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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000302/LER-1997-040, Corrected Page 1 of LER 97-040-00,adding Rept Date in Block 7.On 971110,inadequate Engineering Documentation for safety- Related Large Bore Piping Analysis & Pipe Supports Noted. Caused by Personnel Error1997-12-0404 December 1997 Corrected Page 1 of LER 97-040-00,adding Rept Date in Block 7.On 971110,inadequate Engineering Documentation for safety- Related Large Bore Piping Analysis & Pipe Supports Noted. Caused by Personnel Error 05000302/LER-1997-039, Corrected Page 1 to LER 97-039-00,adding Rept Date in Block 7.On 971108,unqualified Matl Discovered Left in Reactor Bldg During Const.Caused by Personnel Error.Polystyrene Permanently Installed1997-12-0303 December 1997 Corrected Page 1 to LER 97-039-00,adding Rept Date in Block 7.On 971108,unqualified Matl Discovered Left in Reactor Bldg During Const.Caused by Personnel Error.Polystyrene Permanently Installed 3F0397-01, LER 97-S01-00:on 970130,maint Activities in Circulating Water Sys Resulted in Protected Area Breach.Caused by Failure to Identify Security Function of Plant.Armed Security Was Established1997-03-0303 March 1997 LER 97-S01-00:on 970130,maint Activities in Circulating Water Sys Resulted in Protected Area Breach.Caused by Failure to Identify Security Function of Plant.Armed Security Was Established 05000302/LER-1990-0101990-07-27027 July 1990 LER 90-010-00:on 900626,determined That Voltage Dips Caused by Sluggish Voltage Regulator Response Exceed Reg Guide 1.9 Limits.Caused by Improper Load Sequence Interval.Test Plan Being Developed for Testing Voltage regulator.W/900727 Ltr 05000302/LER-1989-013, Corrected LER 89-013-01:on 890409,when Time Delay Satisfied & Voltage Had Not Recovered,Emergency Diesel Generator Start Signal Was Initiated.Caused by Degraded Voltage on Engineered Safeguard 4,160 Volt Buses1989-07-0505 July 1989 Corrected LER 89-013-01:on 890409,when Time Delay Satisfied & Voltage Had Not Recovered,Emergency Diesel Generator Start Signal Was Initiated.Caused by Degraded Voltage on Engineered Safeguard 4,160 Volt Buses 05000302/LER-1984-001, Updated LER 84-001-01:on 840113,end Cap on Reactor Bldg Side of Spare Penetration 3531 Mistakenly Cut Off.Caused by Personnel Failure to Follow Applicable Engineering Procedures.Personnel Retrained1984-06-26026 June 1984 Updated LER 84-001-01:on 840113,end Cap on Reactor Bldg Side of Spare Penetration 3531 Mistakenly Cut Off.Caused by Personnel Failure to Follow Applicable Engineering Procedures.Personnel Retrained 05000302/LER-1983-058, Updated LER 83-058/03L-1:on 831103,while Performing Maint on 120-volt Ac Vital Bus Transfer Switch,Fuse Blew,Rendering Inverter 3A Inoperable.Caused by Personnel Inadvertently Shorting Out Lamp Base.Inverter repaired.W/840106 L1984-01-0606 January 1984 Updated LER 83-058/03L-1:on 831103,while Performing Maint on 120-volt Ac Vital Bus Transfer Switch,Fuse Blew,Rendering Inverter 3A Inoperable.Caused by Personnel Inadvertently Shorting Out Lamp Base.Inverter repaired.W/840106 Ltr 05000302/LER-1983-053, Updated LER 83-053/03L-1:on 831109,safety-related Hydraulic Snubber MSH-252 Declared Inoperable When Lack of Oil Level Indication Noted in Sightglass.Caused by Loose jam-nut on Stationary End of Snubber,Allowing rotation.W/84011984-01-0606 January 1984 Updated LER 83-053/03L-1:on 831109,safety-related Hydraulic Snubber MSH-252 Declared Inoperable When Lack of Oil Level Indication Noted in Sightglass.Caused by Loose jam-nut