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PAGE 43 CRYSTAL RIVER UNIT 3 o i5 I o Io I o i 31012 1 lor l 0 2 1
TITLE see AUXILIARY BUILDIflG EXHAUST FAf1S DUT OF SERVICE FOR MAltlTEllAllCE IVGNT DATE 156 Lim NuesetRse REPORT DAf t til QTHER P ACILifitS INv0LV10 (St IE0
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LICENSet CONTACT POR THit LER 1:21 as?.Mt TELEPMONE NyustR AmtA CODE W. K. Bandhauer, fluclear Safety Supervisor 86 904 795 i -i 64 i i
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ASSTAACT ftemet to F.017 apse.s e e..sereseees y arreea pape essee ryneentfen eness it si On February 12,1985, the Auxiliary Building Exhaust Fans were taken out of service in order to perform modifications to the ventilation system dampers.
Technical Specification 3.7.8.1 requires two independent pairs of exhaust fans be operable. With both pairs of exhaust fans out of service, the limiting condition as specified in Technical Specification 3.7.8.1 was not met and Technical Specification 3.0.3 was entered.
l This evolution is non-reportable since Technical Specification 3.0.3 was entered l
voluntarily for maintenance purposes and exited prior to being required to place the j
plant in HOT STANDBY. A voluntary report is being submitted to document the use of I
Technical Specification 3.0.3 for maintenance activities.
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E APimES 8/3i 55 F ACILITV NAME til DOCKET NUFSER 12) ggn muuggn igs PAGE131 ygag SEQUENYeak
CRYSTAL RIVER UNIT 3 o ls j o lo lo l 3l 0l2 315 0l0l1 0 l0 0l2 oF 0l2 nx1,.v - -..
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EVENT DESCRIPTION
e On February 12,1985 at 0903, the Auxiliary Building Exhaust Fans (VF, FAN) were taken out of service in order to install a blank-off plate (FB) on the exhaust duct for filter bank AHFL-2C (VF, FLT). The purpose of the blank-off plate was to allow the exhaust damper for the filter bank to be replaced. The blank-off plate was installed and the exhaust fans restarted 0953 on February 12,1985.
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The evolution was carefully planned and staged la order to minimize the time period the fans were secured and, hence, minimize the time period that Technical Specifications 3.0.3 was in effect.
SAFETY CONSIDERATIONS The exhaust fans provide a negative pressure within the Auxiliary Building relative to areas outside the building. This. assures all leakage of air will be into the building and all discharges will be filtered and monitored through the exhaust filter and fan system.
For the controlled evolution reported here, the supply and exhaust fans were secured, leaving unpressurized release through building openings as the only release path. All doors to the Auxiliary Building were closed prior to securing the fans, thus restricting the release path. The potential release for the evolution was judged to be well below the release limits and reporting limits.
CORRECTIVE ACTION
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A revision to the action statement of Technical Specification 3.7.8.l which will allow for maintenance has been submitted and is pe,nding approval. No further corrective action is deemed necessary.
PREVIOUS SIMILAR EVENTS
All four Auxiliary Building Exhaust Fans were reported inoperable on four previous occasions. Two of these occasions were due to unplanned equipment failures and two were due to planned maintenance similar to that included in this report.
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Power CORPOR ATIO N March 22,1985 3F0385-20 Document Control Desk U.S. Nuclear Regulation Commission Washington, DC 20555
Subject:
Crystal River Unit 3 Docket No. 50-302 Operating License No. DPR-72 Licensee Event Report No. 85-001-00
Dear Sir:
Enclosed is Licensee Event Report (LER) No. 85-001-00 which is submitted voluntarily by Florida Power Corporation.
Should there be any questions, please contact this office.
