ML20247M866
ML20247M866 | |
Person / Time | |
---|---|
Site: | Byron, 05000000 |
Issue date: | 02/01/1989 |
From: | COMMONWEALTH EDISON CO. |
To: | |
Shared Package | |
ML20247M747 | List: |
References | |
1BEP, 1BEP-0, NUDOCS 8908020242 | |
Download: ML20247M866 (33) | |
Text
- - - ___ _ __ __
?
i ~ ATTADENT L14 ,
r #'.
REV. - l' REACTOR TRIP C1 SAFETY. INJECTION 1BEP4
'WOG-1A UNIT 1 '
3-l-
1 .
4 ,
A. PURPOSE)
This procedure provides actions to verify prope'r response of the automatic protection systems following manual 4r automatic actuation of'a Reactor Trip or Safety. Injection, to assess plant conditions, and to identify the. appropriate recovery procedure.
P. S_yptTryo nn. nrMY WITIONS., .
y 3, ^
3 1) The'following are symptoms that-may require a Reactor Trip, if.one has not occurred:
o Source range high'1evel 1 105 CPS o Intermediate range high level 1 25% power o ! Power range lo-level 1 25% power o Power range hi-level.1 109% power o' Power range positive rate 1 5% power change in 2 seconds-o Power range negative rate 1 5% power change in 2 seconds
- o. Overtemperature Delta T 1 116.4% i penalties o, Overpower Delta T 1 107.2% -penalties
'o High.PZR pressure 1 2385 psig
'o Low PZR pressure 1 1885 psig 3' o. High PZR level 1 92%
.o Single loop loss of flow I 90% loop flow o Two loop loss of flow I 90% loop flow in 2/4 loops o RCP breakers - open o RCP bus low frequency 1 57.0 Hz o RCP bus undervoltage <-5268 volts o Turbine trip emergency trip _ header 1 540 psig oil pressure-or Turbine stop valves shut o SI manual actuation o containment high pressure SI > 3.4 psig o Low PZR pressure SI i 1829 psIg o Low steamline pressure SI 1 640 psig (rate sensitive) o Steam Generator water level low-low < 40.8% of narrow range span
- 2) The following are symptoms of a reactor trip: ,
o Any Reactor Trip first out annunciator lit.
o Rapid decrease'in neutron level indicated by nuclear instrumentation.
Step continued on next page APPROVED FEB 011989 8908020242 890727 PDR ADOCK 05000454 B.O.S.R.
4 P PDC _.
-(0304E/0035E/042088)
W__-__-___---___-_ __ _ -
i REV. 1 OPERATOR ACTION
SUMMARY
1BEP-F.0' WOG-1A FOR 2BEP-0 SERIES PROCEDURES TRIP RCPS WHEN: RED PATH
SUMMARY
o CC water to RCP lost 1. Subcriticality - NUCLEAR
. (affected pumps only) POWER >5%
-OR-o Cnmt Phase B actuated 2 Core cooling - CORE EXIT
-OR- TCs >1200*F o ALL of the following conditions exist: 3. Heat sinh-ALL SGs NR wnn p mi.=r,yo
~'~
- Luntrolled Rua cooldown,HQ1 . ADVERSE CNMT) AND TOTAL _
in progress FEEDWATER FLOW <500 GPM
-AND AVAILABLS
-AND- 4. Integrity - DICEIASI_
- High head SI pump flow indicator > 100
- F Ui LAST 60 MINUTES __
(lFI-917) >50 GPM flow or -
AND RCS COLD LEG <246*I SI pumps >100 GPM SI ACTUATION: 5. Containment - CNMT PRESSURE >50 PSIG Actuate SI and GO TO.lBEP-0, REACTOR TRIP OR SAFETY INJECTION, IF CST LEVE_ <20%, THEN Step 1, if: CONSIDEfL THE FOLLOWING:
o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CAUNOT BE MAINTAINED of 3 SGs
> 47. (387. FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :EED )UiP JA TANK .fVEL
< 16% T i EN P ER FOR 1 'HE F0E_0 WING: I: CST LEVEL <3%, TiEN P ERFORfl TH E FOLLOWI 4G:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
(0386E/0042E/042488)
APPROVED JAN 311989 B.O.S.R.
f**
REV. 1 REACTOR. TRIP'OR SAFETY I.JECTION 1BEP-0 lWOG-1A' UNIT l' l-Stop B-2) (continued) o All shutdown and control rods fully inserted and rod. bottom-g' ,
lights lit.
o Rapid.dtcrease in Unit load to zero power.
3 ). m' e i nowin n?" ' - -- nne..c.c M at9xc
~ - t r e a %a r .or N i a -'
Safety Injection, if one bas not occur' red:
o Low PZR pressure 1 1829 psig.
~o Low steamline pressure 1 640 psig (ra e sensitive) o Containment high pressure 1 3.4 psig
- 4) The following may be symptoms of a Reactor Trip and Safety Injection:
o Any SI first'out annunciator lit. ,
o All Group 2 cold leg injection monitor lights lit.
o ESF equipment actuated.
o SI actuated BYPASS-PERMISSIVE light lit.
- 5) This procedure may also be entered from:
o 1BEP ES-0.1, REACTOR TRIP RESPONSE, Step 7, when PZR pressure 1 1829 psig.
APPROVED FCB011989 B. o. s. R.
_ _ _ . - - =
(0304E/0035E/042088)
i REV 1 OPERA'0R ACTION
SUMMARY
- 1BEP-F.0 -
WOGI1A FOR 1BEP-0 SER?ES PROCEDURES i
TRIP RCPS WHEN: [ RED PATH
SUMMARY
o CC water to RCP lost- 1. Suberiticality - NUCf. EAR (affected pumps only) POWER >5%
-OR-o Cnmt Phase B actuated 2. Core cooling - CORE EXIT 1
-OR- TCs >1200*F o ALL of the following conditions exic.: 3. Heat sink-ATL SGs NR !
% LT.YEL <4% (34% FOR
- Concrol' leo.Aca couauvwa E /eVEuE C..... ! .u'D L -
in progress ,
FRRnWATER FLOW <500 GPM j
-AND AVAILABLE q
- RCS pressure - <1370 PSin
-AND- 4. Integrity - DECREASE
- High head SI pump flow indicator >100'F IN LAST 60 MINUTES (lFI-917) >50 GPM flow or AND RCS COLD LEG <246*F SI pumps >100 GPM SI ACTUATION: 5. Containment - CNMT PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, IF' CST _ EVE _ <20%, 'iEN Step 1 if: CONSIDE R'"iE FOLL0tG Q:
o RCS subcooling - NOT ACCEPTAlSLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste -
ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CANNOT BE MAINTAINED of 3 SGs
> 4% (38% FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :E ED jug _ )A" TA4K _ EVE _
< 16% T i E 4P err 6R 4 IHE FOL _0WI 4G: I: CST LEVEL <3%, TJ EN P ERFORM TH E FOLLOWI G:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
(0386E/0042E/042488) APPROVED JM 311989 B. O. S. R.
p :.
I-1 REV. 1 . REACTOR TRIP OR-SAFETY INJECTION 1BEP-0 WOG-1A UNIT 1 i L
)
1 STEP ACTION / EXPECTED RESPONSE RE?FONSE NOT 0 iTAiNED I
. f CAUTION During a loss of offsite power, I operator action will be necessary to actuate PZR PORVs.
__s
- eenen**ene**eenemen**enenemmenen e.. . I e *
- NOTE =
With this procedure in effect,
- notify the Station Director who will*
- evaluate for GSEP conditions per *
- BZP-200-A1, BYRON EMERGENCY ACTION ' *
- LEVELS.
- emene**eneesee ******enene**ene*********
emmeenen*menneesene** nene**eneseen ****
e e
- NOTE *
- Steps 1 through 15 are IMMEDIATE *
- ACTION steps. .
- enene ***meneme****ene****mene********
- senene******* e**ene*eammenene e
- NOTE
- " Adverse Containment" as used in *
- Byron Emergency Procedures is
- defined as:
- o Containment pressure GREATER *
- THAN 5 PSIG *
- -OR-
- APPROVED
- o Contaiment radiation level
- GREATER THAN 105 R/HR.
n FEB 011969 e
- e IRT-AR020 Grid 4 4AS120
- B.O.S.R. e e IRT-AR021 Grid 4 4AS121
- enemmenene***menennename***eemene*****me lil VERIFY REACTOR TRIP ' Manually trip the Reactor, o Rod bottom lights - LIT IF the Reactor will NOT trip,
- Reactor trip and bypass TiiEN GO TO 1BFR-S.1, breakers - OPEN RESPONSE TO NUCLEAR POWER e Neutron flux - DECREASING GENERATION /ATWS, Step'1.
1 1
- Page 3 of 33 (0304E/0035E/042088) 4
- _ _ _ = _ - _ _ _ - - _ .-
i REV 1 OPERATOR ACTION SU' dARY 1BEP-F.0 -
i WOG11A FOR 1BEP-0 SERIES PROCEDURES j 1
j TRIP RCPS WHEN: RED PATH ' UMMARY:-
o CC water to RCP lost 1. Subcriticality - NUCLTAR
'(affected pumps only) POWER >57.
-OR-o Cnat Phase B actuated 2. Core cooling - CORE EXII
-OR- .
TCs >1200'F o ALL of the follotdng conditions exist: 3. Heat sink-ALL SGs NR
~
' 3 VEL . (4% (la_7 F.QB
in progress FTFDWATER FLOW <500 GPM ,
-AND AVAILABLE l
-AND- 4. Integrity - DECREASE
- High head SI pump flow indicator >100'r IN LAST 60 MINUTES (1FI-917) >50 GP2 flow or AND RCS COLD LEG <246*F SI pumps >100 GPM SI ACTUATION: 5. Containment - CHMI PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, IF CST _ EVE _ <20%, JEN Step 1, if: CONSIDE RT i E F0 _ LOW:: sG:
o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or radwaste PER ICONIC DISPLAY OR ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CANNOT BE MAINTAINED of 3 SGs
> 4% (38% FOR ADVERSE CNMT4's o Crosstie unit's CST
,, V o Reduce cooldown rate
- IF AUX :E ED )UiP :)A" TA4K _ EVE _P#
< 16% T i E 9P ER:0R i 'HE :0L _0WI1G:'
I: CST LEVEL <3%, "iEN P ERFORM TH E FOLLOW:: 4G:
- Refill the day tank
, a. Verify secondary side of 3 SGs isolated
l l ..
REV.-1 REACTOR TRIP OR SAFETY INJECTION 1.,EP-0 WOG-1A UNIT 1 l
STEP ACTION / EXPECTED RESPON5E RESPONSE NOT OBT AINED l2l VERIFY. TURBINE TRIP: Perfor.n the following:
- All Turbine throttle stop 1) Manually trip the turbine valves:- CLOSED 2)_IF turbine will NOT trip, j
- All Turbine governor valves - THEN manually run back {
CLOSED
~~~
the turbine at maximum {
rate by the follmsic, method:
1 a) Press TURB MAN..
b) Press FAST ACTION and GOV LWR. simultaneously. 1 IF turbine can NOT be run back, THEN place EH pumps in PULL OUT position.
IF Turbine still will NOT trip, THEN manually initiate Main Steamline Isolation and manually close MSIV bypass valves.
l31 VERIFY POWER TO 4KV ESF BUSSES:
y a.ESFbusses-ATLEASTOlb "
- a. Try to restore power to at ENERGIZED: y least one ESF bus, o Bus 141 alive light - IF power can NOT be LIT restored to at least one
-OR- ESF bus, o Bus 142 alive light - THEN GO TO 1BCA-0.0, LIT LOSS OF ALL AC POWER, Step 1.
- Bus 141 alive light - LIT continuing with this
-AND- procedure.
- Bus 142 alive light - LIT APPROVED FEB 011989 s.o.S.R.
(0304E/0035E/042088)
i REV :1 OPERATOR ACTION
SUMMARY
1BEP-F.0 WOG '-1A FOR 1BEP-0 SERIES PROCEDURES TRIP RCPS-WHEN: RED PATH
SUMMARY
o CC water to RCP lost 1. Subcriticality - JiUCT. EAR (affected pumps only) POWER > 57.
