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Category:INSPECTION REPORT
MONTHYEARIR 05000245/19990081999-09-14014 September 1999 Insp Repts 50-245/99-08,50-336/99-08 & 50-423/99-08 on 990615-0809.Four Violations Noted & Being Treated as Ncvs. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000423/19990071999-08-27027 August 1999 Insp Rept 50-423/99-07 on 990614-0715.Violations Noted & Being Treated as Ncvs.Major Areas Inspected:Review of C/A Program Using IP 40500, Effectiveness of Licensee Controls in Identifying,Resolving & Preventing Problems IR 05000336/19990061999-07-19019 July 1999 Insp Repts 50-336/99-06 & 50-423/99-06 on 990420-0614.Ten Violations Occurred & Being Treated as non-cited Violations. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000336/19982191999-06-10010 June 1999 Insp Rept 50-336/98-219 on 981214-18,990126-29,0208-19 & 0301-05.Noncited Violations Identified.Major Areas Inspected:Exam of Licensee Corrective Action Implementation IR 05000245/19990051999-06-0404 June 1999 Errata to Insp Repts 50-245/99-05,50-336/99-05 & 50-423/99-05,consisting of Figure 1 ML20207G1211999-06-0303 June 1999 Insp Repts 50-245/99-05,50-336/99-05 & 50-423/99-05 on 990302-0419.No Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000336/19990031999-05-10010 May 1999 Insp Rept 50-336/99-03 on 990322-26.No Violations Noted. Major Areas Inspected:Review of Actions Taken by Util to Resolve Significant Issues List Item 21,fire Protection ML20206F4601999-04-30030 April 1999 Insp Rept 50-336/99-04 on 990315-31.Violation Noted.Major Areas Inspected:Monitored Licensee Activities During Plant Transition Between Operational Modes,Both During Normal & off-normal Working Hours IR 05000245/19990021999-04-0202 April 1999 Insp Repts 50-245/99-02,50-336/99-02 & 50-423/99-02 on 990112-0301.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000336/19990011999-03-29029 March 1999 Insp Rept 50-336/99-01 on 990117-0217.Violations Noted.Major Areas Inspected:Licensee C/A Program Implementation Using Guidance of NRC IP 40500, Effectiveness of Licensee Controls in Identifying,Resolving & Preventing Problems IR 05000245/19980061999-03-0101 March 1999 Insp Repts 50-245/98-06,50-336/98-06 & 50-423/98-06 on 981123-990111.No Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support IR 05000245/19982171999-01-22022 January 1999 Evaluation Repts 50-245/98-217,50-336/98-217 & 50-423/98-217 Conducted on 981026-30.Areas Evaluated:Whether NNECO Has Improved Sufficiently & Has Demonstrated Sustained Performance in Maintaining safety-conscious Work Environ IR 05000336/19980051999-01-0707 January 1999 Insp Repts 50-336/98-05 & 50-423/98-05 on 981006-1123. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support IR 05000245/19982161998-11-18018 November 1998 Insp Repts 50-245/98-216,50-336/98-216 & 50-423/98-216 on 980818-1005.Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support IR 05000336/19982031998-11-0505 November 1998 Insp Rept 50-336/98-203 on 980824-0904.No Violations Noted. Major Areas Inspected:Effectiveness of Configuration Mgt Plan IR 05000336/19982131998-10-23023 October 1998 Insp Rept 50-336/98-213 on 980810-0903.Violations Noted. Major Areas Inspected:Certain Aspects of Accident Mitigation Sys IR 05000245/19982151998-10-14014 October 1998 Evaluation Repts 50-245/98-215,50-336/98-215 & 50-423/98-215 on 980824-28.Major Areas Evaluated:Whether Licensee Has Improved Sufficiently & Has Demonstrated Sustained Performance in Maintaining safety-conscious Work Environ IR 05000336/19980041998-10-0101 October 1998 Insp Rept 50-336/98-04 on 980914-18.No Violations Noted. Major Areas Inspected:Mov Program Associated with GL 89-10 IR 05000245/19982121998-09-25025 September 1998 Insp Repts 50-245/98-212,50-336/98-212 & 50-423/98-212 on 980630-0817.No Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support IR 05000423/19982111998-09-11011 September 1998 Insp Rept 50-423/98-211 on 980413-24,0511-15,27-29,0609-11 & 23-25.Violation Noted.Major Areas Inspected:Evaluation of Licensee C/As & Other ICAVP Process Activities IR 05000424/19980061998-09-10010 September 1998 Insp Repts 50-424/98-06 & 50-425/98-06 on 980628-0815.No Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support IR 05000245/19982081998-08-12012 August 1998 Insp Repts 50-245/98-208,50-336/98-208 & 50-423/98-208 on 980428-0629.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000336/19982011998-08-12012 August 1998 Insp Rept 50-336/98-201 on 980413-0508.Violations Noted. Major Areas Inspected:Licensee Ability to Identify & Resolve Deficiencies Focusing,But Not Limited To,Period of CMP Implementation & ICAVP at Parsons Power Group,Inc IR 05000245/19982071998-06-19019 June 1998 Insp Repts 50-245/98-207,50-336/98-207 & 50-423/98-207 on 980301-0427.Violations Noted.Major Areas Inspected:Maint, Operations,Engineering & Plant Support IR 05000423/19970831998-06-12012 June 1998 Insp Rept 50-423/97-83 on 980413-24.Violations Noted. Major Areas Inspected:Readiness of Plant Hardware,Staff & Mgt Programs to Support Safe Restart & Continued Operation of Plant Unit 3 IR 05000423/19970821998-06-11011 June 1998 Insp Rept 50-423/97-82 on 980209-20.Violations Noted.Major Areas Inspected:Corrective Actions Processes IR 05000336/19982021998-06-11011 June 1998 Insp Rept 50-336/98-202 on 980302-0409.Violations Noted. Major Areas Inspected:Cooling Water Sys ML20248E6131998-05-26026 May 1998 Insp Repts 50-245/98-206,50-336/98-206 & 50-423/98-206 on 980101-0228.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000423/19980811998-05-22022 May 1998 Insp Rept 50-423/98-81 on 980302-31 & 0412.Violations Noted. Major Areas Inspected:Plant Support IR 05000423/19982051998-05-0808 May 1998 Insp Rept 50-423/98-205 on 980223-0306.Violations Noted. Major Areas Inspected:Corrective Action Implemention Insp IR 05000423/19980011998-05-0606 May 1998 Insp Rept 50-423/98-01 on 980223-26.Violation Noted.Major Areas Inspected:Emergency Preparedness Program,Plant Support IR 05000245/19982101998-04-21021 April 1998 Evaluation Repts 50-245/98-210,50-336/98-210 & 50-423/98-210 on 971208-12 & 980105-09.No Violations Noted.Major Areas Inspected:Status & Effectivness of Independent third-party, Oversight Program,Established to Oversee ECP Implementation IR 05000245/19970121998-04-20020 April 1998 Evaluation Repts 50-245/97-12,50-336/97-12 & 50-423/97-12 on 971208-12 & 980105-09.No Violations Noted.Major Areas Evaluated:Implementation of ECP & Employee Concerns Oversight Program at Millstone IR 05000423/19972101998-04-0303 April 1998 Insp Rept 50-423/97-210 on 980105-0206.Violations Noted. Major Areas Inspected:Effectiveness of Configuration Mgt Program,Effectiveness of Sargent & Lundy Review of Sys Objectives & Quench & Recirculation Spray Sys IR 05000245/19980801998-04-0101 April 1998 Insp Repts 50-245/98-80,50-336/98-80 & 50-423/98-80 on 980223-26.No Violation Noted.Major Areas Inspected:Status of EP Facilities,Equipment & Resources,Ep Procedures & Documentation & Staff Knowledge & Performance IR 05000423/19972091998-04-0101 April 1998 Insp Rept 50-423/97-209 on 971027-980128.Violations Noted. Major Areas Inspected:Licensee Ability to Identify & Resolve Licensing Bases Deficiencies IR 05000423/19980821998-03-27027 March 1998 Insp Rept 50-423/98-82 on 980209-27.Violations Noted.Major Areas Inspected:Millstone Unit 3 MOV Program,Including Various C/A Taken IR 05000245/19972081998-02-25025 February 1998 Insp Repts 50-245/97-208,50-336/97-208 & 50-423/97-208 on 971201-31.Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support IR 05000336/19970841998-02-0909 February 1998 Insp Repts 50-336/97-84 & 50-423/97-84 on 970915-19.No Violations Noted.Major Areas Inspected:Review of post-fire Safe Shutdown Program for Unit 2 & Control of Configuration of post-fire Safe Shutdown Equipment for Unit 3 IR 05000336/19972111998-02-0909 February 1998 Insp Rept 50-336/97-211 on 970825-29,0902-05 & 1201-05.No Violations Noted.Major Areas Inspected:Evaluation of Parson Implementation of Independent CA Verification Program Audit Plan IR 05000245/19970851998-02-0606 February 1998 Insp Repts 50-245/97-85,50-336/97-85 & 50-423/97-85 on 971001-17,1120-21 & 1204-12.No Violations Noted.Major Areas Inspected:Simulator Portion of Annual Operating Tests of Licensed Operator Requalification Training Programs IR 05000245/19972071998-01-0909 January 1998 Insp Repts 50-245/97-207,50-336/97-207 & 50-423/97-207 on 971002-1130.No Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support ML20202J8191997-12-0505 December 1997 Insp Rept 50-423/97-206 on 970818-29 & 0908-19.Violations Noted.Major Areas Inspected:Licensees Configuration Mgt Plan & Emergency Core Cooling & Seal Injection Functions of Charging Sys ML20202A7071997-11-24024 November 1997 Insp Repts 50-245/97-81,50-336/97-81 & 50-423/97-81 on 970820-22.No Violations Noted.Major Areas Inspected: Licensee Emergency Response Organization During Biennial, full-participation Exercise IR 05000245/19972031997-11-21021 November 1997 Insp Repts 50-245/97-203,50-336/97-203 & 50-423/97-203 on 970722-1001.Violations Noted.Major Areas Inspected:Maint, Engineering,Plant Support & Conduct of Operations ML20210S8861997-08-29029 August 1997 Insp Repts 50-245/97-202,50-336/97-202 & 50-423/97-202 on 970520-0721.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support Re Performance in Emergency Preparedness & Control of FP Activities IR 05000245/19972021997-08-29029 August 1997 Insp Repts 50-245/97-202,50-336/97-202 & 50-423/97-202 on 970529-0721.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support,Including Emergency Preparedness Issues & Fire Protection Activities ML20141E3411997-06-24024 June 1997 Insp Repts 50-245/97-02,50-336/97-02 & 50-423/97-02 on 970311-0519.Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support ML20140C5641997-04-11011 April 1997 Insp Repts 50-245/97-01,50-336/97-01 & 50-423/97-01 on 970101-0310.Violations Noted.Major Areas Inspected:Maint, Engineering & Plant Support ML20140C0421997-03-26026 March 1997 Insp Repts 50-245/97-03,50-336/97-03 & 50-423/97-03 on 970203-07.No Violations Noted.Major Ares Inspected: Audits,Security Training,Equipment Testing & Management Support 1999-09-14
[Table view] Category:NRC-GENERATED