Sincerely, G. R. Westafer Manager, Nuclear Operations Licensing and Fuel Management AEF/feb Enclosure cc:
Dr. 3. Nelson Grace Regional Administrator, Region II Office of Inspection & Enforcement U.S. Nuclear Regulatory Commission 101 Marietta Street N.W., Suite 2900 Atlanta, GA 30323 GEN ERAL OFFICE 3201 Thirty fourth Street South. P.O. Box 14042, St. Petersburg, Florida 33733 813-866 5151
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| 05000302/LER-1985-001, :on 850212,auxiliary Bldg Exhaust Fans Taken Out of Svc for Mods to Ventilation Sys Dampers.Voluntary Rept Submitted to Document Use of Tech Spec 3.0.3 for Maint Activities |
- on 850212,auxiliary Bldg Exhaust Fans Taken Out of Svc for Mods to Ventilation Sys Dampers.Voluntary Rept Submitted to Document Use of Tech Spec 3.0.3 for Maint Activities
| | | 05000302/LER-1985-002, :on 850222,emergency Diesel Generator Started. Caused by Failure of Drain Petcock on Air Start Solenoid Air Filter EGFL-4.Filter Will Be Replaced W/Filters Designed for Higher Pressure |
- on 850222,emergency Diesel Generator Started. Caused by Failure of Drain Petcock on Air Start Solenoid Air Filter EGFL-4.Filter Will Be Replaced W/Filters Designed for Higher Pressure
| | | 05000302/LER-1985-003, :on 850403,determined That 1980 Inservice Insp of once-through Steam Generator B Had Not Fully Examined Length of Generator Tubes.Caused by Personnel Error.Mod of Tech Spec Re Tube Insp Requirements Proposed |
- on 850403,determined That 1980 Inservice Insp of once-through Steam Generator B Had Not Fully Examined Length of Generator Tubes.Caused by Personnel Error.Mod of Tech Spec Re Tube Insp Requirements Proposed
| | | 05000302/LER-1985-004, :on 850425,determined That Heating & Ventilation Ductwork Improperly Installed.On 850501, Determined That Deceit Bolts Installed in HVAC Sys.Repairs & Seismic Design Analysis Completed |
- on 850425,determined That Heating & Ventilation Ductwork Improperly Installed.On 850501, Determined That Deceit Bolts Installed in HVAC Sys.Repairs & Seismic Design Analysis Completed
| | | 05000302/LER-1985-005, :on 850530,emergency Diesel Generator Actuated. Caused by Lifting Leads on Protective Relays Due to Computer Program Input Error.Error Corrected |
- on 850530,emergency Diesel Generator Actuated. Caused by Lifting Leads on Protective Relays Due to Computer Program Input Error.Error Corrected
| | | 05000302/LER-1985-006, :on 850615,blown Fuses Resulted in Automatic Actuation of Emergency Diesel Generator.Caused by Misunderstanding of Process for Turning Over Plant Sys After Mod.Fuses Replaced & Procedures Reemphasized |
- on 850615,blown Fuses Resulted in Automatic Actuation of Emergency Diesel Generator.Caused by Misunderstanding of Process for Turning Over Plant Sys After Mod.Fuses Replaced & Procedures Reemphasized
| | | 05000302/LER-1985-007, :on 850619,emergency Diesel Generator a Actuated.Caused by Failure of Fuse in Automatic Start Circuit.Fuse Replaced After Circuit Investigated for Faults. No Faults Found & Replacement Fuse Functioning |
- on 850619,emergency Diesel Generator a Actuated.Caused by Failure of Fuse in Automatic Start Circuit.Fuse Replaced After Circuit Investigated for Faults. No Faults Found & Replacement Fuse Functioning
| | | 05000302/LER-1985-008, :on 850729,actuation of Engineered Safeguards Sys Experienced.Caused by Operator Inadvertently Placing Reset Switch in Wrong Position.Operator Counseled on Proper Control Switch Designation & Position |
- on 850729,actuation of Engineered Safeguards Sys Experienced.Caused by Operator Inadvertently Placing Reset Switch in Wrong Position.Operator Counseled on Proper Control Switch Designation & Position