-OR-o Cnat Phase B actuated 2. Core cooling - CORE EXIT-
-OR- TCs >1200*F 0 ALL of the following conditions exist: 3. Heat sink-AT.T. SGs NR I.EVEL <4'l M47. FOR ..,
- Controttea RC5 anouwn lid J'Ju Cf*MT- m ... 10. n ' -
in progress FREDWATER FLOW (500 GPM
-AND AVAILABLE
-AND- 4. Integrity - DECREASE
- High head SI pump flow indicator >100*F IN LAST 'O MINUTES (lFI-917) >50 GPM flow or AND RCS COLD LEG <246*F SI pumps >100 GPM SI ACTUATION: 5. Containment - CNMT PRESSURE >50 PSIG Actuate SI and GO T0 1BEP-0, REACTOR TRIP OR SAFETY INJECTION., IF CST _ EVE _ <20%, -EN Step 1, if: CONSIDE RT i E F0 _LOWL VG:
o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - C_ANNOT BE MAINTAINED of 3 SGs
> 47. (387. FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :E ED )UiP ")A" TANK _ EVE _
< 16% T i E 4P ER:0R1 IHE FOL _0W I .4G: I: CST LEVEL <3%, '-EN P ERFORM-TH E FOLLOWL s 3:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
l (Final)
(0386E/0042E/042488) APPROVED
- N 311989 s.o.s.R.
_ _ _ _ - - _ - - _ _ _ _ - - _ - . )
l REV. 1 REACTOR TRIP OR SAFETY INJECTION 1BEP-0 WOG-1A UNIT 1 STEP ACTION / EXPECTED RESPON5E RESPONSE NOT OBTAINED I
l51 CHECK IF SI ACTUATED: Check if SI required:
- Any SI first out o PZR pressure less than annunciator - LIT 1829 PSIG.
e Group 2 Cold Leg -OR-Injection monitor lights o Steamline pressure less
- LIT than 640 ?SIG.
-OR-o Containment pressure greater than 3.4 PSIG.
IF SI required, THEN manually actuate.
IF SI NOT required, THEN GO To IBEP ES-0.1, REACTOR TRIP RESPONSE, Step 1.
APPROVED FEB 01 1989 B. O. S. R.
Page 5 of 33 (0304E/0035E/042088)
REV 1 OPERATOR ACTION
SUMMARY
1F P-F.0 '
, WOG'1A FOR 1BEP-0 SERIES PROCEDURES TRIP RCPS WHEN: RED PATH
SUMMARY
o CC water to RCP lost 1. Suberiticality - NUCf. TAR (affected pumps only) POWER >5% .
-OR-o Cnmt Phase B actuated 2. Core cooling - CORE EXIT
-OR- TCs >1200'F o ALL of the following conditions exist: . Heat sink-ATT.SGs NR LEVJk < 41 04LEQB_ . _
6 Controlled RCS cooloOer. mlI* ADVElil mGMT"; dGJTOTAL in progress FTEDWATER FLOW <500 GPM
-AND AVAILABLE
-AND- 4. Integrity - DECREASE
- High head SI pump flow indicator >100*F IN LAST 60 MINUTES (1FI-917) >50 GPM flow or AND RCS COLD LEG <246*F SI pumps >100 GPM SI ACTUATION: 5. Containment - CNMT PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, IF CST _ EVE _ <20%, " FEN Step 1, if: CONSIDE RT i E FOLLOW 1 3: ,
o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CANNOT BE MAINTAINED of 3 SGs
> 4% (38% FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :E ED 'UiP JA" TA 4K _ EVE _
< 16% T i E 4P ER :0R i 'HE :0L _0WI 4G: I: CST LEVEL <3%, "iEN P ERFORM TH E FOLLOWL 4G:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
(0386E/0042E/042488) APPROVED JAN 311989 B.O.S.R.
REY. 1 REACTOR TRIP OR SAFETY INJECTION 1BEP-0 WOG-1A UNIT 1 STEP ACT!ON/ EXPECTED RE5 C;N5E RESPONSE NOT OST AINED 4
l$l VERIFY FW ISOLATION:
- a. FW purops-TRIPPED: a. Manually trip pumps.
- W PUMPS TRIP alarms - LIT b FW numpe <94echaran v=1vec b. Manu 11y clos? alvec..
- CLOSED:
- 1FWOO2A
- 1FWOO2B e 1FWOO2C
- 1FW510
- IFW520 IF any valve vill NOT
- IFW530 close,
- 1FW540 THEN close its associated FW shutoff valve:
o IFWOO6A -
o IFWOO6B o IFWOO6C o 1FWOO6D
- d. FW reg byp valves - CLOSED: d. Manually close valves.
- IFW510A
- 1FW520A
- IFW530A
- e. 1FW540A
- e. FW isol valves - CLOSED: e. Manually close valves.
- IFWOO9A
- IFWOO9B e 1FW009C
- 1FWOO9D Step continued on next page APPROVED FEB 011989 B.O.S.R.
Page 6 of 33 O __ __ _(0304E/0035E/042088) ---
REV 1 OPERATOR ACTION
SUMMARY
1BEP-F.0
! WOG-1A FOR 1BEP-0 SERIES PROCEDURES-l TRIP RCPS MIEN: RED PATH
SUMMARY
o CC water to RCP lost 1 Suberiticality - NUCf. EAR (affected pumps only) POWER >57.
-OR-o Cnat Phase B actuated 2. Core cooling - CORE EXIT
-OR- TCs >1200*F o ALL of the following conditions exist: 3. Heat sink G .1Gs NR LEVEL <47. (3A7,_f0R_
-AND AVAILABLE
-AND- 4. Integrity - DECREASE
- High head SI pump flow indicator >100'F IN LAST 60 MINUTES (1FI-917) >50 GPM flow or AND RCS COLD LEG <246*F SI pumps >100 GPM ]
SI ACTUATION: 5. Containment - CB1T PRESSURE >50 PSIG Actuate SI and.GO TO 1BEP-0.
. REACTOR TRIP OR-SAFETY INJECTION, IF CST _ EVE _ <20%, 'iEN Step 1, if: CONSIDE RT (E FOLLOW.. 9G: ,
o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or -;
PER ICONIC DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CANNOT BE MAINTAINED of 3 SGs
> 47. (387. FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown rate ,
- IF AUX :EED )UiP JA" TAVK _ EVE _
< 16% T i E 9P ER:0R i 'HE :0L _0WI 4G: 1: CST LEVEL <3%, "HF.N P ERFORM TH E FOLLOWLNG:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated i
I l
(Final)
(0386E/0042E/042488) APPROVED aa 31 m . !
s.o.s.n.
- - _ _ _ _ _ _ _ . J
l l
REV. 1 REACTOR TRIP OR SAFETY INJECTION 1BEP-0 WOG-1A UNIT 1 STEP ACTION / EXPECTED FES GN5E RESPCNSE NOT OSTAINED Step 5 (continued)
- f. FW temprng flow cont valves - f. Manually close valves.
CLOSED:
- 1FWO34A -
- 1FWO34B
- 13034C
- 1FWO34D
- g. FW temprng isol valves - g. Manually close valves.
CLOSED:
i
- 1FWO35A
- IFWO35B e 1FWO35C
- 1FWO35D -
- h. FW prehtr byp isol valves - h. Manually close valves.
. CLOSED: .
- IFWO39A
- 1FWO39B
- 1FWO39C -
- 1FWO39D
- 1. FWIV byp isol valves - i. Manually close valves.
CLOSED:
- 1FWO43A
- IFWO43B
- 1FWO43C
- 1FWO43D l
APPROVED FEB 01 1989.
B.O.S.R.
Page 7 of 33 (0304E/0035E/042088)
e REV 'l OPERATOR ACTION
SUMMARY
1BEP-F.0 WOG-1A FOR 1BEP-0 SERIES PROCEDURES s
TRIP RCPS WHEN: RED PATH
SUMMARY
{
o CC water to RCP lost 1. Subcriticality - NU,CTRAR (affected pumpe only) POWER >57. ~
-OR-o Cnat Phase 3 actuated 2. Core cooling - GQRE EXIT
-OR- TCs >1200*F
- o. -ALL of the folloving conditions exist: 3. Heat sink-AT.T. SGs NL_ l LEVTL 3 47. f447,_ FOX _
- Controfled nCS cooluvwn ma AuvEnSE uind aND TGIAu 4 in progress F m WATER FLOW <500 GPM
-AND AVAILABLE
-AND- 4. Integrity - DECREASE
- High head SI pump flow indicator >100*F IN LAST 60 MINUTES (1FI-917) >50 GPM flow or AND RCS COLD LEG <246*F SI pumps >100 GPM SI ACTUATION: 5. Containment - CNMT PE SSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, IF CST _ EVE _ <20L T W EN Step 1, if: . CONSIDE R TH E FOLLOWI \ G:
o RCS subcooling - NOT ACCEPTABLE o Makeup 2 rom MUDS or PER ICONIC DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-OR- secendary supply side o PZR level - CAHMl_BE MAINTAINED of 3 SGs
> 47. (38% FOR ADVERSE CNMTS o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :E ED JUMP DA3' TAVK _ EVE _
Ll6% Ti E 9 P ERFOR1 rHE 0L _0WI VG: I:: CST LEVEL <3L NEN P ERFORM TH E FOLLOWL s G:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
(Final)
(0386E/0042E/042488') APPROVED JM 311989 s.o.s.R.
l
- _ _ _ _ _ - - _ - - - - - - - - - _ _ -- l
, . . . - - . , . . . . - - - - - - . . - - . - - - - . - . . . , . ., - - - - .,_,-.-_--__-- - ,._- --- - - . - - . . . . . _ - - - . _ . , - . - - _ - - - - . - - - - - - - - - . . - - _,.--,.---,.n . - - . . , , - - . - - -
' N '-
I
'REV. 1 REACTOR TRIP OR SAFETY INJECTION 1BEP-0 WOG-1A . UNIT 1 STEP . ACTION /E"FECTED REE 0N5E PESPCNSE NOT OSTAINED 16l VERIFY ECCS PUMPS RUNNING: Manually start pumps.
- CENT CHG pumps run lights - LIT
- SI pumps run lights - LIT
- RH pumps run lights - LIT jil Vt-RIFY LOhri AINMENT ISOLATION PHASE Af
- a. Cnmt Phase A valves - CLOSED: a. Manually actuate Cnmt Isol Phase A and verify
- Group 3 Cnmt Isol valves closed, monitor lights - LIT lHl VERIFY CONTAINMENT VENTILATION ESOLATION:
~
- a. Cnmt Vent Isol valves - C_LOSED: a. Manually close valves.
- Group 6 Cnmt' Vent Isol monitor lights - LIT lHl VERIFY AF PUMPS RUNNING: I
- a. AF pumps run lights - LIT a. Manually start pumps.
lEl VERI:Y RCFCS RUNNING IN.. LOW SPEE7:
- a. RCFC low speed run a. Manually start RCFCs in lights - LIT low speed. f l Hl VERIFY CC PUMPS RUNNING:
- a. CC pumps run lights - LIT a. Manually start pumps.
lElyERIFY SX PUMPS RUNNING:
- a. SX pumps run lights - LIT a. Manually start pumps.
, APPROVED fEB 011989 B.o.S.R.
Ppge 8 of .33 (0304E/0035E/042088)
RE V . 1-- OPERATOR ACTION
SUMMARY
1BEP-F.0-WOG-1A FOR'1BEP-0 SERIES PROCEDURES ,,
TRIP RCPS WHEN:. RED PATH
SUMMARY
o CC wat.er to RCP lost 1. Subcriticality. - ECLEAR (affeeted pumps only) POWER > 57a ,
-OR-o Cnat Phase B actuateA 2. Core cooling - CORE EXIT
, -OR- TCs >1200*F o- ALL of the following conditions exist: ~...
- 3. Heat sink-ATL SGs NR LEYEL_147..J141 FOR 6 (,outrollea RCb coolouwn dQ1 eavnet CET)_ er r',4 in progress FrrnWATER FLOW <500 GPM ~
-AND AVAILABLE
-AND- 4. Integrity - DECREASE
- High head SI pump flow indicator >100*F IN LAST 60 MINUTES.
(1FI-917) >50 GPM flow or AND RCS COLD LEG (246*F .
