05000416/LER-1982-031, Interim LER 82-031/99X-1:on 820722,HVAC Penetration Seal CV-19G Found Not Installed During Insp.Caused by Const Oversight.Maint Work Order Released to Install Seal & Hourly Fire Watch Established Until Task Completed

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Interim LER 82-031/99X-1:on 820722,HVAC Penetration Seal CV-19G Found Not Installed During Insp.Caused by Const Oversight.Maint Work Order Released to Install Seal & Hourly Fire Watch Established Until Task Completed
ML20079J025
Person / Time
Site: Grand Gulf Entergy icon.png
Issue date: 12/15/1982
From: Rohrer M
MISSISSIPPI POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20079J023 List:
References
LER-82-031-99X, LER-82-31-99X, NUDOCS 8212280081
Download: ML20079J025 (1)


LER-2082-031, Interim LER 82-031/99X-1:on 820722,HVAC Penetration Seal CV-19G Found Not Installed During Insp.Caused by Const Oversight.Maint Work Order Released to Install Seal & Hourly Fire Watch Established Until Task Completed
Event date:
Report date:
4162082031R00 - NRC Website

text

I- NRC FORM

  • 366 U. S. NUCLE AR REIULATORY COMMISSION l (F77)*

l LICENSEE EVENT REPORT Attachment to AECM-82/607

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l CONTROL BLOCK: l l l l l l

  • lh (PLliASE PRINT OR TYPE ALL REQUIRED INFORMATION) l 1

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i 8 9 lM l LICENSEE S l CCODE l G lS l 1 l@l 0 l0 l- LICENSE 14 15 l0 l0NUMBERl0 l0 l0 l- l0 l0 25 l@ 26 4l LICENSE 1l 1l TYPE 1l 1l@l JO l

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7 8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2 During a special inspection by the Fire-Protection / Safety Coordinator, penetration l l0l3l l seal CV-19G was found not installed. The HVAC penetration is located on the 189 feet l lo l4 j l elevation east passageway room OC711 of the Control Building. The event is being j lTTin I reported pursuant to T.S.6.9.2. The event had no effect on the health and safety of l l O l6 l l the public and did not constitute a threat to plant safety. l 10171 I i l O lH l l  !

7 8 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE O 9 IA lB lh [B is _

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} SEQUE NTI AL OCCURRENCE REPORT REVISION I LE _ EVENT YEAR REPORT NO. CODE TYPE N O.

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3i L1_J 32 T K N T OJ L NT MET HOURS SB IT D FOR B. 5 PPLIER MANUFACTURER l2_]@Lxl@

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43 44 47 CAUSE DESCRIPTION ^ND CORRECTIVE ACTIONS h 11lollThe open penetrat ion wa_s a constructinn nunrnight. A mninennnnro unrk nrdor _was l 1 1 frolonned to thn field tn innen11 thn non1_ An hnur1v firn unech was established l

? I in accordance with T.S.3.7.7.a until the work task was completed. This in a final l I1 13l lrenort. _ _ _ _ _ _ _

l 1 4 l l 7 8 9 80 ST s  % POWE R OTHE R STATUS dis O RY DISCOVERY DESCRIPTION 1 5 Wh l0 l0 l0 lhl NA _

l dhl_ Special Inspection l A TIVITY CO TENT RE LE ASED OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELEASE 1 6 8 9 d h lZ_j @ l 10 NA l l NA l 7 11 44 45 80 PERSONNE L EXPOSURES NUMBE R 1YPE DE SCHlP TION -

i i I O I O I O l@LZ_J@l NA l PERSONNE L INJU IES NUVBER DESCRIP f ION 7

1 R 8 9 l 0 l0 h_lhl n i2 NA l 63 toss OF OR DAYAGE TO F ACILt TY 43

_8212280001 821215 - 3 TYPE N i 9 (_Z_j@l oE SC"'"

NA PM MOCK 0%O0416 i S PDR l 7 H 9 to 80 PU B L ICi1 Y ISSUEp DE SCRIP TION NRC USE ONLY 2 o a 9 Ln.181 to ni i 68 69 IIIIiiIIIIiIl%1 80 %

NAME OF PREPAHEROriginal nicnod by Mntehnu v. Unhver PHONE: