reactor Coolant System Pressure Boundary Leakage Limit Exceeded Due to Pressurizer Instrument Tap Nozzle Cracks2003-11-19019 November 2003 Regarding Reactor Coolant System Pressure Boundary Leakage Limit Exceeded Due to Pressurizer Instrument Tap Nozzle Cracks 05000302/LER-2003-001, Regarding Incorrectly Set Motor Overload Relays Resulted in Loss of Both Control Complex Chillers2003-08-0707 August 2003 Regarding Incorrectly Set Motor Overload Relays Resulted in Loss of Both Control Complex Chillers 05000302/LER-2002-002, For Crystal River Unit 3 Regarding Reactor Trip Due to Substation Generator Output Breaker Relay Mis-Operation2002-12-10010 December 2002 For Crystal River Unit 3 Regarding Reactor Trip Due to Substation Generator Output Breaker Relay Mis-Operation 05000302/LER-2002-001, Automatic Start of an Emergency Diesel Generator Due to Loss of the Offsite Power Transformer2002-08-14014 August 2002 Automatic Start of an Emergency Diesel Generator Due to Loss of the Offsite Power Transformer 2013-07-25
[Table view] |
LER-2009-003, Regarding Manual Reactor Trip Due to Group 7 Control Rods Insertion Caused by Inadequately Protected Test Jumper |
Event date: |
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Report date: |
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Reporting criterion: |
10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(i)
10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded
10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition
10 CFR 50.73(a)(2)(iii)
10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability
10 CFR 50.73(a)(2)(viii)(A)
10 CFR 50.73(a)(2)(viii)(B)
10 CFR 50.73(a)(2)(ix)(A)
10 CFR 50.73(a)(2)(x) |
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3022009003R00 - NRC Website |
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text
Progress Energy Crystal River Nuclear Plant Docket No. 50-302 Operating License No. DPR-72 Ref: 10 CFR 50.73 October 21, 2009 3F1009-04 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555-0001
Subject:
LICENSEE EVENT REPORT 50-302/2009-003-00
Dear Sir:
Please find enclosed Licensee Event Report (LER) 50-302/2009-003-00. The LER discusses a manual reactor trip due to insertion of the Group 7 control rods caused by inadvertent contact of an inadequately protected (fused) test jumper to an unintended point.
This report is being submitted pursuant to 1 OCFR50.73(a)(2)(iv)(A).
No new regulatory commitments are made in this letter.
If you have any questions regarding this submittal, please contact Mr. Dan Westcott, Superintendent, Licensing and Regulatory Programs at (352) 563-4796.
Sil James W. Holt Plant General Manager Crystal River Nuclear Plant JWH/dwh Enclosure xc:
Regional Administrator, Region II Senior Resident Inspector NRR Project Manager Progress Energy Florida, Inc.
Crystal River Nuclear Plant 15760 W. Power Line Street Crystal River, FL 34428 I1Jf":,
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 08/31/2010 (9-2007)
, the NRC may digits/characters for each block) not conduct or sponsor, and a person is not required to respond to, the information collection.
- 3. PAGE CRYSTAL RIVER UNIT 3 05000302 1 of 6
- 4. TITLE Manual Reactor Trip Due To Group 7 Control Rods Insertion Caused By Inadequately Protected Test Jumper
- 5. EVENT DATE
- 6. LER NUMBER
- 7. REPORT DATE
- 8. OTHER FACILITIES INVOLVED SEQUENTIAL REV MONTH FACTY NAME DOCKET NUMBER NUMBER NO.