SI' pumps >100 GPM SI ACTUATION: 5. Containment - CmiI PREESURE >50 PSIG '
Actuate SI and'GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, IF CST _ EVE _ <20%, "E EN 'l Step 1,'if: CONSIDE RT i E F0 _LOWLh 3:
o RCS'subcooling - NOT ACCEPTABLE o . Makeup from MUDS or PER ICONIC DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-OR- secondary supply side j o PZR level - CANNOT BE MAINTAINED of 3 SGs j
> 4% (38% FOR ADVEREE CNMT) o Crosstie unit's CST ;
_ EVE _f
- y o Reduce cooldown r-ate I IF AUX :E ED 2. iP JA" TA4K
< 16% T H4P E UOR 1 PHE :0L _0WI 4G: I: CST LEVEL <3%, T"EN EBEORM TH E ,FOLLOWI sG:
- Refill the 6ay tank ,
- a. Verify secondary side of 3 SGs isolated
- b. Switch /J suction to SX supply (Final)
(0386E/0042E/042488) APPROVED JNI 311989 s.o.s.R.
REV. 1 REACTCR TRIP OR SAFETY INJECTION 1BEP-0 WOG-1A U' LIT 1 5TEF ACTION / EXPECTED REE'Gh5E i PESPONSE NOT GSTalNED l[1l CHECK.IFMAINSTEAMLINESSHOULD BE ISOLATED: -
l 1
- a. Check one or more of the a. GO TO Step 14.
. i following conditions:
ANY STEAMI'NE PPCSS!mE -
, 1 LESS THAN OR EQUAL TO 640 PSIG
-OR- ;
o CONTAINMENT PRESSURE GREATER THAN 8.2 PSIG (1PI-CS934 THRU 1PI-CS937) '(
- b. Verify Main Steamline Isolation:
- b. Manually initiate Main !
Steamline Isolation and
- MSIVs - CLOSED manuallycloseMSIVbypass.{
- MSIV bypass valves - CLOSED valves.
-llEl VERIFY CONT'AINMENT SPRAY NOT REQUIRED:
- a. Cnmt pressure - HAS a. Perform the following:
REMAINED LESS THAN 20 PSIG, (IPI-CS934 THRU 1PI-CS947; 'or 1) Verify Containment recorder IPR-937)
V Spray actuated. I
)k'p
' ' IF NOT, THEN manually y' actuate.
- 2) Verify Cnmt Isol Phase B valves closed:
e All Group 6 Phase B isol monitor lights LIT.
IF NOT, THEN manually close valves.
- 3) Stop all PCPs.,
APPROVED FEB 011989-l B.O.S.R.
i-(0304E/0035E/042088) ,
REV 1 OPERATOR ACTION
SUMMARY
1BEP-F.0 WOG-1A FOR 1BEP-0 SERIES PROCEDURES TRIP RCPS WHEN: RED PATH
SUMMARY
o CC water to RCP lost , 1. Suberiticality - NUCLFAR (affected pumps only) POWER >EL
-OR-o Cnat Phase B actuated 2. Core cooling - CORI EXIT
-OR- TCs >1200*F 0 ALL of the following cond,itions erist: 3. Heat sink-ALL SGs NR LEVEL (4% (34% FOR
- uvatzs n cd m.o cooidown M no.z.sE C h , Mw avism in progress FFFDWATER FLOW <500 GPM
-AND AVAILABLE
- RCS pressure - <l370 PSIQ
-AND- 4. Integrity - DEEEASE--
- High head SI pump flow indicator >100'F IN LAST 60 MINUTES (lFI-917) >50 GPM flow or AND RCS COLD LEG (246*F SI pumps >100 GPM :
SI ACTUATION: 5. Containment - CNMT PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, IF CST _ EVE L <20%, " lien Step 1, if: CONSIDER T 4 E FO'_ LOW 14G:
o RCS subcooling - NOT ACCEDTABLE o nakeup from MUDS or PER ICONIC DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CANNOT BE. MAINTAINED of 3 SGs d
> 4? (38% FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :E ED )U'iP 3A" TAVK _ EVE'_
< 16% T i E 4P ER :0R 1 HE :0L _0WI:4G: I: CST LEVEL <3%, T EN P ERFORM TH E FOLLOW 3 G:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
(Final) )
(0386E/0042E/042488) APPROVED i
J6N 31 M49 B.O.S.R.
I
R$V. 1- REACTOR TR'IP OR SAFETY INJECTION 1BEP-0 1
WOG-1A. UNIT 1 STEP ACTION / EXPECTED RES?ONSE RESPONSE NOT OSTAINED I
l3l VERIFY'DIESELGENERATORSRUNNING:
~
IF DGs can NOT be started iiianually, W EN Ic m 11.y :'a~* rer 1 BOA ELEC-3, LOCAL EMERGENCY START OF A
, DIESEL GENERATOR.
16 ANN 00NCE CONDITION OVER PAGE, U VIT . REACTOR TRIP - SAF ETY I VJEC" ION 17 VERIFY GENERATOR TRIP 30 SECONJS AFT ER TURBINE TRIP:
- a. Unit 1 Main Transformer feed to a. Manually open breakers 345KV Swyd breakers-OPEN: as necessary:
- OCB 3-4 o OCB 3-4
- OCB 4-5 o OCB 4-5
e 41 Brkr
- c. Generctor lockout relay trip alarm - LIT APPROVED i
FEB 011989 I B.O.S.R.
l (0304E/0035E/042088)
i REV 1 OPERATOR ACTION
SUMMARY
1BEP F.0 WOGI1A FOR 1BEP-0 SERIES PROCEDURES -
, TRIP RCPS WHEN: RED PATH
SUMMARY
o CC water to RCP lost 1. Suberiticality - NUCf.FAR (affected' pumps only)
POWER >5%
-OR-o Cnat Phase B actuated 2. Core cooling - CORE EXIT
-OR- 2Cs >1200*F o ALL of the follow'ng conditions exist: 3. Heat sink-AT.T. SGs NR LEVIL <4% (34% FOR
- com. rolled hCS 'chuww DEA
- ~
~ . m ,i Ciin > 1 2 J !n_
in progress INFnWATER FLOW <500 GPM
-AND AVAILABLE
-AND- 4. Integrity - DECREASE
- High head SI pump flos. indicator >100*F IN LAST 60 MINUTES (1FI-917) >50 GPM flow or* AND RCS COLD LEG (246*F SI pumps >100 GPM SI ACTUATION: 5. Containment - CNMT PRESSURE >50 PSIG Actuate SI and-GO TO 1BEP-0, .
REACTOR TRIP OR SAFETY INJECTION, IF CST '_EV E _ <20%, " TEN Step 1, if: CONSIDE R i E - F0 _LOWL 03:
o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste -
ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CANNOT BE MAINTAINED of 3 SGs
> 4% (38% FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :EED SUiP :)A" TA4K _ EVE _
< 16% T i E 4P ER :0R i 'HE ;0L _0WI 4G: I: CST LEVEL <3%, EN P ERFORM TH E FOLLOWD G:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
(0386E/0042E/042488) APPROVED JM 311989 B.O.S.R.
REV. 1 REACTOR. TRIP OR SAFETY INJEC120N 1BEP-0 WOG-1A UNIT 1 STEP ACTION / EXPECTED RE5:GN5E FESPC.iSE NOT GSTAINED 18 VERIFY ECCS FLOWa
- a. High head SI pump flow a. Manually s. Art CENT CHG I indicator (1FI-917) - pumps and align valves is GREATER THAN 50 GPM necessary.
b.'RCS pressure (1PI-403A/405) - b. GO TO Step 19.
'ISS m AN :T,0 Pc'e i
- c. SI pumps discharge flow c. Manually start SI pumps andl indicators (1FI-918/922) - align valves er necessary. n GREATER THAN 100 GPM -
LESS THAN 300 PSIG
- e. RH pumps discharge. flow e. Manually start RH pumps and indicators (1FI-618/619) - align valves as necessary. 1 GREATER THAN 500 GPM 19 VERIFY ECCS VALVE ALIGNMENT: )
- a. Group 2 Cold Leg Injection a. Manually align valves as monitor lights required for necessary.
ECCS valve alignment - LIT l
l 1
1 l
APPROVED FEB 011989 B.O.S.R.
e (0304E/0035E/042088)
L.-____--____----_..-------------
= _ - - .--
REV 1 OPERATOR Af" ION
SUMMARY
.1BEP-F.0 WOGI1A FOR 1BEP-0 SERIES PROCEDURES.
TRIP PCPS WHEN: Rf-) PATH SUMMAR1:
o CC water to RCP lost 1. Suberiticality - NUCf.FAR (affected pumps only) POWER 35%
-OR-o Cnet Phase B actuated 2. Core cooling - CORE EXIT
-OR- .
TCn >1200*F o ALL of the following coaditions ex3.s t : - 3. Heat sink-AT.T. SGs NR LEVEI_< 4L( EFQ1.
- t.,ontrob'e,c ht;b cvvAcuwia uni '~ "
ADvME Chii1"i r.#w Tv AL in progrecs FrrnWATER FLOW <500 GPM
-AND AVAILABLE
. -AND- 4. Integrity - DECREASE..
- High head SI pump flow indicator- >100*F IN LAST 60 MINUTES (1FI-917) >50 GPM flow or AND RCS COLD LEG (246*F SI pnaps >100 GPM SI ACTUATION: 5. Containment - CNMT PRFRSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, IF CST _ EVE _ <20%, TiEN Step 1, if: CONSIDE RT i E F0 _LOWI 6:
, o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or EER ICONIC DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CANNOT BE MAINTAINED of 3 SGs
> 47. (38% FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :
E ED 'UiP ')A" TA4K _ EVE _
< 16% T i E 4P ER :0R i 'HE :0L _0WI 4G: I: CST LEVEL <3%. -
EN P ERFORM TH E FOLLOWL VG:
- . Refill the day tank
- a. Verify secondary side of 3.SGs isolated
(Final)
(0386E/0042E/042488) APPROVED JM 311989 a.o.s.R.
_ - _ - - - - - - _ - - - - - - _ - . _ - - - - - - - - - - - - - .I
REV.'l REACTOR TRIP OR SAFETY INJECTION 1BEP-0 WOG-1A UNIT 1 STEF dCTION/ EXPECTED REE GN5E RESPONSE NOT OE 'AiNED CAUTION AF flow must remain GREATER THAN 500 GPM until water level is GREATER THAN J% (34% FOR ADVERSE CNMT) for an indicatien. y SG narrow range I
20 VERIFY TOTAL AF FLOW:
- a. AF flow - GREATER THAN 500 GPM a. IF SG narrow range level AVAILABLE IE greater than 4% (34% FOR ADVERSE CNMT) in any SG, THEN control feed flm; to maintain SG narrow range.
level.
IF SG narrow range level Ti less than 4% (34% FOR ADVERSE CNMT) in all SGs, THEN manually start AF pumps and align valves as necessary.
IF AF flow can NOT be established greater than 500 GPM, THEN GO TO 1BFR-H.1, RESPONSE TO LOSS OF SECONDARY HEAT SINK, Step 1.
e l
APPROVED FEB 011989.
B.O.S.R.
age 12 of 33 (0304E/0035E/042088)
REV 1 OPERATOR ACTION SUMM/dY 1BEP-F.0 WOG'1A FOR 1BEP-0 SERIES PROCEDURES TRIP'RC_Ps WHEN: RED PATH SUPiAR1:
o CC water to RCP lost 1. Subcritic.tlity - NUCLEAR (aff ected pumps only) POWER >5%
-OR-o Cnmt Phase B actuated 2. Core cooling - CORE EXIT
-OR- TCs >1200*F o ALL of the followir; conditions exist: 3. Heat sink-ALL SGs NR LT2W < 41 04% J_0R_
-AND AVAILABLE
-AND- 4. Integrity - DECREASE
- High head SI pump flow indicator >100*F .N LAST 60 MINUTES (lFI-917) >50 GPM flow or AND RCS COLD LEG <246*F SI pumps >100 GPM SI ACTUATION: 5. Containment - CNMT PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, IF CST _ EVE _ <20%, T:iEN Step 1, if: CONSIDE RT i E FOLLOWI 1G:
o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-OR- secondary. supply side o PZR level - CANNOT BE MAINTAINED of 3 SGs
> 4% (38% FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :EED ' vip 3A" TAiK _ EVE _
< 16% T i E 4P ERFOR i 'HE 0L _0WI 4G: I: CST LEVEL <3%, EN P ERFORM TH E FOLLOWL NG:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
(0386E/0042E/042488) APPROVED JM 311969 B.O.S.R.
l
- _ _ - - - - - - - - - - - I
> +
REV. 1 REACTOR TRIP OR SAFETY _ INJECTION 1BEi-0
-WOG-1A UNIT 1 1
5TEP ACTION /EXF.ECTED RE5?ON5E PE9PONSE NOT CSieiNED 21 VERIFY AF VALVE ALIGNMENT:
a.~AF isol valves - OPEN: a. Mrc~ illy OPEN valves.