| | | 05000302/LER-1985-009, :on 850710,both Emergency Diesel Generators Inoperable for Approx 28 Days.Caused by Failure to Perform Load Sequence Timer Surveillance Test of Emergency Diesel Generator B within Prescribed Frequency |
- on 850710,both Emergency Diesel Generators Inoperable for Approx 28 Days.Caused by Failure to Perform Load Sequence Timer Surveillance Test of Emergency Diesel Generator B within Prescribed Frequency
| | | 05000302/LER-1985-010, :on 850808,grab Samples Not Taken Upon Entry Into Mode 4.Caused by Personnel Error.Scheduling Procedures Will Be Changed to Improve Tracking of Action Statements |
- on 850808,grab Samples Not Taken Upon Entry Into Mode 4.Caused by Personnel Error.Scheduling Procedures Will Be Changed to Improve Tracking of Action Statements
| | | 05000302/LER-1985-011, :on 850812,sump Pump Operability Verification & Breaker Alignment Verification Not Performed During Emergency Generator Maint.Caused by Operator Error. Surveillance Performed.Procedures Changed |
- on 850812,sump Pump Operability Verification & Breaker Alignment Verification Not Performed During Emergency Generator Maint.Caused by Operator Error. Surveillance Performed.Procedures Changed
| | | 05000302/LER-1985-012, :on 850809-16,low Steam Generator Level Feature of Emergency Feedwater Initiation & Control Sys Actuated 12 Times.Caused by Insufficient Margin Between Normal Level Control & Low Level Actuation Setpoints |
- on 850809-16,low Steam Generator Level Feature of Emergency Feedwater Initiation & Control Sys Actuated 12 Times.Caused by Insufficient Margin Between Normal Level Control & Low Level Actuation Setpoints
| | | 05000302/LER-1985-013, :on 850815,unit Experienced Inadvertent Partial Actuation of Emergency Feedwater Initiation & Control Sys. Caused by Unplanned Shutting of Main Steam Valve MSV-159 in Response to Steam Leak on Valve VI |
- on 850815,unit Experienced Inadvertent Partial Actuation of Emergency Feedwater Initiation & Control Sys. Caused by Unplanned Shutting of Main Steam Valve MSV-159 in Response to Steam Leak on Valve VI
| | | 05000302/LER-1985-014, :on 850816,two Actuations of Emergency Feedwater Initiation & Control Sys Occurred Due to Low Steam Generator Level.Caused by Temporary Imbalance Between Feed & Steam Flow Levels Due to Operator Error |
- on 850816,two Actuations of Emergency Feedwater Initiation & Control Sys Occurred Due to Low Steam Generator Level.Caused by Temporary Imbalance Between Feed & Steam Flow Levels Due to Operator Error
| | | 05000302/LER-1985-015, :on 850820,automatic Reactor Trip Occurred Due to Severed Drain Line for Main Turbine High Pressure Crossover Line.Caused by Fatigue Failure of Socket Weld Due to Fabrication Defect.Weld Repaired |
- on 850820,automatic Reactor Trip Occurred Due to Severed Drain Line for Main Turbine High Pressure Crossover Line.Caused by Fatigue Failure of Socket Weld Due to Fabrication Defect.Weld Repaired
| | | 05000302/LER-1985-016, :on 850820,trip Occurred on High RCS Pressure Due to Feedwater Sys Transient.Analysis of Event in Progress.Rept Will Be Submitted on 850926 |
- on 850820,trip Occurred on High RCS Pressure Due to Feedwater Sys Transient.Analysis of Event in Progress.Rept Will Be Submitted on 850926
| | | 05000302/LER-1985-016-01, :on 850820,RCS High Pressure Trip Occurred Due to RCS Pressure & Temp Perturbations.Caused by Sluggish Main Feedwater Control Response & Improper Settings on Reactor Control Module.Control Module Replaced |
