ML20140E726
ML20140E726 | |
Person / Time | |
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Site: | Wolf Creek |
Issue date: | 04/25/1997 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
To: | |
Shared Package | |
ML20140E710 | List: |
References | |
50-482-97-08, 50-482-97-8, NUDOCS 9704290128 | |
Download: ML20140E726 (18) | |
See also: IR 05000482/1997008
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ENCLOSURE 2
U.S. NUCLEAR REGULATORY COMMISSION
REGION IV
Docket No.: 50-482
License No. NPF-42
Report No.- 50-482/97-08
Licensee: Wolf Creek Nuclear Operating Corporation
Facility: Wolf Creek Generating Station
Location: 1550 Oxen Lane, NE
Burlington, Kansas
Dates: February 23 through April 5,1997
Inspectors: J. F. Ringwald, Senior Resident inspector
J. L. Dixon-Herrity, Resident inspector
G. L. Guerra, Jr., Radiation Specialist
Approved By: W. D. Johnson, Chief, Reactor Projects Branch B
ATTACHMENT: Supplemental information
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9704290128 970425
PDR ADOCK 05000482
G PDR
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EXECUTIVE SUMMARY
Wolf Creek Generating Station
NRC Inspection Report 50-482/97-08
Operatj ans
The operators exhibited good attention to detail in identifying a small step change in
reactor coolant pump seal flow. The corrective actions taken by tha licensee were
conservative and appropriate (Section 01.1).
- Operator actions and the corrective actions taken in response to the failure of
Component Cooling Water Train A surge tank level indications were appropriate and
in accordance with procedures (Section 01.2).
- The inspector identified an additional example of a violation cited in a previous
report when the shift supervisor failed to recognize that maintenance on a
containment isolation valve would render the valve inoperable, and this condition, l
therefore, required entry into Technical Specification 3.6.3 (Section 01.3). )
- The operators responded appropriately in recognizing the concern with performing I
two radwaste releases in a manner inconsistent with the Updated Safety Analysis ,
Report (USAR) requirements (Section 04.1). I
- Radwaste operators' failure to follow procedures when filling Waste Monitor Tank B i
was identified as a violation (Section 08.1).
Maintenance j
- The system engineer's initiative to recommend component cooling water pump
bearing replacement was considered to be a strength in monitoring and addressing
concerns with the system's performance (Section M1.3).
- An electrical technician exhibited good attention to detailin noting inadequate
surface contact on half of the connections to the bus on a breaker (Section M1.4).
- Appropriate actions were taken by maintenance planning in addressing a missing roll
pin on the diesel generator mechanical governor (Section M1.4).
- The inspector noted a concern in communications within the planning department
when concerns raised during a work critique meeting about planning were not
relayed to planning management (Section M1.5). l
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- The failure to update the operational risk assessment document maintained in the
control room was identified as a violation (Section M1.6).
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- The licensee identified violation of Technical Specification 3.8.1.1 was cited ;
because the inspector identified that inadequate corrective actions led to a I
recurrence of a related event. In both events, inadequate communication between l
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the shift supervisor and maintenance technicians resulted in the shift supervisor not
understanding the impact of the proposed work on the operability of safety-related
equipment (Section M8.1).
Enaineerina
- The inspector identified an unresolved item associated s A a USAR change which
deleted time response requirements for the control room ventilation radiation
monitors (Section E1.1)
- The failure to update the USAR to reflect the actual plant design for containment
penetrations was identified as a violation of 10 CFR 50.71(e) (Section E8.1).
Plant Suncort
- The licensee found that the chemistry department prepared liquid release permits
which would not have met the USAR requirements for alarm setpoints
(Section 04.1)
- A noncited violation resulted when an engineer and a quality control inspector failed
to follow procedures by entering the radiation controlled area without
thermoluminescent dosimetry (Section R1.1).
- A radioactive source spill caused three personnel to become contaminated when a
check source separated from an area radiation monitor detector due to adhesive ,
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degradation. The initial technician response was appropriate and effective in
limiting the spread of contamination and cleaning up the spill (Section R1.2).
- The licensee identified and appropriately addressed a chemistry technician training I
deficiency (Section R5.1).