MONTHYEARIR 05000245/19990081999-09-14014 September 1999 Insp Repts 50-245/99-08,50-336/99-08 & 50-423/99-08 on 990615-0809.Four Violations Noted & Being Treated as Ncvs. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000423/19990071999-08-27027 August 1999 Insp Rept 50-423/99-07 on 990614-0715.Violations Noted & Being Treated as Ncvs.Major Areas Inspected:Review of C/A Program Using IP 40500, Effectiveness of Licensee Controls in Identifying,Resolving & Preventing Problems IR 05000336/19990061999-07-19019 July 1999 Insp Repts 50-336/99-06 & 50-423/99-06 on 990420-0614.Ten Violations Occurred & Being Treated as non-cited Violations. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000336/19982191999-06-10010 June 1999 Insp Rept 50-336/98-219 on 981214-18,990126-29,0208-19 & 0301-05.Noncited Violations Identified.Major Areas Inspected:Exam of Licensee Corrective Action Implementation IR 05000245/19990051999-06-0404 June 1999 Errata to Insp Repts 50-245/99-05,50-336/99-05 & 50-423/99-05,consisting of Figure 1 ML20207G1211999-06-0303 June 1999 Insp Repts 50-245/99-05,50-336/99-05 & 50-423/99-05 on 990302-0419.No Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000336/19990031999-05-10010 May 1999 Insp Rept 50-336/99-03 on 990322-26.No Violations Noted. Major Areas Inspected:Review of Actions Taken by Util to Resolve Significant Issues List Item 21,fire Protection ML20206F4601999-04-30030 April 1999 Insp Rept 50-336/99-04 on 990315-31.Violation Noted.Major Areas Inspected:Monitored Licensee Activities During Plant Transition Between Operational Modes,Both During Normal & off-normal Working Hours IR 05000245/19990021999-04-0202 April 1999 Insp Repts 50-245/99-02,50-336/99-02 & 50-423/99-02 on 990112-0301.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000336/19990011999-03-29029 March 1999 Insp Rept 50-336/99-01 on 990117-0217.Violations Noted.Major Areas Inspected:Licensee C/A Program Implementation Using Guidance of NRC IP 40500, Effectiveness of Licensee Controls in Identifying,Resolving & Preventing Problems IR 05000245/19980061999-03-0101 March 1999 Insp Repts 50-245/98-06,50-336/98-06 & 50-423/98-06 on 981123-990111.No Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support IR 05000245/19982171999-01-22022 January 1999 Evaluation Repts 50-245/98-217,50-336/98-217 & 50-423/98-217 Conducted on 981026-30.Areas Evaluated:Whether NNECO Has Improved Sufficiently & Has Demonstrated Sustained Performance in Maintaining safety-conscious Work Environ IR 05000336/19980051999-01-0707 January 1999 Insp Repts 50-336/98-05 & 50-423/98-05 on 981006-1123. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support IR 05000245/19982161998-11-18018 November 1998 Insp Repts 50-245/98-216,50-336/98-216 & 50-423/98-216 on 980818-1005.Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support IR 05000336/19982031998-11-0505 November 1998 Insp Rept 50-336/98-203 on 980824-0904.No Violations Noted. Major Areas Inspected:Effectiveness of Configuration Mgt Plan IR 05000336/19982131998-10-23023 October 1998 Insp Rept 50-336/98-213 on 980810-0903.Violations Noted. Major Areas Inspected:Certain Aspects of Accident Mitigation Sys IR 05000245/19982151998-10-14014 October 1998 Evaluation Repts 50-245/98-215,50-336/98-215 & 50-423/98-215 on 980824-28.Major Areas Evaluated:Whether Licensee Has Improved Sufficiently & Has Demonstrated Sustained Performance in Maintaining safety-conscious Work Environ IR 05000336/19980041998-10-0101 October 1998 Insp Rept 50-336/98-04 on 980914-18.No Violations Noted. Major Areas Inspected:Mov Program Associated with GL 89-10 IR 05000245/19982121998-09-25025 September 1998 Insp Repts 50-245/98-212,50-336/98-212 & 50-423/98-212 on 980630-0817.No Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support IR 05000423/19982111998-09-11011 September 1998 Insp Rept 50-423/98-211 on 980413-24,0511-15,27-29,0609-11 & 23-25.Violation Noted.Major Areas Inspected:Evaluation of Licensee C/As & Other ICAVP Process Activities IR 05000424/19980061998-09-10010 September 1998 Insp Repts 50-424/98-06 & 50-425/98-06 on 980628-0815.No Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support IR 05000245/19982081998-08-12012 August 1998 Insp Repts 50-245/98-208,50-336/98-208 & 50-423/98-208 on 980428-0629.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000336/19982011998-08-12012 August 1998 Insp Rept 50-336/98-201 on 980413-0508.Violations Noted. Major Areas Inspected:Licensee Ability to Identify & Resolve Deficiencies Focusing,But Not Limited To,Period of CMP Implementation & ICAVP at Parsons Power Group,Inc IR 05000245/19982071998-06-19019 June 1998 Insp Repts 50-245/98-207,50-336/98-207 & 50-423/98-207 on 980301-0427.Violations Noted.Major Areas Inspected:Maint, Operations,Engineering & Plant Support IR 05000423/19970831998-06-12012 June 1998 Insp Rept 50-423/97-83 on 980413-24.Violations Noted. Major Areas Inspected:Readiness of Plant Hardware,Staff & Mgt Programs to Support Safe Restart & Continued Operation of Plant Unit 3 IR 05000423/19970821998-06-11011 June 1998 Insp Rept 50-423/97-82 on 980209-20.Violations Noted.Major Areas Inspected:Corrective Actions Processes IR 05000336/19982021998-06-11011 June 1998 Insp Rept 50-336/98-202 on 980302-0409.Violations Noted. Major Areas Inspected:Cooling Water Sys ML20248E6131998-05-26026 May 1998 Insp Repts 50-245/98-206,50-336/98-206 & 50-423/98-206 on 980101-0228.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000423/19980811998-05-22022 May 1998 Insp Rept 50-423/98-81 on 980302-31 & 0412.Violations Noted. Major Areas Inspected:Plant Support IR 05000423/19982051998-05-0808 May 1998 Insp Rept 50-423/98-205 on 980223-0306.Violations Noted. Major Areas Inspected:Corrective Action Implemention Insp IR 05000423/19980011998-05-0606 May 1998 Insp Rept 50-423/98-01 on 980223-26.Violation Noted.Major Areas Inspected:Emergency Preparedness Program,Plant Support IR 05000245/19982101998-04-21021 April 1998 Evaluation Repts 50-245/98-210,50-336/98-210 & 50-423/98-210 on 971208-12 & 980105-09.No Violations Noted.Major Areas Inspected:Status & Effectivness of Independent third-party, Oversight Program,Established to Oversee ECP Implementation IR 05000245/19970121998-04-20020 April 1998 Evaluation Repts 50-245/97-12,50-336/97-12 & 50-423/97-12 on 971208-12 & 980105-09.No Violations Noted.Major Areas Evaluated:Implementation of ECP & Employee Concerns Oversight Program at Millstone IR 05000423/19972101998-04-0303 April 1998 Insp Rept 50-423/97-210 on 980105-0206.Violations Noted. Major Areas Inspected:Effectiveness of Configuration Mgt Program,Effectiveness of Sargent & Lundy Review of Sys Objectives & Quench & Recirculation Spray Sys IR 05000245/19980801998-04-0101 April 1998 Insp Repts 50-245/98-80,50-336/98-80 & 50-423/98-80 on 980223-26.No Violation Noted.Major Areas Inspected:Status of EP Facilities,Equipment & Resources,Ep Procedures & Documentation & Staff Knowledge & Performance IR 05000423/19972091998-04-0101 April 1998 Insp Rept 50-423/97-209 on 971027-980128.Violations Noted. Major Areas Inspected:Licensee Ability to Identify & Resolve Licensing Bases Deficiencies IR 05000423/19980821998-03-27027 March 1998 Insp Rept 50-423/98-82 on 980209-27.Violations Noted.Major Areas Inspected:Millstone Unit 3 MOV Program,Including Various C/A Taken IR 05000245/19972081998-02-25025 February 1998 Insp Repts 50-245/97-208,50-336/97-208 & 50-423/97-208 on 971201-31.Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support IR 05000336/19970841998-02-0909 February 1998 Insp Repts 50-336/97-84 & 50-423/97-84 on 970915-19.No Violations Noted.Major Areas Inspected:Review of post-fire Safe Shutdown Program for Unit 2 & Control of Configuration of post-fire Safe Shutdown Equipment for Unit 3 IR 05000336/19972111998-02-0909 February 1998 Insp Rept 50-336/97-211 on 970825-29,0902-05 & 1201-05.No Violations Noted.Major Areas Inspected:Evaluation of Parson Implementation of Independent CA Verification Program Audit Plan IR 05000245/19970851998-02-0606 February 1998 Insp Repts 50-245/97-85,50-336/97-85 & 50-423/97-85 on 971001-17,1120-21 & 1204-12.No Violations Noted.Major Areas Inspected:Simulator Portion of Annual Operating Tests of Licensed Operator Requalification Training Programs IR 05000245/19972071998-01-0909 January 1998 Insp Repts 50-245/97-207,50-336/97-207 & 50-423/97-207 on 971002-1130.No Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support ML20202J8191997-12-0505 December 1997 Insp Rept 50-423/97-206 on 970818-29 & 0908-19.Violations Noted.Major Areas Inspected:Licensees Configuration Mgt Plan & Emergency Core Cooling & Seal Injection Functions of Charging Sys ML20202A7071997-11-24024 November 1997 Insp Repts 50-245/97-81,50-336/97-81 & 50-423/97-81 on 970820-22.No Violations Noted.Major Areas Inspected: Licensee Emergency Response Organization During Biennial, full-participation Exercise IR 05000245/19972031997-11-21021 November 1997 Insp Repts 50-245/97-203,50-336/97-203 & 50-423/97-203 on 970722-1001.Violations Noted.Major Areas Inspected:Maint, Engineering,Plant Support & Conduct of Operations ML20210S8861997-08-29029 August 1997 Insp Repts 50-245/97-202,50-336/97-202 & 50-423/97-202 on 970520-0721.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support Re Performance in Emergency Preparedness & Control of FP Activities IR 05000245/19972021997-08-29029 August 1997 Insp Repts 50-245/97-202,50-336/97-202 & 50-423/97-202 on 970529-0721.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support,Including Emergency Preparedness Issues & Fire Protection Activities ML20141E3411997-06-24024 June 1997 Insp Repts 50-245/97-02,50-336/97-02 & 50-423/97-02 on 970311-0519.Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support ML20140C5641997-04-11011 April 1997 Insp Repts 50-245/97-01,50-336/97-01 & 50-423/97-01 on 970101-0310.Violations Noted.Major Areas Inspected:Maint, Engineering & Plant Support ML20140C0421997-03-26026 March 1997 Insp Repts 50-245/97-03,50-336/97-03 & 50-423/97-03 on 970203-07.No Violations Noted.Major Ares Inspected: Audits,Security Training,Equipment Testing & Management Support 1999-09-14
[Table view] Category:INSPECTION REPORT