05000 FACILITY NAME DOCKET NUMBER
- - 003 -
00 10 21 2009 05000
- 11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR§: (Check al/that apply) 20.2201 (b) 20.2201(d) 20.2203(a)(1) 20.2203(a)(2)(i) 20.2203(a)(2)(ii) 20.2203(a)(2)(iii) 20.2203(a)(2)(iv) 20.2203(a)(2)(v) 20.2203(a)(2)(vi)
El El El 1:1 El El El 1J I-]
20.2203(a)(3)(i) 20.2203(a)(3)(ii) 20.2203(a)(4) 50.36(c)(1)(i)(A) 50.36(c)(1 )(ii)(A) 50.36(c)(2) 50.46(a)(3)(ii) 50.73(a)(2)(i)(A) 50.73(a)(2)(i)(B)
[I '50.73(a)(2)(i)(C)
[I 50.73(a)(2)(ii)(A)
El 50.73(a)(2)(ii)(B)
El 50.73(a)(2)(iii)
Z 50.73(a)(2)(iv)(A)
[I 50.73(a)(2)(v)(A)
El 50.73(a)(2)(v)(B)
El 50.73(a)(2)(v)(C)
[I 50.73(a)(2)(v)(D)
El El El El El E]
El El 50.73(a)(2)(vii) 50.73(a)(2)(viii)(A) 50.73(a)(2)(viii)(B) 50.73(a)(2)(ix)(A) 50.73(a)(2)(x) 73.71 (a)(4) 73.71 (a)(5)
OTHER Specify in Abstract below or in NRC Form 366A
- 12. LICENSEE CONTACT FOR THIS LER FACILITY NAME TELEPHONE NUMBER (Include Area Code)
Dennis W. Herrin, Lead Engineer (Licensing and Regulatory Programs) 352-563-4633SYMANU-REPORTABLE CS SYSTM C NU-REPORTABLE
CAUSE
SYTMCOMPONENT FACTURER TO EPIX
CAUSE
SYTMCPOETATUR TOPX FATRE O
PXFACTURER TO EPIX
- 14. SUPPLEMENTAL REPORT EXPECTED
- 15. EXPECTED MONTH DAY YEAR SUBMISSION El YES (If yes, complete 15. EXPECTED SUBMISSION DATE) 0 NO DATE ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines)
At 11:00, on August 24, 2009, Progress Energy Florida, Inc. (PEF), Crystal River Unit 3 (CR-3) was operating in MODE 1 (POWER OPERATION) at 100 percent RATED THERMAL POWER when the Control Room staff received multiple alarms and observed the Group 7 control rods fully insert into the reactor core. The reactor was manually tripped prior to automatic actuation of the Reactor Protection System (RPS). Prior to this event, electricians were implementing Preventive Maintenance procedure PM-126, "Electrical Checks of CRD [Control Rod Drive]
Power Train." When the Integrated Control System was placed in Automatic, the output driver within the Group 7 programmer caused an erroneous phase sequence to the control rod drive stators, culminating in inadequate magnetic force to restrain the rods from dropping during movement. The RPS responded as expected to the manual trip signal, control rods fully inserted and safety systems functioned as required. No reduction in the public health and safety was created. The programmer failure was caused by inadvertent test jumper contact while using an improperly fused test jumper. This caused an over-current failure of the output driver within the programmer. The programmer was replaced and PM-1 26 was placed on administrative hold.
This report is submitted under 1 OCFR50.73(a)(2)(iv)(A). No previous similar occurrence has been reported to the NRC.
NRC FORM 366 (9-2007)
PRINTED ON RECYCLED PAPERU.S. NUCLEAR REGULATORY COMMISSION (9-2007)
LICENSEE EVENT REPORT (LER)
- 1. FACILITY NAME
- 2. DOCKET
- 6. LER NUMBER
- 3. PAGE YEAR SEQUENTIAL I REVISION YEAR NUMBER NUMBER CRYSTAL RIVER UNIT 3 05000-302 2009 003 00 2
OF 6
EVENT DESCRIPTION
At 11:00, on August 24, 2009, Progress Energy Florida, Inc. (PEF), Crystal River Unit 3 (CR-3) was operating in MODE 1 (POWER OPERATION) at 100 percent RATED THERMAL POWER when the Control Room staff received multiple alarms and observed all eight of the Group 7 control rods [AA, ROD] fully insert into the reactor core [AC]. The reactor was manually tripped prior to automatic actuation of the Reactor Protection System (RPS) [JD]. Emergency Operating Procedure EOP-2, "Vital System Status Verification," was immediately entered before eventually transitioning to EOP-1 0, "Post-Trip Stabilization," at 11:28, on August 24, 2009.
The Group 7 control rods are the controlling group at CR-3. They are expected to insert and withdraw in small increments corresponding to Integrated Control System (ICS) [JA] commands when the ICS is in Automatic. Movement of the rods is supervised by a programmer/controller (programmer) [AA, PMC] dedicated to Group 7. It is a microcontroller based component which responds to commands from ICS (or alternately, manual control) by sequencing the firing of the six phases of the control rod drive stators, as needed, to provide motion. If no movement requests are initiated, the programmer will maintain two phases continuously energized to hold the rods in a fixed position. If the programmer does not provide any Silicon Controlled Rectifier (SCR) [AA, SCR] firing demand outputs, the rods will be released. The ICS signal is provided to the programmer via relays to move rods, depending on the command initiated.
Prior to this event, experienced electricians were in the process of implementing Preventive Maintenance procedure PM-126, "Electrical Checks of CRD [Control Rod Drive] Power Train."
