IR 05000443/1997099

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SALP Rept 50-443/97-99 for 960505-971206
ML20199F157
Person / Time
Site: Seabrook NextEra Energy icon.png
Issue date: 01/23/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20199E647 List:
References
50-443-97-99, NUDOCS 9802030074
Download: ML20199F157 (6)


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Enclosure 1 SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE (SALP)

SEABROOK NUCLEAR POWER STATION Report No. 50-443/97-99 BACKGROUND The SALP Board convened on December 18,1997, to assess the nuclear safety performance of the Seabrook Nuclear Power Station for the period from May 5,1996, through December 6,1997. The Board was conductcd pursuant to NRC Management Directive (MD) 8.6 (see NRC Administrative Letter 93-20). The Board members were Cherles W. Hehl (Board Chairman), Director, D: vision of Reactor Projects, Region I (RI), l Larry E. Nicholson, Deputy Director, Division of Reactor Safety, Rl, and John A. Zwolinski, Deputy Director, Division of Reactor Projects 1/11, Office of Nuclear Reactor Regulatio The Board developed this assessment for the approval of the Region I Administrato The performance ratings and the functional areas used below are described in NRC MD 8.6, " Systematic Assessment of Licensee Performance (SALP)."

1 PERFORMANCE ANALYSIS - OPERATIONS I

t Overall the Station was operated safely throughout the period and operator performance was generally good. Several events occurred, however, that were attributed to weak operatnr assessa.ent of plant parameters and control of complex evolutions. Deficiencies were noted involving the use and quality of procedures. Operators and station i

mancgement were not consistently effective in ensuring the prompt resolution of degraded  !

equipment conditions. The problem reporting system appears to have improved, however, l weaknesses we noted involving the quality and depth of root cause analysis, and corrective actions. Licensed operator training continued to be effectiv {

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Operators have been generally effective at identifying and ensuring the prompt resolution

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of plant equipment problems. However, a number of degraded equipment conditions were l identified for which operations had not promptly pursued resoiution. These conditions included a positive displacement charging pump oil leak, a low boron co scentration in the refueling water storage tank, evidence of long term boric acid leakage on a safety injection pump mechanical seal, and several outstanding emergency diesel generator deficiencie While individually some of these problems were minoi in nature, collectively they raise questions regarding operators and Station Management resolve to promptly correct degraded plant condition Operators were professicnal, performed well during shift turnovers, and were

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knowledgeable of plant conditions. Operator performance during routine and planned '

evolutions was good as demonstrated by a low number of plant events due to operator error. Refueling activities, drain down to and recovery from mid-loop operations, and a j

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Technical Specification required shutdown were planned and executed well. However, there were some weaknesses noted involving the assessment of plant parameters, and the coordination of outage activities. These operator performance weaknesses were highlighted by a preventable reactor trip that occurred during the shutdown for refueling, and three inadvertent feedwater isolation actuation events which occurred during outage surveillanco testin The implementation of the revised problem identification and resolution process varied with some improvements noted. Problem ideritification has improved as evidenced by the low threshold and large number of issues identified. The root cause analysis and corrective '

actions for identified issues were generally good, however, in some cases generic concerns or contributing causes for adverse conditions were not adequately addressed, in particular actions to identify and address the underlying causes for human errors and discrepancies in the station tagging processes were not fully effectiv Some deficiencies were identified in procedure use and quality. For example, operators aligned the safety injection system in a configuration that was not specified by a procedure. Additionally, the plant was operated for eleven days without the correct boron injection concentrations being incorporated into an emergency operating procedure and an abnormal operating procedure.