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Report Details
Summary of Plant Status
The plant operated at essentially 100 percent power throughout the inspection period.
I. Operations
01 Conduct of Operations
01.1 Reactor Coolant Pumo C Seal 1 Dearadation
a. Inspection Scope (71707)
On March 21,1997, operators in the control room noted an unexpected response of
Reactor Coolant Pump C sealleakoff flow after switching charging flow from the
normal charging pump to Centrifugal Charging Pump B. It increased from
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approximately 4.9 to 5.1 gpm, then stabilized at 4.9 gpm. The inspectors observed
the corrective actions taken after the anomaly was identified, reviewed plant
parameters, and reviewed the applicable procedures.
b. Observations and Findinas
The operators reviewed recent history for the leakoff flow parameter in the
computer. They noted step increases from 3.2 to 4.0 gpm on March 9,1997, and
from 4.0 to 4.9 gpm on March 18,1997. In each of these cases, the flow
remained at the higher level, rather than stabilizing back to a lower flow. The
licensee had previously noted that temperature changes in the reactor coolant
system caused flow increases in sealleskoff, but the flow returned to normal when
the system stabilized. The operators reviewed related procedures and contacted
management. Management personnel determined that the current flow did not
exceed the specified maximum flow, but that the condition was not desirable.
Management personnel directed that changes in temperature were to be minimized
and that the manufacturer was to be contacted early Monday morning to discuss
the trend. Plans were also made to set up a contingency plan for a forced outage
to replace the seal.
The inspector reviewed both the Alarm Response Procedure ALR 00-072A, "RCP
Seal No.1 Flow Hi," Revision 7, and Offnormal Procedure OFN BB-005, "RCP
Malfunctions," Revision 2, and noted that there were no actions required for the
current plant conditions. When the flow reached 5.7 gpm, the procedures required
that the manufacturer be contacted. The procedures required that operators
immediately trip the reactor if the flow reached 6 gpm. Seal 1 is a controlled-
leakage film-riding seal with a normal controlled leakage of approximately 3 gpm.
The inspector observed the briefing for the oncoming crew on the evening of
March 22,1997. Relevant procedures and the activities that could affect seal
leakoff flow were discussed. The inspector determined that the briefing on the
concern was thorough and noted that activities that could affect sealleakoff flow
over the weekend were postponed when possible.
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The manufacturer reviewed the problem and suggested that the temperature of
coolant to the seals be lowered and that the seal filter be changed to a finer size
filter. The licensee replaced the 5 micron seal injection filter with a 2 micron filter.
Af ter the filter was installed, the sealleakoff flow decreased to approximately
3.2 gpm. In addition to this action, the licensee developed a procedure to lower the
volume control tank temperature two degrees. The manufacturer reviewed the
results of the actions taken and determined that the cause of the problem was
probably particulate deposition on the seal surface and that no further action was
required for the seal package.
c. Conclusions
The operators exhibited good attention to detail in identifying the small step change
in the seal flow. The inspector determined that the corrective actions taken by the
licensee were conservative and appropriate.
01.2 Component Coolina Water Surae Tank A Loss of Level
a. inspection Scone (71707)
On March 31,1997, at 9:37 p.m., operators in the control room noted that the
level was quickly decreasing in the Component Cooling Water Train A surge tank as
they transferred the nonsafety-related service loop from Train B to Train A. The
inspectors reviewed the licensee's actions associated with the decreasing surge
tank level indication and subsequent corrective actions.
b. Observations and Findinas ,
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The operators appropriately transferred the service loop back to Train B, entered
Procedure OFN EG-004, "CCW System Malfunctions," Revision 1, took Component ,
Cooling Water Train A out of service, placed the pumps in pull to lock, and entered l
Technical Specification 3.7.3. The change in level initiated an auto makeup and i
isolation of component cooling water to the postaccident sampling system and the
radwaste building. Operators toured the auxiliary building and found no component !
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cooling water leaks or damage. However, operators reported that the suction
pressure gage for Component Cooling Water Pump A was overranged high. An
operator unisolated the Surge Tank A sight glass and reported that the tank was 4
three-quarters full. Operators appropriately isolated makeup to the tank. Operators l
noted that Surge Tank A level indication started working again, the indicated level I
increased to 95 percent, and the level high alarm actuated.