- 1AF013A-
- - 1AF013B 1AF013C "
~
n .AF013p
- 1AF013E
- 1AF013F
- 1AF013G
- 1AF013H b._AF flow control valves - b. Manually throttle valves THROTTLED OPEN: OPEN.
- 1AF005A
- 1AF005B
- 1AF005C
- 1AF005D -
- 1AF005E
- 1AF005F -.
- 1AF005G -l
- 1AF005H 1 APPROVED FEB 011989i B.O.S.R.
Page 13 of 33 (0304E/0035E/042088)
REV 1 OPERATOR ACTION
SUMMARY
1BEP F.0 WOG11A FOR 1BEP-0 SERIES PROCEDURES TRIP RCPS WHEN: RED PATH
SUMMARY
o CC water to RCP lost 1. Subtriticality - HIElluE (affected pumps only) POWER >5%
-OR- .
o Cnmt Phase B actuated 2. Core cooling - G RE EXIT
-OR- TCs >1200*F o ALL of the following conditions exist: 3. Ec;.t :: ink-ALL SGs NR LEVEL < Q 11A% FOR
- t.,ontrollec KCS
-AND AVAILABLE
-AND- 4. Integrity - DEL 2EASX_
- High head SI pun:p flow indicator >100*F IN LAST 62. MINUTES (1FI-917) >50 GPM flow or ARD RCS COLD LEG <1(th,*E SI pumps >100 GPM SI ACTUATION: 5. Containment - CNMT PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, IF CST _ EVE 1 (20%, TiEN Step 1, if: CONSIDE RT i E FOLLOWI 9G:
o RCS subcooling - NOT ACCEPTABLE o Maheup from MUDS or PER ICONIC DISPLAY OR radwaste A'I*fACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CANNOT BE MAINTAINED of 3 SGs
> 4% (38% FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :EED DUiP DAl' TA4K _ EVE __"c.V
< 16% T i EN P ER :0RM 'HE 0L _0WI W:# I: CST LEVEL <3%. THEN
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
(0386E/0042E/042488) pp g l JAN 311989 B.O.S.R.
i
j '. ;
f.
/ $
REV. 1 REACTOR TRIP OR SAFETY INJECTION 1BEP-0 s
.,WOG-1A UNIT 1 STEP ACT80N/ EXPECTED RE5 GN5E RESPONSE NOT OSTAiNED s . j CAUTION If a radioactive release to the i
, atmosphere occurs, then Control Room i Offices vent fans,-OVVOICA and i OVV01CB should be verified tripped {
g: at panc1 TiV01J.
.4, l 22 VERIFY CONTROL ROOM VENTILATION SYSTEM ALIGNED FOR EMERGENCY i OPERATIQN j i
- a. Control Room chillers run a. Manually start chiller for lights - LIT: VC train in operation.
Train A - MCR CHLR 0A
.* Train B - MCR CHLR OB D. M/U' air _ source aligned for b. Manually align Train A or B L emergency, operation: makeup air source to emer-gency source as necessary:
o TRAIN A FILTER light - LIT -
o OVC25Y/09Y- OPEN
-OR- o OVC32Y/16Y - CLOSED is o TRAIN B FILTER light-a* LIT o OVC281Y/282Y - CLOSED-o OVC312Y/313Y
- c. VC train in operaticp,'M U' 1eP , CLOSED
- c. Perform the 'following; air filter unit fan run light
- LIT and-discharge flow control 1) Place non-operating VC damper - NOT FULLY CLOSED: train equipment in operation:
o Train A - M/U Fan OA and
- Supply fan J damper OVC24Y e Return fan
.-OR- e M/U air filter o Train B - M/U Fan OB and unit fan k damper OVC08Y
- 2) RETURN TO Step 22a.
- d. VC train in operation, recire d. Manually close recire charcoal absorber bypass damper: charcoal absorber bypass damper on VC train in o Train A OVC43Y - CLOSED operation.
-OR- APPROVED o Train B OVC44Y - CLOSED Step continued on next page
- B.O.S.R.
(0304E/0035E/042088)
m ;
]%,$di!, s.
3, ,o .
,h.'l ~
3VREV. 1" .
OPERATOR ACTION
SUMMARY
.1BEP-F 1 ,
FOR 1BEP-0 SERIES PROCEDURES-c $.
WOG-1A' my RED PATH
SUMMARY
. TRIP RCPS WHEN:
-o-CC water to RCP lost 1. Suberiticality - NUCLEAR (affected pumps only) POWER >5%
-OR-
- 2. Core cooling.- CORE EXIT o' Cnet Phase B actuated
-OR .
TCs >1200'F ALL of-the following conditions o
exist: 3.-Es.: sink-ALL SGs NR-LEHI;_L4% (_34%. FO.R . . . ,
- ~ Contro,Lled RCS .coolaown !!Q1 -
ADVERhi, ma',MJTalm" '
in progIess e FFFNdATER FLOW < 500 GPM
-AND AVAILABLE
-AND- 4. Integrity.- DECREASE
- High head SI pump flow-indicator >100*F IN LAST 60 MINUTES (1FI-917) >50 GPM flow or AND RCS COLD LEG <246*F-SI pumps.>100 GPM SI ACTUATION: 5. Containment - CNMT PRRCSURE >SO PSIG LActuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, IF CST _EV E _ <20%, ' "
EN i E' F0 _LOWM s if Step 1. if: CONSIDE R o .RCS subcooling NOT ACCEPTABLE o Mckeup from MUDS ~or PER ICONIC DISPL AY OR- radwaste ATTACHMENT A o Prepare to. isolate
-OR- secondary supply side o PZR level - CANNOT BE MAINTAINED of 3 SGs
> 41 (381 FOR ADVERKE CNMT) o Crosstie unit's CST o Reduce cooldown' rate
- IF AUX :
< 16% T i E 4P E ( :0R 1 'HE :0L _0WI 4G: IF CST LEVEL <3%, TiEN PER-:0RM TH E FOLLOWI 4 3;
- Refill the day tank
L 1
(Final)
(0386E/0042E/042488) APPROVED JNI 311989 s.o.s.n.
a
y l
.REV. 1- REACTOR TRIP OR SAFETY INJECTION 1BEP-0' l WOG-1A UNIT 1 1 i
jSTEP ACTION / EXPECTED RE5:0N5E , RE5FONSE NOT OST AiNED Step 22 (continued)-
- e. Control Room pressure.- GREATER e. Refer to BOP VC-14, MAIN THAN +0.125" H90, (MCR/TB CONTROL ROOM PRESSURE _ LOW, DP, OPDI-VC038) while continuing with)this procedure.
l APPROVED l ftB 011989 1 B.O.S.R.
(')3 04E/0035E/042088 )
REV 1 OPERATCR ACTION
SUMMARY
1BEP-F.0 i; WOG-1A FOR 1BEP-0 SERIES PROCEDURES TRIP RCPS WHEN: RED PATH
SUMMARY
o CC water to RCP lost 1. Subcriticality - NUCTTAR (affected pumps only) POWER 357.
-OR-o Cnmt Phase B actuated 2. Core cooling - CORE EXIT
-OR- ICs >1200'F o ALL of the following conditions exist: 3. Heat sink-AT.L SGs NR LEYEk_547. ..( 3 4%_I,02_
-AND AVAILABLE
-AND- '4. Integrity - DECREASE
- High head SI pump flow indicator >100*F IN LAST 60 MINUTES (IFI-917) 250 GPM flow or AND RCS COLD LEG <246*F
.SI' pumps 1100 GPM SI ACTUATION: 5. Containment - CNMT PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP'OR SAFETY INJECTION, IF CST _ EVE _ <20L JEN i E FOLLOWL \ G:
Step 1, if: CONSIDE R o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or PER IC6I?TC DISPLAY OR radweste ATTACHMFRf_A o Prepare to isolate
-OR- secondary supply side o PZR level - CANHOT BE MAINTADIED of 3 SGs
-> 47, (38'I FOR ADVERSE CNMT) o Crosstie unit's CST
- IF AUX :EID 'UiP JA" TA4K _ EVE _
l
< 16% T iE 4P ER FOR 1 'HE :0L _0WI 4G: I : CST LEVEL <3L T EN ;
PERFORM THE FOLLQ1GE: I
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
}
(Final)
(0386E/0042E/042438) APPROVED JM 311989 s.o.s.R.
}
REV. 1 REACTOR TRIP OR SAFETY INJECTION IBEP-0 WOG-1A UNIT 1 i
.. .L._ .
5TEP A; TION / EXPECTED RES GN5E PESPONSE NOT OSTAINED emeenemanna**eameneenna*manen**n********
- NOTE *
- Only or9 Aux Bldg Charcoal Booster
- Fan should be started in each
- non-accessible area exhaust filter
- plenum.
Only two plenums can be
- used at t n; 'm o t i me . *
- ,.........**......=*****ne********a 23 YERifhAUXBLDGVENTILAIl0N SYSTF2 ALIGNED FOR EMERJiEHQ' OPERATION:-
- a. Two non-accessible AB Charcoal a. Start non-accessible Booster Fans run lights - LIT: AB Charcoal Booster Fans as
. necessary per BOP VA-5, o OVA 03CA or OVA 03CB for Plenum A AUX BLDG CHARCOAL BOOSTER o OVA 03CC or OVA 03CD for Plenum B FAN OPERATION.
o OV.A03CE or OVA 03CF for Plenum C
- ne nn **n **. .*nen.. ****e*************
NOTE
- Only one Fuel Bldg Charcoal Booster
- Fan should be run at a time.
nma...
- .....ne.. * . *** ant... enamen 24 VERIFY FUEL BLDG VENTILATION S_YSTEM ALIGNED FOR EMERGENCY OPERATION:
- a. Train A or Train B Fuel a. Start Train A or B Bldg Charcoal Booster Fan run light - LIT:
Charcoal Booster Fan.
per BOP VA-6, FUEL HANDLING BLDG CHARCOAL o FHB Booster Fan OA BOOSTER FAN OPERATION.
- OVA 04CA
-OR-o FHB Booster Fan OB
- OVA 04CB APPROVED FEB 01 1969.
, s.o.S.R.
- l. - - ,. .
Page 16 of 33 (0304E/0035E/042088)
L REV 1 OPERATOR ACTION SUMMAR7 1BEP-F.0 WOG-1A FOR 1BEP-0 SERIES PROCEDURES -
JIIP RCPS WHEN: RED PATH
SUMMARY
o CC water to RCP lost 1. Suberiticality - MTCT.FAR (affected pumps only) POWER >57.
-OR-o Cnmt Phase B actuated 2. Core cooling - CORE EXIT
-Oh- TCs >1200*F o ALL of the following conditions exist: 3. Heat sink-ATL SGs NR IZVEL < 47,114_7._FOR_
- control. Leo RW cooJ,uvwn JQ1 rw v ERam CIM , 12"3 iJTAL in progress FKrnWATER FLOW <500 GPM
-AND AVAILABLE
-AND- 4. Integrity - DECREASE
- High head SI pump flow indicator >100*F IN LAST 60 MINUTES (1FI-917) >50 GPM flow or AND RCS COLD LEG <246*F SI pumps >100 GPM SI ACTUATION: 5. Containment - CNMT PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, ' IF CST LEVE _ <20L ' WEN i E F0 _ LOW::
Step 1, if: CONSIDE R s G:
o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-0R , secondary supply side o PZR level - CANNOT BE MAINTAINED of 3 SGs
> 47. (3Q7. FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :E ED PUiP 3A TA4X _ EVE _
< 16% T i E 4 PER 0Ri 'HE ;0L_0WliG1 I: CST LEVEL <3L ' "EN P ERFORM TH E FOLLOW:: s G:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
(0386E/0042E/042488) APPROVED JAN 311969 B.O.S.R.
i REV. 1 REACTOR TRIP OR SAFETY INJECTION 1BEP-0 WOG-1A UNIT 1
{
l 1
STEF ACTION /EXPEC 'ED RES:GN5E RESPONSE NOT OSTAINED 25 CHECK RCS AVERAGE TEMPERATURE:
i
- a. RCS average temperature - a. IF RCS temperature less STABLE AT OR TRENDING TO 557'F than 557'F and decreasing, t THEN:
1)'Stop dumping steam.
