text
>
e U.S. NUCLEAta LEGubATORY COnsMeSSeO8e assec Pe as 388 19438 Appse0viO Onse sec.3190 010e
'" ass. si3iese LICENSEE EVENT REPORT (LER) 4 00 Cast mousseen as PA8K G
, ACILify maase nn CRYSTAL RIVER UNIT 3 o Is I o Io i o 131012 loFl013
' ' ' " ' " VOLUNTARY ENTRY INTO TECHNICAL SPECIFICATION 3.0.3 FOR MAINTENANCE ON EMERGENCY FEEDWATER INITIATION AND CONTR01 SYSTFM EVENT DATE 458 Lim seumssG A is AGPORT DAT1179 OTMSR F ACILITIES INWObvec tel taQ8eTM QAv vfAM vtAR 88,0$$'b
,8 woa TM OAy vgan FAC16ste seanees DOCKET feuteSERISI N/A o is to lo g o, 0l1 0l 1 87 8l7 0l0l1 0l 0 0l1 2l 9 8l7 N/A ois oio,oi i,
s r
Twis aeron? is SuennTTso avaeuA=T To fue asOuensasswTs oc to Can 1: iCn-.
a.=== a sw aw.- e# nu
==s ia 1
mm m4 mnwuHm ruim Tuu.
m o n.
= =.in.
mnwaH.,
so.nwaHai
=a,;s.,gg 0i3i9 m anwnHa se m.iui JdisAJ n.,
98.78teH2 Hit 90.73teluHveleHA) meeBlaH1Hilli
]
20.4881aH1 Hies 98.734eH2 Hits es.714aH2HvasiHel 20.4084eH t Het 30 734eH2H4e4 30 73teH2Hd LICtpuSSE COseTACT POR TMs8 Lee (121 TELEPHONG peauttR maug AAtACQQt L. W. M0FFATT, NUCLEAR SAFETY SUPERVISOR 9 0:4 7i9 :51 -i614 i8 l6 COMPLEf t One Lime FOR EACM COMPO8eGNT S AILumE DE ACAletO 18e THIS REPORT (13)
Caust svtTEu C0wpON E'87
"'yy" "h
^((E Uki!
"O
"'y"hO C& ult 5YSTtw CCuPCht8ef 7
en s X
JtE XI TI i V i l l 214 Yes i
! i i
! I i i
I i i I ! !
I I I I I I I SupptgesegTAL REPORT EXPtCTED stas neoseTM DAY vtAn its 110 v.e. som.n.ee Ex9tCT90 sugertstrQN CA rts no l
l l
j T.A.T_.,...~._.._...I On December 31, 1986, Crystal River Uni t 3 was operating at 39%
reactor power and producing 325 megawatts electric.
At approximately 2200 the Nuclear Operator received a half-trip signal on the "A" channel of the main steam line isolation (MSLI) for the "B" once through steam generator (OTSG).
The main steam isolation system is part of the Emergency Feedwater Initiation and Control (EFIC) System.
The operator determined the half-trip to be unwarranted and I
inadvertent.
Subsequent investigation identified a faulty light emitting diode (LED).
At 0025 on January 1, 1987, Technical Specification 3.0.3 was voluntarily entered and the EFIC actuation signal output breakers were temporarily opened to prevent spurious EFIC actuations while repairs were being performed.
t l
The f aul ty LED was repl aced.
The applicable post maintenance testing was satisfactorily, completed and the output signal breakers were then re-closed.
At 0042 on January 1, 1987, the EFIC system was returned to an operable status.and Technical Specification 3.0.3 was exited.
8702040340 e70129 h
DR ADocx 03o003og s
PDR
.g.- =.
NRC Fonn 304A U S NUCLEA3 KETULATORY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION
Ex*tRES. 8/31 119 FACILif v NAME 11B DOCKET NUMSER 121 Lgg gygggg,g, pagg g33
,,b
.7,*,y" vtam 88 8
CRYSTAL RIVER UNIT 3 l0 ls lo lo lo l31012 81 7 01011 010 nip F 013 rExt ~
wc w ma..nm
EVENT DESCRIPTION
On December 31, 1986, Crystal River Unit 3 was operating at 39%
reactor power and producing 325 megawatts electric.