MONTHYEARIR 05000245/19990081999-09-14014 September 1999 Insp Repts 50-245/99-08,50-336/99-08 & 50-423/99-08 on 990615-0809.Four Violations Noted & Being Treated as Ncvs. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000423/19990071999-08-27027 August 1999 Insp Rept 50-423/99-07 on 990614-0715.Violations Noted & Being Treated as Ncvs.Major Areas Inspected:Review of C/A Program Using IP 40500, Effectiveness of Licensee Controls in Identifying,Resolving & Preventing Problems IR 05000336/19990061999-07-19019 July 1999 Insp Repts 50-336/99-06 & 50-423/99-06 on 990420-0614.Ten Violations Occurred & Being Treated as non-cited Violations. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000336/19982191999-06-10010 June 1999 Insp Rept 50-336/98-219 on 981214-18,990126-29,0208-19 & 0301-05.Noncited Violations Identified.Major Areas Inspected:Exam of Licensee Corrective Action Implementation IR 05000245/19990051999-06-0404 June 1999 Errata to Insp Repts 50-245/99-05,50-336/99-05 & 50-423/99-05,consisting of Figure 1 ML20207G1211999-06-0303 June 1999 Insp Repts 50-245/99-05,50-336/99-05 & 50-423/99-05 on 990302-0419.No Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000336/19990031999-05-10010 May 1999 Insp Rept 50-336/99-03 on 990322-26.No Violations Noted. Major Areas Inspected:Review of Actions Taken by Util to Resolve Significant Issues List Item 21,fire Protection ML20206F4601999-04-30030 April 1999 Insp Rept 50-336/99-04 on 990315-31.Violation Noted.Major Areas Inspected:Monitored Licensee Activities During Plant Transition Between Operational Modes,Both During Normal & off-normal Working Hours IR 05000245/19990021999-04-0202 April 1999 Insp Repts 50-245/99-02,50-336/99-02 & 50-423/99-02 on 990112-0301.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000336/19990011999-03-29029 March 1999 Insp Rept 50-336/99-01 on 990117-0217.Violations Noted.Major Areas Inspected:Licensee C/A Program Implementation Using Guidance of NRC IP 40500, Effectiveness of Licensee Controls in Identifying,Resolving & Preventing Problems IR 05000245/19980061999-03-0101 March 1999 Insp Repts 50-245/98-06,50-336/98-06 & 50-423/98-06 on 981123-990111.No Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support IR 05000245/19982171999-01-22022 January 1999 Evaluation Repts 50-245/98-217,50-336/98-217 & 50-423/98-217 Conducted on 981026-30.Areas Evaluated:Whether NNECO Has Improved Sufficiently & Has Demonstrated Sustained Performance in Maintaining safety-conscious Work Environ IR 05000336/19980051999-01-0707 January 1999 Insp Repts 50-336/98-05 & 50-423/98-05 on 981006-1123. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support IR 05000245/19982161998-11-18018 November 1998 Insp Repts 50-245/98-216,50-336/98-216 & 50-423/98-216 on 980818-1005.Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support IR 05000336/19982031998-11-0505 November 1998 Insp Rept 50-336/98-203 on 980824-0904.No Violations Noted. Major Areas Inspected:Effectiveness of Configuration Mgt Plan IR 05000336/19982131998-10-23023 October 1998 Insp Rept 50-336/98-213 on 980810-0903.Violations Noted. Major Areas Inspected:Certain Aspects of Accident Mitigation Sys IR 05000245/19982151998-10-14014 October 1998 Evaluation Repts 50-245/98-215,50-336/98-215 & 50-423/98-215 on 980824-28.Major Areas Evaluated:Whether Licensee Has Improved Sufficiently & Has Demonstrated Sustained Performance in Maintaining safety-conscious Work Environ IR 05000336/19980041998-10-0101 October 1998 Insp Rept 50-336/98-04 on 980914-18.No Violations Noted. Major Areas Inspected:Mov Program Associated with GL 89-10 IR 05000245/19982121998-09-25025 September 1998 Insp Repts 50-245/98-212,50-336/98-212 & 50-423/98-212 on 980630-0817.No Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support IR 05000423/19982111998-09-11011 September 1998 Insp Rept 50-423/98-211 on 980413-24,0511-15,27-29,0609-11 & 23-25.Violation Noted.Major Areas Inspected:Evaluation of Licensee C/As & Other ICAVP Process Activities IR 05000424/19980061998-09-10010 September 1998 Insp Repts 50-424/98-06 & 50-425/98-06 on 980628-0815.No Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support IR 05000245/19982081998-08-12012 August 1998 Insp Repts 50-245/98-208,50-336/98-208 & 50-423/98-208 on 980428-0629.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000336/19982011998-08-12012 August 1998 Insp Rept 50-336/98-201 on 980413-0508.Violations Noted. Major Areas Inspected:Licensee Ability to Identify & Resolve Deficiencies Focusing,But Not Limited To,Period of CMP Implementation & ICAVP at Parsons Power Group,Inc IR 05000245/19982071998-06-19019 June 1998 Insp Repts 50-245/98-207,50-336/98-207 & 50-423/98-207 on 980301-0427.Violations Noted.Major Areas Inspected:Maint, Operations,Engineering & Plant Support IR 05000423/19970831998-06-12012 June 1998 Insp Rept 50-423/97-83 on 980413-24.Violations Noted. Major Areas Inspected:Readiness of Plant Hardware,Staff & Mgt Programs to Support Safe Restart & Continued Operation of Plant Unit 3 IR 05000423/19970821998-06-11011 June 1998 Insp Rept 50-423/97-82 on 980209-20.Violations Noted.Major Areas Inspected:Corrective Actions Processes IR 05000336/19982021998-06-11011 June 1998 Insp Rept 50-336/98-202 on 980302-0409.Violations Noted. Major Areas Inspected:Cooling Water Sys ML20248E6131998-05-26026 May 1998 Insp Repts 50-245/98-206,50-336/98-206 & 50-423/98-206 on 980101-0228.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000423/19980811998-05-22022 May 1998 Insp Rept 50-423/98-81 on 980302-31 & 0412.Violations Noted. Major Areas Inspected:Plant Support IR 05000423/19982051998-05-0808 May 1998 Insp Rept 50-423/98-205 on 980223-0306.Violations Noted. Major Areas Inspected:Corrective Action Implemention Insp IR 05000423/19980011998-05-0606 May 1998 Insp Rept 50-423/98-01 on 980223-26.Violation Noted.Major Areas Inspected:Emergency Preparedness Program,Plant Support IR 05000245/19982101998-04-21021 April 1998 Evaluation Repts 50-245/98-210,50-336/98-210 & 50-423/98-210 on 971208-12 & 980105-09.No Violations Noted.Major Areas Inspected:Status & Effectivness of Independent third-party, Oversight Program,Established to Oversee ECP Implementation IR 05000245/19970121998-04-20020 April 1998 Evaluation Repts 50-245/97-12,50-336/97-12 & 50-423/97-12 on 971208-12 & 980105-09.No Violations Noted.Major Areas Evaluated:Implementation of ECP & Employee Concerns Oversight Program at Millstone IR 05000423/19972101998-04-0303 April 1998 Insp Rept 50-423/97-210 on 980105-0206.Violations Noted. Major Areas Inspected:Effectiveness of Configuration Mgt Program,Effectiveness of Sargent & Lundy Review of Sys Objectives & Quench & Recirculation Spray Sys IR 05000245/19980801998-04-0101 April 1998 Insp Repts 50-245/98-80,50-336/98-80 & 50-423/98-80 on 980223-26.No Violation Noted.Major Areas Inspected:Status of EP Facilities,Equipment & Resources,Ep Procedures & Documentation & Staff Knowledge & Performance IR 05000423/19972091998-04-0101 April 1998 Insp Rept 50-423/97-209 on 971027-980128.Violations Noted. Major Areas Inspected:Licensee Ability to Identify & Resolve Licensing Bases Deficiencies IR 05000423/19980821998-03-27027 March 1998 Insp Rept 50-423/98-82 on 980209-27.Violations Noted.Major Areas Inspected:Millstone Unit 3 MOV Program,Including Various C/A Taken IR 05000245/19972081998-02-25025 February 1998 Insp Repts 50-245/97-208,50-336/97-208 & 50-423/97-208 on 971201-31.Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support IR 05000336/19970841998-02-0909 February 1998 Insp Repts 50-336/97-84 & 50-423/97-84 on 970915-19.No Violations Noted.Major Areas Inspected:Review of post-fire Safe Shutdown Program for Unit 2 & Control of Configuration of post-fire Safe Shutdown Equipment for Unit 3 IR 05000336/19972111998-02-0909 February 1998 Insp Rept 50-336/97-211 on 970825-29,0902-05 & 1201-05.No Violations Noted.Major Areas Inspected:Evaluation of Parson Implementation of Independent CA Verification Program Audit Plan IR 05000245/19970851998-02-0606 February 1998 Insp Repts 50-245/97-85,50-336/97-85 & 50-423/97-85 on 971001-17,1120-21 & 1204-12.No Violations Noted.Major Areas Inspected:Simulator Portion of Annual Operating Tests of Licensed Operator Requalification Training Programs IR 05000245/19972071998-01-0909 January 1998 Insp Repts 50-245/97-207,50-336/97-207 & 50-423/97-207 on 971002-1130.No Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support ML20202J8191997-12-0505 December 1997 Insp Rept 50-423/97-206 on 970818-29 & 0908-19.Violations Noted.Major Areas Inspected:Licensees Configuration Mgt Plan & Emergency Core Cooling & Seal Injection Functions of Charging Sys ML20202A7071997-11-24024 November 1997 Insp Repts 50-245/97-81,50-336/97-81 & 50-423/97-81 on 970820-22.No Violations Noted.Major Areas Inspected: Licensee Emergency Response Organization During Biennial, full-participation Exercise IR 05000245/19972031997-11-21021 November 1997 Insp Repts 50-245/97-203,50-336/97-203 & 50-423/97-203 on 970722-1001.Violations Noted.Major Areas Inspected:Maint, Engineering,Plant Support & Conduct of Operations ML20210S8861997-08-29029 August 1997 Insp Repts 50-245/97-202,50-336/97-202 & 50-423/97-202 on 970520-0721.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support Re Performance in Emergency Preparedness & Control of FP Activities IR 05000245/19972021997-08-29029 August 1997 Insp Repts 50-245/97-202,50-336/97-202 & 50-423/97-202 on 970529-0721.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support,Including Emergency Preparedness Issues & Fire Protection Activities ML20141E3411997-06-24024 June 1997 Insp Repts 50-245/97-02,50-336/97-02 & 50-423/97-02 on 970311-0519.Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support ML20140C5641997-04-11011 April 1997 Insp Repts 50-245/97-01,50-336/97-01 & 50-423/97-01 on 970101-0310.Violations Noted.Major Areas Inspected:Maint, Engineering & Plant Support ML20140C0421997-03-26026 March 1997 Insp Repts 50-245/97-03,50-336/97-03 & 50-423/97-03 on 970203-07.No Violations Noted.Major Ares Inspected: Audits,Security Training,Equipment Testing & Management Support 1999-09-14
[Table view] Category:UTILITY
MONTHYEARIR 05000245/19900231990-11-15015 November 1990 Insp Repts 50-245/90-23,50-336/90-25 & 50-423/90-23 on 901001-05.No Violations Noted.Major Areas Inspected: Radiological Controls Program IR 05000423/19900191990-11-14014 November 1990 Insp Rept 50-423/90-19 on 900905-1015.Violations Noted. Major Areas Inspected:Operations,Radiological & Chemistry Controls & Security & Maint & Surveillance IR 05000213/19900831990-11-0505 November 1990 Insp Repts 50-213/90-83,50-245/90-82,50-336/90-82 & 50-423/90-83 on 900924-28.No Violations Noted.Major Areas Inspected:Licensee Timeliness for Reporting/Operability Determinations IR 05000336/19900181990-11-0505 November 1990 Insp Rept 50-336/90-18 on 900822-1001.One Cited Violation, One Noncited Violation & One Deviation Noted.Major Areas Inspected:Plant Operations,Surveillance,Maint,Previously Identified Items,Engineering/Technical Support IR 05000245/19900191990-10-26026 October 1990 Safety Insp Repts 50-245/90-19,50-336/90-21 & 50-423/90-17 on 900904-07.No Violations or Deviations Identified.Major Areas Inspected:Qa Program Implementation IR 05000213/19900821990-10-23023 October 1990 Insp Repts 50-213/90-82,50-245/90-81,50-336/90-81 & 50-423/90-82,on 901001-12.No Violations Noted.Major Areas Inspected:Licensee Occupational Radiation Protection Program Activities During Unit 1 Refueling Outage IR 05000336/19900191990-10-15015 October 1990 Insp Rept 50-336/90-19 on 900910-14.No Violations Noted. Major Areas Inspected:Open Items & Allegations from Insp Rept 50-336/89-13 IR 05000245/19900161990-10-0303 October 1990 Partially Withheld Insp Repts 50-245/90-16,50-336/90-17 & 50-423/90-16 on 900827-31.Violations Noted IR 05000423/19900101990-08-17017 August 1990 Insp Rept 50-423/90-10 on 900612-0723.Violations Noted.Major Areas Inspected:Normal & Backshift Work Periods of Plant Operations,Maint & Surveillance,Security,Engineering & Technical Support,Radiological Controls & Safety Assessment IR 05000245/19900141990-08-16016 August 1990 Insp Repts 50-245/90-14,50-336/90-15 & 50-423/90-13 on 900723-27.One Noncited Violation Noted.Major Areas Inspected:Radiological Controls IR 05000423/19900061990-08-14014 August 1990 Insp Rept 50-423/90-06 on 900604-08.No Violations or Deviations