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Category:Inservice/Preservice Inspection and Test Report
MONTHYEARRA23-018, Post-Outage Inservice Inspection (ISI) Summary Report2023-06-27027 June 2023 Post-Outage Inservice Inspection (ISI) Summary Report RA22-051, Submittal of the Snubber Program Plan for the Fourth 10-Year Interval2022-11-16016 November 2022 Submittal of the Snubber Program Plan for the Fourth 10-Year Interval RA22-021, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2022-06-0808 June 2022 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report ML21196A5022021-07-15015 July 2021 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA21-017, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2021-04-0909 April 2021 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report NMP2L2711, Byron Station; Calvert Cliffs; Clinton Power Station; LaSalle County Station; Limerick Generating Station; and Nine Mile Point Nuclear Station - Proposed Alternative to Utilize Code Case N-8792019-10-16016 October 2019 Byron Station; Calvert Cliffs; Clinton Power Station; LaSalle County Station; Limerick Generating Station; and Nine Mile Point Nuclear Station - Proposed Alternative to Utilize Code Case N-879 RA19-034, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2019-06-0707 June 2019 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report NMP2L2700, Co. - Submittal of Proposed Alternative to Utilize Code Case N-879 for Plants2019-04-30030 April 2019 Co. - Submittal of Proposed Alternative to Utilize Code Case N-879 for Plants ML18200A0802018-07-18018 July 2018 Submittal of Fourth 10-Year Interval Inservice Testing (IST) Program Plan RA18-059, Inservice Testing Program Plan, Technical Position TP-052018-07-18018 July 2018 Inservice Testing Program Plan, Technical Position TP-05 ML17314A0082017-11-10010 November 2017 Submittal of Program Plan Associated with the Fourth Lnservice Inspection (ISI) Interval and the Third Containment Lnservice Inspection (Cisi) Interval RA17-055, Post-Outage 90-Day Lnservice Inspection (ISI) Summary Report2017-06-0707 June 2017 Post-Outage 90-Day Lnservice Inspection (ISI) Summary Report RA16-020, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2016-06-0808 June 2016 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA16-021, Cycle 17 Startup Test Report Summary2016-05-12012 May 2016 Cycle 17 Startup Test Report Summary RA15-028, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2015-06-26026 June 2015 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA15-035, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2015-05-28028 May 2015 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RS-15-011, Proposed Alternative to the Examination Requirements for Nozzle-to-Vessel Welds and Inner Radii Sections in Accordance with 10 CFR 50.55a(z)(1)2015-01-29029 January 2015 Proposed Alternative to the Examination Requirements for Nozzle-to-Vessel Welds and Inner Radii Sections in Accordance with 10 CFR 50.55a(z)(1) RA14-018, Post-Outage 90-Day Inservice (ISI) Summary Report2014-05-29029 May 2014 Post-Outage 90-Day Inservice (ISI) Summary Report ML14149A2732014-05-29029 May 2014 LaSalle County Station, Unit 1 - Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA13-023, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2013-05-31031 May 2013 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA12-052, Amended Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2012-10-26026 October 2012 Amended Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA12-018, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2012-06-0505 June 2012 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA11-024, Unit 2 - Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2011-06-0303 June 2011 Unit 2 - Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA10-023, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2010-06-0404 June 2010 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA09-041, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2009-05-0808 May 2009 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA08-070, Submittal of Third 10-Year Inservice Testing (IST) Interval Program Plan2008-12-17017 December 2008 Submittal of