At approximately 2200 the licensed Nuclear Operator received a
h al f-tri p signal on the "A"
actuation c h a n rie l (initiated by "C"
cabinet) of the main steam line isolation (MSLI) for the "B"
once through steam generator (OTSG) [HX, ABl.
The main steam isolation system is part of the Emergency Feedwater Ini ti a ti on and Control (EFIC) System [JEl.
The operator determined the half-trip to be unwarranted-and inadvertent based upon instrumentation which indicated pertinent parameters were normal and stable.
Subsequent investigation identified a faulty light emitting diode (LED) [JE, XTl in the "C" EFIC cabinet.
Notifications were then made to the appropriate management personnel and the resident NRC inspector.
Based upon a previous Pl an t Review Commi ttee (PRC) evaluation of a similar event (LER 86-16); the man on call determined that during the repair activities the pl an t safety would be enhanced by temporarily disabling the automatic actuation function for both "A"
and "B" EFIC channels.
This would preclude the possibility of a
transient res ul ti ng from a
spurious EFIC actuation.
Thus permission was given to temporarily disable both EFIC channels (automatic functions only) and voluntarily enter Technical Specification 3.0.3.
The remote manual functions of the EFIC system remained completely operable from the control room.
At 0025 on January 1,
- 1987, Technical Specification 3.0.3 was voluntarily entered and one of the on-shift licensed operators was stationed as a dedicated operator at the EFIC controls.
Al thoug h the EFIC cabinets "A & B" remained energized, the actuation signal output breakers were temporarily opened to prevent spurious EFIC actuations while repairs were being performed.
The f aul ty LED was repl aced, the applicable post maintenance testing was sati sf actorily completed and the output signal breakers were then re-closed.
At 0042 on January 1,
1987, the EFIC system was returned to an operable status and Technical Speci fication 3.0.3 was exi ted.
CAUSE
The cause of the LED failure is unknown.
Technical Specification 3.0.3 was voluntarily entered to perform planned maintenance.
- .g.a....
L
NRC Form 384A U.S. NUCLEA3 [ELUL& TORY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION 4 caovsO ows No siso-oio.
EXPIRES s/3115 P ACILITV NAME tu DOCKET NUMSER (23 gg g g g,g, pggg gy 9,y,"
vEam
.S E g 8 9,[,' b l 0.
, y 9 CRYSTAL RIVER UNIT 3 o 1510 lo lo 131012 817 0[0l1 0j0 013 0F QlJ TEXT f# more space e restored. ese seeksoner MAC Form M'sJ (1M SAFETY CONSIDERATIONS While the EFIC automatic actuation functions were inoperable, a licensed operator was stationed to observe actuation parameters and initiate the protective actions if the actuation limits were reached.
Manually, all of the EFIC control functions were operable at all times.
All EFIC actuation parameters were observed to be within limi ts and EFIC was not actuated.
Al l repair activities were completed within the one hour time limit specified by Technical Specification 3.0.3.
This event did not have any impact on' the health and safety of the general public.
CORRECTIVE ACTION
The affected LED was replaced.
The root cause of the LED failure continues to be under review and evaluation by a special EFIC engineering task group which was established in early 1986.
PREVIOUS SIMILAR EVENTS
Eight previous similar events (voluntary entry into Technical Specification 3.0.3) have occurred at Crystal River Unit 3 and were reported in LERs 84-14 (two events), 85-01, 85-22, 85-29, 85-33, 86-11, and 86-16.
Four of these events were associated with the EFIC system and two of the four (85-22 and 86-16) were associated with LED failures.
- g,0 M
i ke
$ co*e:
k, e'
bb Power CORPOAATION January 29, 1987 3F0187-25 U.S. Nuclear Regulatory Commission Attn:
Document Control Desk Washington, DC 20555 Subject: Crystal River Unit 3 Docket No. 50-302 Operating License No. DPR-72 Licensee Event Report No. 87-001-00
Dear Sir:
Enclosed is Licensee Event Report (LER) No. 87-001-00 which is submitted in accordance with 10 CFR 50.73.