Noted.Major Areas Inspected:Training Program, Including Licensed Operator Training Program for Initial Licensing & Requalification Program for Licensed Operators IR 05000245/19900111990-08-0909 August 1990 Insp Repts 50-245/90-11,50-336/90-12 & 50-423/90-09 on 900611-15 & 25-29.No Violations Noted.Major Areas Inspected: Review of Licensee Emergency Diesel Generator Fuel Oil Program IR 05000423/19900801990-08-0202 August 1990 Insp Rept 50-423/90-80 on 900416-25.No Violations Noted. Major Areas Inspected:Development of Sufficient Procedures in Appropriate Areas to Cover Broad Spectrum of Accidents & Equipment Failures IR 05000336/19900111990-07-31031 July 1990 Insp Rept 50-336/90-11 on 900530-0711.Noncited Violations Noted.Major Areas Inspected:Plant Operations,Radiological Controls/Emergency Preparedness,Maint/Surveillance, Engineering/Technical Support & Security IR 05000245/19900131990-07-24024 July 1990 Insp Repts 50-245/90-13,50-336/90-13 & 50-423/90-11 on 900609-13.No Violations or Deviations Noted.Major Areas Inspected:Radiological Environ Monitoring Program,Including Mgt Controls,Audits & Surveillance Procedures IR 05000245/19900091990-07-20020 July 1990 Insp Rept 50-245/90-09 on 900515-0625.No Violations Noted. Major Areas Inspected:Plant Operations,Radiological Controls,Maint/Surveillance,Security,Engineering/Technical Support & Safety Assessment/Quality Verification IR 05000245/19900071990-07-0606 July 1990 Insp Rept 50-245/90-07 on 900403-0514.No Violations Noted. Major Areas Inspected:Plant Operations,Radiological Controls,Maint/Surveillance,Security,Engineering/Technical Support & Safety Assessment/Quality Verification IR 05000423/19900081990-07-0303 July 1990 Partially Withheld Insp Rept 50-423/90-08 on 900503-0611 (Ref 10CFR73.21).Violations Noted.Major Areas Inspected: Maint & Surveillance,Security,Engineering & Technical Support & Safety Assessment & Quality Verification IR 05000336/19900081990-07-0202 July 1990 Insp Rept 50-336/90-08 on 900425-27.No Violations Noted. Major Areas Inspected:Results of Eddy Current Exam of Steam Generators Performed During Oct 1989,w/emphasis on Acceptable Period of Operation for Steam Generators ML20055E7991990-06-29029 June 1990 Insp Rept 50-336/90-09 on 900417-0529.Violations Noted. Major Areas Inspected:Plant Operations,Surveillance,Maint, Previously Identified Items,Engineering/Technical Support, Committee Activities,Periodic Repts,Lers & Allegations ML20055D1431990-06-20020 June 1990 Enforcement Conference Rept 50-245/90-08 on 900615.Major Areas Discussed:Findings in Insp Rept 50-245/90-08 Re Shipment of Irradiated Hardware as Radwaste to Low Level Waste Disposal Facility in Barnwell,Sc on 900507 ML20055C3161990-02-21021 February 1990 Insp Rept 50-245/89-19 on 891023-27.Unresolved Items Noted. Major Areas Inspected:Review of Selected Deviations from Rev 4 to to GE Topical Rept NEDO-31331, Emergency Procedure Guidelines & Response to NRC Bulletin 88-007,Suppl 1 IR 05000423/19890191989-09-22022 September 1989 Insp Rept 50-423/89-19 on 890828-0901.No Violations Noted. Major Areas Inspected:Radiological & non-radiological Chemistry Program Including Confirmatory Measurements, Chemistry & Lab Qa/Qc IR 05000245/19890181989-09-13013 September 1989 Insp Repts 50-245/89-18,50-336/89-18 & 50-423/89-15 on 890807-11.No Violations Noted.Major Areas Inspected:Util Compliance W/Atws Rule (10CFR50.62) & QA Annual Review, Including Procurement Program & Matl Receipt & Storage IR 05000245/19890801989-08-31031 August 1989 Insp Repts 50-245/89-80,50-336/89-80 & 50-423/89-80 on 890530-0616 & 0710-14.No Violations Noted.Major Areas Inspected:Units 1,2 & 3 Maint Program & Implementation, Review of Maint Documents & Observation of Work in Progress IR 05000336/19890161989-08-21021 August 1989 Insp Rept 50-336/89-16 on 890616-0726.Violation Noted.Major Areas Inspected:Plant Operations,Surveillance,Maint, Previously Identified Items,Committee Activities,Emergency Diesel Generator Operation & Fuel Oil Sys IR 05000423/19890131989-08-21021 August 1989 Insp Rept 50-423/89-13 on 890724-28.No Violations Noted. Major Areas Inspected:Fire Protection Prevention Program IR 05000245/19890161989-08-0202 August 1989 Insp Repts 50-245/89-16 & 50-336/89-15 on 890711-14.No Violations Noted.Major Areas Inspected:Implementation of Radiation Protection Program IR 05000423/19890111989-08-0202 August 1989 Insp Rept 50-423/89-11 on 890613-0717.No Violations Noted. Major Areas Inspected:Facility Tours of MP-3 Site,Esf Sys Walkdowns of Recirculation Spray Sys,Si Pump Cooling Sys, Turbine Driven Auxiliary Feed Pump Sys & Review of LERs IR 05000245/19890141989-07-28028 July 1989 Insp Rept 50-245/89-14 on 890616-0717.No Unsafe Conditions Noted.Major Areas Inspected:Plant Operations,Physical Security,Control Room Exercise Equipment & NRC Temporary Instruction 2513/93 IR 05000423/19890121989-07-21021 July 1989 Insp Rept 50-423/89-12 on 890626-30.No Violations or Deviations Noted.Major Areas Inspected:Inservice Insp Program,Steam Generator Eddy Current Insps & Water Chemistry Results IR 05000336/19890111989-07-21021 July 1989 Insp Rept 50-336/89-11 on 890505-0615.No Unsafe Conditions Noted.Major Areas Inspected:Plant Operations,Surveillance, Maint,Previously Identified Items,Allegations,Committee Activities,Licensee self-assessment & LERs IR 05000245/19890121989-07-19019 July 1989 Insp Rept 50-245/89-12 on 890509-0615.Major Areas Inspected: Previously Identified Items,Outage Activities,Plant Operations,Physical Security,Recirculation Pump Seal Failure Event,Reactor Scram on Low Main Condenser Vacuum & LERs IR 05000423/19890081989-07-11011 July 1989 Insp Rept 50-423/89-08 on 890515-0612.No Violations Noted. Major Areas Inspected:Plant Operations,Unresolved Item 50-423/87-12-01,previous Insp Findings,Plant Incident Repts, in-core Thimble Degradation & 10CFR50.59 Safety Evalautions IR 05000245/19890151989-07-0505 July 1989 Insp Repts 50-245/89-15,50-336/89-14 & 50-423/89-10 on 890619-23.No Violations or Deviations Noted.Major Areas Inspected:Effluent,Transportation & Solid Radwaste Programs, Including Mgt Controls,Audits,Qa & Program Implementation IR 05000245/19890131989-06-29029 June 1989 Enforcement Conference Rept 50-245/89-13 on 890621.Major Areas Discussed:Shipment of High Pressure Pump & Trailer W/ Removable External Radioactive Contamination from Licensee Reactor Site to Vendor Site in Moorestown,Nj IR 05000423/19890041989-06-28028 June 1989 Insp Rept 50-423/89-04 on 890405-0515.No Violations Noted. Major Areas Inspected:Plant Incident Repts,Reactor Scrams, Shutdown to Repair High Unidentified Leakage & Repair to Svc Water Piping & Physical Security IR 05000336/19890081989-06-20020 June 1989 Insp Rept 50-336/89-08 on 890324-0504.No Violations Noted. Major Areas Inspected:Plant Operations,Outage Activities, Surveillance,Maint,Plant Incident Repts & Allegations IR 05000245/19890081989-06-15015 June 1989 Insp Rept 50-245/89-08 on 880328-0508.No Unsafe Plant Conditions Noted.Major Areas Inspected:Plant Operations, Physical Security,Licensee Receipt Insp of New Fuel, Refueling,Plant Mods & LERs ML20245A8371989-06-0909 June 1989 Insp Rept 50-245/89-13 on 890517-18.Violations Noted Re Shipment of Package W/Removable External Radioactive Contamination in Excess of Limits & Failure to Supply Shipping Papers.Major Areas Inspected:Shipment of Pump IR 05000245/19890101989-06-0707 June 1989 Insp Repts 50-245/89-10 & 50-336/89-12 on 890515-19.No Violations Noted.Major Areas Inspected:Fire Protection & Prevention Program,Including Program Administration & Organization & Administrative Control of Combustibles ML20245A6781989-06-0707 June 1989 Insp Rept 50-245/89-11 on 890501-05.No Violations Noted. Major Areas Inspected:Observations,Review of Data,Licensee Response to Generic Ltr 88-01,NDE Procedures,Engineering Support & QA Involvement IR 05000245/19890091989-05-18018 May 1989 Insp Repts 50-245/89-09 & 50-336/89-10 on 890417-21.No Violations Noted.Major Areas Inspected:Review of Radiation Protection Activites at Unit 2 & Begining of Refueling Outage at Unit 1 IR 05000245/19890051989-05-17017 May 1989 Insp Repts 50-245/89-05 & 50-336/89-07 on 890417-21.No Violations Noted.Major Areas Inspected:Engineering Organization & Staffing,Qa,Plant Mods & Technical Training IR 05000423/19890031989-05-0303 May 1989 Insp Rept 50-423/89-03 on 890228-0404.No Violations Noted. Major Areas Inspected:Plant Operations,Status of Previous Insp Findings,Fuel Receipt & Insp,Generic Concerns About Steam Generator Tube Plugs,Esf Walkdown & LERs IR 05000245/19890041989-05-0303 May 1989 Insp Rept 50-245/89-04 on 8902214-0327.Major Areas Inspected:Previously Identified Items,Plant Operations, Physical Security,Ultrasonic Testing of Condensate Storage Tank,Maint Program Implementation & Committee Activities ML20246K0931989-04-26026 April 1989 Insp Rept 50-336/89-05 on 890211-0323.No Violations Noted. Major Areas Inspected:Outage Activities,Surveillance,Maint, Previously Identified Items,Plant Incident Repts & Allegations IR 05000245/19890061989-04-0707 April 1989 Insp Repts 50-245/89-06,50-336/89-09 & 50-423/89-06 on 890306-10.No Violations Noted.Major Areas Inspected:Review of Implementation of Radiation Protection Program at Unit 2 During Refueling Outage & Preparation of Outages for Units IR 05000245/19890071989-03-23023 March 1989 Insp Repts 50-245/89-07,50-336/89-06 & 50-423/89-07 on 890221-0303.No Violations or Deviations Noted.Major Areas Inspected:Site Observations & in-ofc Review of Data in Areas of Inservice Insp & Secondary Water Chemistry IR 05000245/19890031989-03-15015 March 1989 Insp Repts 50-245/89-03 & 50-336/89-04 on 890213-17.No Violations Noted.Major Areas Inspected:Unit 2 Refueling Outage Activities,Unit 1 Refueling Outage Preparation Activities & Station ALARA Practices 1990-08-09