on Stationary End of Snubber,Allowing rotation.W/840106 Ltr 05000302/LER-1983-045, Rev 1 to LER 83-045/03X-1:on 831016,1104 & 08,175-ft Wind Speed Instrumentation & on 831028 & 1102,33-ft Wind Direction Instrumentation Discovered Inoperable.Caused by Severe Weather Damage & Component Failure1983-12-0101 December 1983 Rev 1 to LER 83-045/03X-1:on 831016,1104 & 08,175-ft Wind Speed Instrumentation & on 831028 & 1102,33-ft Wind Direction Instrumentation Discovered Inoperable.Caused by Severe Weather Damage & Component Failure 05000302/LER-1983-031, Supplementary LER 83-031/03L-1:on 830725,containment Isolation Valve CAV-6 & -7 Would Not Close Under Sys Pressure of 1,000 Psi.Caused by Insufficient Design &/Or Inadequate Maint Procedures1983-09-0707 September 1983 Supplementary LER 83-031/03L-1:on 830725,containment Isolation Valve CAV-6 & -7 Would Not Close Under Sys Pressure of 1,000 Psi.Caused by Insufficient Design &/Or Inadequate Maint Procedures 05000302/LER-1983-023, Updated LER 83-023/01T-1:on 830613,fire Damper Discovered Missing.Approx 55 Addl Dampers & Chase Connecting Control Complex 108 & 165 Ft Elevations Degraded Due to Incorrect Fire Rating.Caused by Personnel Error1983-07-20020 July 1983 Updated LER 83-023/01T-1:on 830613,fire Damper Discovered Missing.Approx 55 Addl Dampers & Chase Connecting Control Complex 108 & 165 Ft Elevations Degraded Due to Incorrect Fire Rating.Caused by Personnel Error 05000302/LER-1983-018, Updated LER 83-018/01T-1:on 830413,preliminary Repts Received from B&W Indicated 51 of 120 Upper Core Barrel Bolts W/Ultrasonic Flaw Indications.Caused by Intergranular Stress Corrosion Cracking.Bolts Replaced1983-07-12012 July 1983 Updated LER 83-018/01T-1:on 830413,preliminary Repts Received from B&W Indicated 51 of 120 Upper Core Barrel Bolts W/Ultrasonic Flaw Indications.Caused by Intergranular Stress Corrosion Cracking.Bolts Replaced 05000302/LER-1981-031, Updated LER 81-031/01T-1:on 810624,Henry Pratt Co Notified That Containment Purge Valves AHV-1A,1B,1C & 1D Could Fail During Loca.Cause Unknown.Valves Modified on 810701.Mods Resolved 10CFR100 Dose Rate Excess Identified on 8211982-11-15015 November 1982 Updated LER 81-031/01T-1:on 810624,Henry Pratt Co Notified That Containment Purge Valves AHV-1A,1B,1C & 1D Could Fail During Loca.Cause Unknown.Valves Modified on 810701.Mods Resolved 10CFR100 Dose Rate Excess Identified on 821101 ML20062G2891978-12-19019 December 1978 /01T-0 on 781218:during Routine Oper,Discovered That AHF-14C Was Overloaded & Was Secured to Attempt to Balance Air flow.AHF-14C Was Tripped During Restart & Cause Was Attributed to Not Allowing Sufficient Time for Restart 1997-03-03
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G0191999-10-15015 October 1999 Safety Evaluation Concluding That Licensee Followed Analytical Methods Provided in GL 90-05.Grants Relief Until Next Refueling Outage,Scheduled to Start on 991001.Temporary non-Code Repair Must Then Be Replaced with Code Repair 3F1099-19, Part 21 Rept Re Damage on safety-grade Cable Provided to FPC by Bicc Brand-Rex Co.Damage Was Created During Cabling Process While Combining Three Conducters.Corrective Action Program Precursor Card PC99-2868 Was Initiated1999-10-13013 October 1999 Part 21 Rept Re Damage on safety-grade Cable Provided to FPC by Bicc Brand-Rex Co.Damage Was Created During Cabling Process While Combining Three Conducters.Corrective Action Program Precursor Card PC99-2868 Was Initiated ML20217B0931999-10-0606 October 1999 Part 21 Rept Re Damaged Safety Grade Electrical