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Category:Inservice/Preservice Inspection and Test Report
MONTHYEARRA23-018, Post-Outage Inservice Inspection (ISI) Summary Report2023-06-27027 June 2023 Post-Outage Inservice Inspection (ISI) Summary Report RA22-051, Submittal of the Snubber Program Plan for the Fourth 10-Year Interval2022-11-16016 November 2022 Submittal of the Snubber Program Plan for the Fourth 10-Year Interval RA22-021, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2022-06-0808 June 2022 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report ML21196A5022021-07-15015 July 2021 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA21-017, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2021-04-0909 April 2021 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report NMP2L2711, Byron Station; Calvert Cliffs; Clinton Power Station; LaSalle County Station; Limerick Generating Station; and Nine Mile Point Nuclear Station - Proposed Alternative to Utilize Code Case N-8792019-10-16016 October 2019 Byron Station; Calvert Cliffs; Clinton Power Station; LaSalle County Station; Limerick Generating Station; and Nine Mile Point Nuclear Station - Proposed Alternative to Utilize Code Case N-879 RA19-034, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2019-06-0707 June 2019 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report NMP2L2700, Co. - Submittal of Proposed Alternative to Utilize Code Case N-879 for Plants2019-04-30030 April 2019 Co. - Submittal of Proposed Alternative to Utilize Code Case N-879 for Plants ML18200A0802018-07-18018 July 2018 Submittal of Fourth 10-Year Interval Inservice Testing (IST) Program Plan RA18-059, Inservice Testing Program Plan, Technical Position TP-052018-07-18018 July 2018 Inservice Testing Program Plan, Technical Position TP-05 ML17314A0082017-11-10010 November 2017 Submittal of Program Plan Associated with the Fourth Lnservice Inspection (ISI) Interval and the Third Containment Lnservice Inspection (Cisi) Interval RA17-055, Post-Outage 90-Day Lnservice Inspection (ISI) Summary Report2017-06-0707 June 2017 Post-Outage 90-Day Lnservice Inspection (ISI) Summary Report RA16-020, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2016-06-0808 June 2016 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA16-021, Cycle 17 Startup Test Report Summary2016-05-12012 May 2016 Cycle 17 Startup Test Report Summary RA15-028, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2015-06-26026 June 2015 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA15-035, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2015-05-28028 May 2015 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RS-15-011, Proposed Alternative to the Examination Requirements for Nozzle-to-Vessel Welds and Inner Radii Sections in Accordance with 10 CFR 50.55a(z)(1)2015-01-29029 January 2015 Proposed Alternative to the Examination Requirements for Nozzle-to-Vessel Welds and Inner Radii Sections in Accordance with 10 CFR 50.55a(z)(1) RA14-018, Post-Outage 90-Day Inservice (ISI) Summary Report2014-05-29029 May 2014 Post-Outage 90-Day Inservice (ISI) Summary Report ML14149A2732014-05-29029 May 2014 LaSalle County Station, Unit 1 - Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA13-023, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2013-05-31031 May 2013 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA12-052, Amended Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2012-10-26026 October 2012 Amended Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA12-018, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2012-06-0505 June 2012 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA11-024, Unit 2 - Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2011-06-0303 June 2011 Unit 2 - Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA10-023, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2010-06-0404 June 2010 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA09-041, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2009-05-0808 May 2009 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA08-070, Submittal of Third 10-Year Inservice Testing (IST) Interval Program Plan2008-12-17017 December 2008 Submittal of Third 10-Year Inservice Testing (IST) Interval Program Plan RA07-045, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2007-06-0101 June 2007 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA07-036, Submittal of Relief Requests Associated with the Third Inservice Inspection (ISI) Interval and the Second Containment Inservice Inspection (Cisi) Interval2007-04-30030 April 2007 Submittal of Relief Requests Associated with the Third Inservice Inspection (ISI) Interval and the Second Containment Inservice Inspection (Cisi) Interval RS-07-058, Amergen/Exelon Nuclear - Request for Relief - Use of the Boiling Water Reactor Vessel and Internals Project (BWRVIP) Guidelines in Lieu of Specific ASME Code Requirements2007-04-19019 April 2007 Amergen/Exelon Nuclear - Request for Relief - Use of the Boiling