ML20195E216

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Application for Amends to Licenses DPR-77 & DPR-79, Consisting of Tech Spec Change 88-21,revising Tech Spec Limiting Condition for Operation 3.7.5 to Increase Max UHS Temp from 83 to 84.5 F & Add Min Water Level.Fee Paid
ML20195E216
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 06/20/1988
From: Michael Ray
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
Shared Package
ML20195E221 List:
References
TAC-R00375, TAC-R00376, TAC-R375, TAC-R376, NUDOCS 8806230327
Download: ML20195E216 (2)


Text

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TENNESSEE VALLEY AUTHORITY CHATTANOOGA. TENNESSEE 374o1 SN 157B Lookout Place gun 201988 TVA-SQN-TS-88-21 10 CFR 50.90 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555 Gentlemen:

In the Matter of ) Docket Nos. 50-327 Tennessee Valley Authority ) 50-328 SEQUOYAH NUCLEAR PLANT (SQN) UNITS 1 AND 2 - TECHNICAL SPECIFICATION (TS)

CHANGE 88-21 In accordance with 10 CFR 50.90, we are enclosing a requested amendment to licet. sos DPR-77 and DPR-79 to change the technical specifications of SQN units 1 and 2. The proposed change revises limiting condition for operation (LCO) 3.7.5 to increase the maximum allowable ultimate heat sink (UHS) temperature from 83 degrees Fahrenheit (F) to 84.5 degrees F. A minimum water-level requirement is added to LCO 3.7.5 by the proposed change. The format and wording of specification 3/4.7.5 are revised to incorporate the new reservoir lesel requirements. The revised format and wording are consistent with the draft revision 5 of the Westinghouse Standard Technical Specification. Additionally, the wording of LCO 3.7.5 and surveillance  ;

requirement 4.7.5 is modified to Jpecify that the UHS temperature limit applies to the essential raw cooling water (ERCW) supply water temperature. l l

The proposed TS change is identified in enclosure 1. The justification for  :

the proposed TS change is provided in enclosure 2. A proposed determination of no significant hazards consideration performed pursuant to 10 CFR 50.92 is provided in enclosure 3.

Enclosed is a check for the $150 amendment application fee required by 10 CFR 170.12.

This proposed change is necessitated by the ongoing drought in the Tennessee i River watershed. Current projections indicate that the present UHS l temperature limit of 83 degrees F may be exceeded in mid- to late-July.

Because of the potential for a forced unit shutdown, TVA requests that this proposed change be processed as expeditiously as possible.

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WfChfC 8806230327 DR 880620 '

' #9M p ADOCK 05000327 An Equal Opportunity Employer DCD "

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! g U.S. Nuclear Regulatory Comission 'JUN 201988 Please direct questions you may have concerning this issue to Russell R. Thompson at (616) 870-7470.

Very truly yours, TENNESSEE VALLEY AUTHORITY M. J. ay, Dep Director Nuclear Licensing and Regulatory Affairs Sworn a d subscr bed before me this day of 18 1988 Solary Public J~'

My Comission Expires l

Enclosures cc (Enclosures):

Mr. K. B. Barr, Acting Assistant Director l for Inspection Programs I TVA Projects Division U.S. Nuclear Regulatory Comission Region II 101 Marietta Street, 1W, Suite 2900 Atlanta, Georgia 30323 Ms. S. C. Black, Assistant Director for Projects i TVA Projects Division U.S. Nuclear Regulatory Comission One White Flint, North 11555 Rockville Pike Rockville, Maryland 20852 Mr. Michael H. Mobley, Director (w/o enclosures)

Division of Radiological Health T.E.R.R.A. Buliding 150 9th Avenue, N Nashville, Tennessee 37203 Sequoyah ReJident Inspector Sequoyah Nuclear Plant 2600 Igou Ferry Road Soddy Daisy, Tennessee 37379