Shortly after completing Section 4.6, which performs electrical checks of the Group 7 regulating power supply, the Group 7 control rod drives were transferred back from the Auxiliary supply to their Normal supply and the ICS was placed back into Automatic. After being placed back in Automatic, the Neutron Error signal monitored by ICS approached the set-point, corresponding to an automatic rod movement demand. The expected response to a movement demand is that the ICS command would be received by the CRD command logic. It would then be passed on along with the speed ("run" speed when in Automatic) to the controlling group's (Group 7) programmer. The programmer should translate the input into the proper sequence before it is output to the Gate Drives which are used to fire the SCRs, resulting in repositioning the Group 7 rods to provide correction to the Neutron Error. When fired by the Gate Drives, the SCRs output 120VDC to their associated Control Rod Drive Stator coil. The programmer should fire SCRs in a 2-3-2-3 phase sequence for rod movement or simply maintain 2 phases steady for holding rods.
In this event, the first time rod movement was requested by ICS after transferring back to Automatic, the Group 7 control rods erroneously responded and dropped into the core. The deviation between the expected response and the actual response was that rather than moving incrementally in accordance with the received commands, the rods dropped completely into the core.
Upon initiation of the manual reactor trip, the main turbine [TA] automatically tripped and the 'A' and 'B' 4160V Unit Buses [EB, BUS] transferred from the Unit Auxiliary Transformer [EB, XMFR] to the Startup Transformer per design.PRINTED ON RECYCLED PAPERPRINTED ON RECYCLED PAPERU.S. NUCLEAR REGULATORY COMMISSION (9-2007)
LICENSEE EVENT REPORT (LER)
- 1. FACILITY NAME
- 2. DOCKET
- 6. LER NUMBER
- 3. PAGE YER SEQUENTIAL REVISION YEAR NUMBER NUMBER CRYSTAL RIVER UNIT 3 05000-302 2009 003 00 3
OF 6
No structures, systems or components were inoperable at the start of the event that contributed to the event. No other pertinent maintenance or surveillance activities were in progress. Plant protection and non-protection systems operated normally during the manual reactor trip, with the exception of the following:
Four (4) Main Steam Safety Valves (MSSVs) [SB, RVI that opened required operator action to lower pressure in accordance with EOP-1 0 guidance to reseat post-trip.
When the programmer for Group 7 failed, Rod 7-5 indicated a slower drop response than the other rods in Group 7. (Nuclear Condition Report (NCR) 351744)
Pressure pulsations occurred in various Condensate System [SD] lines until Condensate Pump CDP-1B [SD, P] was re-coupled. (NCR 351741)
Manual actuation of the RPS is reportable to the NRC. At 12:48, on August 24, 2009, a non-emergency four-hour notification was made to the NRC Operations Center (Event Number 45286) in accordance with 1 OCFR50.72(b)(2)(iv)(B). This report is being submitted pursuant to 1 OCFR50.73(a)(2)(iv)(A).
SAFETY CONSEQUENCES
Manual actuation of the RPS occurred to shut down the reactor while the Main Feedwater System [SJ] maintained adequate Once-Through Steam Generator (OTSG) [SB, SG] levels.
Upon initiation of the manual reactor trip, the RPS responded as expected, control rods fully inserted and safety systems functioned as required. No challenges to the RPS setpoints were identified. Both Main Feedwater Pumps [SJ, P] remained in operation throughout this event.
No Emergency Feedwater Initiation and Control System [JB] actuation occurred or was required.
The event did not result in the release of radioactive material. No design safety limits were exceeded and no fission product barriers or components were damaged as a result. The manual reactor trip is bounded by the Final Safety Analysis Report accident analysis.
Based on the above discussion, PEF concludes that the RPS performed as designed and did not represent a reduction in the public health and safety. Since no loss of safety function occurred, this event does not meet the Nuclear Energy Institute (NEI) definition of a Safety System Functional Failure (reference NEI 99-02, Revision 6).
CAUSE
The unexpected drop of the Group 7 control rods was due to the failure of the programmer caused by inadvertent test jumper contact during PM-i 26, using an improperly fused test jumper. These two conditions caused an over-current failure of the output driver within the Group 7 CRD programmer, causing an erroneous phase sequence to the control rod drive stators, culminating in inadequate magnetic force to restrain the rods from dropping during movement. The improper placement of an improperly fused jumper is a combination of twoPRINTED ON RECYCLED PAPERPRINTED ON RECYCLED PAPERU.S. NUCLEAR REGULATORY COMMISSION (9-2007)
LICENSEE EVENT REPORT (LER)
- 1. FACILITY NAME
- 2. DOCKET
- 6. LER NUMBER
- 3. PAGE YEAR SEQUENTIAL REVISION YEAR NUMBER NUMBER CRYSTAL RIVER UNIT 3 105000-302 2009 003 00 4
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inappropriate acts. Since a proper fuse in the test jumper alone would have prevented the event, it is considered to be the root cause for this event.