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Licensed operator training continued to be effective. The facility successfully prepared all five senior reactor candidates for initiallicensing examinations. The licensed operator requalification training program was thorough and effective. Good performance was noted in the development and administration of requalificatior, examination Overall, the Management Review Team and safety review committees were effective in i ensuring the quality of event ev duation The Operations area is rated Category . PERFORMANCE ANALYSIS - MAINTENANCE Maintenance activities were effective as evidenced by reliable safety-system performanc Overall, the identification of and response to equipment deficiencies was good. Station management provided good direction and support of maintenance backlog reduction efforts and progress was made late in the period. However, some maintenance >lanning and procedure weaknesses were observed that adversely impacted on availability of safety related equipment. Personnel performance and supervisory oversight were good, howevu, recent events indicate some weakness in maintenance work practices. The quality and control of on-line meintenance activities improved over the period. Surveillance testing was performed well, and was effective in identifying degraded equipment condition Assessment and correction of maintenance deficiencies was very goo In general, maintenance and surveillance activities were conducted well. The oa-line

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maintenance program was effectively restructured early in the period and recent on-line I maintenance performance was good. Assessment ano correction of maintenance deficiencies was noted to be very good overall. For example the licensee responded well a

to a hot leg temperature instrument failure, in addition, the foreign material exclusion

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program was considered excellent. Also, it was noted that the "fix-it now" team was fully implemented toward the end of the SALP period. While too early to assess its overall effectiveness, this effort was viewed as a positive initiativ Maintenance personnel performance and sapervisory oversight were noted to be generally good throughout the assessment period. Examples included good coordination and oversight during the conduct of troubleshooting and repairs for the emergercy diesel generators and the planning for a temporary leak seal repair of a main steam valve packing leak. Further, it was noted that there were no plant trips during the assessment period attributed to maintenance or surveillance performance. However, several recent problems indicated that some human performance weaknesses exist. For example improper pressure-rated tubing used to vent a flow transmitter failed resulting in the unnecessary release of contamination within the primary auxiliary building (fourth such occurrence during the period), in another example maintenance technicians were observed to be improperly handling safety-related bolts. Additionally, the environmental qualification of an emergency feedwater system steam admission valve was challenged when a limit switch connector was not properly tightened during an outage maintenance activit Maintenance rule implementation was considered to have a number of strengths including:

incorporation of Probabilistic Safety Assessment (PRn) insights into planned maintenance activities; and, utilization of industry operating experience into maintenance practices and planning. Further, the NFC concluded that the overall safety-related equip'.ient reliability was generally maintained in a high state of readiness. However, we noted some maintenance planning and procedural weaknesses were evident during the asse.csment period. For example procedural deficiencies resulted in the improper installation of a turbine driven emergency feedwater pump seal, unclear work package instructions complicated the repair of a seal table leak, and positive measures were not implemented to eruure that a preventive maintenance activity would not impact emergency diesel generator surveillance test results. The im;.oper sealinstallation was subsequently determined to be a risk signilicant fai!ur Surveillance testing showed sound performance. Test conduct was performed well and was noted to be effective at identify;ng degraded equipment conditions. For example, the licensee's staff identified and resolved problems associated with uncontrolled unloading of a diesel generator. The equipment monitoring programs were considered strong, as evidenced by the identification and correcticn of an adverse trend in the emergency diesel generator start time The Maintenance area was rated Category I PERFORMANCE ANALYSIS - ENGINEErilNG dngineering management oversight and involvement in plant activities generally goo Support to operations and maintenance was normally effective but, in some instances, engineering failed to adequately address problems such as long-standing control building air conditioning compressor deficiencies. Although design change and modification work was performed well, some design changes were adversely impacted by the quality of design

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change packages. The 10 CFR 50.54(f) effort was very good with a detailed plan that included numerous vertical slices of systems. Extensive effort to evaluate the causes of the failed fuel rods was particularly noteworth I Engineering support to operations and maintenance was mixed. System engineers were experienced and demonstrated good knowledge of their systems. Problems with the main feed pump control circuit and uncontrolled loading of the emergency diesel generator were effectively resolved. Engineering work to evaluate potentially high primary component cooling water temperatures during post-accident conditions was good, in contrast, previous engineering efforts to resolve control building air conditioning compressor problems were not effective. Late in the period, it was identified that engineering had failed to promptly evaluate and initiate corrective actions for a longstanding degraded condition concerning a through wall pipe sk in the residual heat removal system, in addition, a poor engineering evaluation of a replacement valve spring resulted in an unauthorized modification of a safety injection valv Cssign change and modification work was performed well. Safety evaluations were generally of adequate scope and of good quality. The primary component cooling water heat exchangers were replaced to address a longstanding problem with tube erosion.