Cabling Found in Supply on 990831.Damage Created During Cabling Process While Combining Three Conductors Just Prior to Closing.Vendor Notified of Reporting of Issue ML20212L0881999-10-0404 October 1999 SER Accepting Licensee Requests for Relief 98-012 to 98-018 Related to Implementation of Subsections IWE & Iwl of ASME Section XI for Containment Insp for Crystal River Unit 3 ML20212J8631999-10-0101 October 1999 Safety Evaluation Supporting Licensee Proposed Alternatives to Provide Reasonable Assurance of Structural Integrity of Subject Welds & Provide Acceptable Level of Quality & Safety.Relief Granted Per 10CFR50.55a(g)(6)(i) ML20212E9031999-09-30030 September 1999 FPC Crystal River Unit 3 Plant Reference Simulator Four Year Simulator Certification Rept Sept 1995-Sept 1999 3F1099-02, Monthly Operating Rept for Sept 1999 for Crystal River,Unit 3.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Crystal River,Unit 3.With ML20212E6911999-09-21021 September 1999 Safety Evaluation Supporting Proposed EALs Changes for Plant Unit 3.Changes Meet Requirements of 10CFR50.47(b)(4) & App E to 10CFR50 ML20211L1321999-08-31031 August 1999 EAL Basis Document 3F0999-02, Monthly Operating Rept for Aug 1999 for Crystal River,Unit 3.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Crystal River,Unit 3.With ML20212C1501999-08-31031 August 1999 Non-proprietary Version of Rev 0 to Crystal River Unit 3 Enhanced Spent Fuel Storage Engineering Input to LAR Number 239 ML20211B7291999-08-16016 August 1999 Rev 2 to Cycle 11 Colr ML20210P1111999-08-0505 August 1999 SER Accepting Evaluation of Third 10-year Interval Inservice Insp Program Requests for Relief for Plant,Unit 3 ML20210U5341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Crystal River,Unit 3 ML20209F5601999-07-31031 July 1999 EAL Basis Document, for Jul 1999 3F0799-01, Monthly Operating Rept for June 1999 for Crystal River,Unit 3.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Crystal River,Unit 3.With ML20210U5411999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Crystal River,Unit 3 3F0699-07, Monthly Operating Rept for May 1999 for Crystal River,Unit 3.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Crystal River,Unit 3.With ML20210U5601999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Crystal River,Unit 3 ML20195C6271999-05-28028 May 1999 Non-proprietary Rev 0 to Addendum to Topical Rept BAW-2346P, CR-3 Plant Specific MSLB Leak Rates ML20196L2031999-05-19019 May 1999 Non-proprietary Rev 0 to BAW-2346NP, Alternate Repair Criteria for Tube End Cracking in Tube-to-Tubesheet Roll Joint of Once-Through Sgs 3F0599-04, Monthly Operating Rept for Apr 1999 for Crystal River Unit 3.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Crystal River Unit 3.With ML20210U5631999-04-30030 April 1999 Revised Monthly Operating Rept for Apr 1999 for Crystal River,Unit 3 3F0499-04, Monthly Operating Rept for Mar 1999 for Crystal River Unit 3.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Crystal River Unit 3.With ML20204D9661999-03-31031 March 1999 Non-proprietary Rev 1,Addendum a to BAW-2342, OTSG Repair Roll Qualification Rept 3F0399-04, Special Rept 99-01:on 990310,discovered Containment Tendons That Required Grease Addition in Excess of Prescribed Limits During Recent Insp Activites.Six Tendons Were Refilled with Appropriate Amount of Grease1999-03-10010 March 1999 Special Rept 99-01:on 990310,discovered Containment Tendons That Required Grease Addition in Excess of Prescribed Limits During Recent Insp Activites.Six Tendons Were Refilled with Appropriate Amount of Grease 3F0399-03, Monthly Operating Rept for Feb 1999 for Crystal River Unit 3.