Third 10-Year Inservice Testing (IST) Interval Program Plan RA07-045, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2007-06-0101 June 2007 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA07-036, Submittal of Relief Requests Associated with the Third Inservice Inspection (ISI) Interval and the Second Containment Inservice Inspection (Cisi) Interval2007-04-30030 April 2007 Submittal of Relief Requests Associated with the Third Inservice Inspection (ISI) Interval and the Second Containment Inservice Inspection (Cisi) Interval RS-07-058, Amergen/Exelon Nuclear - Request for Relief - Use of the Boiling Water Reactor Vessel and Internals Project (BWRVIP) Guidelines in Lieu of Specific ASME Code Requirements2007-04-19019 April 2007 Amergen/Exelon Nuclear - Request for Relief - Use of the Boiling Water Reactor Vessel and Internals Project (BWRVIP) Guidelines in Lieu of Specific ASME Code Requirements RA06-063, Proposed Third Ten-Year Interval Inservice Testing Program2006-10-16016 October 2006 Proposed Third Ten-Year Interval Inservice Testing Program ML0629704302006-09-29029 September 2006 Proposed Third Ten-Year Interval Inservice Testing Relief Request RA06-038, Post-Outage 90-Day Inservice Inspection Summary Report2006-06-16016 June 2006 Post-Outage 90-Day Inservice Inspection Summary Report ML0518004412005-06-10010 June 2005 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report ML0429405252004-10-15015 October 2004 Amended 90-Day Post Outage ISI Summary Reports ML0414201292004-05-0707 May 2004 Post-Outage 90-Day Inservice Inspection Summary Report ML0314900182003-05-21021 May 2003 Post-Outage 90-Day Inservice Inspection Summary Report ML0213307432002-05-0606 May 2002 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report 2023-06-27
[Table view] Category:Letter
MONTHYEARIR 05000373/20230042024-01-24024 January 2024 County Station - Integrated Inspection Report 05000373/2023004 and 05000374/2023004 ML24024A1332024-01-24024 January 2024 Confirmation of Initial License Examination IR 05000373/20230122024-01-18018 January 2024 County Station - Biennial Problem Identification and Resolution Inspection Report 05000373/2023012 and 05000374/2023012 ML23354A2902024-01-0505 January 2024 Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0028 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) ML23360A6082023-12-27027 December 2023 County Station Request for Information for NRC Commercial Grade Dedication Inspection: Inspection Report 05000373/2024010 and 05000374/2024010 ML23278A1292023-12-14014 December 2023 Units 1 & 2; Limerick, Units 1 & 2; Nine Mile Point, Units 1 & 2; and Peach Bottom, Units 2 & 3 -Revision to Approved Alternatives to Use Boiling Water Reactor Vessel and Internals Project Guidelines ML23305A1402023-12-13013 December 2023 Units 1 & 2; Nine Mile Point, Unit 2; Peach Bottom, Units 2 & 3; and Quad Cities, Units 1 and 2 - Issuance of Amendments to Adopt Traveler TSTF-580 ML23317A1192023-11-10010 November 2023 Constellation Energy Generation, LLC - 2023 Annual Report - Guarantees of Payment of Deferred Premiums RS-23-120, Supplemental Information Letter for Part 73 Exemption Request - Responses to Request for Confirmatory Information2023-11-10010 November 2023 Supplemental Information Letter for Part 73 Exemption Request - Responses to Request for Confirmatory Information IR 05000373/20230032023-11-0909 November 2023 County Station Integrated Inspection Report 05000373/2023003, 05000374/2023003, and 07200070/2023001 ML23286A2602023-11-0808 November 2023 Issuance of Amendment Nos. 260 and 245 to Renewed Facility Operating Licenses Relocation of Pressure and Temperature Limit Curves to the Pressure Temperature Report IR 05000373/20234012023-11-0707 November 2023 County Station Security Baseline Inspection Report 05000373/2023401 and 05000374/2023401 RS-23-103, Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation2023-10-13013 October 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation RS-23-097, Constellation Energy Generation, LLC, Advisement of Leadership Changes and Submittal of Updated Standard Practice Procedures Plans2023-10-12012 October 2023 Constellation Energy Generation, LLC, Advisement of Leadership Changes and Submittal