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000245/19990081999-09-14014 September 1999 Insp Repts 50-245/99-08,50-336/99-08 & 50-423/99-08 on 990615-0809.Four Violations Noted & Being Treated as Ncvs. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000423/19990071999-08-27027 August 1999 Insp Rept 50-423/99-07 on 990614-0715.Violations Noted & Being Treated as Ncvs.Major Areas Inspected:Review of C/A Program Using IP 40500, Effectiveness of Licensee Controls in Identifying,Resolving & Preventing Problems IR 05000336/19990061999-07-19019 July 1999 Insp Repts 50-336/99-06 & 50-423/99-06 on 990420-0614.Ten Violations Occurred & Being Treated as non-cited Violations. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000336/19982191999-06-10010 June 1999 Insp Rept 50-336/98-219 on 981214-18,990126-29,0208-19 & 0301-05.Noncited Violations Identified.Major Areas Inspected:Exam of Licensee Corrective Action Implementation IR 05000245/19990051999-06-0404 June 1999 Errata to Insp Repts 50-245/99-05,50-336/99-05 & 50-423/99-05,consisting of Figure 1 ML20207G1211999-06-0303 June 1999 Insp Repts 50-245/99-05,50-336/99-05 & 50-423/99-05 on 990302-0419.No Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support ML20207F1521999-05-25025 May 1999 Notice of Violation from Investigation Rept 1-94-021 on 940506-960329.Violation Noted:Between 740831-910407,licensee Made Changes to Facility Described in Safety Analysis Rept for Refueling Core Offloads Without Performing Evaluation ML20196K2621999-05-24024 May 1999 EN-99-020:on 980525,notice of Violation & Exercise of Enforcement Discretion Will Be Issued to Licensee.Action Based on Severity Level III Problem Consisting of Four Individual Violations Involving Refueling Outage PNO-I-99-022, on 990509,Millstone Unit 2 Established Reactor Criticality.Nrc Staff Providing Augmented Insp Coverage of Restart Activities,Including round-the-clock Observations of Licensee Activities During Key Operational Evolutions1999-05-11011 May 1999 PNO-I-99-022:on 990509,Millstone Unit 2 Established Reactor Criticality.Nrc Staff Providing Augmented Insp Coverage of Restart Activities,Including round-the-clock Observations of Licensee Activities During Key Operational Evolutions IR 05000336/19990031999-05-10010 May 1999 Insp Rept 50-336/99-03 on 990322-26.No Violations Noted. Major Areas Inspected:Review of Actions Taken by Util to Resolve Significant Issues List Item 21,fire Protection ML20206F4601999-04-30030 April 1999 Insp Rept 50-336/99-04 on 990315-31.Violation Noted.Major Areas Inspected:Monitored Licensee Activities During Plant Transition Between Operational Modes,Both During Normal & off-normal Working Hours PNO-I-99-016, on 990406,operators Initiated Plant Cooldown from Normal Operating Pressure & Temp in Mode 3,hot Standby. Cooldown Was Necessary to Minimize Further Degradation of Bonnet Pressure Seal for Valve 2-SI-652 & to Repair Valve1999-04-0707 April 1999 PNO-I-99-016:on 990406,operators Initiated Plant Cooldown from Normal Operating Pressure & Temp in Mode 3,hot Standby. Cooldown Was Necessary to Minimize Further Degradation of Bonnet Pressure Seal for Valve 2-SI-652 & to Repair Valve ML20205M7201999-04-0606 April 1999 Notice of Violation from NRC OI Case 1-96-002 & Conclusions of Millstone Independent Review Team.Violation Noted. E Debarba,Deliberately Discriminated Against Supervisor in Performance Engineering Group at Millstone Station ML20205M7351999-04-0606 April 1999 Notice of Violation from Investigation in Case Numbers 1-96-002 & 1-97-007.Violation Noted:Licensee Discriminated Against Supervisor in Performance Engineering Group at Plant Due to Involvement in Protected Activities IR 05000245/19990021999-04-0202 April 1999 Insp Repts 50-245/99-02,50-336/99-02 & 50-423/99-02 on 990112-0301.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000336/19990011999-03-29029 March 1999 Insp Rept 50-336/99-01 on 990117-0217.Violations Noted.Major Areas Inspected:Licensee C/A Program Implementation Using Guidance of NRC IP 40500, Effectiveness of Licensee Controls in Identifying,Resolving & Preventing Problems ML20205J0941999-03-12012 March 1999 Rept of Review of Millstone Units 1,2 & 3:Allegations of Discrimination in NRC Ofc of Investigations Cases 1-96-002, 1-96-007,1-97-007 & Associated Lessons Learned ML20207M1131999-03-0909 March 1999 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $88,000.Violation Noted:Employment of Two Contractor Employees Terminated in Aug 1997,in Part Because Individuals Raised Concerns Re MOV Program Manual ML20205G6161999-03-0909 March 1999 EN-99-010:on 990309,notice of Proposed Imposition of Civil Penalty in Amount of $88,000 Issued to Licensee.Action Based Upon Severity Level II Problem Involving Discrimination Against Two Contractor Employees at Millstone MOV Dept IR 05000245/19980061999-03-0101 March 1999 Insp Repts 50-245/98-06,50-336/98-06 & 50-423/98-06 on 981123-990111.No Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support PNO-I-99-006, on 990128,operators Inadvertently Reduced Spent Fuel Pool Water Level by Two Inches When Purification of Spent Fuel Pool Water Initiated.Operators Held Shift Briefing to Discuss Realigning Purification Sys1999-01-29029 January 1999 PNO-I-99-006:on 990128,operators Inadvertently Reduced Spent Fuel Pool Water Level by Two Inches When Purification of Spent Fuel Pool Water Initiated.Operators Held Shift Briefing to Discuss Realigning Purification Sys IR 05000245/19982171999-01-22022 January 1999 Evaluation Repts 50-245/98-217,50-336/98-217 & 50-423/98-217 Conducted on 981026-30.Areas Evaluated:Whether NNECO Has Improved Sufficiently & Has Demonstrated Sustained Performance in Maintaining safety-conscious Work Environ PNO-I-99-004, on 990115,carbon Dioxide Was Inadvertently Discharged Into Unit 3 Cable Spreading Room,Containing Electrical Wiring.Ambulance Reported to Site as Precautionary Measure.Licensee Assembled Event Review1999-01-20020 January 1999 PNO-I-99-004:on 990115,carbon Dioxide Was Inadvertently Discharged Into Unit 3 Cable Spreading Room,Containing Electrical Wiring.Ambulance Reported to Site as Precautionary Measure.Licensee Assembled Event Review IR 05000336/19980051999-01-0707 January 1999 Insp Repts 50-336/98-05 & 50-423/98-05 on 981006-1123. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support ML20199C6381999-01-0707 January 1999 Notice of Violation from Insp on 981006-1123.Violation Noted:On or Before 981120,conduit 9-15,in Fire Area A-24,not Sealed & Tested in Accordance with Astme E-119,fire Endurance Test PNO-I-99-001, on 981231,Millstone Unit 2 Began Reloading Fuel Into Reactor After Extended Shutdown.Millstone Unit 3 Went Critical on 981230,after Forced Outage Due to Inadvertent MSIV Closure During Surveillance Testing at Power1999-01-0404 January 1999 PNO-I-99-001:on 981231,Millstone Unit 2 Began Reloading Fuel Into Reactor After Extended Shutdown.Millstone Unit 3 Went Critical on 981230,after Forced Outage Due to Inadvertent MSIV Closure During Surveillance Testing at Power PNO-I-98-062, on 981211,Millstone Unit 3 Tripped from 100% Reactor Power During MSIV Partial Stroke Testing.Solenoid Valve Integral to MSIV Failed to Reopen When Licensed Operator Released Test Switch1998-12-15015 December 1998 PNO-I-98-062:on 981211,Millstone Unit 3 Tripped from 100% Reactor Power During MSIV Partial Stroke Testing.Solenoid Valve Integral to MSIV Failed to Reopen When Licensed Operator Released Test Switch ML20195H6901998-11-18018 November 1998 Notice of Violation from Insp on 980818-1005.Violation Noted:Engineering Evaluations Not Performed When RCS Heatup Rate Limit Exceeded on 951217 & When RCS Cooldown Rate Limit Exceeded on Three occasions,940424,0728 & 951215 IR 05000245/19982161998-11-18018 November 1998 Insp Repts 50-245/98-216,50-336/98-216 & 50-423/98-216 on 980818-1005.Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support IR 05000336/19982031998-11-0505 November 1998 Insp Rept 50-336/98-203 on 980824-0904.No Violations Noted. Major Areas Inspected:Effectiveness of Configuration Mgt Plan ML20155B1521998-10-23023 October 1998 Notice of Violation from Insp on 980810-0903.Violation Noted:Design Basis,As Described in FSAR Chapter 14,Accident Analyses Had Not Been Correctly Translated Into Plant Procedures & Acceptance Criteria IR 05000336/19982131998-10-23023 October 1998 Insp Rept 50-336/98-213 on 980810-0903.Violations Noted. Major Areas Inspected:Certain Aspects of Accident Mitigation Sys IR 05000245/19982151998-10-14014 October 1998 Evaluation Repts 50-245/98-215,50-336/98-215 & 50-423/98-215 on 980824-28.Major Areas Evaluated:Whether Licensee Has Improved Sufficiently & Has Demonstrated Sustained Performance in Maintaining safety-conscious Work Environ IR 05000336/19980041998-10-0101 October 1998 Insp Rept 50-336/98-04 on 980914-18.No Violations Noted. Major Areas Inspected:Mov Program Associated with GL 89-10 IR 05000245/19982121998-09-25025 September 1998 Insp Repts 50-245/98-212,50-336/98-212 & 50-423/98-212 on 980630-0817.No Violations Noted.Major Areas Inspected: Operations,Maintenance,Engineering & Plant Support IR 05000423/19982111998-09-11011 September 1998 Insp Rept 50-423/98-211 on 980413-24,0511-15,27-29,0609-11 & 23-25.Violation Noted.Major Areas Inspected:Evaluation of Licensee C/As & Other ICAVP Process Activities ML20154D1151998-09-11011 September 1998 Notice of Violation from Insp on 980413-24-0511-15,27-29, 0609-11 & 23-25.Violation Noted:Program Implemented TS 6.8.4.a,failed to Include Provisions to Reduce Leakage from RSS Heat Exchangers to SW Sys IR 05000424/19980061998-09-10010 September 1998 Insp Repts 50-424/98-06 & 50-425/98-06 on 980628-0815.No Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support PNO-I-98-039, 980812,Millstone Unit 3 Was Shutdown to Repair Small Leak on Afws Discharge Noted.Current Leakage Does Not Exceed Regulatory Requirements & Shutdown Not Required by Tech Specs.Licensee Issued Press Release on 9808111998-08-12012 August 1998 PNO-I-98-039:980812,Millstone Unit 3 Was Shutdown to Repair Small Leak on Afws Discharge Noted.Current Leakage Does Not Exceed Regulatory Requirements & Shutdown Not Required by Tech Specs.Licensee Issued Press Release on 980811 ML20237D3041998-08-12012 August 1998 Notice of Violation from Insp on 980413-0508.Violations Noted:Two Examples Identified Where Licensee Not Performing Leakage Testing of safety-related Valves in Sys That Could Contain Highly Radioactive Fluids During Accident IR 05000245/19982081998-08-12012 August 1998 Insp Repts 50-245/98-208,50-336/98-208 & 50-423/98-208 on 980428-0629.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support ML20237B0741998-08-12012 August 1998 Notice of Violation from Insp on 980428-0629.Violation Noted:Licensee Failed to Direct Test Personnel to Close & Lock RHR Outboard Drain Valve IR 05000336/19982011998-08-12012 August 1998 Insp Rept 50-336/98-201 on 980413-0508.Violations Noted. Major Areas Inspected:Licensee Ability to Identify & Resolve Deficiencies Focusing,But Not Limited To,Period of CMP Implementation & ICAVP at Parsons Power Group,Inc PNO-I-98-026, on 980701,Millstone Unit 3 Criticality Update Made.Nrc Staff Continues to Provide Augmented Insp of Unit 3 Restart Activities,Including round-the-clock Coverage of Key Operational.Licensee Plans No Press Release1998-07-0101 July 1998 PNO-I-98-026:on 980701,Millstone Unit 3 Criticality Update Made.Nrc Staff Continues to Provide Augmented Insp of Unit 3 Restart Activities,Including round-the-clock Coverage of Key Operational.Licensee Plans No Press Release PNO-I-98-025, on 980630,unit 3 Established Reactor Criticality,However Reactor Was Shut Down When Control Room Operator Noticed Spiking Intermediate Range Monitor.Licensee Troubleshooting1998-06-30030 June 1998 PNO-I-98-025:on 980630,unit 3 Established Reactor Criticality,However Reactor Was Shut Down When Control Room Operator Noticed Spiking Intermediate Range Monitor.Licensee Troubleshooting IR 05000245/19982071998-06-19019 June 1998 Insp Repts 50-245/98-207,50-336/98-207 & 50-423/98-207 on 980301-0427.Violations Noted.Major Areas Inspected:Maint, Operations,Engineering & Plant Support ML20249C6931998-06-19019 June 1998 Notice of Violations from Combined Insp on 980301-0427. Violations Noted:Prior to 980424,instrument Min Accuracy of Wind Speed Channels Were Not Measured as Required by Table 3.3-8 of Unit 2 TS 3/4.3.3.4 IR 05000423/19970831998-06-12012 June 1998 Insp Rept 50-423/97-83 on 980413-24.Violations Noted. Major Areas Inspected:Readiness of Plant Hardware,Staff & Mgt Programs to Support Safe Restart & Continued Operation of Plant Unit 3 ML20249B0421998-06-12012 June 1998 Notice of Violations from Insp on 980413-24.Violations Noted:Only 1 RCS Loop Operable W/Plant in Mode 4 on 980407 IR 05000423/19970821998-06-11011 June 1998 Insp Rept 50-423/97-82 on 980209-20.Violations Noted.Major Areas Inspected:Corrective Actions Processes 1999-09-14