Should there be any questions, please contact this office.
Sincerely, 62 E. C. Simpson Director, Nuclear Operations Engineering and Licensing AEF/sdr Enclosure cc:
Dr. J. Nelson Grace Regional Administrator, Region II Mr. T. F. Stetka Senior Resident Inspector
((
i GENERAL OFFICE: 3201 Thirty-fourth Street South (813) 866 5151 St. Petersburg, Florida 33733 P.O. Box 14042
+
A Florida Progress Company
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000302/LER-1987-001, :on 861231,half-trip Signal Received on Main Steam Line Isolation Channel A.Caused by Faulty Light Emitting Diode (Led).On 870101,Tech Spec 3.0.3 Voluntarily Entered to Replace Led |
- on 861231,half-trip Signal Received on Main Steam Line Isolation Channel A.Caused by Faulty Light Emitting Diode (Led).On 870101,Tech Spec 3.0.3 Voluntarily Entered to Replace Led
| | | 05000302/LER-1987-002, :on 870221,during Monthly Surveillance of Emergency Feedwater Initiation & Control Sys,Technicians Unable to Place Channel B in Bypass for Maint & Testing. Caused by Failure of light-emitting Diode |
- on 870221,during Monthly Surveillance of Emergency Feedwater Initiation & Control Sys,Technicians Unable to Place Channel B in Bypass for Maint & Testing. Caused by Failure of light-emitting Diode
| | | 05000302/LER-1987-003, :on 870327,deficiency Discovered in Surveillance Procedure for Weekly Containment Penetrations Checks During Refueling Operations.Caused by Inadequate Procedure.Change to Procedure Initiated |
- on 870327,deficiency Discovered in Surveillance Procedure for Weekly Containment Penetrations Checks During Refueling Operations.Caused by Inadequate Procedure.Change to Procedure Initiated
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000302/LER-1987-004, :on 870124,while at 75% Power,Gaseous Radioactive Release Made W/O Performing Flow Instrument Channel Check.Caused by Personnel Error.Procedure for Performing Gaseous Releases Revised |
- on 870124,while at 75% Power,Gaseous Radioactive Release Made W/O Performing Flow Instrument Channel Check.Caused by Personnel Error.Procedure for Performing Gaseous Releases Revised
| | | 05000302/LER-1987-006, :on 870415,ammonia Detectors of Both Channels Discovered to Be Inoperable Due to Placement of Key Switch in Test Position.Caused by Inadequate Control Over Sys Removal from Svc.Procedures Revised |
- on 870415,ammonia Detectors of Both Channels Discovered to Be Inoperable Due to Placement of Key Switch in Test Position.Caused by Inadequate Control Over Sys Removal from Svc.Procedures Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000302/LER-1987-007, Extends Projected Due Date for Suppl to LER 87-007-00 from 870730 to 871030.Extra Time Needed for Satisfactory Analysis of Event | Extends Projected Due Date for Suppl to LER 87-007-00 from 870730 to 871030.Extra Time Needed for Satisfactory Analysis of Event | | | 05000302/LER-1987-008, :on 870420,monthly Channel Check Not Performed on post-accident Monitor Recorders & Quarterly Calibr Not Performed on Power Range Nuclear Flux Recorder.Caused by Personnel Error.Surveillance Procedure Revised |
- on 870420,monthly Channel Check Not Performed on post-accident Monitor Recorders & Quarterly Calibr Not Performed on Power Range Nuclear Flux Recorder.Caused by Personnel Error.Surveillance Procedure Revised
| | | 05000302/LER-1987-009, :on 870702,while Performing Surveillance Testing,Crd Mechanism Circuit Breaker Opened When Shunt Trip Device Tested,But Would Not Reclose After Testing.Caused by Failure of Inverter.Inverter Repaired |
- on 870702,while Performing Surveillance Testing,Crd Mechanism Circuit Breaker Opened When Shunt Trip Device Tested,But Would Not Reclose After Testing.Caused by Failure of Inverter.Inverter Repaired
| | | 05000302/LER-1987-010, :on 870618,discovered That Requirements for once-through Steam Generator Operating Range Level Did Not Meet Tech Spec Requirements.Caused by Personnel Error.Plant Procedure Revised |