of Updated Standard Practice Procedures Plans IR 05000374/20230102023-10-11011 October 2023 NRC Inspection Report 05000374/2023010 IR 05000373/20233012023-09-15015 September 2023 Errata to NRC Initial License Examination Report 05000373/2023301; 05000374/2023301 RS-23-080, Constellation Energy Generation, LLC, Application to Revise Technical Specifications to Adopt TSTF-264-A, Revision 0, 3.3.9 and 3.3.10 - Delete Flux Monitors Specific Overlap Requirement SRs2023-08-30030 August 2023 Constellation Energy Generation, LLC, Application to Revise Technical Specifications to Adopt TSTF-264-A, Revision 0, 3.3.9 and 3.3.10 - Delete Flux Monitors Specific Overlap Requirement SRs RS-23-087, Revision to Approved Alternatives Associated with the Use of the BWRVIP Guidelines in Lieu of Specific ASME Code Requirements on Reactor2023-08-0404 August 2023 Revision to Approved Alternatives Associated with the Use of the BWRVIP Guidelines in Lieu of Specific ASME Code Requirements on Reactor ML23212A9012023-08-0303 August 2023 Regulatory Audit Report to Support the Review of the Amendments to Relocation of the Pressure Temperature Limit Curves to the Pressure and Temperature Limits Report IR 05000373/20230022023-08-0101 August 2023 County Station - Integrated Inspection Report 05000373/2023002 and 05000374/2023002 ML23208A3182023-07-27027 July 2023 Notification of an NRC Biennial Licensed Operator Requalification Program Inspection and RFI RS-23-084, Response to Request for Additional Information Regarding the Application to Revise Design Basis to Allow Use of Plastic Section Properties in Lower Downcomer Braces Analysis2023-07-24024 July 2023 Response to Request for Additional Information Regarding the Application to Revise Design Basis to Allow Use of Plastic Section Properties in Lower Downcomer Braces Analysis ML23192A5272023-07-12012 July 2023 NRC Initial License Examination Report 05000373/2023301; 05000374/2023301 ML23186A2062023-07-0606 July 2023 Information Request for a NRC Post-Approval Site Inspection for License Renewal 05000374/2023010 ML23181A1502023-06-30030 June 2023 Combined Response to Request for Additional Information and Supplemental Information in Support of LAR to Relocate Pressure and Temperature Limit Curves to the Pressure and Temperature Limits Report ML23178A2422023-06-28028 June 2023 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief in the Division of Operating Reactor Licensing for Plant Licensing Branch III IR 05000373/20230112023-06-26026 June 2023 County Station - Quadrennial Fire Protection Team Inspection Report 05000373/2023011 and 05000374/2023011 RS-23-077, Response to NRC Regulatory Issue Summary 2023-01, Preparation and Scheduling of Operator Licensing Examinations2023-06-16016 June 2023 Response to NRC Regulatory Issue Summary 2023-01, Preparation and Scheduling of Operator Licensing Examinations ML23167A0352023-06-16016 June 2023 Registration of Use of Cask to Store Spent Fuel ML23171A9562023-06-12012 June 2023 Post Exam Ltr RS-23-042, Application to Revise Technical Specifications to Adopt TSTF-580, Provide Exception from Entering Mode 4 with No Operable RHR Shutdown Cooling2023-05-25025 May 2023 Application to Revise Technical Specifications to Adopt TSTF-580, Provide Exception from Entering Mode 4 with No Operable RHR Shutdown Cooling IR 05000373/20230012023-05-10010 May 2023 County Station - Integrated Inspection Report 05000373/2023001 and 05000374/2023001 ML23123A2202023-05-0303 May 2023 Relief Request I4R-14 for Alternative Frequency to Containment Unbonded Post-Tensioning System Inservice Inspection ML23118A3472023-05-0101 May 2023 County, 1 & 2; Nine Mile Point, 2; and Quad Cities, 1 & 2 - Correction of Amendment No. 193 Adoption of TSTF-306, Revision 2, Add Action to LCO 3.3.6.1 to Give Option to Isolate the Penetration EPID L-2022-LLA-0143 ML23121A1612023-05-0101 May 2023 Information Meeting (Open House) with a Question-and-Answer Session to Discuss NRC 2022 End-of-Cycle Plant Performance Assessment of LaSalle County Station, Units 1 and 2 ML23114A2522023-04-28028 April 2023 Request to Use a Provision of a Later Edition of the ASME Boiler & Pressure Vessel Code, Section XI ML23081A0382023-04-25025 April 2023 County, 1 & 2; Nine