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U.S. NUCLEAR REGULATORY COMMISSION
REGION I
j Report N /89-02 Docket N License N NPF-49 Licensee: . Northeast Nuclear Energy Company P. O. Box-270 Hartford, CT 06101-0270 Facility Name: . Millstone Nuclear Power Station, Unit 3 Inspection At: Waterford, Connecticut Inspection Conducted: 1/24/89 - 2/27/89 Reporting Inspector: .G. S. Barber, Resident Inspector Inspectors: W. J. Raymond, Senior Resident Inspector G. S. Barber, Resident' Inspector E. Yachimiak, Operations Engineer D. Jaffe, Licensing Project Manager Approvedby : deO. k O du E. C. McCabe, Chief,.R6 actor Projects Section IB
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3_/10l 89 Date Inspection Summary:
L Areas Inspected: Routine onsite inspection (115 inspection hours, with 11-.5 deep backshift hours and 16 total backshift hours) cf plant operations, Licensee Event Reports (LERs), maintenance, surveillance, Shutdown Bank "D" failing to move on command, "B" Reactor Coolant Pump (RCP) high stator temperature, safety injection with the Reactor Coolant System (RCS) in mid-loop conditions, Plant Incident Re-ports (PIRs), station blackout test; TI 2515/100, Proper Receipt, Storage, and Handling of Emergency Diesel Generator (EDG) Fuel Oil; Rosemount transmitter oil leaks, and licensed operator renewal application practice Results: No unsafe plant conditions, violations, or unresolved items were identi-fied. TI 2515/100 was closed. Control of entering Containment at power to deter-mine the cause for a high RCP stator temperature and the subsequent shutdown and cooldown demonstrated a strong safety attitude. Testing of potentially defective Rosemount transmitters was thorough. Prompt and consistent submission of a Trouble Report (TR) to generate the needed repair of degraded / defective equipment was not being accomplished (Detail 3.1). Licensee PIRs continue to identify repetitive instances of fire watches not being stationed as required (Detail 4.1). j 8903240297 890315 ~ .,
PDR ADOCK 05000423(
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PAGE 1.0 Persons
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Contacted.................................................... 1 2.0 Summary of Facility Activities........................... ........... 1 3.0 P.eview of Facility Activities......... .............................. 1 3.1 Shutdown Bank "D" Failed to Move on Command (71707).......... .. 1 l 3.2 Unplanned Shutdown Due to "B" RCP High Stator Temperature (71707)................................ ...................... 2 3.3 Safety Injection with the RCS in Mid-Loop Conditions (93702). . .. 2 3.4 MSIV Solenoid Vent Valve Stroke Failure (61726)................. 3 3.5 Reactor Plant Component Cooling Water (RPCCW) System Leaks (71707)......................... .... ........................ 4 3.6 Station Blackout Test (37700)........................ .......... 4 4.0 Plant Operational Status Reviews (71707)............................. 5 4.1 Review of Plant Incident Reports (PIRs) (90712)................. 6 5.0 (Closed) TI 2515/100, " Proper Receipt, Storage, and Handling of i Emergency Diesel Generator (EOG) Fuel Oil" (25500). . . . . . . . . . . . . . . . . 7 5.1 Fuel Oil Sampling and Tank Inspection........................... 7 5.2 System Design and Operation.............. ....... .............. 7 i 5.3 Filter / Strainer Preventive Maintenance.... ..................... 8 5.4 Seismic Qualifications of Instruments and Controls. . . . . . . ..... 9 5.5 Conclusions. .................................. ................ 9 6.0 Licensed Operator Renewal Application Practices (NRC Form 398)
(41701)..................................................... ...... 9 7.0 10 CFR 21 - Rosemount Transmitter Oil Leaks (36100)............... .. 10 l
l 8.0 Review of Licensee Event Reports (LERs) (92700). . . . . . . . . . . . . . . . . . . . . 13 l 9.0 Maintenance (62703)... ............................. ..... .. .... .. 14 10.0 Surveillance (61726).............................................. .. 14 11.0 Management Meeti ng s ( 31703) . . . . . . . . . . . . . . . . . . . . . . ...... ....... 15 l
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DETAILS 1.0 Persons Contacted Inspection findings were discussed periodically with the supervisory and man-agement personnel identified below:
S. Scace, Station Superintendent C. Clement, Unit Superintendent, Unit 3 M. Gentry, Operations Supervisor R. Rothgeb, Maintenance Supervisor K. Burton, Staff Assistant to Unit Superintendent J. Harris, Engineering Supervisor D. McDaniel, Reactor Engineer R. Satchatello, Health Physics Supervisor M. Pearson, Operations Assistant R. Stotts, Operations Training Supervisor B. Ruth, Operations Training Manager K. Covin, Operations Assistant 2.0 Summary of Facility Activities The plant began the inspection period at full powe Long term monitoring of "B" RCP Stator Temperature showed a slow increase to 292-294 degrees F over the 6 weeks prior to February 11 (see Detail 4.2). On February 11, power was reduced to 45%-50% to reduce containment radiation levels. A containment ;
entry was made at 10:21 The entry team exited at 11:46 Management I reviewed the team's findings and concluded it was necessary to shut down and i proceed to cold shutdown (Mode 5) to replace the "B" RCP stator cooler. Ex-cessive boric acid buildup on the stator cooling coils did not allow adequate cooling air flo Mode 5 was entered at 2:33 p.m. , February 12. The source of boric acid was a leaky hot leg stop valve that was repaired and satisfactorily reteste Heatup was commenced. The turbine was on-line at 11:22 a.m. , February 23 with 95% power being reached at 4:00 p.m., February 24. Power was limited since the "A" heater drain pump was removed for repairs. Power remained at 95%
through the end of the perio .0 Review of Facility Activities 3.1 Shutdown Bank "D" Failed to Move on Command (71707)
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Shutdown Bank "D" failed to move when commanded at 6:25 p.m., February J 11 during reactor shutdown. The reactor was being shut down to correct I the cause for a high "B" RCP stator temperature. The on-shift operators contacted Instrumentation & Control (I&C) to troubleshoot the proble I&C recommended cycling the bank select switch and attempting to move the rods again. The switch was cycled and rods were driven inwar i l
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The inspector reviewed-this event and noted that the Shift Supervisor's (SSs) log did not document the submission of a trouble report, nor did the select switch have a trouble sticker on i The submission of a trouble, report (TR) and its documentation in the SSs log assures that L equipment problems are addressed. Timely submittal of TRs ensures that work packages will be written to correct problems. In this case, in--
spector followup on the faulty rod select switch was necessary to initi-ate a trouble report. The submission of TRs and.their documentation in the SSs log will be reviewed further during future routine inspection .2 Unplanned Shutdown Due to "B" RCP High Stator Temperature (71707)
The licensee began a downpower at 1:05 a.m., February 11 to make a con-tainment entry to evaluate a "B" Reactor Coolant Pump (RCP) high stator temperature. Plant power was reduced to 45-50% power to lower the dose rates inside containment prior to the entr The licensee's maintenance and I&C (Instruments and Controls) organizations participated in the entr The spare Reactor Coolant Pump was used as a mock-up in pre-planning the. entry. Maintenance determined that boric acid buildup in the area surrounding the RCP stator cooling coils had reduced air flow enough'to impede RCP stator heat removal. I&C measured the spare RTDs'
output by using a digital voltmeter and comparing it to the indicated temperature of 292 degrees. This comparison confirmed that an actual high temperature condition did exist. The licensee evaluated the cause as boric acid buildup on the stator cooling coils based on reports from the entry team. Per Westinghouse, the primary function of these coolers is to minimize the heat load on the containment atmospher The licensee, in conjunction with Westinghouse, determined that, if stator temperature exceeded 311 degrees F, then the RCP must be shut down within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> to prevent excessive insulation breakdown. Although the limit was not exceeded, the licensee decided to continue to shut down and to cool down to cold ;onditions. While shutdown, a contamination survey identified the source of boric acid as a leaking hot leg stop valve. The RCS was drained to mid-loop and the valve was disassemble Licensee inspection showed that the valve's gasket was slightly cu The gasket was replaced and the surface was cleaned and leak checke A successful post repair test was conducted. Heatup was commenced. Mode 3 was entered on 4:10 p.m. , February 21. The turbine was on-line at 11:22 a.m. , February 23, and 95% power was reached at 4:00 p.m. , February 2 Power was limited since the "A" heater drain pump was removed for repairs. The licensee plans to inspect all eight stop valve gasketed surfaces during the next refueling outage. The inspector had no more question .3 Safety Injection with the RCS in Mid-Loop Conditions (93702)
A safety injection (SI) occurred at 8:23 p.m., February 17 with the plant in cold shutdown at mid-loop condition The plant had been shut down earlier with RCS level drained to mid-loop to repair a leaky hot leg stop l
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valve. The plant responded as designed to the."B" train SI with one ,
exception: one chill water. containment isolation valve (3CDS*CTV40) on one of four. return lines failed to clos ~
That. valve'was closed. manuall Subsequent retests showed acceptable operation. Feasibility of periodic
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valve cycling to assure operability will be addressed in future inspec-tion !