- on 870618,discovered That Requirements for once-through Steam Generator Operating Range Level Did Not Meet Tech Spec Requirements.Caused by Personnel Error.Plant Procedure Revised
| | | 05000302/LER-1987-011, :on 870710,reactor Trip Occurred Due to Loss of Reactor Coolant Pump (RCP) Power Monitors.Caused by Failed Relay in RCP B Power Monitor Circuit Due to Open Power Fuse. Monitor Relay & Fuse Replaced |
- on 870710,reactor Trip Occurred Due to Loss of Reactor Coolant Pump (RCP) Power Monitors.Caused by Failed Relay in RCP B Power Monitor Circuit Due to Open Power Fuse. Monitor Relay & Fuse Replaced
| | | 05000302/LER-1987-012, :on 870702,reactor Tripped Following Failure of Inverter a Feeding Vital Bus a Causing Downstream Transfer Switch to Transfer to Alternate Power Supply.Caused by Personnel Error.Tech Specs Will Be Revised |
- on 870702,reactor Tripped Following Failure of Inverter a Feeding Vital Bus a Causing Downstream Transfer Switch to Transfer to Alternate Power Supply.Caused by Personnel Error.Tech Specs Will Be Revised
| | | 05000302/LER-1987-013, :on 870716,during Surveillance,Indication of Partial Trip in Emergency Feedwater Initiation & Control Sys (EFIC) Received.On 870716-18,output Breakers of EFIC a & B Channels Opened,Disabling Automatic Functions |
- on 870716,during Surveillance,Indication of Partial Trip in Emergency Feedwater Initiation & Control Sys (EFIC) Received.On 870716-18,output Breakers of EFIC a & B Channels Opened,Disabling Automatic Functions
| | | 05000302/LER-1987-014-02, :on 870722,oncoming Shift Supervisor Discovered That Daily Heat Balance Calculation Not Performed within Allowable Surveillance Window of Tech Spec 4.3.1.1.1.Caused by Personnel Error.Personnel Counseled |
- on 870722,oncoming Shift Supervisor Discovered That Daily Heat Balance Calculation Not Performed within Allowable Surveillance Window of Tech Spec 4.3.1.1.1.Caused by Personnel Error.Personnel Counseled
| | | 05000302/LER-1987-015, :on 870727,phase Fuses Opened Due to Contact W/Hook Causing Bus Undervoltage & Rendering Engineered Safeguards Trains Inoperable.Caused by Personnel Error.Fuses Replaced & Equipment Operability Verified |
- on 870727,phase Fuses Opened Due to Contact W/Hook Causing Bus Undervoltage & Rendering Engineered Safeguards Trains Inoperable.Caused by Personnel Error.Fuses Replaced & Equipment Operability Verified
| | | 05000302/LER-1987-016, :on 870803,discovered That Surveillance Procedure for Calibr of Reactor Protection Sys Did Not Contain Proper Setpoints.Caused by Personnel Error. Procedure Revised & Personnel Counseled |
- on 870803,discovered That Surveillance Procedure for Calibr of Reactor Protection Sys Did Not Contain Proper Setpoints.Caused by Personnel Error. Procedure Revised & Personnel Counseled
| | | 05000302/LER-1987-017, :on 870808,problems During CRD Mechanism Repairs Delayed Plant Heatup Preventing Pump Restoration. Caused by Securing of Steam Supply to Emergency Feedwater Pump.Tech Spec Rev Submitted |
- on 870808,problems During CRD Mechanism Repairs Delayed Plant Heatup Preventing Pump Restoration. Caused by Securing of Steam Supply to Emergency Feedwater Pump.Tech Spec Rev Submitted
| | | 05000302/LER-1987-022, :on 871106,circuit Breakers Tripped Actuating Engineered Safeguards.Caused by Technicians Creating Short Circuit While Installing Jumper Lead.Procedure to Be Revised |
- on 871106,circuit Breakers Tripped Actuating Engineered Safeguards.Caused by Technicians Creating Short Circuit While Installing Jumper Lead.Procedure to Be Revised
| | | 05000302/LER-1987-023, :on 870930,Mode 6 Entered Before Neutron Flux Monitor Audible Indication in Control Room & Containment re-energized as Required by Tech Specs.Caused by Defective Procedures.Procedures Revised |
- on 870930,Mode 6 Entered Before Neutron Flux Monitor Audible Indication in Control Room & Containment re-energized as Required by Tech Specs.Caused by Defective Procedures.Procedures Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000302/LER-1987-024, :on 871008,unlicensed Nuclear Auxiliary Operator Exposed to Radiation Field of 55 Rem//H in Basement Level of Reactor Bldg.Caused by Lack of Good Method for Early Detection of Water Leakage |
- on 871008,unlicensed Nuclear Auxiliary Operator Exposed to Radiation Field of 55 Rem//H in Basement Level of Reactor Bldg.Caused by Lack of Good Method for Early Detection of Water Leakage
| | | 05000302/LER-1987-025, :on 871016,engineered Safeguards Sys Actuated & Offsite Power Interrupted.Caused by Accidental Grounding of Unit Startup Transformer 230 Kv Feeder.Feeder Repaired & Electrical Distribution Sys Lineups Restored |
- on 871016,engineered Safeguards Sys Actuated & Offsite Power Interrupted.Caused by Accidental Grounding of Unit Startup Transformer 230 Kv Feeder.Feeder Repaired & Electrical Distribution Sys Lineups Restored
| | | 05000302/LER-1987-026, :on 871109,new Fuel Assembly Placed in Spent Fuel Pool Due to Error on Fuel Movement Sheet.Caused by Personnel Error.Fuel Assembly Moved to Proper Location & Independent Review of Move Sheets Implemented |
- on 871109,new Fuel Assembly Placed in Spent Fuel Pool Due to Error on Fuel Movement Sheet.Caused by Personnel Error.Fuel Assembly Moved to Proper Location & Independent Review of Move Sheets Implemented
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000302/LER-1987-027, :on 871026,valving Out of Incorrect Transmitter Occurred,Resulting in Train a Engineered Safeguards Actuation.Caused by Personnel Error.Personnel Counseled & Safeguards Actuation Reset by Operators |
- on 871026,valving Out of Incorrect Transmitter Occurred,Resulting in Train a Engineered Safeguards Actuation.Caused by Personnel Error.Personnel Counseled & Safeguards Actuation Reset by Operators
| | | 05000302/LER-1987-028, :on 871205,during Operations to Power Down B Inverter for Maint,Improper Vital Bus Switching Sequence Led to Engineered Safeguards Sys Actuation.Caused by Inadequate Operator Training.Addl Training Program Set |
- on 871205,during Operations to Power Down B Inverter for Maint,Improper Vital Bus Switching Sequence Led to Engineered Safeguards Sys Actuation.Caused by Inadequate Operator Training.Addl Training Program Set
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000302/LER-1987-029, :on 871118,determined That Monthly Surveillance for Liquid Process & Effluent Radiation Monitors Not Performed & Three Surveillances Exceeded by One Day.Caused by Personnel Error.Personnel Instructed |
- on 871118,determined That Monthly Surveillance for Liquid Process & Effluent Radiation Monitors Not Performed & Three Surveillances Exceeded by One Day.Caused by Personnel Error.Personnel Instructed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000302/LER-1987-030, :on 871120,Train B Engineered Safeguards (Es) Actuation Occurred.Cause Unknown.Es Actuation Reset by Control Room Operators & Affected Components Returned to Required Positions |
- on 871120,Train B Engineered Safeguards (Es) Actuation Occurred.Cause Unknown.Es Actuation Reset by Control Room Operators & Affected Components Returned to Required Positions
| | | 05000302/LER-1987-031, :on 871218,discovered Seismic Monitor W/ Measurement Ranges Not in Compliance W/Tech Specs.Caused by Personnel Error in Performance of Safety Evaluation for 1979 Procedure Change.Detectors Replaced |
- on 871218,discovered Seismic Monitor W/ Measurement Ranges Not in Compliance W/Tech Specs.Caused by Personnel Error in Performance of Safety Evaluation for 1979 Procedure Change.Detectors Replaced
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
|