Mile Point, 2; and Quad Cities, 1 & 2 - Issuance of Amendments to Adopt TSTF-306, Rev. 2, Add Action to LCO 3.3.6.1 to Give Option to Isolate the Penetration ML23110A3202023-04-21021 April 2023 Information Request to Support the NRC Annual Baseline Emergency Action Level and Emergency Plan Changes Inspection ML23107A1822023-04-18018 April 2023 Operator Licensing Examination Approval Lasalle County Station, May 2023 RS-23-049, Constellation Energy Generation, LLC, Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations2023-03-23023 March 2023 Constellation Energy Generation, LLC, Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations ML23073A2182023-03-22022 March 2023 Issuance of Amendment No. 258 to Renewed Facility Operating Licenses Exigent Amendment to Revise Design Basis Related to Seismic Requirements RS-23-048, Exigent Amendment Request to Revise Design Basis Related to Seismic Requirements2023-03-0707 March 2023 Exigent Amendment Request to Revise Design Basis Related to Seismic Requirements ML23061A1632023-03-0303 March 2023 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief in the Division of Operating Reactor Licensing for Plant Licensing Branch 3 IR 05000373/20220062023-03-0101 March 2023 Annual Assessment Letter for LaSalle County Station, Units 1 and 2 (Report 05000373/2022006 and 05000374/2022006) RS-23-045, Constellation Energy Generation, LLC Submittal of Fitness for Duty Performance Data Reports for 2022 Per 10 CFR 26.717(c) & 10 CFR 26.2032023-02-28028 February 2023 Constellation Energy Generation, LLC Submittal of Fitness for Duty Performance Data Reports for 2022 Per 10 CFR 26.717(c) & 10 CFR 26.203 RS-23-037, Annual 10 CFR 50.46 Report of Emergency Core Cooling System Evaluation Model Changes and Errors for LaSalle County Station2023-02-22022 February 2023 Annual 10 CFR 50.46 Report of Emergency Core Cooling System Evaluation Model Changes and Errors for LaSalle County Station ML23024A1372023-02-0303 February 2023 Request for Withholding Information from Public Disclosure for LaSalle County Station, Unit Nos. 1 and 2 ML23031A1972023-01-31031 January 2023 Notification of NRC Fire Protection Team Inspection Request for Information, Inspection Report Nos. 05000373/2023011 and 05000374/2023011 IR 05000373/20220042023-01-31031 January 2023 County Station - Integrated Inspection Report 05000373/2022004 and 05000374/2022004 RS-23-003, Constellation Energy Generation, LLC, Summary of Changes to Quality Assurance Topical Report, NO-AA-10, and Decommissioning Quality Assurance Program, NO-DC-102023-01-31031 January 2023 Constellation Energy Generation, LLC, Summary of Changes to Quality Assurance Topical Report, NO-AA-10, and Decommissioning Quality Assurance Program, NO-DC-10 2024-01-05
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LaSalle County Station Exelon Generation . 2601 North 21 " Road Marseilles, IL 61341 815-415-2000 Telephone www.exeloncorp.com RA21-042 10 CFR 50.55a(g)
July 15, 2021 United States Nuclear Regulatory Commission Attention: Document Control Desk Washington, D.C. 20555 LaSalle County Station, Unit 2 Renewed Facility Operating License No. NPF-18 NRC Docket No. 50-374
Subject:
Post-Outage 90-Day lnservice Inspection (ISi) Summary Report Exelon Generation Company, LLC (EGC) provides the attached Post-Outage 90-Day lnservice Inspection (ISi) Summary Report for LaSalle County Station Unit 2, submitted in accordance with 10 CFR 50.55a, "Codes and Standards," and the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code Case N-532-5, "Repair/Replacement Activity Documentation Requirements and lnservice Inspection Summary Report Preparation and Submission Section XI, Division 1."
The attached Post-Outage 90-Day ISi Summary Report is for examinations and repair/replacement activities performed between the end of LaSalle County Station Unit 2 seventeenth refueling outage on March 9, 2019, through the end of the eighteenth refueling outage (L2R18). This refueling outage started on February 15, 2021 and ended on April 19, 2021.
There are no regulatory commitments contained in this report. Should you have any questions concerning this letter, please contact Mr. Daniel Mearhoff, Regulatory Assurance Manager, at (815) 415-2800.