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Crystal River Unit 3.With ML20203A4381999-02-0303 February 1999 Safety Evaluation Supporting EAL Changes for License DPR-72, Per 10CFR50.47(b)(4) & App E to 10CFR50 ML20206E9891998-12-31031 December 1998 Kissimmee Utility Authority 1998 Annual Rept ML20206E9021998-12-31031 December 1998 Florida Progress Corp 1998 Annual Rept ML20206E9701998-12-31031 December 1998 Ouc 1998 Annual Rept. with Financial Statements from Seminole Electric Cooperative,Inc 3F0199-05, Monthly Operating Rept for Dec 1998 for Crystal River Unit 3.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Crystal River Unit 3.With ML20206E9261998-12-31031 December 1998 Gainesville Regional Utilities 1998 Annual Rept 3F1298-13, Monthly Operating Rept for Nov 1998 for Crystal River,Unit 3.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Crystal River,Unit 3.With 3F1198-05, Monthly Operating Rept for Oct 1998 for Crystal River,Unit 3.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Crystal River,Unit 3.With ML20155F4071998-10-31031 October 1998 Rev 2 to Pressure/Temp Limits Rept ML20155J2701998-10-28028 October 1998 Second Ten-Year Insp Interval Closeout Summary Rept 3F1098-06, Monthly Operating Rept for Sept 1998 for Crystal River Unit 3.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Crystal River Unit 3.With ML20206E9461998-09-30030 September 1998 Utilities Commission City of New Smyrna Beach,Fl Comprehensive Annual Financial Rept Sept 30,1998 & 1997 ML20206E9561998-09-30030 September 1998 City of Ocala Comprehensive Annual Financial Rept for Yr Ended 980930 ML20206E9101998-09-30030 September 1998 City of Bushnell Fl Comprehensive Annual Financial Rept for Fiscal Yr Ended 980930 ML20206E9811998-09-30030 September 1998 City of Tallahassee,Fl Comprehensive Annual Financial Rept for Yr Ended 980930 ML20195E3121998-09-30030 September 1998 Comprehensive Annual Financial Rept for City of Leesburg,Fl Fiscal Yr Ended 980930 3F0998-07, Monthly Operating Rept for Aug 1998 for Crystal River Unit 3.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Crystal River Unit 3.With ML20236W6501998-07-31031 July 1998 Emergency Action Level Basis Document 3F0898-02, Monthly Operating Rept for Jul 1998 for Crystal River,Unit 11998-07-31031 July 1998 Monthly Operating Rept for Jul 1998 for Crystal River,Unit 1 ML20236V8801998-07-30030 July 1998 Control Room Habitability Rept 3F0798-01, Monthly Operating Rept for June 1998 for Crystal River Unit 31998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Crystal River Unit 3 ML20236Q4611998-06-30030 June 1998 SER for Crystal River Power Station,Unit 3,individual Plant Exam (Ipe).Concludes That Plant IPE Complete Re Info Requested by GL 88-20 & IPE Results Reasonable Given Plant Design,Operation & History 3F0698-02, Monthly Operating Rept for May 1998 for Crystal River Unit 31998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Crystal River Unit 3 1999-09-30
[Table view] |
LER-2084-001, Updated LER 84-001-01:on 840113,end Cap on Reactor Bldg Side of Spare Penetration 3531 Mistakenly Cut Off.Caused by Personnel Failure to Follow Applicable Engineering Procedures.Personnel Retrained |
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3022084001R00 - NRC Website |
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u.3. NUCLEM4 E.EQuLATOT;Y Cu senc Pee aos IS42) ap, ROVED Oase peo 31to-410e LICENSEE EVENT REPORT (LER) ,.