- 2) IF cooldown continues, THEN maintain total feed flow greater than 500 GPM until SG narrow range level greater than 4% (34% FOR ADVERSE CNMT) in at least one SG.
- 3) IF cooldown continues, THEN shutdown unnecessary main steam roads.
IF RCS temperature greater than 557'F and increasing, THEN dump steam to condenser:
- 1) Check condenser available. .
- 2) Place MS header pressure controller in MANUAL and reduce demand signal to zero.
- 3) Place steam dumps mode selector switch in STEAM PRESSURE mode.
Step continued on next page i APPROVED FEB 011989 B.O.S.R.
(0304E/0035E/042088)
L REV . OPERATOR ACTION
SUMMARY
1BEP-F.0 WOGI14 FOR 1BEP-0 SERIES PROCEDURES TRIP RCPS WHIN:, RED PATH
SUMMARY
-o CC water to RCP lost 1. Suberiticality - NUCT.vAg (affected pumps only) POWER >5%
-OR- -
o Cnmt Phase B actuated 2. Core cooling - CORE EXIT
-OR- TCs >1200*F o ALL of the following conditions exist: 3. Heat sink-Af1 SGs NR LEVEL < 4% (34*/._EO.R '-
- Controlilen AGS couloown DEA m cn5c uNM1i ,de luT/t in progress FEEDWATER FLOW (500 GPM
-AND AVAILABLE
-AND- 4. Integrity - DECREASE
- High head SI pump flow indicator >100*F IN LAST 60 MINUTES (IFI-917) >50 GPM flow or AND RCS COLD LEG <246*F SI pumps >100 GPM SI ACTUATION: 5. Containment - CaiI PRESSURE >SO PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, IF CST _ EVE'_ <20%, '-EN Step 1, if: CONSIDE RT i E FOLLOWL s G:
o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste .
ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CANNOT ,BE MAINTAINED of 3 SGs
> 4% (38% FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :E ED OU'iP ")A" TA4K _EVEL
< 16% T i E 9P ERFOR 1 'HE :0L _0 WING: 11: CST LEVEL <3%, " HEN P ERFORM TH E FOLLOW"NG:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
(0386E/0042E/042488) APPROVED J M 3 1 1969 B. O. S. R.
REV. 1 REACTOR TRIP OR SAFETY INJECTION 1BEP-0 WOG-1A UNIT 1~
STEP ACTION / EXPECTED RES?Of.5E RE?FONSE NOT OSTArNED Step 25a (continued) 4)' Adjust MS header pressure controller to initiate cooldown rate less than 50*F/Hr.
E vneble to dump stew &
condenser, THEN dump steam using SG PORVs.
26 CHECK PZR PORVS AND SPRAY VALVES:
- IRY455A THEN manually close.
- 1RY456 PORVs.
I_F any PORV can NOT be closed, THEN manually close its isol valve:
o 1RY8000A (IRY455A) o 1RY8000B (IRY456)
IF PORV isol valve can N6T be closed, THEN Go TO 1BEP-1, LOSS OF REACTOR OR SECONDARY COOLANT, Step i' 1.
- b. Normal PZR spray valves - b. I_F PZR pressure less CLOSED: than 2260 PSIG, THEN manually close valves:
- 1RY455B
- 1RY455C o E spray valve IRY455B can NOT be closed, THEN stop RCP 1D.
APPROVED o E spray valve 1RY455C can NOT be closed, THEN stop RCP 1C.
fE8 011989 B.O.S.R.
Page 18 of 33 j (0304E/0035E/042088) j
e REV 1 OPERATOC ACTION
SUMMARY
1BEP-F.0 WOG-1A FOR 1BEF-0 SERIES PROCEDURES TRIP RCPS WHEN: RED PATH
SUMMARY
o CC water to RCP lort 1. Suberiticality - NUCTTAR (aff ected pumps only) POWER >5%
-OR-o Cnst Phase B actuated 2. Core cooling - CORE EXIT
-OR- TCs >1200*F-o ALL of the following conditions exist: 3. Heat sink-ALL SGs NR
- LEVEL (4% (34% FOR
~
- controllud'RCb cooldown HQ1 Auvtx3n CIid , mw moinu
~~ in progress EEEDWATER FLOW <500 GPM
-AND AVAILABLE
. -AND- 4. Integrity - DECREASE
'~
AND RCS COLD LEG <246',E SI pumps >100 GPM SI ACTUATION: 5. Containment - CNMT PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0,
_ <20%,
REACTOR TRIP OR SAFETY INJECTION, IF CST _ EVE FEN i E F0 _LOWL 13:
Step 1, if: CONSIDE R o RCS,subcooling - NOT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste '
ATTACHMENT A o Prepare to leolate
-OR- secondary supply side o PZR level - CANNOT BE MAINTAINED of 3 SGs
> 4% (38% FOR ADVERSE CNMT) o Crosstie unit's CST i
'"" o Reduce cooldown r-ate
- IF AUX :E ED )UiP JA" TA4K _ EVE
< 16% T i E VP ER:0Ri 'HE :0L _0WI il!'n F. I: CST LEVEL <3%, THEN {
r P ERFORM TH E FOLLOWING. i
- Refill the day tank
- a. Verify seconfsry side of 3 SGs isolated
)
l (Final)
(0386E/0042E/042488) APPROVED JAN 31869 B.O.S.R.
J
[
y 4
!~ ,
i L-REVi 1- 1BEP-0 REACTOR TRIP OR SAFETY INJECTION WOG-1A- UNIT 1
~
STEP ACT ON/ EXPECTED RESPON5E PESFONSE NOT OSTAiNED CAUTION Seal injection must be maintained to all RCPs to prevent seal damage due to overheating.
' Z/ 'CnEEk IF kLPS SHOULD 8E siOveED:
- a. ECCS flow: a. GO TO Step 28.
o High head SI flow indicator (IFI-917) -
GREATER THAN 50 GPM
-OR-o Any SI pump discharge
-flow (IFI-918/922) -
GREATER THAN 100 GPM
. b. RCS pressure - LESS THAN b. GO TO Step 28.
1370 PSIG
- c. Stop all'RCPs , . . , ,
- d. Verify steam dumps in S M d. Perform the following:
PRESSURE mode of operaflon 1) Check condenser ,
V available. I
- 2) Place MS header !
pressure controller in !
MANUAL and reduce I demand signal to zero.
- 3) Place steam dumps mode selector switch in STEAM PRESSURE mode.
APPROVED j j
fEB 011989 i B.O.S.R.
Page 19 of 33 (0304E/0035E/047088) 1 j
OPERATOR ACTION
SUMMARY
1BEP-F.0 h*ik FOR 1BEP-0 SERIES PROCEDURES RED PATH
SUMMARY
M ' RCPS WHEN:
o CC water to RCP lost 1. Subcriticality - NUCTTAR (affected pumps only) POWER >5%
-OR-o Cnmt Phase B actuated 2. Core cooling - CORE EXIT
-OR- TCs >1200'F-o ALL of the following conditions exist: .... 3. Heat sink-ATL SGs NR LEVEL <4%.(.34% FOR., .
- Csat.rolted Es esvAduwe M ALva3E onrIT + .uis TL,.aL in progress FrrnWATER FLOW <500 GPM
-AND AVAILABLE
-AND- 4. Integrity - DECREASE
- High head SI pump flow indicator >100*F IN LAST 60 MINUTES (1FI-917).>50 GPM flow or AND RCS COLD LEG <246*F SI pumps >100 GPM SI ACTUATION: 5. Containment - CNMT PRESSURE >50 PSIG Actuate SI and GO TO IBEP-0, REACTOR TRIP OR SAFETY INJECTION, IF CST _ EVE L <20%, JEN Step 1, if: CONSIDE R i E F0_ LOW:: s G:
o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CANNOT BE MAINTAINED of 3 SGs
> 4% (38% FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldewn rate
< 16% T i E 4P ERFOR1 'HE :0L _0WI 4G: 1: CST LEVEL <3%, J EN P ERFORM TH E FOLLOW:: s G:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
(0386E/0042E/042488) APPROVED l m 3 1 1989
! s.o.s.n.
u _ __ _
i REV. 1 REACTOR TRIP OR SAFETY INJECTION 1BEP-0 WOG-1A UNIT 1 STEP ACTION / EXPECTED FIS ON5E PEEFONSE NOT OST A,NED 28 CHECK IF SG(s) SECONDARY PRESSURE BOUNDARIES ARE INTACT:
- a. Check pressures in all SGs: a. GO TO 1BEP-2, FAULTED STEAM GENERATOR ISOLATION, l o NO SG PRESSURE DECREASING Step 1.
IN AN UNCONTROLLED MANNER-u NO SG CO/IPLETELY
{
D_ PRESSURIZED 29 CHECK IF SG TUBES ARE INTACT: GO TO IBEP-3, STEAM GENERATOR TUBE RUPTURE, l o SJAE/ Gland Steam Exhaust Gas Step 1.
radiation - LESS THAN ALERT ALARM SETPOINT:
- IPR 27J Grid 1 1PS127 l o SG Blowdown Liquid radiation -
LESS THAN ALERT ALARM SETPOINT:
- IPR 08J Grid 1 1PS108 l o Main Steamline radiation -
LESS THAN ALERT ALARM SETPOINT:
- 1RT-AR022 Grid 1 4AA122
e IRT-AR022 Grid 1 4AB222
- 1RT-AR023 Grid 1 4AB223
- 1RT-AR022 Grid 1 4AC322
- 1RT-AR023 Grid 1 4AC323
- Main Steamline 1D, MSIV Rm:
APPROVED
- 1RT-AR022 Grid 1 4AD422
- 1RT-AR023 Grid 1 4AD423 f[6 01 1969 B.O.S.R.
(0304E/0035E/042088)
REV 1 OPERATOR ACTION
SUMMARY
1BEP-F.0 l WOG-1A FOR 1BEP-0 SERIES PROCEDURES 1
TRIP RCPS WHEN: RED PATH
SUMMARY
o CC water to RCP lost 1. Suberiticality - NUCLFAR (affected pumps only) POWER 35%
\ -OR- ~
l o Cnet Phase B actuated 2. Core cooling - CORE EXIT
-OR- TCs >1200'F o ALL of the following conditions exist: 3. Heat sink-ALL SGs NR LEVEL <4% (34% FOR 6 Cst." :;Jtied ACs vvido-a IiiI ~ ' c ?'LE T2...T: /1_ JOTI- -
in progress EEEDWATER. FLOW <500 GPM
-AND .AYelLABLE
-AND- 4. Integrity - DECREASE
- High hea. JI pump flow indicator >100'F IN LAST 60 MINUTES (lFI-917) >50 GPM flow or AND RCS COLD LEG <246'F SI pumps >100 GPM SI ACTUATION: 5. Containment - CNMT PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, IF CST _EV E'_ <20%, 'i:EN Step 1, if: CONSIDE RT i E FOLLOWL 4G:
o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste
. ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CANNOT BE MAINTAINED of 3 SGs
> 4% (38% FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :EED 3 UMP 3A" TA4K LEVEL
< 16% T i E 9P ERFORi HE :0L_0 WING 1 l': CST LEVEL <3%, 'iEN P ER :0RM TH E FOLLOWL 4G:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
(Final)
(0386E/0042E/042488) APPROVED JAN 31 M49 B.O.S.R.
l
lh REV. 1 REACTOR TRIP OR SAFETY INJECTION 1BEP-0 WOG-1A UNIT 1 STEP ACTION / EXPECTED RE3:GN5E PESPONSE NOT OBTAINED 30 CHECK IF RCS IS INTACT: GO TO 1BEP-1, LOSS'OF REACTOR OR SECONDARY COOLANT, Step 1.
l o Cnmt radiation monitors - LESS THAN ALERT ALARM SETPOINTS:
- Cnmt area monitors:
- IRT-ARO14 Grid 4 4AS303
- 1RT-AR011 Grid 4 4AS111
- 1RT-AR012 Grid 4 4AS112
- 1RT-AR020 Grid 4 4AS120 1RT-AR021 Grid 4 4AS121 i o Cnmt pressure - LESS THAN 3.4 PSIG l' o Cnmt recirc sump' levels - NORMAL:
- Cnmt sump levels indicator lights - NOT LIT:
- ILL-SIO75A
- ILL-SIO75B APPROVED FEB 011989-B.O.S.R.