The licensee performed surveillance tests on the instruments and gages involved in
the event and found that they were calibrated. The suction gages that were ;
overranged high were determined to be operable after the surveillance was i
satisfactorily performed. Engineering personnel performed an inventory balance and l
determined that approximately 2,000 gallons of water were transferred from the
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demineralized water tank to Surge Tank A. Instrumentation and controls personnel
replaced the level transmitter and flushed the sensing line. A small quantity of
sludge was flushed out of the lower instrument tap that connects to the transmitter
high pressure side. The licensee determined that this was the probable cause of the
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decrease in indicated level.
In addition to the above actions, instrumentation and controls personnel performed
a field walkdown, operations personnel verified that the system was vented, and
the licenseu verified that there were no similar events in industry.
c. Conclusions
Operator actions and the corrective actions taken in response to the failure of
Component Cooling Water Train A surge tank level indication were appropriate and
in accordance with procedures.
01.3 Ooerations Miscommunication with Maintenance Technicians
a. Inspection Scope (71707)
The inspector reviewed the circumstances surrounding the failure of a shift
supervisor to log entry into Technical Specification 3.6.3.
b. Observations and Findinas
On March 5,1997, the inspector noted that during Valve Operation Test and
Evaluation System testing on Valve EF-HV0034, the essential service water supply
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to Train B containment coolers inside containment isolation valve, the shift
supervisor did not log entry into Technical Specification 3.6.3. Upon questioning,
the shift supervisor acknowledged that this should have occurred, and made the
appropriate entries to correct the situation. The shift supervisor also directed
operators to make a similar entry into the equipment out-of-service log. Operations
personnel initiated Performance improvement Request 97-0716 which identified that
inadequate communication between the electrical maintenance technicians and the
shift supervisor resulted in the shift supervisor not recognizing that the maintenance
rendered the valve inoperable.
Administrative Procedure AP 21-001, " Operations Watchstanding Practices,"
Revision 4, Step 6.2.3.d, required the shift supervisor's log to contain log entries
for entry into Technical Specification action statements due to major equipment
being out of service for maintenance or due to equipment failure. NRC Inspection
- Report 50-482/97-04, Section 08.1, described a violation of this requirement. This
l issue is being considered an additional example of the previously cited violation
l (482/9704-01) because it occurred prior to the issuance of the previous Notice of
l Violation.
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c. Conclusions
The inspector identified an additional example of a violation cited in a previous
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report when the shift supervisor failed to recognize that maintenance on a
containment isolation valve would render the valve inoperable and require entry into
Technical Specification 3.6.3.
04 Operator Knowledge and Performance
04.1 Good Ooerator Recoanition of Liauid Radwaste Release USAR Reauirements
a. Insoection Scoce (71707)
The inspector reviewed the circumstances associated with an operator discovering
that an anticipated liquid radwaste release would not meet USAR release
requirements.
b. Observations and Findinas
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On February 24,1997, a chemistry technician brought Liquid Release
Permit 97-015 to the control room. An operator noted that the expected response
for process Radiation Monitor HB RE-018, liquid radwaste discharge monitor, was
higher than the calculated setting low alarm setting. Consequently, it was expected
that the low alarm would actuate during the release. The operator questioned
whether or not this was permitted by USAR Section 11.5.2.1.2, which described
two alarm setpoints to provide sequential alarms on increasing radioactivity levels.
The shift supervisor recognized the concern, withdrew the release authorization,
and informed the chemistry technician. The operator subsequently initiated
Performance Improvement Request 97-0558 to address this concern.
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On March 24,1997, a chemistry technician brought Liquid Release Permit 97-019
to the control room. While setting the alarms for process Radiation
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Monitor HB RE-018, liquid radwaste discharge monitor, the low alarm setpoint was
determined to be below the background level. Operators again recognized that this
release was not permitted by USAR Section 11.5.2.1.2, and the shift supervisor
again withdrew the release authorization. The shift supervisor also initiated
Performance improvement Request 97-0884.