DOCERT seuGAGER (2) PAGE 43 p ACILify esAast qu CRYSTAL RIVER UNIT 3 o 15 t o 10 I o 13I 0 l2 1 loFl 013 nrtt .
REACTOR BUILDING CONTAINMENT PENETPATION NOT DESIGNED IN ACCORDANCE WITH FSAR Evges? OATE 193 LER NuesMR te) RGPORT DATE (71 OTHER PACILITIES INVOLVED (41 uCNT* OAv vtAR vtAR ag~ p,^, 6 a,*;;j;; .ON Ti. oAv vtAR P.civvv .-u oecmET ...ERis, N/A o,5go,o,o, , ,
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LICE 8 USEE CONTACT POR TMIS LER (129 8sLME TELEPHONE NUMSER AREA CODE R. H. Thompson, Engineer I 9101 4 7 i 915 i -i 3181012 '
ConsPLETE ONE LINE FOR EACM COesPONENT PaltuRE DESCRISED IN TMis REPORT 113)
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A NIH P i EiN i Ci3 ll i 0 Y i i i i i I I I I I I I I I I I I I I SUPPLEMENTAL REPORT EXPECTEO H44 WONTM OAV vtAR vis !!! vee eenwere EMPLCTfD $UOhil3310N CA TR, NO l l l AS$TA ACT (&na,e to F400 speces. I a, eseresunem,ypesa e,ay.e-soere rysewe,resa I,aesi t1sa During a refueling outage (May 1983) the end cap of a penetration in the reactor containment building was incorrectly cut off. Subsequently a plant modification package was issued to replace the end cap. A routine review of the modification package on January 13,1984, discovered several ,
d: sign specifications that were inconsistent with FSAR commitments. oersonnel error is the cause l
( of this event in tt +t both the design engineer (on contract to Florida Power Corporation) and the verification engineer (a Florida Power Corporation employee) failed to follow applicable i cngineering procedures. The verification engineer has been retrained on following applicable
- cngineering procedures. The design engineer no longer works for Florida Power Corporation. The
! results of the local leak rate test that was performed on the penetration (July 2,1983) and l
subsequent engineering evaluation (January,1984) indicate that the end cap will perform its intended safety function under the worst case LOCA conditions and thus justifies continued operation with the as-built penetration until the next refueling outage (March,1985). An cngineering evaluation was performed which concluded that the penetration is acceptable "as is" for the remainder of plant life.
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4 s esac Feene 3ssa U 8 NUCLEAR KECULATORY COidMisslON UCENSEE EVENT REPORT (LER) TEXT CONTINUATION ***aoveo cus No si5o-oica EXPsRES 8/3 115
, ACILetv NA.se Hi DOCKET NURAGER (2) Lgg ggg,gg, gg, pggg gg, vaan SEQVENT'ab af visions CRYSTAL RIVER UNIT 3 " * " . "'"
0 [51e 10 l0 l 3[ 0[2 814 01011 oF 011 012 0 13 r xr ,, . , w aae r.-e assa mm BACKGROUND In May,1983, during a refueling outage, the end plate on the reactor building side of spare penetration #3531 was mistakenly cut off. A plant modification package was issued on May 19, 1983, to replace the end cap on this penetration. The modification was installed on July 5,1983. >
IDENTIFICATION OF EVENT ,
A routine review of the modification package on January 13,1984, discovered:
- 1. ASTM A-36 was specified as the new end plate material (FSAR sections 5.2.2.4 and 5.2.2.4.2 require SA-516 Grade 60, impact tested to SA-300, and having certified mill test reports). li
- 2. All welding was required to be inspected per B31.7 - 1969. (FSAR sections 5.2.2.4.1, 5.2.2.4.3, and 5.2.2.4.4 require the NDE to be per ASME Section III Class B.)
3, The Modification Approval Record (MAR) specified a " soap test" to be performed on the welds on the Auxiliary Building side of the penetration during the Integrated Leak Rate Test.
This is not in compliance with 10CFR50, Appendix 3,Section IV. A, " Containment Modification." The proper test, however, was performed despite the MAR specifying the wrong test.
- 4. The safety evaluation in the MAR indicated that no changes to the FSAR were required.
(This is a violation of Safety Related Engineering Procedure (SREP) 6 Section V.3, in that the Design Engineer failed to identify the FSAR change, and a violation of SREP-4 in that the Verification Engineer failed to detect the error.)
5._ The applicable design drawing, S-521-036, was not changed to reflect the changes in the end plate thickness, plate material, and NDE. (This is a violation of SREP-2, Section D in that the Design Engineer did not correctly translate the design information onto the drawing and issue it as an interim drawing, and a violat6n of SREP-4 in that the Verification Engineer
' failed to detect the error.).
CAUSE OF EVENT Personnel error is the cause of this event in that both the Design Engineer (on contract to Florida P wer Corporation) and the Verification Engineer (a Florida Power employee) failed to follow applicable engineering procedures.
t INH, PEN, Chicago Bridge & Iron (C310)
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- g NRC Pere 3eeA U.S. NUCLEAR EECULATORY COMMSSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION An*Rovfo oue No nso-oice IXPiRES 8/311S F Aclu Y W NAME G U DOCKET NUMBER (21 ggg gygggg gg, pagg g vgAR SE Qve %T8 AL , *E v @ON CRYSTAL RIVER UNIT 3 rExt- - . .
eo,. =r.,on o ls io lo jo l 3l 0l2 8 14 0 l0l 1 -
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j ANALYSIS OF EVENT An engineering evaluation was performed subsequent to the discovery of the erroneous design specifications. The results of the engineering evaluation and the local leak rate test that was performed on the penetration after the end cap was installed (July 2,1983) indicate that the end cap will perform its intended safety function under the worst case LOCA conditions, thus justifying continued operation with the as-built penetration until Refuel V (March,1985). An engineering cvaluation was performed to review the above five discrepancies and to determine if the as-built l reactor containment building penetration is adequate for the remainder of plant life (beyond Refuel V) or if another nodification is required to make the penetration consistent with FSAR c:mmitments. The engineering evaluation concluded that the penetration is acceptable "as is" for the remainder of plant life. A copy of the detailed evaluation is available on site and has been forwarded to the NRC Senior Resident inspector.
The applicable Safety Related Engineering Procedures governing plant modifications were also reviewed and are considered adequate if properly used.
Several other reactor containment building penetration plant modification packages were reviewed and found to comply with the FSAR. Hence, this event appears to be an isolated occurrence.
CORF":CTIVE ACTION Both the Design Engineer and the Verification Engineer had been trained in the use of applicable 5:fety Related Engineering Procedures governing plant modifications. The Verification Engineer has been tetrained on following applicable engineering procedures. The Design Engineer no longer works for Florida Power Corporation.
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June 26,1984 3F0684-15 Document Control Desk U.S. Nuclear Regulatory Commission Washington, DC 20555
Subject:
Crystal River Unit 3 Docket No. 50-302 Operating License No. DPR-72 Licensee Event Report No. 84-001-01
Dear Sir:
Enclosed is Revision 1 to Licensee Event Report No.84-001 and the attached supplcmentary information sheet, which are submitted as stated in Florida Power Corporation's submittal of the subject LER on February 10,1984.
Should there be any questions, please contact this office.
Sincerely, t i G.R. Westafer Manager Nuclear Operations Licensing and Fuel Management RHT/nsw Enclosure ce: Mr. James P. O'Reilly Regional Administrator, Region II Office of Inspection & Enforcement -
U.S. Nuclear Regulatory Commission 101 Marietta Street N.W., Suite 2900 Atlanta, GA 30323 I
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GENERAL OFFICE 3201 Thirty fourth Street South e P.O. Box 14042, St. Petersburg, Florida 33733 e 813- 5151