PM-126 directs use of a fused jumper, with a current limit of 0.1 amp. The jumper fuse was checked and found to be a 1.0 amp fuse. This is not consistent with the procedure, and is not adequate to protect the associated equipment which has a maximum current rating of 0.5 amp.
The jumper made inadvertent contact with a positive voltage/current source. It is feasible that the contact was momentary, and unknown to the worker, as the jumper may have simply brushed across an adjacent terminal on the way to the intended terminal.
CORRECTIVE ACTIONS
- 1.
Surveillance Procedure SP-1 02, "Control-Rod Drop Time Tests," was performed and demonstrated that control rod 7-5 will perform as required for plant shutdown conditions if the programmer releases the control rod normally. NCR 351744 was initiated.
- 2.
A walkdown was performed on the Condensate System in accordance with Administrative Instruction Al-1701, "System Engineering Standards." No visible damage from the pressure pulsation was identified. NCR 351741 was initiated.
- 3.
The programmer for the Group 7 control rods was replaced under Work Order 1609125-03.
- 4.
An accountability session was conducted with personnel qualified to perform PM-126 and their Supervisors. Inadequate use of human performance tools regarding confirmation of jumper fuse rating and proper jumper placement for this event were discussed.
- 5.
PM-126 has been placed on Administrative Hold pending human performance improvements.
- 6.
Additional corrective actions are identified in NCR 351705.
PREVIOUS SIMILAR EVENTS
No previous similar events have been reported to the NRC.
ATTACHMENTS -Abbreviations, Definitions, and Acronyms - List of CommitmentsPRINTED ON RECYCLED PAPERPRINTED ON RECYCLED PAPERU.S. NUCLEAR REGULATORY COMMISSION (9-2007)
LICENSEE EVENT REPORT (LER)
- 1. FACILITY NAME
- 2. DOCKET
- 6. LER NUMBER
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Abbreviations, Definitions, and Acronyms Al Administrative Instruction CFR Code of Federal Regulations CR-3 Crystal River Unit 3 CRD Control rod Drive CDP Condensate System Pump EOP Emergency Operating Procedure ICS Integrated Control System MSSV Main Steam Safety Valve NCR Nuclear Condition Report NEI Nuclear Energy Institute NRC Nuclear Regulatory Commission PEF Progress Energy Florida, Inc.
PM Preventive Maintenance RPS Reactor Protection System SCR Silicon Controlled Rectifier SP Surveillance Procedure V
Volt Vdc Volts direct current NOTES:
Improved Technical Specification Defined terms appear capitalized in LER text
{e.g., MODE 1}.
Defined terms/acronyms/abbreviations appear in parenthesis when first used
{e.g., Reactor Building (RB)}.
EIIS codes appear in square brackets {e.g., reactor building penetration [NH, PEN]}PRINTED ON RECYCLED PAPERPRINTED ON RECYCLED PAPERU.S. NUCLEAR REGULATORY COMMISSION (9-2007)
LICENSEE EVENT REPORT (LER)
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- 2. DOCKET
- 6. LER NUMBER
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LIST OF COMMITMENTS The following table identifies those actions committed by PEF in this document. Any other actions discussed in the submittal represent intended or planned actions by PEF. They are described to the NRC for the NRC's information and are not regulatory commitments. Please notify the Superintendent, Licensing and Regulatory Programs of any questions regarding this document or any associated regulatory commitments.
COMMITMENT
DUE DATE No new regulatory commitments are contained in this N/A submittal.PRINTED ON RECYCLED PAPER
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05000302/LER-2009-001, Re Manual Reactor Trip Due to Loss of a 4160V Unit Bus Loads Caused by Incorrectly Connected Test Leads | Re Manual Reactor Trip Due to Loss of a 4160V Unit Bus Loads Caused by Incorrectly Connected Test Leads | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000302/LER-2009-002, Regarding in Technical Specification 3.0.3 Greater than One Hour Due to Loss of Motor Control Center During Testing | Regarding in Technical Specification 3.0.3 Greater than One Hour Due to Loss of Motor Control Center During Testing | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000302/LER-2009-003, Regarding Manual Reactor Trip Due to Group 7 Control Rods Insertion Caused by Inadequately Protected Test Jumper | Regarding Manual Reactor Trip Due to Group 7 Control Rods Insertion Caused by Inadequately Protected Test Jumper | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000302/LER-2009-004, Regarding Main Steam Safety Valve Setpoints Outside Required Tolerance Longer than Allowed by Technical Specifications | Regarding Main Steam Safety Valve Setpoints Outside Required Tolerance Longer than Allowed by Technical Specifications | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) |
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