- The SI was reset one minute af ter'it initiated. Only the "A" charging ;
E' pump injected because the SI pump breakers were racked down and the RHR' l pumps remained in their shutdown cooling mode, which interlocked their RWST suction valves close The maximum volume injected was estimated at less than 650 gallons since this equates to the maximum flow expected-at pump runout conditions. RCS level rise remained below the top of the hot leg. Hot leg stop valve repairs had been completed just prior.to this event. No increase was noted in containment radiation levels. All equipment started by the SI was stopped by 8:34 p.m. and was returned'
to a standby statu The licensee declared an Unusual Event at 8:35 p.m. because of the actual injection of water to the core. Per the SSs log, the State of Connecticut and NRC were notified at 8:45 and 8:47 p.m.,- respectively. The NRC Operations Center provided a notification time of 9:03 p.m., a 16 minute reporting time discrepanc CFR 50.72 requires that the licensee notify the NRC immediately after notifying state and local agencies but, in all cases, within the one hour of event classification. The licen-see's notification was within one hour requirement, but the inspector questioned the immediacy of the NRC notification since it was 16 minutes after the state notification. After further investigation, the licensee determined that the time delay resulted from filling out a three page form and specifying the correct 10 CFR 50.72 reference. The inspector questioned the licensee to determine if the State and NRC form could be combined or other actions taken to speed up NRC ENS notification. The licensee stated that combining forms would delay initial callouts and delay the State's ability to protect the public. The inspector deter-mined that some delay in NRC ENS notification is consistent with the Statements of Consideration for the Rulemaking that generated the "new" 10 CFR 50.72 rule. Per this reference, the licensee primary responsi-bility is to notify the State to allow them to protect the publi No inadequacies were note .4 MSIV Solenoid Vent Valve Stroke Failure (61726)
During partial stroke testing of the Main Steam Isolation Valves (MSIVs),
the "A" MSIV (3 MSS *CTV27A) above the piston vent so'lenoid failed to close as required. This testing was performed in conjunction with the February 11 shutdown described in Detail The MSIV is closed when steam is admitted to the above piston are Steam is admitted to the above the piston area by opening the steam ad-mission solenoid valve while closing the vent valv _ _ _ _ _ _ _ _ _ _ _ - - _ _ - _ _ _ - _ _ _ _ _ - _ _ _ _ _ _ _ - _ - _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ - _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ - _ - _ - _ _ - _ _ _ _ _ _ _ _ _
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- Two safety-related trains of solenoid valves ensure MSIV closure even if one vent valve is stuck ope This design feature was demonstrated h[! during the MSIV partial strcke testing on February 11 (both trains were tested simultaneously). Thus, even though 3 MSS *CTV27A1A valve failed i to close, the "B" train provided the needed safety functio The licen- i see performed a detailed investigation to identify and correct the root l
cause of this proble After vent valve disassembly, the licensee noted tarnish marks on the inner solenoid housing near the main spring area. The tarnish marks were on one side only and not symmetrical, which indicated a side loading by the spring. Spring measurements were taken and the results discussed with the vendor (Sulzer, Inc.). Tolerances on these springs are to the tenth of a millimeter. Some of these springs were found out of toleranc The as-supplied springs were canted slightly from the true vertical, causing an inherent alignment problem after vent valve assembly. For all the MSIVs, the licensee machined the spring bases and tops to return the spring alignments to vertical. That returned the springs to within tolerance. The machined springs were reinstalled and retested during the subsequent heatup and startup. Retest results were acceptable. The inspector had no further question .5 Reactor Plant Component Cooling Water (RPCCW) System Leaks (71707)
The licensee has been investigating leaks in the Reactor Plant Component Cooling Water (RPCCW) system. RPCCW provides a fresh water heat sink to various safety-related systems during accident conditions. As of February 27, the "A" RPCCW heat exchanger (HX) had a 4.3 gpm tube lea Since RPCCW is at a higher pressure than service water (SW), leaks are from the fresh water portion of the system to the salt water portio Approximately 6000 gallons of fresh water was needed daily to make up for the February 27 leak. Licensee maintenance discovered another prob-lem during post-repair testing. The Pratt HX inlet and outlet isolation valves had excessive seat leakage. They were sent to the manufacturer for refurbishment and returned for reinstallation. The licensee has scheduled valve replacement for the week of March Other RPCCW heat exchangers have developed leaks in the past. On August 23, 1988, the "B" RPCCW HX developed a leak which was subsequently plugge In the recent past, the "C" RPCCW HX developed a tube leak which was plugged on February 1 Further licensee review is needed to ensure that repeated leaks are not due to a generic problem. RPCCW HX leak tightness will be reviewed in future inspection '
3.6 Station Blackout Test (37700) i Regulatory Guide (RG) 1.68 identifies a means for licensees to demon-strate the dynamic response of the plant for a loss of turbine generator coincident with a loss of offsite powe This test was to be run, during startup testing, in the 10% to 20% power range. The licensee provided the following abstract for this test in FSAR Table 14.2-2:
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Test Objective and Summary ,
This test will demonstrate that the plant responds as designed fol- ]
lowing a plant trip with no offsite power. The reactor will be, j-tripped. The diesel start, load sequencing, and plant response in-cluding natural circulation will be monitored. . The_ turbine-driven l l-- auxiliary feedwater pump shall be run for a minimum of two hours )
I with motor-driven auxiliary feedwater pumps and turbine-driven
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' auxiliary feedwater pump cubicle ventilati_on secured. AC power to; the inverters and battery chargers will be removed for a period of two hours.to force battery operatio Acceptance Criteria The plant responds i
in accordance with design. The turbine-driven auxiliary feedwater pump remains within design limits, and pump room ambient conditions do not exceed environmental qualification limits for safety-related equipment in the roo This test, Startup Test 26 - Station Blackout, was reviewed in NUREG 1031, the Safety Evaluation Report (SER) for operation of Millstone 3. Step (7) of the Phase IX - Warranty Run of the SER reviewed each test to de-termine whether the test objectives, prerequisites, test methods, and acceptance criteria for each test demonstrate functional adequacy of the structures, systems, componi, s, and design feature Startup Test 26 objectives, prerequisites, test methods and acceptance criteria were reviewed and accepted by the staf The staff requested that the licensee modify Test 26 to ensure operation of the batterie This modification was agreed to by the licensee. The staff accepted the revised Test 26 in the SE Subsequent to NRC acceptance of the test, the licensee deleted the Test 26 requirement for the main generate- to be on-line. NRC staff review of the licensee's 10 CFR 50.59 change to Test 26 questioned the accept-ability of the change. A meeting was held on February 22 between the staff and the licensee to discuss the acceptability of Test 26. The licensee presented facts related to testing and analysis performed to date to validate their test. The staff is continuing their review of this issue, which will be further reviewed in future inspection .0 Plant Operational Status Reviews (71707)
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The inspector reviewed plant operations from the control room and reviewed the operational status of plant safety systems to verify safe operation, and compliance with technical specifications and plant operating procedures. Ac- I tions to meet technical specification requirements when equipment was inoper-able were reviewed to verify the limiting conditions for operation were me Plant logs and control room indicators were reviewed to identify changes in plant operational status since the last review, and to verify that changes
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in the status of plant equipment was properly communicated in the logs and record Control room instruments were observed for correlation between channels, proper functioning, and conformance with technical specification Alarm conditions in effect were reviewed with control room operators to verify proper response to off-normal conditions and to verify operators were knowl-edgeable of plant status. Operators were found to be cognizant of control room indications and plant statu Control room manning and shift staffing were reviewed and compared to technical specification requirements. No in-adequacies were identified. The following specific activities were also ad-
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4.1 Review of Plant Incident Reports (PIRs) (90712)
The plant incident reports (PIRs) listed below were reviewed to (i) de-termine the significance of the events; (ii) review the licensee's evaluations; (iii) verify the licensee's response and corrective actions were proper; and (iv) verify that the licensee reported the events in accordance with applicable requirements. The PIRs reviewed were: 13-89 dated 1/26/89, 15-89 dated 1/22/89, 16-89 dated 2/1/89, 17-89 dated 2/6/89, 18-89 dated 2/7/89, 19-89 dated 2/7/89, 22-89 dated 2/16/89, 23-89 dated 2/15/89, 27-89 dated 2/20/89, 28-89 dated 2/17/89, 29-89 dated 2/20/89, 30-89 dated 2/21/89, 31-89 dated 2/16/89, 32-89 dated 2/21/89, 33-89 dated 2/22/89, 34-89 dated 2/23/8 No inadequacies were ,
note i The following items warranted inspector followup:
PIR 20-89 dated 2/11/89 documented a shutdown caused by a "B" RCP high stator temperatur See Detail 3.2 for more informatio PIR 21-89 dated 2/21/89 documented the failure of the "A" MSIV solenoid vent valve to stroke closed during surveillance testin See Detail for more informatio PIRs 14-89, 24-89 and 25-89 dated 1/27/89, 2/16/89 and 2/17/89, respec-tively, documented three instances of fire watches not being statione There were five similar events documented in the previous month's in-spection report (50-423/88-24) and a violation was written in this area in December, 1988 (50-423/88-23). Performance is improving (three events vs. five events), but continued licensee attention is needed to reduce event frequenc Licensee corrective action will be reviewed in future inspections.
l PIR 26-89 documented a Safety Injection with the RCS in Mid-loop condi-l tion See Detail 3.3 for more informatio ___
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7 5.0 (Closed) TI 2515/100, " Proper Receipt, Storage, and Handling of Emergency Diesel Generator (EDG) Fuel Oil" (25500)
NRC Information Notice 87-09 dated January 16, 1987 documents the June 27, 1986 Arkansas Nuclear One Unit 2 (ANO-2) inoperability of an emergency diesel generator due to a high concentration of particulate in the fuel oil. Also, at Millstone Unit 3 on November 20, 1987 (PIR 223-87), an EDG was declared inoperable due to particulate matter in the EDG fuel exceeding the Technical Specification (TS) 4.8.1.1.2e limit of 10 mg/ liter. At that time, the plant was in a refueling outage, the EDG was not in operation, and core alterations were suspended until an acceptable supply of fuel oil was obtaine .1 Fuel Oil Sampling and Tank Inspection Technical Specification 4.8.1.1.2 contains an extensive program for sampling new and existing fuel oil:
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TS 4.8.1.1.2b - Monthly check and removal of water from day tank (Surveillance Procedure SP 3646A.1-1, A.2-1, " Diesel Generator Operability Test")
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TS 4.8.1.1.2C - Monthly check and removal of water from the fuel l oil storage tanks. (SP 3646B.5-1, " Diesel Generator Fuel Oil Storage Tank Dewatering and Sample")
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TS 4.8.1.1.2d - Verification of new fuel oil properties in accord-ance with ASTM-0975-81. (Surveillance Procedure 36468.7-1, B.7-2,
"New Fuel Oil Delivery Sampling")
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TS 4.8.1.1.2e - Monthly test of fuel oil for particulate to verify that particulate concentration is less than 10 mg/ liter. (Surveil-lance Procedure 36468.8-1, " Emergency Generator Fuel Oil Particulate Sample Analysis")
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TS 4.8.1.1.2h - Fuel oil storage tank cleaning and inspection every j 10 years (Surveillance Procedure 3712L, " Emergency Generator Fuel i 011 Storage Tank Cleaning").
The referenced surveillance procedures were reviewed in order to assure that the licensee is in compliance with the Technical Specification In addition, a sanple of completed data sheets were inspected to assure that the results of the inspection program were acceptable. No discre-pancies were note .2 System Design and Operation The EDG fuel oil system is described in Section 9.5.4 of the Millstone Unit 3 FSA Each of the two trains of the EDG fuel oil system have the following design featur l l
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An underground fuel oil storage tank with a. dewatering syste Two fuel oil transfer pumps, each with a discharge strainer equipped with pressure drop' instrumentatio An EDG fuel oil day tan .Two fuel pumps, ~ one-engine driven _ and one DC , motor-drive l
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A duplex, engine mounted, fuel oil filter equipped with pressure .
drop instrumentatio !
The EDG fuel oil system operates' automatically to maintain acceptable fuel oil pressure via use of the fuel oil pump Alarms' associated with the EDG fuel oil system appear locally at each of the'two EDG control panels. The control room has two alarms associ-
- ated with the EDG fuel oil system; each alarm indicates that a local (EDG control panel) alar has been sounde The following was noted regarding EDG fuel o1.1 system alarm The FSAR incorrectly describes th'e storage tank level alarms as being level-low and level-high: no level-high alarm is provide The' fuel oil transfer pump strainer pressure drop alarm is described-incorrectly as the " transfer pump" pressure drop alarm in the Con-trol Response. Alarm Book, Operating Procedure 3346A Step 8.2.35, and on the local control pane The " subsequent action" in the event of a " Fuel Oil Pressure Low" alarm (OP 3346A, Step 8.2.15) does not address the possibility that this condition might result from a. clogged duplex filte The above documentation / procedure problems were referred to the licensee for corrective action; these actions were reviewed prior to completion of the inspection and, with the exception of the change to the FSAR, were found to be acceptable. The change to the FSAR is minor and will be re-examined when the next FSAR update is issue In addition to the design features already addressed, the licensee in-tends to purchase a filter skid to be used to filter fuel oil in the storage tanks during refueling outages (per PIR 223-87).
5.3 Filter / Strainer Preventive Maintenance Maintenance Procedure 3720CB, "PM Diesel Generator Mechanical Mainten-ance", addresses preventive maintenance for the EDG fuel oil strainers and filters during refueling outage Step 5.5.14 of MP 3720CB requires
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I inspection and cleaning (as necessary) of the EDG fuel oil transfer pump strainer Step 5.5.15 of MP 3720CB requires inspection and cleaning or replacement of the (duplex) fuel oil filter element .4 Seismic Qualifications of Instruments and Controls Representative instrument / control components were reviewed to determine the adequacy of their seismic design. A pressure switch that automatic-ally starts an auxiliary (DC Motor Driven) fuel pump, 3EGF*PS38A and two !
level switches tha+ control the level of a day, tank 3EFG*LS40A and 41A, were reviewed. T h. - :eismic review of the selected control elements was undertaken via .a 'er of the associated purchase specifications (Spec E-241 and I-626). R was determined that the instruments in question were qualified to IEEE-344-1975 and thus are considered to be Seismic Category .5 Conclusions The EDG fuel oil is sampled using acceptable industry standard The results of recent tests indicate that the qualify of the EDG fuel oil is being maintained in an acceptable manne The licensee's commitment to use a portable filter skid to filter the contents of the fuel oil storage tanks during refueling outages should further reduce particulate in the fuel oi :
With regard to the EDG fuel oil system, sufficient alternate flow paths exist to assure a reliable flow of fuel oi In this regard, the fuel filters and strainers are adequately addressed within the preventive maintenance progra Based upon the above, it is unlikely that the Millstone 3 EDGs will ex-perience fuel oil flow starvation as described in I&E Information Notice No. 87-04. The inspr tor had no further question .0 Licensed Operator Renewal Application Practices (NRC Form 398) (41701) j A review of the license application renewal practices in both the Licensed Operator Training (LOT) and Operations (OPS) departments was performed to veri fy: (1) that information supplied in two recent license renewal applica-tions was complete and accurate; and (2) that the facility licensee had an established process by which to ensure the requirements of 10 CFR 55.53 (e)
were being maintained for all active license holder This review was prompted by a discrepancy in the information supplied by the licensee for a group of operator license renewal applications. The discre-pancy was between the current duties performed by two applicants as licensed l plant equipment operators (LPE0s) and the time which they reported as having l operated the facility during the license renewal period. This discrepancy led the inspector to question the mechanism by which the licensee tracks the active versus inactive status of their licensed personne i
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.To- verify- that-licensed OPS personnel who stood control'. room watches were being maintained in an active status, discussions were conducted with the OPS-assistant and the OPS. supervisor. From these discussions and independent ,
audits of the shift' supervisor's logs and' time keeping records, it was deter-
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i mined that licensed reactor operators [ control operators (COs) and LPE0s] who are'used as part of the control room shift complement are being maintained in an active status in accordance with 10 CFR 55.53(e).