Respectfully,
~ .J--
Joh~ . u hko Site Vice President LaSalle County Station
Attachment:
Form OAR-1 Owner's Activity Report cc: Regional Administrator - NRC Region Ill NRC Senior Resident Inspector - LaSalle County Station
FORM OAR-1 OWNER'S ACTIVITY REPORT Report Number L2R 18 Plant LaSalle County Station, 2601 North 21st Road, Marseilles, IL 61341-9757 Unit No. 2 Commercial Service Date October 17, 1984 Refueling Outage Number L2R18 (if applicable)
Current Inspection Interval Fourth Inspection Interval (ISi), Third Inspection Interval (Containment ISi)
(1st, 2"'. 3, 4th , other)
Current Inspection Period Second Inspection Period (ISi and Containment ISi)
(1", 2"'. 3)
Edition and Addenda of Section XI applicable to the inspection plans ASME Section XI 2007 Edition through 2008 Addenda Date and Revision of inspection plans ISi Program Plan- February 11, 2021 Revision 1 Edition and Addenda of Section XI applicable to repair/replacement activities, if different than the inspection plans Same as above Code Cases used for inspection and evaluation: N-508-4, N-532-5, N-578-1, N-586-1, N-639, N-648-1, N-702, N-747, N-805 (1f applicable, including cases modified by Case N-532 and later revisions)
CERTIFICATE OF CONFORMANCE I certify that (a) the statements made in this report are correct; (b) the examinations and tests meet the Inspection Plan as required by the ASME Code,Section XI; and (c) the repair/replacement activities and evaluations supporting the completion of L2R18 conform to the requirements of Section XI. (refueling outage number)
Signed '?Jt+~----1 ~ /?/J IC fl.1 Ill (Owner or Owner's designee. Title)
- i 6 µ<;. 111,1 c.en. Date CERTIFICATE OF INSERVICE INSPECTION I, the undersigned, holding a valid commission issued by the National Board of Boiler and Pressure Vessel Inspectors and employed by The Hartford Steam Boiler Inspection and Insurance Company of Hartford, Connecticut have inspected the items described in this Owner's Activity Report, and state that, to the best of my knowledge and belief, the Owner has performed all activities represented by this report in accordance with the requirements of Section XI.
By signing this certificate neither the Inspector nor his employer makes any warranty, expressed or implied, concerning the repair/replacement activities and evaluation described in this report. Furthermore, neither the Inspector nor his employer shall be liable in any manner for any personal injury or property damage or a loss of any kind arising from or connected with this inspection.
{67rJ A I ~ (
(National Board Number a~dKorsement)
Date
TABLE 1 ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE Examination Examination Item Description Evaluation Description Category Item Number During a non-Code inspection of the upper tendon covers, 3/4" of water EC 633743 Rev 1, tendon V213B and None None was found inside the upper cover containment based on L2R 18 inspection (outside of the grease cap) of tendon results.
V213B. (IR 4406796)
TABLE 2 ABSTRACT OF REPAIR/REPLACEMENT ACTIVITIES REQUIRED FOR CONTINUED SERVICE Code Item Date Repair/Replacement Description of Work Class Description Com pleted Plan Number WO 4691305-47:2B33-F060B; BLEND 1 2B33-F060B INDICATION IN THE BOTTOM OF VALVE 04/16/2021 2797 BODY WO 4697590-59:2B33-F060A; BLEND 1 2B33-F060A INDICATION IN THE BOTTOM OF VALVE 04/14/2021 2798 BODY 1 WO 4691305-42: 2B33-F060B; Machining 2B33-F060B where anti-rotation segment and lower guide 04/20/2021 2803 plug set in the valve body.
1 WO 4697590-55: 2B33-F060A; Machining 2B33-F060A where anti-rotation segment and lower guide 04/13/2021 2804 plug set in the valve body.
1 WO 4697590-01 :2B33-F060A: Replace Ball 2810 2B33-F060A Shaft Assembly, Nuts Studs & Anti-Rotational 04/19/2021 Segment (non-pressure boundary) 1 WO 4691305-01 :2B33-F060B: Replace Ball 2B33-F060B Shaft Assembly, Nuts Studs & Anti-Rotational 04/19/2021 2811 Segment (non-pressure boundary)
WO 4902321-02: Plug and seal weld leaking 3 2E12-B001A tubes identified by eddy current testing and 03/04/2021 2672 inspection WO 5048109-03:2RT06AC-4" & 2RT06A-4":
RT piping 3 REPLACE DEGRADED SECTION(S) OF 03/02/2021 2691 replacement PIPING/ FITTINGS