! Engineering developed an innovative solution to resolve the degraded field weld joints in l the 24.ir W service water piping. However, several deficiencies were noted during modifict. tion of the turbine driven emergency feedwater pump : team admission valv Examples included specifying an incorrect switch and problems in the circuit wiring connection design, field installation, materials selection and the testing packag Corrective actions 'uere being formulated to address an adverse trend with the quality of design change package Strong performance was noted associated with the engineering activities directed toward maintaining the design and licensing basis of the plant. An extensive engineering review was conducted pursuant to the NRC 10 CFR 50.54(f) letter. The findings from this review were incorporated into the corrective action program and appropriately prioritized for resolution. For example, a single failure vulnerability wa:. :dentified and resolved regarding the absence of automatic initiation of the emergency feedwater system during certain accident conditions. The lessons and experience gained from this review were used to f acilitate continued improvement of the Seabrook design basi The Engineering area is rated Category PERFORMANCE ANALYSIS - PLANT SUPPORT Performance in the plant support functional area continued to effectively support safe plant operation. Overall performance in the various programs under the radiological controls area continued to be strong. The licensee continued to maintain a good emergency preparedness program. The secur:ty program was determined to be effectiv Overall performance in radiological controls was excellent as evidenced by extensive planning and effective impler entation of radiological controls for outage work including

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strong radiological worker performance. The station staff successfully met a significant radiation protection chauenge with the unexpected quantity of fuel defects identified when the plant shutdown for refueling. Strong perforrmance was evident in the handling of the resultant elevated in-plant airborne radioactivity levels. Health physics controls for most key outage activities were excellent, including: pre-job briefings, radiation work permit controls, and communications. Excellent ALARA planning was implemented for removal of a Reactor Vessel Stud and installation of temporary shielding in the containmen Radioactive waste and transportation programs were effectively implemented. The volume of low level radioactive dry active waste was significantly reduced. Also, an excellent radwaste technician training program was implemente The radiological environmental monitoring and effluent control programs continued to exhibit excellent performance, and were effective in ensuring that the impact on public health and safety and the environment was minima The security program was very effective and continued to exhibit high quality performanc Upgrades to the security communications system, weapons armory, and intrusion detection systems, and the completion of the specifications for a new access control system demonstrated management's commitment to the security function. Security personnel were knowledgeable of their duties and responsibilities. Seceity personnd properly responded to alarm conditione and demonstrated positiv~ ,.; cess control. Controls for identifying, resolving and preventing security program prob 5;ns were effectiv The emergency preparedness program continued to be strong. The 10 CFR 50.54(t) audit process was upgraded using emergency preparedness specialists from other utilitie Emergency preparedness f acilities were maintained in a good state of readiness. The emergency preparedness staff was maintained qualified and training was effective. Drill l and exercise performance were noted to be very goo The fire protection program was effectively implemented and housekeeping was generally goo The Plant Support area was rated a Category .

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Enclosure 2 SEABROOK SALP 12 MONTH INSPECTION PLAN

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I ION INSPECTION TITLE / PROGRAM AREA DATES COMMENTS IP 92903 Engineering Follow up on M&TE Issues 1/21/98 Regional Initiative IP 82301 Emergency Preparedness Exercise 6/1/98 Core inspection . 1 l

IP 81700-01 Physical Security Program 7/13/98- Core inspection IP 83750-01 Occupational Radiation Exposure - Non-outage 7/1/98 Core inspectsn IP 86750-01 Solid Radioactive Waste Management and 12/1/98 Core inspection Transportation of Radioactive Materials iP 64704 Fire Protection Program Review TBD Core inspection Legenc': IP - Inspection Procedure Tl - Temporary Instruction Core inspection - Minimum NRC Inspection Program (mandatory at all plants)

RegionalInitiative - Additionalinspection Effort Planned by Region i

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