Due to the relatively low number of licenses maintained.by the OPS department, only two licensed LPE0s on shift are required to rotate into the control room as'a CO. To ensure that these two LPE0s meet the minimum time requirements-
. prescribed by 10 CFR 55 (approximately 60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br /> per quarter) all three reactor operators (R0s) on the shifts in question rotate into the C0 position approxi-mately two-thirds of the~ tim This provides each of.these C0s with about 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br /> / year of C0 experienc The inspector also noted that there are licensed SR0s who do not maintain the >
SRO portion of their licenses in an active statu These individuals are-
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utilized as C0s and do not perform the duties of the SCO unless they complete the required 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> of shift functions under the direction of an active SR After review of the information on the two recent license renewal applications, ;
one minor discrepancy existe .
Item 13 of the NRC Form 398 requires that.the l applicant. indicate,'in months, the time spent actually exercising the responsi- ,
bilities of each position held during the license renewal perio If an LPE0
. performs licensed duties-in the control room, as was found to be.the case for two of the renewal. applicants, then this time must be reflected in this spac Form 398, Item 16, experience details, should then be used to describe the duties performed while serving in each position. Applicants who exercise the responsibilities of positions other than their own must have that time and duty description reflected in the above two application item spaces. Licensee '
completion of. renewal application forms will~be further reviewed in future inspection .0 10 CFR 21 - Rosemount Transmitter Oil Leaks '(35100)
Five Rosemount Flow transmitters (FTs) failed between March and October of 1987. Only one fai. lure occurred at a given time, and the reactor trip func-tions of the flow instrumentation remained operable. After each failure, the FTs were replaced in kind. The failures were attributed to a loss of fluid from a transmitter sensing module due to internal leakag In November 1987, the licensee's plant engineering organization completed their review of these failures. They concluded that a Potential Substantial Safety Hazard (PSSH) did exist and forwarded their conclusion to corporate engineering. Their conclusion was based on the number of failures, the fail- l ure frequency, and the fact that the mechanisms for all FTS failures were j identical. Corporate engineering began their PSSH review in November 198 !
After contacting Rosemount, corporate engineering disagreed with the plant's
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PSSH evaluation: the vendor stated that the defects were due to a corrected manufacturing problem. After further discussion with the plant, corporate engineering reevaluated their position.and submitted a 10 CFR 21 report in -
March of 1988. 'The inspector reviewed the issue and rioted that the late re- -
porting of this problem unnecessarily delayed 1 report dissemination to other Rosemount user Inspector. followup showed that this same failure mechanism was identified in prior transmitter failures (1985-1986) at the J.~ A. Fitz-patrick Nuclear Power Plant. This issue was documented in Inspection Report 50-423/88-05 and incorporated in Millstone 3 SALP Report 50-423/87-9 The licensee's 10 CFR 21 report was followed by industry attention. The Electric Power Research Institute (EPRI) and the Institute of Nuclear Power Operations-(INPO) have also reviewed this problem. .Rosemount reevaluated their position and submitted their own 10 CFR 21 report. In a letter dated February 8,1989 from Rosemount, Inc. to Northeast Utilities, the vendor documented the potential for failure of Model 1153 and 1154 Rosemount trans-mitter These models are primarily used in safety-related applications; l Models 1151 and 1152 are used for control functions. Rosemount characterized {
the failures as follow !
"The failure mode is a loss of fill fluid from the transmitter sensing module due to internal leak (no oil is lost into the process fluid).
When this condition occurs, the transmitter may exhibit reduced perform-ance prior to a detectable failure. This reduced performance may mani-fest itself as-an output shift, lack of response over it's full range, and/or an increase in time response. The loss of time response may be uni-directional. At this time, we have not been able to determine the '
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limits of this potential performance reduction."
" Based on existing confirmed information, all reported failures to date i occurred during the first 30 months of service and eventually resulted '
in a detectable condition during that 30 month time span. In these^s'itu-ations, the transmitter would show an increasing output shift, and then ,
possibly resulting in high or low offscale reading. Other symptoms that '!
may identify loss of oil include inability to calibrate (sluggish re-sponse or partial response) and reduced noise in a signal that normally would show nois Data available also suggests but does not yet confirm i that transmitters which have been in service for more than 36 months are not going to fail in this way."
"Recent information indicates that prior to detectable failure, the transmitter may continue to provide a signal but not respond over it's full range and/or time response may be significantly degraded." i The inability to quickly detect degraded performance / time response is safety l significant. Many of these transmitters are used to provide reactor trip j and/or engineered safety features actuation signal l l
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Along with the narrative, Rosemount listed the following 16 potentially af-fected transmitters that were delivered to Millston MODEL DEL DATE TRAN SN MOD SN
'1153085 22984 408074 954082 I 1153GD8 122084 411114 951053 !
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l 1153085 20384 408079 954181 1153HD5 20384 408190 954070 1153D05 90784 410157 1053001 1153D85 20384 408078 954100 1153HD5 22984 408197 954097 !
1153H05 22984 408198 954186 l 1153085 20384 408073 954187 i 1153HD5 20384 408193 954128 1153DB5 20384 408076 954104 1153HD5 20384 408188 954095 1153HD5 13185 411942 1129220 .
1153HD5 13185 411943 1129207 !
1153HD5 13185 411944 1129242 !
1154DP4 50686 414993 1329646 The licensee identified that of the 16 transmitters, 13 were for Millstone 3, 3 were from Millstone 2, and 0 were for Millstone 1. Millstone 2 is ad-dressing this issue and will provide their own corrective action progra Millstone 3 is providing checks through the full range of detector operation (full deflection) travel to identify defective transmitter Three types of checks are being used: (i) calibration checks through the full range of de-tector operation, (ii) comparisons of detector response where multiple detec-tors are used to sense a process /ariable, and (iii) review of recent full range OFIS (Offsite Information System) dat During the 2/11/89 cooldown, three of the four reactor coolant pumps (RCPs) ;
were tripped from full flow and each of the 3 loops' flow transmitters (FTs) j was cross compared with the other two transmitter No anomalies were note A failure of an FT would result in a difference in the detector output versus time from the other FT This approach is acceptable because the probability of similar simultaneous failure of all 3 FTs in the same loop is considered ,
extremely small. No inadequacies were note Further licensee review used separate calibration checks or a review of recent full range 0FIS data. The licensee found no evidence of slow time response or excessive drift during their review. Licensee testing of potentially de-fective Rosemount transmitters was thorough. The licensee is evaluating the need to resubmit their March 1988, 10 CFR 21 report. This issue will be re-viewed further in future inspection !
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8.0 Review of Licensee Event Reports (LERs) (92700)
Licensee Event Reports (LERs) submitted during the report period were reviewed to assess' accuracy, the adequacy of corrective actions, compliance with 10 CFR 50.73 reporting requirements, generic implications, and whether further information was required.- Selected corrective actions were reviewed for implementation and thoroughnes The LERs reviewed were:
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LER 88-28-00, Reactor Trip Due to Loss of Normal 4160V Bus, documented l a 5:10 p.m., December 29, 1988 reactor trip from 75% power due to a loss i of gating current to the. control rod's silicon controlled rectifiers ;
(SCRs) due to procedural deficiency. Normally, a trip would not.have
. occurred, but a redundant power supply was degraded at the time. Prior to the trip, the emergency busses were being supplied by the Reserve .
Station Service Transformers (RSSTs). The "B" Emergency Diesel Genera- ;
tor (EDG) was started for surveillance testing. When EDG-B was paral-- I leled to Emergency Bus 340, the normal to emergency bus tie breaker opened on a directional overcurrent trip, deenergizing Normal Bus-34 !
Licensee procedures did not provide adequate operator guidance on the !
required electric plant lineup prior to paralleling an Emergency Diesel '
Generator when 4160V buses were supplied from the RSSTs. The procedure has.been corrected. The redundant power supply degradation will be cor-rected during the next reactor shutdown. See Detail 6.0 of Inspection i Report 50-423/88-24 for additional information, i
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LERs 88-26-01 and LER 88-26-02, Potential Damage to Safety-Related Equip-ment Due to Design Inadequacy, both updated a previously issued LE The original LER described a design inadequacy that could have resulted in an out-of phase transfer to the RSSTs. This transfer would damage any previously running safety-related electrical equipment. The first LER revision was written to address single failures of any of three re- .
lays that would cause the same scenari The second revision stated that i a plant modification will be performed in the next refueling outage to block fast transfer on undervoltage. No inadequacies were note LER 89-01-00, Steam Generator Sample Containment Isolation Valves found open due to Personnel Error, documented that both the "B" and "C" steam generator (SG) blowdown (80) containment isolation valves were found open at 4:30 p.m., January 5 and had been open 10.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. This incident was discovered while performing leak rate calculations to verify the valves were closed. Thc Technical Specification Limiting Condition of Operation i
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(LCO) Action Statement requires that the valves not be open for more than 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> at a time. The root cause of this event was personnel error.
l The valves were opened at 6:00 am to draw steam generator samples. The E open valves were not discussed during the shift turnover and the oncoming l Shift Supervisor (SS) missed the LC0 Action Statement entry in the SSs log. Corrective action included obtaining a timer to alert Control Room operators of the LCO time limitations. An internal memo was routed to all Operations personnel emphasizing the need to pay close attention to detai The individuals directly involved were counseled on proper
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turnover requirement The replacement of these inoperable valves is !
scheduled for the next refueling outage. No inadequacies were note /
This licensee-identified item was evaluated as having low safety signi-ficance, being acceptably corrected, not due to a previous corrective action inadequacy, and not required to be reported to the NR I
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LER 89-02-00, Control Building Purge Exhaust Fan Isolation Valve Position Indication Error due to Personnel Error, documented a miswiring erro At 3:00 p.m., January 6, 1989, the licensee determined that the wiring of the position indication lights for the Control Building Mechanical Equipment Room Purge Exhaust Fan Isolation valve (3HVC*A0V22) was not i per design. While stroke testing the valve, the open position was cor-rectly indicated but the intermediate and closed positions were incor-rectly indicate Position indication on the plant process computer and i Engineered Safety Features status board were accurate. With the wiring f error, actual valve closure time was not accurately being measured. The root cause of this event was personnel erro The wiring error occurred on December 26, 1986 during the landing of wires to the terminal block on the valve switch after maintenance. The faulty valve position indi-cation was not observed during the retest due to the short stroke time for the valve (approximately 1 second). Plant procedures were revised in May,1987 to require independent verification for lifting and landing leads on safety related equipment. An internal memo was routed to all-operations personnel emphasizing the need to pay close attention to in-termediate valve position indication during stroke testing and normal operation of valves. This is especially important for short stroke time valves. The inspector had no further question .0 Maintenance (62703)
The inspector observed and reviewed selected portions of preventive and cor-rective maintenance to verify compliance with regulations, use of administra-tive and maintenance procedures, compliance with codes and standards, proper QA/QC involvement, use of bypass jumpers and safety tags, personnel protection, and equipment alignment and retest. The following activities were included:
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Reactor Plant Component Cooling Water Leak Repair, dated 2/19/89
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MSIV Vent Valve Repair, dated 2/20/89 No inadequacies were identifie .0 Surveillance (61726)
The inspector observed portions of surveillance tests to assess performance in accordance with aporoved procedures and Limiting Conditions of Operation, removal and restoration of equipment, and deficiency review and resolutio The following tests were reviewed:
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"B" QSS (Quench Spray System) Spray Pump Op Test, SP360 Train "A" RHR (Residual Heat Removal) Valve Operability, SP 3610 LPSI (Low Pressure Safety Injection) Valve Stroke Time, SP 3610 Charging /SI Pump Inoperability Verification, SP 3604 Containm9nt Manual Isolations (Outside Containment), SP 3612 No inadequacies were note k 11.0 Management Meetings (30703)
Periodic meetings were held with station management to discuss inspection findings during the inspection period. A summary of findings was also dis-cussed at the conclusion of the inspection. No proprietary information was covered within the scope of the inspectio ;-
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