The inspector discussed this issue with the chemistry manager who explained that
the chemistry department interpretation of USAR Section 11.5.2.1.2 had not been
consistent with the operations department interpretation. However, as a result of
Performance improvement Request 97-0884, the chemistry department changed its
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practice to prepare liquid release permits in the future that will be consistent with
USAR requirements.
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c. Conclusions
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The inspector concluded that the operators responded appropriately in recognizing
the concern wah performing a radwaste release in a manner inconsistent with the
USAR requirements.
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08 Miscellaneous Operations issues (92901) !
08.1 (Closed) Unresolved item (50-482/9617-02) Failure to Follow Procedures:
Performance improvement Request 96-0646 documented a procedure violation that [
occurred on February 27,1996. Radwaste operators had violated Systems :
Procedure SYS HB-135, " Liquid Radwaste Dcmin Floor Drain and Waste Holdup
Tanks Processing," Revision 0, and Alarm Response Procedure ALR 702, " Liquid .
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Process Control Panel HB-115," Revision'2, when they exceeded the 90 percent .
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level limit and continued to 95 i 97 percent levelin accordance with their
supervisor's instructions. Scause of plant conditions, radwaste operations was
taking advantage of any extra tank volume, due to the inability to discharge.
Procedure SYS HB-135, Step 4.12, states: "Do not exceed Waste Monitor Tank A
or B (THB07A or THB078) level of 90 percent to prevent an inadvertent overflow." :
Alarm Respont.e Procedure ALR 702 requires that liquid transfers to Waste Monitor l
Tank 1 (WMT B) be stopped if levei ir greater that 90 percent. Radwaste operators ;
violated these procedures when thw/ 'ollowed their superv:sor's instructions. The ;
supervisor did not follow plant adonnistrative procedures to obtain the proper l
authorization to exceed the tank filllimit. The failure to follow procedural guidance !
is identified as a violation of Technical Specification 6.8.1 (482/9708-01).
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11. Maintenance
M1 Conduct of Maintenance !
M 1.1 General Comments on Maintenance Activities
a. Insoection Scone (62707) ;
The inspectors observed all or portions of the following work activities. l
111643 Task 1 NG003D inspection, cleaning, and testing :
112834 Task 1 Roll pin missing in mechanical overspeed
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device Emergency Diesel Generator A governor
Troubleshoot discrepancy between local VAR
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117729 Task 1
meter on diesel and control room meter
118088 Task 1 Replace mechanical seals and bearings on
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PEG 01 A, Component Cooling Water Pump A
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119899 Task 2 Calibration of emergency fuel oil storage tank
Level A
b. Observations and Findinqs
Except as noted in Sections M1.3, M1.4, M1.5, M1.6, and M1.7, the inspectors
found no concerns with the maintenance observed. ;
c. Con _gl
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l Except as noted in Section M1.3, M1.4, M1.5, M1.6, and M1.7, the inspectors
i concluded that the maintenance activities were being performed as required.
l M 1.2 General Comments on Surveillance Activities
The inspectors observed all or portions of the follJwing surveillance activities.
l a. Inspection Scoce (61726)
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! STS BG-201, Revision 15 Chemical and volume control system
l inservice valve test
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l STS IC.912, Revision 18 Containment Hydrogen Analyzer
GS065A calibration test
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STS CR-001, Revision 34 Shift log for Modes 1,2, and 3
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b. Observations and Findinas
The inspectors fcund no concerns with the surveillances observed.
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c. Conclusions
The inspectors concluded that the surveillance activities were being performed as
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M1.3 Component Coolina Water Pumt A Bearina Replacement
a. Inspection Scope (62707)
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The inspector observed portions of the bearing replacement or. Component Cooling
Water Pump A and evaluated the effectiveness of the licensee's critique following
the maintenance.
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b. Observations and Findinos l
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On March 10,1997, operators removed Component Cooling Water Pump A from
service for planned maintenance which included replacing the bearings. The system j
engineer recommended replacing the pump bearings after noting and evaluating an I
increasing trend in the pump bearing vibration. Mechanical maintenance
technicians performed the maintenance smoothly, in accordance with the work
instructions, and completed the work without significant problems. The inspector
noted supervisory presence in the field during the work, and noted that the
maintenance planner properly incorporated vendor guidance using revisions to the
work instructions.
M 1.4 Emeraency Diesel Generator Outaae
a. Inspection Scope (62707)
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The inspectors reviewed the work in progress during a planned outage for
Emergency Diesel Generator Train A. The inspection included a review of the work I
packages being used and the actions taken in response to problems identified. ,
b. Observations and Findinas
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On March 16,1997, the inspector observed maintenance personnel identify and
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resolve two concerns while performing work on Emergency Diesel Generator
Train A. The technicians assigned to reinstall a roll pin on the mechanical portion of
the governor noted that the pin was not installed through the casing and bolt in
accordance with instructions in the package. The inspector reviewed the actions
taken in response to this observation. The planner contacted the manufacturer to
i address the problem. Operability of the governor was not affected because a lock
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nut was designed to hold the bolt in place. This nut was properly installed. The pin
v *as properly installed prior to the end of the diesel generator outage.
While performing maintenance on the Emergency Diesel Generator Train A motor
control center, an electrical technician noted that three of six stab connectors on
the ventilation supply fan breaker failed to make complete contact with the bus
, bars. The technician contacted the system engineer and maintenance supervision
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and informed them of the concern. The operability of the ventilation fan was not
affected because one set of three stabs, which were installed in parallel with the
three that were not in full contact, made full contact with the bus bar. The problem
was appropriately addressed and repaired prior to exiting the equipment outage.
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M 1.5 Critiaue on Comoonent Coolina Water and Emeraency Diesel Generator Eauipment
Outaaes
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a. Inspection Scope (62707)
On March 21,1997, the inspector observed the licensee critique of the work t.iat
occurred on safety-related equipment during a 2-weA period.
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b. Observations and Findinas ,
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The inspector noted that the critique was thorough and very self-critical. A
representative from each group that participated in the three different safety-related
equipment outages that occurred during the two previous weeks attendeu. Most of
the discussions dealt with improvements that could be made in timeliness and
scheduling. One of the more notable concerns addressed dealt with planning. For
example, a system engineer indicated that he provided complete detailed !
instructions to the planner for work to address a vibration problem on the l
component cooling water pump. These instructions were not used in developing
the work package. As a result, the pump outage was extended to completely
address the vibration concerns. The engineer developed Performance improvement
Request 97-867 to address the concerns with the planning for the component
cooling water work.
On March 27,1997, the planning supervisor criticized tr.e performance i
improvement request and stated that it failed to adequately explain the concern.
The inspector reviewed the performance improvement request and noted that it
addressed the generic concerns identified during the critique and provided the root
cause that was discussed at the time, a heavy work load in the planning
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department, but did not go into detail on each specific concern. The inspector
l discussed the performance improvement request with the supervisor the next day.
At that point. the supervisor was still not aware of the c.oncerns that the engineer
l had expressed during the critique. The inspector described the concerns that were
! discussed during the critique and expressed concern at the failure of the planning
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representative at the critique to inform planning management of the concerns that
were expressed at the meeting. The supervisor indicated that they were not aware
that the component cooling water work had been added to the critique and did not
have representation for that work item at the meeting. The inspector noted that the
electrical planner for the diesel generator breaker work was at the meeting and
j could have communicated the planning concerns to management. The supervisor
! agreed that this communication should have occurred.
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- M1.6 Undatina of Operational Rok Assessment
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On April 2,1997, when Comp 7nent Cooling Water Train A was declared operable,
the central work authority rescheduled many of the work tasks that had been
- deferred due to the emergent wo.k on Component Cooling Water Train A. While
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risk was considered during rescheduling, the risk assessment document maintained
in the control room was not updated to reflect the revised scheduling of the work.
Administrative Procedure AP 22C-003, " Operational Risk Assessment Program,"
Revision 1, Step 6.1.3, required that any activities added to or slipped from the
current weekly Revision 0 schedule be assessed and documented on the original
operational risk assessment. When the activities were slipped from the schedule on
March 31,1997, integrated plant scheduling personnel updated the operational risk
assessment to reflect slipping these activities from the schedule. However, on
April 2,1997, when these activities were added back into the schedule, the
operational risk assessment was not updated. This failure to comply with the
requirements of Procedure AP 22C-003 is a violation of 10 CFR 50, Appendix B,
Criterion V (482/9708-02).
