ML20084T846

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LER BFRO-50-259/772:on 761229,pressure Switch PS-3-74B Exceeded Tech Spec Setpoint.Caused by Setpoint Drift.Switch Inspected,Recalibr & Functionally Tested for Repeatability
ML20084T846
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 01/20/1977
From: Fox H
TENNESSEE VALLEY AUTHORITY
To: Moseley N
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
LER-BFRO-50-259-772, NUDOCS 8306240190
Download: ML20084T846 (2)


Text

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UCENSEE EVENT REPORT CONTnOt etOCol l$

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fang DCfNSE NUMBEA Y

TYPE I:T Al1.1BIRIFlil Io 101-1oI oi ni nI nl-l ni nl It I, I, 11 1, i 10 I, 1 25 28 30 31 32 7 6b 14 15 y7p DOCKET NVMDE A EVENT DATE AipORT CATE ECOrt I 'l I

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57 SG 59 60 61 68 89 74 75 80 EVENT DESCR:PTION f5Ts1 l During surveillance testing, pressure switch PS-3-74B (RHR pump discharge low j

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[5i3] l pressure) exceeded technical specification setpoint.

Redundant switches were l

60 cl4] l available and this 'is not a repetitive problem.

Switch was recalibrated and

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BFRn 50-259/772.

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Ml 80 7 89 pavt b[t coYpCNENT ' CODE MAUF Clu A VOLATON cooE h l Cl Fl d l Il Nl SI 'll El U l lN!

lBl0l8!ol lJ_l u 69 10 11 12 17 43 44 47 48 CAUSE CESCRIPTION Switch was l

g lBarton model 288 pressure indicating switch #1 drifted below setpoint.

80 7 89 Serial # 6644 l

g l inspected, recalibrated, and functionally tested for repeatability.

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During surveillance testing l

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10 12 13 44 45 46 AC Tr.vT Y CONTENT LOCATON OF RELEASE I

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10 11 44 45 PEPSONNEt EXPOSURES NuY2E4 TYOL DESCA;PTON l

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80 7 89 11 12 13 PERSCNNEL INJUR:ES enxcin OEsCn# TON 10 l O ! 01 l

NA 7 80 11 12 OFFSITE CONSECUENCES l

rg5] l NA 80 7 89 LOSS CA OAMAGE TO FACILITY l

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l NA 7 89 10 0306240190 770120 PUBUCITY PDR ADOCK 05000259 PDR l

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80 7 89 ADDITIONAL FACTORS hl NA B0 7 09 l

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NAME:

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"_ / anuary 20, 1977 IE FILE COPY 2

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Mr. Norman C. Moseley, Director E4 7977 L,

U.S. Nuclear Regulatory Cornission p

Office of Inspection and Enforcenant Es. %,y %

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Region II g

230 Peachtree Street, NW., Suito 1217 Atlanta, Georgia 30303 8

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Dear Mr. Moseley:

TEN!iESSEE VALLET AUTHnRITY - BRINNS FERRY NUCLEAR PLANT UNIT 1 -

DOCKET MO. 50-259 - FACILITT OPERATING LICENSE DPR REPORTABLE OCCURRE' ICE REPORT BFRO-50-259/772 The enclosed report is to provide details concerning pressure switch PS-3-743 (RHR pump dischstge low pressure) that exceeded technical specification satpoint during surveillance testing. This report is sobmitted in accordance with Browns Ferry Technical Specifications

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Section 6.

This event occurred on Browns Ferry Nuclear Plant unit 1.

s Very truly yours, TENNESSEE VALLEY AUTHORITT

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H. S. Fox Director of Power Production Enclosure (3)

CC (Enclosure):

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Director (3)

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Office of Management Information and Program Control U.S. Nuclear Regulatory Commission Washington, D.C.

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