ML20064H877

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/01T-0 on 781205:during Refueling Outage 6 Msiv'S Exceeded Leakage Limits.Caused by Degradation of Valve Seating Surfaces Thru Normal Oper
ML20064H877
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 12/18/1978
From:
TENNESSEE VALLEY AUTHORITY
To:
Shared Package
ML20064H876 List:
References
LER-78-034-01T, LER-78-34-1T, NUDOCS 7812270269
Download: ML20064H877 (2)


Text

NRC FORM 366 U. S. NUCLEAR REOULATORY COMMISSl!N CL77)

LICENSEE EVENT REPORT

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7 8 60 61 OCCKET NUM8ER EVf NT DES RIPTION AND PROBABLE CONSEQUENCES h '

IO I2l l During a refueling outage, while performing local leak rate tesCing, six MSIV's, FCV's IO ia i l 1-14,1-15,1-51,1-52,1-37, and 1-38, exceeded the leakage limits of T.S.4.7. A.2.1. l 10141 l FCV's 1-14,1-15,1-51, and 1-52 leakage was greater than 2,196 SCFH.FCV's 1-37 and 1-38 i i lo Isl I leakage was greater than 1,986 SCFH. Redundant systees were not applicable since the l l o is i l reacter was in the refueling mode. There was no hazard to the public health or safety.l l

LO W [ Previcus occurrence: BFRO-50-259/7723.

I I'O ITl i E CODE SU C E COMPONENT CODE Sus E S E

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  • 6/09/78 i LER SUPPLDIENTAL INFORMATION "BFRO 259 / 7834 Technical Specification Involved 4.7.A.2.1 Reported Under Technical Specification 6.7.2.a (3) 12/5/78 unknown Unit 1 Date of Occurrence Time of Occurrence .

Identification and Descriotion of Occurrence: -

Six MSIV's, FCV's 1-14, 1-15, 1-51, 1-52, 1-37, and 1-38, exceeded the leak rate allowed by T.S. 4.7.A.2.1 during local leak rate testing. The following are the leak rares:

FCV's 1-14, 1-15, 1-51,and 1-52 indicated a leak rate greater than 2,196 SCFH.

FCV's.1-37 and 1-38 indicated a leak race greater than 1,986 SCFH.

Conditions Price to Occurrence: - ,

Unit shutdown for refueling. The' reactor head was off. ,

Action specified in the Technical Specification Surveillance Requirements met due to inoperable eauioment. Describe .

Repair and retest to be completed. .

Apparent Cause of Occurrence:

Degradation of valve seating surface due to normal wear.

Analysis of Occurrence:

Nond Corrective Action:

Valves will be repaired and satisfactorily retested prior to return to service of the unit.

Failure Data:

BFRO-50-259/7723 Tennessee Valley Authority - Browns. Ferry Nuclear Plant l

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