- on 850820,RCS High Pressure Trip Occurred Due to RCS Pressure & Temp Perturbations.Caused by Sluggish Main Feedwater Control Response & Improper Settings on Reactor Control Module.Control Module Replaced
| | | 05000302/LER-1985-017, :on 850830,unusual Event Declared Due to Threat of Hurricane Elena.Watertight Flood Control Doors Closed & Plant Staff Augmented W/Addl Personnel |
- on 850830,unusual Event Declared Due to Threat of Hurricane Elena.Watertight Flood Control Doors Closed & Plant Staff Augmented W/Addl Personnel
| | | 05000302/LER-1985-018, :on 850412,technicians Failed to Note in Appropriate Spaces of Transmittal Document That Seismic Trigger Removed & Surveillance Procedure Did Not Meet Acceptance Criteria.Personnel Counseled |
- on 850412,technicians Failed to Note in Appropriate Spaces of Transmittal Document That Seismic Trigger Removed & Surveillance Procedure Did Not Meet Acceptance Criteria.Personnel Counseled
| | | 05000302/LER-1985-019, :on 851008,unplanned Automatic Actuation of Emergency Diesel Generator a Occurred.Caused by Electrician Error.Electrician Counseled to Read Drawings & Warning Labels More Carefully |
- on 851008,unplanned Automatic Actuation of Emergency Diesel Generator a Occurred.Caused by Electrician Error.Electrician Counseled to Read Drawings & Warning Labels More Carefully
| | | 05000302/LER-1985-020, :on 851009,both MSIVs from Steam Generator B Automatically Closed Due to Spurious Emergency Feedwater Initiation & Control Actuation.Caused by Low Steam Generator Level Indication.Trip Module Replaced |
- on 851009,both MSIVs from Steam Generator B Automatically Closed Due to Spurious Emergency Feedwater Initiation & Control Actuation.Caused by Low Steam Generator Level Indication.Trip Module Replaced
| | | 05000302/LER-1985-021, :on 851006,NRC Notified Health Physics Personnel of Two Unmarked & Unposted Waste Drums Which Met Criteria for High Radiation Areas.Caused by Personnel Error.Technicians Counseled |
- on 851006,NRC Notified Health Physics Personnel of Two Unmarked & Unposted Waste Drums Which Met Criteria for High Radiation Areas.Caused by Personnel Error.Technicians Counseled
| | | 05000302/LER-1985-022, :on 851013,half-trip Signal Received on Channel B of Emergency Feedwater Initiation & Control Sys for Main Steamline Isolation from once-through Steam Generator B. Source of Signal Could Not Be Determined |
- on 851013,half-trip Signal Received on Channel B of Emergency Feedwater Initiation & Control Sys for Main Steamline Isolation from once-through Steam Generator B. Source of Signal Could Not Be Determined
| | | 05000302/LER-1985-023, :on 851026,turbine/reactor Trip Occurred & Automatic Runback Initiated.Control Board Operation Manually Tripped Main Turbine,Resulting in Anticipatory Reactor Trip. Caused by Defective Oscillator Board |
- on 851026,turbine/reactor Trip Occurred & Automatic Runback Initiated.Control Board Operation Manually Tripped Main Turbine,Resulting in Anticipatory Reactor Trip. Caused by Defective Oscillator Board
| | | 05000302/LER-1985-025, :on 851108,RCS High Pressure Trip Occurred Due to Feedwater Booster Pump Trip.Cause Not Determined.Covers Placed Over Pump Control Switches to Prevent Accidental Actuation.Valves Inspected & Adjusted |
- on 851108,RCS High Pressure Trip Occurred Due to Feedwater Booster Pump Trip.Cause Not Determined.Covers Placed Over Pump Control Switches to Prevent Accidental Actuation.Valves Inspected & Adjusted
| | | 05000302/LER-1985-026, :on 851122,feedwater Transient Resulted in Emergency Feedwater Initiation & Control (EFIC) Sys Actuation & Reactor Trip on High RCS Pressure.Further Training on EFIC Sys Provided to Operators |