Page .21 o'f 33 (0304E/0035E/042088) ,
i
REV 'l OPERATOR ACTION
SUMMARY
1BEP-F.0 WOG-1A FOR 1BEP-0 SERIES PROCEDURES
^
TRIP RCPS WHEii: RED PATH
SUMMARY
o CC water to RCP icst 1. Subcriticality - NUCT. EAR (affecte.d pumps only) POWER >5%
-OR-o Cnst Phase B actuated 2. Core cooling - CORE EXIT
-OR- TCs >l200*F o ALL of the following conditions exist: 3. Heat sink-ALL SGs NR LEVEL <4% (34% FOR
.~.CC1 Lea RCS c:~.1 an C .0 . 1SL 2 2:' % :^T_7**
in progress EEEDWATER FLOW <500 GPM
-AND AVAILABMC
-AND- 4. Integrity - DECREASE
- High head SI pump flow indicator >100*F IN LAST 60 MINUTES (1FI-917) >50 GPM flow or AND RCS COLD LEG <246*F SI pumps >100 GPM' SI ACTUATION: 5 Containment - CNMT EELGURE >50 PSIG Actuate SI and GO TO 1BEP-0 '
REACTOR TRIP OR' SAFETY INJECTION, JF CST EN Step 1, if: CONSIDE V:i.(20%,
l F0 _LOWL' sG: "
o RCS succooling - liOT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CANNOT BE MAINTAINED of 3 SGe
> 4% (38% FOR. ADVERSF,,.QMU o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :EED ) UMP DA" TANK _ EVE,
< 16% T i E 4P ERFORi 'HE FOL _0W1 4G: I: CST LEVEL <3%, ' EN P ERFORM TH E FOLLOWL NG:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
)
l l
4 (Final) 1 (0386E/0042E/042488) APPROVED !
.J u 3 1 1969 B.O.S.R.
)
i
_ _ - __ - __ _ i
l -
c .
REV. 1 REACTOR TRIP OR SAFETY LJJECTION 1BEP-0 WOG-1A UNIT 1 i
' STEP ACTION / EXPECTED RESPON5E ~E?FONSE NOT OSTA NED 31 CHECK IF ECCS FLOW SHOULD BE TERMINATE ):
ACCEPTABLE per: GO TD Step 33.
o ICONIC DISPLAY
-OR-o ATTACHMENT A
- b. Secondary heat sink:- b. IF neither condition iidtisfied, .
o Total feed flow to SGs - THEN DO NOT STOP ECCS GREATER THAN 500 GPM PUMPS. GD To Step 33.
AVAILABLE
-OR-o Narrow range level in at least one SG - GREATER THAN 4% ,
~
- c. DO NOT STOP ECCS PUMPS-INCREASING Go TD Step 33.
- d. PZR level - GREATER THAN 4% d. DO NOT STOP ECCS PUMPS.
RETOTifi TO Step 31a.
32 GO TO 1BEP ES-1.1, SI TERMINATION, STEP 1 33 INITLATE MONlTORING OF' CRITICAL SAFE"Y FUNCT :0N STATUS TREES APPROVED FEB 011989 B.O.S.R.
~
Page 22 cf 33 (0304E/0035E/042088)
REV 1 OPERtTOR ACTION
SUMMARY
1BEP-F.0 -
WOG-1A FOR 1BLP-0 SERIES PROCEDURES 1
l TRIP RCPS WHEN: RED PATH
SUMMARY
o CC water to'RCP lost 1. Subcriticality - NUCTIAR .
(affected pumps only) POWER 351
-OR-o Cnmt Phsse B actuated 2. Core cooling - CORE EXII
-OR- TCs >12( 3'F o ALL. of the following conditions exfe : 3. Heat sink-ALL SGa_HE_
~ LEVEL.<4% (34% FOR-
- Cvut.tvlA.a how co..adurr !!QI . uNE .J O. _ _ * . .iik T 'T_'
in progress EEERW&TER FLOW <500 GPM
-AND AY).ILABLE
-AND- 4. Integrity - DECREASE _
- High head SI pump flow indicator >100*F IN LAST 60 MINUTES (1FI-917) >50 GPM flow or 6ND RCS COLD LEG <246*F SI pumps >>100 GPM SI ACTUATION: 5. Containment - CNMT PRESSURE >56 PSIG Actuate Si and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, T LEVE _ <20%, -EN Step 1, if: DERT i E F0_LOWL s G:
o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or EER ICONIC' DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CANNOT BE_MAIETAINED of 3 SGs
> 4% (38% FOR ADVERSE *;NMT) o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :EED')UiP JA" TA4K _EVEL
< 16% T i E 4P ER :0R 1 'HE :0L _0 WING" IF CST LEVEL <3%, " FEN PERFORM TH E FOLLOWTIS. .
I
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
(0386E/0042E/042488) APPROVED JM 311969 B.O.S.R.
_---_-----__----------y REV. 1 REACTOR TRIP-OR SAFETY INJECTION 1BEP-0 WOG-1A UNIT 1 i
STEP. ACTION / EXPECTED RES?ON5E PE?FONSE NOT USTA NED CAUTION Alternate water sources for AF pumps will be necessary if CST level decreases to LESS THAN 3%.
as OjEu $G LEVEL 5:
- a. Narrow range level - GREATER a. Maintain total feed flow THAN 4% greater than 500 GPM until
. narrow range level i.s greater than d in'at least one SG.
- b. Control feed flow to maintain b. IF narrow range level in narrow. range level'- BETWEEN 4% any SG continues to AND 50% increase in an uncontrolled manner,
- THEN GO TO 1BEP-3, STEAM GENERATOR TUBE RUPTURE,
. Step 1.
. i APPROVED FEB 01.1989.
s.o.S.R.
(0304E/0035E/042088) >
{
L-__-__-__-_
I'
\
Cd REV 1 OPERATOR ACTION SI iMARY 'B60-F.0 .
WOGilA FOR 1BEP-0 SERIES Ph0CEDURES TRIP RCPS WHEN: RED PATH
SUMMARY
o CC water to RCP lost 1. Subericicality - NUCT.FAR (affected pumps only) POWER >5%
-OR-0 Cnat Phase B actuated 2. Cere cooling - CORE EXII
-OR- TCs >1200*E .
o ALL of the following conditions exist: 3. Heat sink-ALL SGs NR
,- . 4 IdYEL__L_'L(34% FOR .
- Lati..'o'.ied RCO cuo2uc .. Lua -- -
^':. m . C MT' ANL ICT~ .
in progress FERDWATER FLOW (500 GPM
-AND AVAILABLE
-AND- 4 Integrity - DECREASE
- High head SI pump flow indicator >100'F IN LASt 60 MINUTES (lFI-917) >50 GPM flow or AND RCS COLD LEG <246*F SI pumps >100 GPM SI ACTUATION: 5. Containment - CRiI PRESSURE >50 PSIG Actuate SI and GO TO 1BEF-0 REACTOR TRIP OR SAFETY INJECTION, IF CST LEVE_ <20%, JEN Step 1, if:
~
CONSIDER T i E F0'_LOWL N G:
o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OE radwaste ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CANHOT BE MAINTAINED of 3 SGs
> 4% (38% FOR ADVERSE CNMT) *s o Crosstie unit's CST o . Reduce cooldown rate
- IF AUX :E'ED )U'iP JAY TAVK _ EVE'_fr,, y
< 16% T i E 9P ER:0R i THE :0L _0WI G- I: CST LEVEL <3%, T JEN
' P ERFORM TH E FOLLOWI NG:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
(0386E/0042E/% 488) gpp g JAN 311969 B.O.S.R.
REV. 1 REACTOR TRIP OR SAFETY INJECTION 1BEP-0
'WOG-1A UNIT 1
-5TEF ' ACTION / EXPECTED DES GN5E PESPONSE NOT OST AINE. l CAUTION Following SI reset., automatic SI will NOT occur, until reactor trip breakers have been. cycled.
CAUTION If offsite power is lost after SI reset, then manual action may be required to restart safeguards.-
equipment.
35' RESET SI: Reset SI per 1 BOA PRI-5, CONTROL ROOM INACCESSIBILITY,
- a. Depress both SI reset ATTACHMENT r..
pushbuttons
- b. Verify SI ACTUATED permissive light - NOT LIT
- c. Verify AUTO SI LLOCKED" " 'y permissivelight-LITf..f -
d APPROVED
' I FEB 01 1989 B.O.S.R.
U (0304E/0035E/042088) .___- ___-__________ _ - - - -
y
'REV 1 . OPERATOR ACTION-
SUMMARY
1BEP-F.0-WOG11A FOR 1BEP-0 SERIES PROCEDURES TRIP R' CPS WHEN: RED PATH
SUMMARY
o' .CC water to RCP lost 1. Suberiticality - NUCT FAR -
(affected pumps only) POWER >5%
-OR-o 'Cnet Phase B actuated 2. Core cooling - CORE EXIT
-OR- TCs >1200*F o ALL of.the following cond.itions exist: 3. Heat sink-AT T. SGs NR IJLVEL ^*L .Q_4% F0lt ,
- ControIlied KCSiooAdowr H21 L.ME'Cm , es .9TAL
'in progress FREDWATER FLOW <500 GPM
-AND AVAILABLE
-AND- 4. Integrity - DECREASE'
.(1FI-917) >50 GPM flow or AND RCS COLD LEG <246'T SI. pumps >100 GPM
'SI' ACTUATION: 5. Containment - CNMT PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, T _ EVE _ <20%, T1EN Step 1, if: DE R TH E F0_LOWI G:
o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CANNOT BE MAllTAINED of 3 SGs
> 4% (38% FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown r-ate
< 16% Ti E 4P ER :0Ri 'HE 0L _0WI 4G: I : CST LEV EL <3%, ~ ENL P ERFORM TH E FOLLOWL s G:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
(Final)
(0386E/0042E/042488) APPROVED .
JM 311969 8.O.S.R.
REV. 1 REACTOR TRIP OR SAFETY INJECTION 1BEP-0 WOG-1A- UNIT 1 STEP ACTION / EXPECTED RESPON5E RESPONSE NOT OSTAINED -
36 RESET CONTAINMENT ISOLATION:
- a. Reset Cnmt Isol Phase A a. Reset per 1 BOA PRI-5, CONTROL ROOM INACCESSIBILITY, ATTACHMENT E.
- b. Reset Cnmt Isol Phase B b. Reset per.IBOA PRI-5. ,
CONTROL ROOM l
3 ACCESSIBILITY ATTACHMENT E.
- c. Reset Cnnt Vent Isol
- d. Check SAC run lights - ANY LIT d. Start one SAC per BOP SA-1, STARTUP AND OPERATION OF THE SAC's.
- e. Open Cnmt instrument air
. isol valves:
- IIA 065 .
- IIA 066
- f. Open Cnmt fire protection isol valve:
- 1FP010 APPROVED FEB 01.1989 B.O.S.R.
Page 25 of 33 (0304E/0035E/042088)
REV. 1 OPERATOR ACTION
SUMMARY
l'1P-F.0
. WOG-1A F0R 1BEP-0 SERIES PROCEDURES TRIP RCPS WHEN: RED PATH
SUMMARY
o CC water to RCP lost 1. Suberiticality'- NUCLEAR (affected pumps only) PfWES.2.51
-LR-o Cnet Phase B actuated 2. Core cooling - CORE EXIT
-OR- TCs >1200*F o E of.the following conditions exist: 3. Heat sink-ATt SGs ME_
LEVEL <47. (34% FOP._..