M1.7 Conclosions on Conduct of Maintenance
The inspector considered the system engineer's initiative to recommend the bearing
replacement to be a strength in monitoring and addressing concerns with the
system's performance. An electrical technician exhibited good attention to detail in
noting inadequate surface contact on half the connections to the bus on a breaker.
Appropriate actions were taken by maintenance planning in addressing a missing roll
pin on the diesel generator mechanical governor. The inspector noted a weakness
l in communications within the planning department when concerns raised during a
! work critique meeting about planning were not relayed to planning management.
i The failure to apdate the operational risk assessment document maintained in the
l control room was identified as a violation.
M8 Miscellaneous Maintenance issues (92902)
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M8.1 (Closed) Licensee Event Reoort (LER) 50-482/96-008: Inoperability of Essential
Service Water Room Ventilation. This item involved the failure of operators and
instrumentation and control technicians to recognize the impact that a
nolsafety-related surveillance procedure had on the operability of the ventilation
sys!em for the Train A essential service water pump. The licensee determined that
the rod r";ue was an inadequate procedure and a contributing f actor was a
i weakness in the communication between the maintenance worker and the shift
supervisor. The licensee revised the inadequate procedure and the inspector
verified that the revision addressed the inadequacy. Additional corrective actions
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included reviewing allinstrumentation and controls nonsafety-related surveillance
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procedures for similar inadequacies, discussing the importance of clear
. communication and the impact of maintenance on the operability of equipment
during shop meetings, and the development of a checklist to ensure complete
communications between the shift supervisor or work control center and
maintenance personnel.
As discussed in Section 01.3, inadequate communication between electricians and
l operators prior to diagnostic testing on a containment isolation valve resulted in
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testing which rendered the valve inoperable.without the shift supervisor recognizing '
that it would. This additional example of a violation demonstrated that the ,
corrective actions for LER 50-482/96-008 were inadequate to prevent recurrence.
While reviewing the corrective actions described in the LER, the inspector found - r
three deficiencies. .Firsti the checklist to ensure complete communication between f
l the shift supervisor or work control center and maintenance personnel did not !
j directly question whether the proposed work affected the operability of I
l safety-related equipment. Second, the LER stated that this checklist would be j
l utilized until such time as WCNOC determined that the interim measure was no .
j longer of value. On March 31,1997, the inspector noted that the work control
center stopped using the checklist, although the operations manager believed that 1
the checklist was r;till being used. Third, the corrective actions associated with i
l reviewing procedures for inadequacy and the shop meeting discussions were not )
performed for the electrical or mechenical maintenance grcups.
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Since the corrective actions for this LER were inadequate to prevent recurrence of i
j this type of event, the violation reported in this LER did not meet the criteria in the l
l NRC Enforcement Policy to not cite the violation. The failure of the licensee to
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! perform Technical Specification Surveillance 4.8.1.1.1 within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> of the !
inoperability of Emergency Diesel Generator A is a violation of Technical i
Specification 3.8.1.1, Action b (482/9708 03). I
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Ill. Enaineerina
E1.1 Resoonse Time Discrecancy With Control Room Ventilation Radioactivity Monitors
a. Insoection Scoce (37551)
The inspector reviewed the licensee's response to identifying a discrepancy
between the USAR and the plant test practices.
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b. Observations and Findinas i
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USAR Table 7.3 7 stated that the response time of the control room ventilation
radioactivity Monitors GKRE04 and GKRE05 was less than 3 seconds. These
devices continuously monitored the supply of air of the normal heating, ventilation,
and air conditioning system for particulate, iodine, and gaseous radioactivity. Their
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purpose was to protect control room operators from high airborne radioactivity by
initiating a control room ventilation isolation when they detected activity above the i
setpoint described in the licensing basis.