Water Reactor Vessel and Internals Project (BWRVIP) Guidelines in Lieu of Specific ASME Code Requirements RA06-063, Proposed Third Ten-Year Interval Inservice Testing Program2006-10-16016 October 2006 Proposed Third Ten-Year Interval Inservice Testing Program ML0629704302006-09-29029 September 2006 Proposed Third Ten-Year Interval Inservice Testing Relief Request RA06-038, Post-Outage 90-Day Inservice Inspection Summary Report2006-06-16016 June 2006 Post-Outage 90-Day Inservice Inspection Summary Report ML0518004412005-06-10010 June 2005 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report ML0429405252004-10-15015 October 2004 Amended 90-Day Post Outage ISI Summary Reports ML0414201292004-05-0707 May 2004 Post-Outage 90-Day Inservice Inspection Summary Report ML0314900182003-05-21021 May 2003 Post-Outage 90-Day Inservice Inspection Summary Report ML0213307432002-05-0606 May 2002 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report 2023-06-27
[Table view] Category:Letter
MONTHYEARIR 05000373/20243012024-10-31031 October 2024 Initial License Examination Report 05000373/2024301 05000374/2024301 IR 05000373/20244042024-10-23023 October 2024 County Station – Security Baseline Inspection Report 05000373/2024404 and 05000374/2024404 RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests 05000373/LER-2023-001-01, Air Circuit Breaker (Acb) Mechanically Operated Contacts (MOC) Switch Failed to Actuate2024-10-0909 October 2024 Air Circuit Breaker (Acb) Mechanically Operated Contacts (MOC) Switch Failed to Actuate ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing IR 05000373/20244012024-09-27027 September 2024 County Station – Security Baseline Inspection Report 05000373/2024401 and 05000374/2024401 ML24263A2062024-09-19019 September 2024 Request for Exemption from Certain Requirements of 10 CFR 72.212 and 10 CFR 72.214 for LaSalle County Station - Holtec MPC-68MCBS ML24260A0492024-09-16016 September 2024 Operator Licensing Examination Approval - Lasalle County Station, Unit 1 and 2, September 2024 RS-24-090, Response to Request for Additional Information - Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds2024-09-12012 September 2024 Response to Request for Additional Information - Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification ML24249A1362024-09-0404 September 2024 EN 57304 - Westinghouse Electric Company, LLC, Final Report - No Embedded Files. Notification of the Potential Existence of Defects Pursuant to 10 CFR Part 21 IR 05000373/20240052024-08-29029 August 2024 Updated Inspection Plan and Assessment Follow-Up Letter for Lasalle County Station (Report 05000373/2024005; 05000374/2024005) IR 05000373/20244022024-08-28028 August 2024 County Station - Cyber Security Inspection Report 05000373/2024402 and 05000374/2024402 ML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 05000373/LER-2024-004-01, Emergency Diesel Generator Auto-Start and Load Due to Loss of System Auxiliary Transformer2024-08-22022 August 2024 Emergency Diesel Generator Auto-Start and Load Due to Loss of System Auxiliary Transformer IR 05000373/20240022024-08-13013 August 2024 County Station - Integrated Inspection Report 05000373/2024002 and 05000374/2024002 ML24222A6772024-08-0909 August 2024 Response to Request for Additional Information for Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition IR 05000373/20244202024-08-0505 August 2024 County Station - Security Baseline Inspection Report 05000373 2024420 and 05000374 2024420 05000373/LER-2024-003-01, Supplement to Technical Specification (TS) Limiting Condition for Operation (LCO) 3.6.1.3 Completion Time Exceeded2024-07-31031 July 2024 Supplement to Technical Specification (TS) Limiting Condition for Operation (LCO) 3.6.1.3 Completion Time Exceeded ML24208A0962024-07-25025 July 2024 57243-EN 57243 - Rssc Wire & Cable LLC, Dba Marmon - Part 21 Notification RS-24-064, Nuclear Radiological Emergency Plan Document Revisions2024-06-28028 June 2024 Nuclear Radiological Emergency Plan Document Revisions ML24178A2522024-06-27027 June 2024 County Station – Acknowledgement of Response to NRC Inspection Report 05000373/2024001 and 05000374/2024001 and Disputed Non-Cited Violation 05000373/LER-2024-004, Emergency Diesel Generator Auto-Start and Load Due to Loss of Station Auxiliary Transformer2024-06-19019 June 2024 Emergency Diesel Generator Auto-Start and Load Due to Loss of Station Auxiliary Transformer RS-24-061, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-06-14014 June 2024 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations 05000373/LER-2024-003, Technical Specification (TS) Limiting Condition for Operation (LCO) 3.6.1.3 Completion Time Exceeded2024-06-0606 June 2024 Technical Specification (TS) Limiting Condition for Operation (LCO) 3.6.1.3 Completion Time Exceeded IR 05000373/20240102024-05-29029 May 2024 County Station - Commercial Grade Dedication Inspection Report 05000373/2024010 and 05000374/2024010 ML24079A0762024-05-23023 May 2024 Issuance of Amendments to Adopt TSTF 264 ML24142A3352024-05-21021 