- Controllec E S cooldu n n2I k .m . J JITS . 1' TOJe. L in progress FMhWATER' FLOW (500 GPM
-AND AVAILABLE
-AND- 4. Integrity - DECREASE
- High head SI pump flow indicator >100'F IN LAST 60 MINUTEE_
(lFI-917) >50 GPM flow or- 6@ RCS COLD LEG < 246
- F SI pumps >100 GPM SI ACTUATION: 5 Containment - CNMT PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY TNJECTION, le CST _EV E _ <20%. ' "
EN Step 1, if: CONSIDE RT i E FOLLOWL s 3:
o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CANNOT BE MAINTAINED of 3 SGs
> 4% (387. FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :E ED )UiP JA" TA4K _ EVE _
< 16% T i E VP ERFOR 1 rHE :0L _0WI 4G: I: CST LEV EL <3%, "EN PERFORM TH E FOLLOWL 3:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
(0386E/0042E/042488) APPROVED JM 311969 B.O.S.R.
o
REV. 1 REACTOR TRIP OR SAFETY. INJECTION 1BEP-0
'WOG-1A UNIT 1 STEP ACTION / EXPECTED RE5?ON5E RESPONSE NOT OSTAiNED CAUTION RCS pressure should be monitored.
If RCS pressure decreases to LESS THAN 300 PSIG, then RH pumps must be manually restarted to supply water -
to the RCS.
l 37 CHECK IF RH PUMPS SHOULD BE STOPPED:
- a. Check RCS pressure:
- 1) Pressure (1PI-403A/405) - 1) GO TO 1BEP-1, LOSS OF GREATER THAN 300 PSIG REACTOR OR SECONDARY COOLANT, Step 1.
- 2) Pressure - STABLE OR 2) Go To Step 38.
INCREASING
- b. Stop RH pumps and place in standby lT CHECK SECONDARY RADIATION GO To 1BEP-3, STEAM NORMAL: GENERATOR TUBE RUPTURE, Step 1.
- a. Sample SGs' blowdown for activity:
- 1) Open SG blowdown sample isol valves: .
e ISD005A
- 1SD005B e ISD005C
- 1SD005D
- 2) Notify Rad Chem to sample SGs' olowdown for activity APPROVED l
FEB 011989.
B.O.S.R.
.l (0304E/0035E/042088)
L_______________. . . _ _ _ _ _ _ - -
REV 1 OPERATOR ACTION
SUMMARY
1BEP-F.0 WOG-1A FOR 1BEP-0 SERIES PROCEDURES TRIP RCPS WHEN: RED PATH
SUMMARY
o CC water to RCP lost 1. Subcriticality - IGCLEAR (affected pumps only) POWER >5%
-OR-o Cnmt Phase B actuated 2. Core cooling - CORE EXIT
-OR- TCs >1200'F o ALL of the .tollowing conditions exist: 3. Heat sint- AT T. SGs NR LEYEL.<4% (34% FOR
- 'wunti vin a . RCo e,c.,c . J u ss. &
3DLtdE CEMT' . .. " " ~"J_f in progress FnnWATER FLOW (500 GPM
-AND AVAIL 6HLE
-AND- 4. Integrity - DECREASE
- High head SI pump flow indicator >100'F IN LAST 60 MINUTES (lFI-917) >50 GEE flow or AND RCS COLD LEG (246'F SI pumps >100 G,PE SI ACTUATION: 5. Containment - CEMI PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0, i
REACTOR TRIP OR SAFETY INJECTION, IF CST LEVE_ <20%, JEN
. Step 1, if: CONSIDER T i E F0 _LOWL s G:
o RCS subcooling - NOT ACCEPTABLE o Makeup.from MUDS or PER ICONIC DISPLAY OR radwaste .
ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CANNOT BE MAINTAINED of 3 SGs
> 4% (38% FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :E ED )UiP 3A1' TA4K _ EVE _
< 16% T i E 4P ER :0R 1 THE ;0L _0WI 4G: I: CST LEVEL <3%, " iEN P EP50RM TH E FOLLOWL 4G:
- Refill the day tank ;
- a. Verify secondary side of 3 SGs isolated
1 (Final) i (0386E/0042E/042488) APPROVED !;
JAN 31 1969 B.O.S.R.
1
y REV. 1 REACTOR TRIP OR SAFETY INJECTION 1BEP-0 WOG-1A UNIT 1
. STEP! ACTION / EXPECTED RESPONSE RESPONSE NOT 06TAINED l39 CHECX AUXILIARY BUILDING Evaluate cause of aonormal RADIATION: conditions.
- a. Aux Bldg vent stack IF cause is loss of RCS effluent monitors (IPR 28J) - idventory outside Cnmt, LESS THAN ALERT ALARM SETPOINT:- .THEN G0,.TO IBCA-1.2, LOCA OUTSIDE CONTAINMENT, Step 1.
Grida2 Beta 1PA228 Grid 2 Gas Low IPB128 Grid 2 Iodine IPC328
- Grid 2 Gas High IPD428 b Aux Bldg vent stack effluent monitors (1PR30J) -
LESS THAN ALERT ALARM SETPOINT:
Grid 2 Gas Low IPA 130 Grid 2 Gas Med 1PB230
- Grid 2 Gas High 1PC330 Grid 2 Effluent 1PF430
- c. ECCS cubicle monitors - LESS THAN ALERT ALARM SETPOINT:
- RH/CS Pump 1A Cubicle (IPR 13J):
Grid 2 Beta 1PA213
- Grid 2 Gas IPB113 t RH/CS Pump 1B Cubicle (IPR 14J):
Grid 2 Beta 1PA214 Grid 2 Gas IPB114 RH HX 1A Cubicle (IPR 15J):
G. rid 2 Beta 1PA215
'* Grid 2 Gas IPB115 Stsp continued on next page !'
APPROVED FEB 0 I 1989 1
B.O.S.R.
Page 27 of 33 (0304E/0035E/042088)
v.,r p 5
REV 1 OPERATOR' ACTION
SUMMARY
1BEP-F.0 W7G-1A FOR 1BEP-0 SERIES PROCEDURES TRIP RCPS WHEN: RED PATH
SUMMARY
, o CC water,to RCP lost 1. Suber.iticality - NUCf7AR (affected pumps only) POWER 351
-OR-o Cnat Phase B actuated 2. Core cooling - CORE EXII
-OR- ICs >1200'F o ALL of the following conditions exist: 3. Heat sink-ALL_1GsJ:.tfR_
LEVEL <4% (34% FOR ,
- Lotat.Jolled Rt:b ' cc,g.i.dsw.. 6 nLVERC :NM., AND _'Crfi in progress FmWATER FLOW < 500 GPM
-AND AVAILABLE
-AND- 4. Integrity - DECREASE
- High head SI pump flow indicator >100*F IN LAST 60 MINUIEH_
t (lFI-917) >50 GPM flow or AND RCS COLD LEG <246*F SI pumps.>100 GPM SI ACTUATION: 5. Containment - CNMT PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, IF CST LEVE _ (20%, 4 EN Step 1, if: CONSIDER i E F0 _LOWL s 3:
o RCS subcooling - HDT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste ATTACHMENT A . o Prepare to isolate
-OR- secondary supply side o PZR level - CANNOT BE MAINTAINED of 3'SGs
> 4% (38% FOR ADVERSE CNMT) 'o Crosstie unit's CST
. o Reduce cooldown rate
- IF AUX :EED 'UiP DA" TA4K _ EVE _
< 16% T 4 E 4P ER:0RM 'HE :0L ;0WI 4G: I: CST LEVIL <3%,' EN P ERFORM TH E FOLL6WL s 3:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
'(Final)
(0386E/0042E/042488) APPROVED JAN 3 1 669 B. O. S. R.
zw m 3
i, ,
c.e v.
5 y,' * :* ,
.v .
- REV. 1 REACTOR TRIP.OR' SAFETY INJECTION '1BEP-0 WOG-1A UNIT 1 STEF- ACTION /E1PECTED RES 0NSE. RESPONSE NOT OSTAINED {
-Step 39c (continued)
,, ~
RH HX IB Cubicle (IPR 16J):
- Grid 2 Beta 1PA216
- " Grid 2' Gas 1PB116 , ,
- CENT CPC Pump -1A Cubicle (IPR 17J):
- Grid 2 Beta IPA 217
- Grid 2 Gas IPB117 Mi
- CENT CHG Pump 1B Cubicle (1PR18J).
- Grid 2 Beta.1PA218
- Grid 2 Gas IPB118
- d. Grid 4 Aux Bldg'arez li
- ' radiation monitors - LESS THAN ALERT ALARM SETPOINT v l 40 CHECK PRT CONDITIONS: Evaluate cause of=-abnormal conditions.
- a. Pressure - LESS THAN 6 PSIG IF any PZR safety valve is
- b. Level - LESS THAN 80% ifetermined to'be the source of leakage into the PRT,
- c. Temperature LESS THAN 125'F THEN GO TO IBEP-1, LOSS OF REACTOR OR SECONDARY COOL 7ET, Step 1.
k h
I APPROVED FEB 01.1989.
s.o.S.R.
(0304E/0035E/042088)
i i
j ' .i n
R!V l' OPERATOR ACTION
SUMMARY
1BEP-F.0 WCG-1A i FOR 1BEP-0 SERIE
S. PROCEDURE
S -
u.
TRIP RCP' WHEU: RED PATH
SUMMARY
o CC water'to RCP lost 1. Suberiticality - LUCf.1MR (affected pumps only) POWER 35%
-OR-o Cnmt Phase B actuated 2. Core cooling - CORE EXIT
-OR- TCs >1200*F :i o ALL of the fc11owing conditions exist: 3. Heat sink-ATL SGs NR _.
LEVEL <4% (34% F_01_
- v'w.4trv11ed RL., cvulow dia ,1. L .ir,;.,nTi rum "_Illif in progress FEEDWATER FLOW <500 GPM
-AND '
AVAILABLE
-AND- 4. Integrity - DECREASE
- ligh head SI pump flow indicator >100*F IN LAST 60 MINUTES._
(1FI-917) >50 GPM flow or AND RCS COLD LEG <246*F SI pumps 2.100 GPM SJ ACTUATION: 5. Containment - CNMT PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, IF CST _ EVE _ <20%, ' HEN Step 1, if: ~ CONSIDE RT i E F0 _ LOW::NG:
o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CAHNOT BE MAINTAINED of'3 SGs
> 4% (38% FOR ADVERSE CNM'.[1 o Crosstie unit's CST
..-* % o Reduce cooldown rate
- IF AUX :iED ) UMP DA" TANK _ EVE V
< 16% T i EN P ERFORM rHE FOL _0WI dg I': CST LEVEL <3%, ' HEN
~
P ERFORM TH E FOLLOW::NG:
- Refill the day tank
- a. Verify secondary sid'e
, of 3 SGs isolated
(0386E/0042E/042488) APPROVED JAN 311969 B.O.S.R.
- _ _ - _ _ - _ _ _ _ _ _ _ - - _ _ _ _ _ _ _ - _- _. i
_y 1
y a . .
1- -
f._
, REV. 1 REAf f0R TRIP OR SAFET INJECTION .1BEP-0 4 WOG-1A UNIT.1 5TEP ACTION / EXPECTED R ~5:0N5E RESPONSE NOT OBTAINED CAUTION Do NOT exceed DG loadirq-requirements:
o 5500 KW continuous duty 6 '
, Q%A AMDS g;gi7gg u 5935 AW continuous for zu00. hours 6 1030 AMPS maximum o 6050 KW continuous for 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> 6 1050 AMPS maximum. d CAUTION If po'ssible, PZR heaters should be loaded on only one ESF' bus at a time.
Additional NON-ESF loads should be loaded on the other ESF bus.
41 CFECK I: DIESEL GENERATORS SF 00LD BE STOPPE7:
a.VerifyESF4KVbusses-fkfRh'12ED a. Try to restore offsite BY OFFSITE POWER: f; ' power to ESF busses e SAT 142-1 Bus alt 0e light - Ij[ offsite power can NOT LIT be restored,
- ACB 1412 - CLOSED THEN notify System Load
- SAT 142-2 Bus' alive light - Dispatcher of existing LIT conditions so an e ACB-1422 - CLOSED emergency AC restoration program can be implemented.
Step continued on next page APPROVED fEB 01.1989.
B.O.S.R.
Page 29 of 33 (0304E/0035E/042088)
7 t-
-REV 1 OPERATOR ACTION
SUMMARY
1BEP-F.0 WOG-1A FOR 1BEP-0 SERIES PROCEDURES TRIP RCPS WHEN: RED PATH
SUMMARY
o CC water to RCP lost 1. Subcriticality - NUCLEAR (affecte.d pumps only) POWER >57.