- on 851122,feedwater Transient Resulted in Emergency Feedwater Initiation & Control (EFIC) Sys Actuation & Reactor Trip on High RCS Pressure.Further Training on EFIC Sys Provided to Operators
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000302/LER-1985-027, :on 851123,spurious Actuation & Loss of Emergency Feedwater Occurred During Calibr of once-through Steam Generator Level Instruments.Caused by Pressure Surge. Changes to Actuation Circuitry Being Considered |
- on 851123,spurious Actuation & Loss of Emergency Feedwater Occurred During Calibr of once-through Steam Generator Level Instruments.Caused by Pressure Surge. Changes to Actuation Circuitry Being Considered
| | | 05000302/LER-1985-028, :on 851203,fault of 6,900-volt Bus Caused Loss of Reactor Coolant Pumps Resulting in Reactor Trip.Caused by Loose Connector on Bus Side of Motor Breaker RCP-10. Switchgear Repaired.Connectors Tightened |
- on 851203,fault of 6,900-volt Bus Caused Loss of Reactor Coolant Pumps Resulting in Reactor Trip.Caused by Loose Connector on Bus Side of Motor Breaker RCP-10. Switchgear Repaired.Connectors Tightened
| | | 05000302/LER-1985-029, :on 851204,Channel B of Emergency Feedwater Initiation & Control Sys Could Not Be Electrically Switched Into Maint Bypass & All Automatic Functions Rendered Inoperable.Caused by Failed Module |
- on 851204,Channel B of Emergency Feedwater Initiation & Control Sys Could Not Be Electrically Switched Into Maint Bypass & All Automatic Functions Rendered Inoperable.Caused by Failed Module
| | | 05000302/LER-1985-030, :on 851207,reactor Trip Occurred During Switchover of Pumps.Caused by Reactor Coolant Pump Power Monitors Not Bypassed Before Performing Switchover.Procedure Revised & Operator Counseled |
- on 851207,reactor Trip Occurred During Switchover of Pumps.Caused by Reactor Coolant Pump Power Monitors Not Bypassed Before Performing Switchover.Procedure Revised & Operator Counseled
| | | 05000302/LER-1985-032, :on 851205,confirmed That Equipment Associated w/230 Kv Switchyard Installed on 780701 Not in Compliance W/Design & Regulatory Requirements.Caused by Personnel Error.Changes Made to Protective Relays |
- on 851205,confirmed That Equipment Associated w/230 Kv Switchyard Installed on 780701 Not in Compliance W/Design & Regulatory Requirements.Caused by Personnel Error.Changes Made to Protective Relays
| | | 05000302/LER-1985-033, :on 851226,automatic Functions of Emergency Feedwater Initiation & Control Sys Rendered Inoperable to Preclude Spurious Actuation Due to Defective once-through Steam Generator Low Level Initiate Bistable |
- on 851226,automatic Functions of Emergency Feedwater Initiation & Control Sys Rendered Inoperable to Preclude Spurious Actuation Due to Defective once-through Steam Generator Low Level Initiate Bistable
| | | 05000302/LER-1985-034, :on 850809,RCS Pressure Raised Above 750 Psig W/O Meeting Required Operability Surveillances Per Tech Spec 3.5.1.a.Caused by Inadequate Procedure.Procedure Revised.W/ |
- on 850809,RCS Pressure Raised Above 750 Psig W/O Meeting Required Operability Surveillances Per Tech Spec 3.5.1.a.Caused by Inadequate Procedure.Procedure Revised.W/
| | | 05000302/LER-1985-054, :on 851212,all Offsite Power Lost.Emergency Diesel Generators Started in Emergency Mode & Restored Power to Essential Loads.Caused by Lightning Fault.Relay Setpoints Changed as Preventive Measure |
- on 851212,all Offsite Power Lost.Emergency Diesel Generators Started in Emergency Mode & Restored Power to Essential Loads.Caused by Lightning Fault.Relay Setpoints Changed as Preventive Measure
| 10 CFR 50.73(a)(2)(iv), System Actuation |
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