May 2024 Quad Cities—Information Request to Support the NRC Annual Baseline Emergency Action Level and Emergency Plan Changes 05000373/LER-2024-002, Reactor Protection System Half Scram Due to Motor Generator Set Electric Power Monitoring Assembly Output Breaker Trip2024-05-17017 May 2024 Reactor Protection System Half Scram Due to Motor Generator Set Electric Power Monitoring Assembly Output Breaker Trip RS-24-055, 2023 Corporate Regulatory Commitment Change Summary Report2024-05-17017 May 2024 2023 Corporate Regulatory Commitment Change Summary Report ML24131A1512024-05-13013 May 2024 County Station - Integrated Report 05000373/2024001 and 05000374/2024001 IR 05000373/20240012024-05-13013 May 2024 County Station - Integrated Report 05000373/2024001 and 05000374/2024001 RS-24-038, Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds2024-05-0202 May 2024 Relief Request Concerning Extension of Permanent Relief from Ultrasonic Examination of Reactor Pressure Vessel Circumferential Shell Welds RS-24-041, Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-04-30030 April 2024 Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests 05000373/LER-2024-001, Core Operating Limits Report Thermal Limits Exceeded2024-04-26026 April 2024 Core Operating Limits Report Thermal Limits Exceeded ML24108A1562024-04-15015 April 2024 Updated Final Safety Analysis Report (Ufsar), Revision 26 and Fire Protection Report (Fpr), Revision 11 ML24103A2042024-04-12012 April 2024 Constellation Energy Generation, LLC, Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition RS-24-002, Constellation Energy Generation, LLC - Annual Property Insurance Status Report2024-04-0101 April 2024 Constellation Energy Generation, LLC - Annual Property Insurance Status Report ML24071A2122024-03-12012 March 2024 County Station - Information Request for the Cyber-Security Baseline Inspection, Notification to Perform Inspection IR 05000373/20230062024-02-28028 February 2024 Annual Assessment Letter for Lasalle County Station, Units 1 and 2 (Report 05000373/2023006; 05000374/2023006) RS-24-014, Annual 10 CFR 50.46 Report of Emergency Core Cooling System Evaluation Model Changes and Errors2024-02-22022 February 2024 Annual 10 CFR 50.46 Report of Emergency Core Cooling System Evaluation Model Changes and Errors ML24018A0682024-02-0909 February 2024 Issuance of Amendment Nos. 262 and 247 Revised Design Bases of Lower Downcomer Braces IR 05000373/20230042024-01-24024 January 2024 County Station - Integrated Inspection Report 05000373/2023004 and 05000374/2023004 ML24024A1332024-01-24024 January 2024 Confirmation of Initial License Examination IR 05000373/20230122024-01-18018 January 2024 County Station - Biennial Problem Identification and Resolution Inspection Report 05000373/2023012 and 05000374/2023012 ML23354A2902024-01-0505 January 2024 Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0028 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) ML23360A6082023-12-27027 December 2023 County Station Request for Information for NRC Commercial Grade Dedication Inspection: Inspection Report 05000373/2024010 and 05000374/2024010 ML23278A1292023-12-14014 December 2023 Units 1 & 2; Limerick, Units 1 & 2; Nine Mile Point, Units 1 & 2; and Peach Bottom, Units 2 & 3 -Revision to Approved Alternatives to Use Boiling Water Reactor Vessel and Internals Project Guidelines ML23305A1402023-12-13013 December 2023 Units 1 & 2; Nine Mile Point, Unit 2; Peach Bottom, Units 2 & 3; and Quad Cities, Units 1 and 2 - Issuance of Amendments to Adopt Traveler TSTF-580 05000373/LER-2023-002, Turbine Stop Valve Limit Switch Failure Due to Lubricant Degradation2023-12-0404 December 2023 Turbine Stop Valve Limit Switch Failure Due to Lubricant Degradation 2024-09-06
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LaSalle County Station Exelon Generation . 2601 North 21 " Road Marseilles, IL 61341 815-415-2000 Telephone www.exeloncorp.com RA21-042 10 CFR 50.55a(g)
July 15, 2021 United States Nuclear Regulatory Commission Attention: Document Control Desk Washington, D.C. 20555 LaSalle County Station, Unit 2 Renewed Facility Operating License No. NPF-18 NRC Docket No. 50-374
Subject:
Post-Outage 90-Day lnservice Inspection (ISi) Summary Report Exelon Generation Company, LLC (EGC) provides the attached Post-Outage 90-Day lnservice Inspection (ISi) Summary Report for LaSalle County Station Unit 2, submitted in accordance with 10 CFR 50.55a, "Codes and Standards," and the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code Case N-532-5, "Repair/Replacement Activity Documentation Requirements and lnservice Inspection Summary Report Preparation and Submission Section XI, Division 1."
The attached Post-Outage 90-Day ISi Summary Report is for examinations and repair/replacement activities performed between the end of LaSalle County Station Unit 2 seventeenth refueling outage on March 9, 2019, through the end of the eighteenth refueling outage (L2R18). This refueling outage started on February 15, 2021 and ended on April 19, 2021.