-OR-o Cnmt Phase B actuated 2. Core cooling - CORE EXIT
-OR- ICs >1200*F o ALL of the following conditions exist: .
- 3. Heat sink-ALL SGs NR LEVEL <47, (34% FOR
- .snt *9hl ;Cd Jolkown lJCI - -
in progress FEEDWATER FLOW < 500 GPM AVAILABLE
.-AND
-AND- 4 Integrity - DECREASE
- High head SI pump flow indicator >100*F IN LAST 60 MINUTES _
(lFI-917) >50 GPM flow or' AND RCS COLD LEG (246'Ti SI pumps >100 GPM SI ACTUATION: 5. Containment - C11tiI PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, IF CST _EV E _ <20%, " HEN Step 1, if: CONSIDE RT E FOLLOWLNG:
i o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CANNOT BE MAINTAINED of 3 SGs
> 47. (387. FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown rate
< 16% T i E 1P ER :0R 1 THE :0ETWING:
I': CST LEVEL <3%, THEN P ERFORM TH E FOLLOWING:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
(0386E/0042E/042488) APPROVED JAN 31 1969 B.O.S.R.
p 1 '.
g REV. 1 REACTOR TRIP OR SAFETY INJECTION 1BEP-0 WOG-1A UNIT 1 STEP ACi!ON/EXPECTE3 REE;ON5E PESPON?E NOT OSTAINED Step 41 (continued)
I b. NON-ESF 4 KV Busses: b. IF offsite power can NOT be promptly restored,
- SAT 142-1 Bus alive light - THEN establish'necessary LIT NON-ESF loads to maintain
- ACB 1432 - CLOSED plant conditions.
- SAT 14?.-2 Bus a3ive light -
~
LIT' 1) Verify locally all e ACB 1442 - CLOSED breakers on Bus 143 and 144 OPEN.
2)cPlace all~non-running WS pumps in PULL OUT position.
. e ISI8811A
- ISI8811B
- 4) Energize Bus 143 and 144 from ESF crosstie breakers.
- 5) Open all 480 volt transformer LOW side breakers associated with Bus 143 and 144.
- 6) Reenergize PZR heaters:
a) Close 4160 volt PZR heater transformer's HIGH side breakers at IPM01J.
b) Close 480 volt PZR heater transformer's LOW side breakers at 1PM05J.
APPROVED Step continued on next page B.O.S.R.
(0304E/0035E/042088)
REV 1- OPERATOR ACTION
SUMMARY
1BEP-F.0 WOG11A FOR 1BEP-0 SERIES PROCEDURES TRIP RCPS WHEN: RED PATH
SUMMARY
- l
- o. CCTwater to RCP lost. 1. Suberiticality - NUCLEAR l '(affected-pumps only) POWER >S%
l> ..OR_
l o Cnmt Phase B actuated 2. Core cooling - CORI EXIT
-OR . TCs >1200;;
o ALL of the following conditions exist: 3. Heat sink-ALL SGs NR LEVEL <4% (34% FOR
' + Lv uv11cd E S'coc1%..., NM - .1 . H._. _, m.~' 'PP 5;-
in progress -- FERnWATER FLOW'<500 GPM
-AND AYr LABLE
-AND- 4. Integrity - DECREASE
- High head SI pump flow indicator >100*F'IN LAST 60 MINUTES (1FI-917) >50 GPM flow or AND RCS COLD LEG.<246*F SI pumps >100 GPM-SI ACTUATION: 5. Containment - CNMT PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, IF CST _ EVE _ <20%, "iEN Step 1, if: CONSIDE RT iE F0_LOWL43:
o RCS subcooling - ROT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-0R- secondary supply side o PZR level - CAHHOT BE MAINTAINED of 3 SGs
> 4% (38% FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :E ED ) UMP ')A" TA4K _ EVE _
< 16% T 4 E 4P ERFOR i 'HE :0L _0WI 4G: I : CST LEVEL <3%, " HEN P ERFORM TH E FOLLOWLNG:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
(0386E/0042E/042488) APPROVED JAN 311969 !
B. o. s. R.
h, '
REV. 1 REACTOR TRIP OR SAFETi INJECTION 1BEP-0 WOG-1A UNIT 1 STEP- ACTION / EXPECTED RE5?ONSE RESf 3NSE NOT OSTAINED Step 41b (continued)-
c) Operate PZR heater.
controls.at necessary to control system pressure.
- 7) Start a WE' pump pe:. .A2 WS-1, STARTUP AND OPERATION OF WS SYSTEM,
~
e if necessary. 1
- 8) Start a SAC per BOP SA-1, STARTUP AND 4
OPERATION OF THE SAC's,
- 9) Energize other NON-ESF' loads as necessary..
- 7. DIESEL' GENERATOR SHUTDOWN.
42 RETURN TO STEP 25
_ggp_
4 APPROVED FEB 011989 1
B.O.S.R.
(0304E/0035E/042088)-
REV 1 OPERATOR ACTION
SUMMARY
1BEP-F.0 '
WOG-1A FOR 1BEP-0 SERIES PROCEDURES TRIP RCPS WHEN: ,
BED PATH SLiMARY:
o CC water to RCP lost 1 Subcriticality - NUCLEAR (affecte.d pumps only) POWER >5%
-OR-o Cnmt Phase B actuated 2. Core cooling - CORE EXIT
-OR- TCs >1200*F o ALL of the following conditions
' exist: " 3. Heat sink-ALL SGs NR LEVEL <4% (34% FOR
'- + Jsntro11W ... . . ' 1o5 . X r .. , cOVFRo Cm - "Ic in progress EEEDWATER FLOW <500 GPM
-AMD AVAILABLE
-APD- 4. Integrity - DECREASE
~* High head SI pump flow indicator >100*F IN LAST 60 MINUTES (1FI-917) >50 GPM flow or AND RCS COLD LEG <246*F >
SI pumps >100 GPM SI ACTUATION: 5. Containment - CNMT l PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR FAFETY INJECTION, IF CST _ EVE _ <20%. TFEN Step 1, if: CONSIDE R TH E F0 _LOWIhG:
o RCS subcooli g - HOT ACCEPTABLE o Makeup from MUDS or PER ICONIC Li3 PLAY OR radwaste ATTAChMEN?...A o Prepare to isolate
-Oh- secondary supply side o PZR level - CAHHQIE,JiMNTAINED of 3 SGs
> 4% (38% FOR ADVERSE CMMT) o Crosstie unit's CST ;
o Reduce cooldown rate
- IF AUX :E ED )UiP JA" TANK _ EVE _
< 16% T i E 9P ER 0R 1 lie FOL _0WI 9G: I: CST LEVEL <3%, TiEN P ERFORM TH E FOLLOWING:
- Refill the day tank
- a. Verify secondary side .'
of 3 SGs isolated
{
(Final)
(0386E/0042E/042488) APPROVED I MN 311969 j B.O.S.R. )
1
__-_- _ _ - - - - - a
,0-REV. 1 REACTOR TRIP OR SAFETY INJECTION WOG-1A 1BEP-0 UNIT 1 I
CNORMAL) 222 322 422 522 622 720 260%,,,, , ,, , , ,j ,
4, g , '2622 2522 : ,ll1 + " '
l lo ,, ,l l l 2s22 2422 ,6*tI .'e'
!i rsie #
iII
- a
'I if- L
' 'I '
FI 2422 23?2 -W l l I ' ' l ,' l ,4 -- l l Y- C *
! L'- p - -- ~
'T '
2222 ' l.l ' l l l l l ' '
f [' l} 230io
, 2122 ll,' 'l l ,
l
' /) [ 2222 l 2002 i l ll ,,l'l
( ,/ / ,I 2122 c 1922 : ::'
!// / .
2222 ,
l:ll ; !; , fif l 7 1e2e a
<- 1822 'i i
'^CCGPTABtE ' ' '
'# J l y7gg i t!
6n, e
liilsiei r< '
il 1 i 1832 "
,o.,.,
e i !
tfi F 4 ft gq
., , i, 7gg
_ , i m
lllll ri
" 1622 l l!, ,
l- fj [j 16 2 2 v t.
3-e 1522 --M l- .I '
I / '
- - 1522
'! 1422 ;,l '
j j 7 ,j '
1422 J 1322 ' ' l ,' l' l ' ;' ' ij'/ '
bl 1222 , 1322 J Ihi , l !;l ' ' ,
D7 j ,# j
--, - 7- 1222 Ul i
a 1122 . i,,ei6i......,,i,,j .ii .
r .i r "'T" Ul
,j
,, g -
1122 g Cf 1222 l l'l
(( [ 1222 E A 922
.ieii l.l!l i ADVERSE i, ,
, . // / 922 G.
ty :** i,,,i 1
ro I NOT i i,i
. . ICNMTl i1 /- if A~ 2
, L 722 ![l',
AC C E P TA B L E-- Ul I
/[ [ l'
& yzz '
ti >
722 (_)
1
(
1' \
/[/ /
e gag 1 522 422
, , f 7 '/ --
522
[ ! !. [ f h go7yggyrgs 422 322 ' ' '#' ' '
/ ' '
322
- 222 NCRMAL C NM T ; , , , , , , , , 9 M'/
c 222 l 122 ,i ti
'!!lli 11, 4- tii l..' _
i rt i i l
i'
[ 122 r-222 322 422 Saa 622 722 TEMPERATURE C C)
APPROVED FIGURE IBEP 0-1 RCS SUBCOOLING MARGIN fEB 011989 i
(
B.O.S.R. l
__J1forstwti lasAn wn.' e an" '-
, l 1
' REV 1 OPERATOR ACTION
SUMMARY
1BEP-F.0 WOGI1A FOR 1BEP-0 SERIES PRIJEDURES ,
1 TRIP RCPS WHEN: RED PATH S:JMMARY:
o CC water to RCP lost 1. Suberiticality - NUCLEAR (affected pumps only) POWER >53
-OR-o Cnmt Phase B actuated 2. Core cooling - CORE EXIT. '
-OR- TCs >1200*F o ALL of the following conditions exist: 3. Heat sink-AT.T SGs NR LEVEL <4% (34% FOR
-AND, ., ,
AVAILABLE
-AND- 4. Integrity - DECREASE
- High head SI pump flow indicator >100*F IN LAST 60 MINUTES (lFI-917) >50 GPM flow or AND RCS COLD LEG <246*F SI pumps >100 GPM SI ACTUATION: 5. Containment - CMiI PRESSURE >50 PSIG Actuate SI and GO TO 1BEP-0, REACTOR TRIP OR SAFETY INJECTION, IF CST _ EVE _ <20%, ' HEN Step 1, it: CONSIDE RT i E FOLLOW: NG:.
o RCS subcooling - NOT ACCEPTABLE o Makeup from MUDS or PER ICONIC DISPLAY OR radwaste ATTACHMENT A o Prepare to isolate
-OR- secondary supply side o PZR level - CAHHOT BE MAINTAINED of 3 SGs
> 4% (38% FOR ADVERSE CNMT) o Crosstie unit's CST o Reduce cooldown rate
- IF AUX :
E ED ) UMP JA TAyK _ EVE _
< 16% T 1 E 4P ERFOR i 'HE :0L _0WI 4G: I: CST LEVEL <3%, -
EN P ERFORM TH E FOLLOWL s G:
- Refill the day tank
- a. Verify secondary side of 3 SGs isolated
. supply (Final)
(0386E/0042E/042488) APPROVED JAN311969 B.O.S.R.
w _ _-- _ _ _
l,,.
REV. 1 REACTOR TRIP OR SAFETY INJECTION 1BEP-0 ]
WOG-1A UNIT 1 i
ATTACHMENT A 1
A. Determination of Post-Accident RCS Subcooling:
- 1. Check Cnmt for ADVERSE conditions:
o Cnmt pressure greater than 5 PSIG.
-OR-o Cnmt radiation greater than 10 5R/hr:
- 1RT-AR020 Grid 4 4AS120
- 1RT-AR021 Grid 4 4AS121
- 3. Determine temperature for RCS pressure using NORMAL or ADVERSE Cnmt curves per Figure 1BEP 0-1.
- 5. If average of ten highest core exit TCs less than temperature for RCS pressure, then acceptable subcooling exists.
APPROVED FEB 011989 B.O.S.R.
(0304E/0035E/042088)
FfNAE.
- _ _ _ _ _ _ _ - _ _