There are no regulatory commitments contained in this report. Should you have any questions concerning this letter, please contact Mr. Daniel Mearhoff, Regulatory Assurance Manager, at (815) 415-2800.
Respectfully,
~ .J--
Joh~ . u hko Site Vice President LaSalle County Station
Attachment:
Form OAR-1 Owner's Activity Report cc: Regional Administrator - NRC Region Ill NRC Senior Resident Inspector - LaSalle County Station
FORM OAR-1 OWNER'S ACTIVITY REPORT Report Number L2R 18 Plant LaSalle County Station, 2601 North 21st Road, Marseilles, IL 61341-9757 Unit No. 2 Commercial Service Date October 17, 1984 Refueling Outage Number L2R18 (if applicable)
Current Inspection Interval Fourth Inspection Interval (ISi), Third Inspection Interval (Containment ISi)
(1st, 2"'. 3, 4th , other)
Current Inspection Period Second Inspection Period (ISi and Containment ISi)
(1", 2"'. 3)
Edition and Addenda of Section XI applicable to the inspection plans ASME Section XI 2007 Edition through 2008 Addenda Date and Revision of inspection plans ISi Program Plan- February 11, 2021 Revision 1 Edition and Addenda of Section XI applicable to repair/replacement activities, if different than the inspection plans Same as above Code Cases used for inspection and evaluation: N-508-4, N-532-5, N-578-1, N-586-1, N-639, N-648-1, N-702, N-747, N-805 (1f applicable, including cases modified by Case N-532 and later revisions)
CERTIFICATE OF CONFORMANCE I certify that (a) the statements made in this report are correct; (b) the examinations and tests meet the Inspection Plan as required by the ASME Code,Section XI; and (c) the repair/replacement activities and evaluations supporting the completion of L2R18 conform to the requirements of Section XI. (refueling outage number)
Signed '?Jt+~----1 ~ /?/J IC fl.1 Ill (Owner or Owner's designee. Title)
- i 6 µ<;. 111,1 c.en. Date CERTIFICATE OF INSERVICE INSPECTION I, the undersigned, holding a valid commission issued by the National Board of Boiler and Pressure Vessel Inspectors and employed by The Hartford Steam Boiler Inspection and Insurance Company of Hartford, Connecticut have inspected the items described in this Owner's Activity Report, and state that, to the best of my knowledge and belief, the Owner has performed all activities represented by this report in accordance with the requirements of Section XI.
By signing this certificate neither the Inspector nor his employer makes any warranty, expressed or implied, concerning the repair/replacement activities and evaluation described in this report. Furthermore, neither the Inspector nor his employer shall be liable in any manner for any personal injury or property damage or a loss of any kind arising from or connected with this inspection.
{67rJ A I ~ (
(National Board Number a~dKorsement)
Date
TABLE 1 ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE Examination Examination Item Description Evaluation Description Category Item Number During a non-Code inspection of the upper tendon covers, 3/4" of water EC 633743 Rev 1, tendon V213B and None None was found inside the upper cover containment based on L2R 18 inspection (outside of the grease cap) of tendon results.
V213B. (IR 4406796)
TABLE 2 ABSTRACT OF REPAIR/REPLACEMENT ACTIVITIES REQUIRED FOR CONTINUED SERVICE Code Item Date Repair/Replacement Description of Work Class Description Com pleted Plan Number WO 4691305-47:2B33-F060B; BLEND 1 2B33-F060B INDICATION IN THE BOTTOM OF VALVE 04/16/2021 2797 BODY WO 4697590-59:2B33-F060A; BLEND 1 2B33-F060A INDICATION IN THE BOTTOM OF VALVE 04/14/2021 2798 BODY 1 WO 4691305-42: 2B33-F060B; Machining 2B33-F060B where anti-rotation segment and lower guide 04/20/2021 2803 plug set in the valve body.
1 WO 4697590-55: 2B33-F060A; Machining 2B33-F060A where anti-rotation segment and lower guide 04/13/2021 2804 plug set in the valve body.
1 WO 4697590-01 :2B33-F060A: Replace Ball 2810 2B33-F060A Shaft Assembly, Nuts Studs & Anti-Rotational 04/19/2021 Segment (non-pressure boundary) 1 WO 4691305-01 :2B33-F060B: Replace Ball 2B33-F060B Shaft Assembly, Nuts Studs & Anti-Rotational 04/19/2021 2811 Segment (non-pressure boundary)
WO 4902321-02: Plug and seal weld leaking 3 2E12-B001A tubes identified by eddy current testing and 03/04/2021 2672 inspection WO 5048109-03:2RT06AC-4" & 2RT06A-4":
RT piping 3 REPLACE DEGRADED SECTION(S) OF 03/02/2021 2691 replacement PIPING/ FITTINGS