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- The licensee was never able to show the response time of Monitors GKRE04 and l
j -05 to be less than 3 seconds. Further, the only respor'se time test performed on i
j the monitors was during preoperational testing. The response time reported for the
J. monitors was approximately 4 seconds.
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After identifying the concern, on February 21,1997, the licensee approved USAR
Change Request 97-0081 to remove USAR Table 7.3-7. After reviewing the
10 CFR 50.59 evaluation, the inspector noted that the argument used to justify
deleting USAR Table 7.3-7 was the same argument that could be used to justify the !
removal of Radiation Monitors GKRE04 and -05 from the facility. The licensee
emphasized that this was not the intent, and that they have no plans to remove the
monitors. The inspector noted that, if the time response were not important to
operator safety, the radiation level in the air intake to the control room could rise :
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above trip setpoint and yet not result in a control room ventilation isolation for a
very long time,
in addition, the licensee was not able to determine where the 3-second time
response USAR requirement came from and could not justify why the preoperational
testing was satisfactory without meeting this requirement.
The 10 CFR 50.59 evaluation noted that none of the accident analyses described in
the USAR took credit for the control room ventilation isolation signal from Radiation
- Monitors GKRE04 and -05. However, it was not clear from the USAR
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accident-analysis descriptions whether the control room ventilation was presumed
to be in a recirculation alignment or not. If a recirculation alignment was assumed,
it was not clear when this recirculation alignment was assumed to have occurred.
While the licensee asserted that those accidents which assumed a control room i
ventilation isolation would get the isolation signal from some source other than from i
Radiation Monitors GKRE04 and -05, the licensee offered no documentation to l
demonstrate this and it was not clearly stated in the USAR.
The inspector will continue to review this issue. Pending completion of this review
including an understanding of the basis of the licensee's assertions, this item will
remain an Unresolved. Item (482/9708-04).
c. Donclusions
The inspector identified an unresolved item during the review of a USAR change
which deleted time response requirements for control room ventilation radiation
monitors.
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! E8 Miscellaneous Engineering issues (92903)
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E8.1 (Closed) Unresolved item 50-482/9614-04: USAR Discrepancies. Two issues were
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identified in this item. The first dealt with the centrifugal charging pump discharge j
[ header flow control valve inlet isolation valves. The system drawing in the USAR l
i did not reflect the licensee's practice. The licensee plans to change the note on the
- drawing to allow the discharge header flow control valve inlet isolation valve on
{ either train to be locked closed, rather than limiting it to one. The drawing change
- package has been developed and is scheduled to be implemented the week of
- April 13,1997. !
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The second issue dealt with several inconsistencies between USAR Figure 6.2.4-1,
" Containment Penetrations," and the current plant design. The inspector reviewed
Performance Improvement Request 96-2216, USAR Change Request 97-089, and
the changes that are to be made to the USAR figure. The licensee completed a I
review of the figure and identified eight additional discrepancies. In all but one ;
case, the changes were completed prior to completion of plant construction and the I
architect engineer failed to update the USAR. In the remaining case, the licensee
changed the configuration and failed to update the USAR.
The inspector determined that the corrective actions taken or planned were
appropriate. The failure to maintain the USAR is a violation of 10 CFR 50.71(e)
(482/9708-05).
E8.2 (Closed) LER 50-482/96-006: Actuation of Engineered Safety Features Due to l
Failure of Steam Generator C Feedwater Regulating Valve. A 3/16-inch roll pin in l
the feedwater regulating valve (Valve AE FCV-530) failed resulting in the plug of the
valve separating from the valve stem. The plug dropped into the closed position,
stopping feedwater flow to Steam Generator C. The reactor tripped in response to l
low level in the steam generator. The design of the valve had been changed to
include a solid pin in lieu of the roll pin in 1988 in response to a similar event at
Callaway. However, when the design change was made, the licensee failed to
ensure that spare parts in the warehouse and future procurements were. modified to i
reflect the change. When the valve internals were replaced during March 1996, the l
parts contained the roll pin in lieu of the solid pin. The licensee identified the
inadequate design modification procedures as the root cause of the event. This !
same modification was made on the main feedwater regulating bypass vahres, but
spare parts were not addressed. The valve assemblies in two of four bypass valves
were replaced in May 1990, with assemblies that contained roll pins. 3
The immediate corrective actions taken were to replace the roll pins in three of the
four main feedwater regulating valves. The fourth valve still contained the solid pin
that was installed in 1988. The roll pins in the two main feedwater regulating
bypass valves are to be replaced with solid pins during the next outage. The
licensee placed a hold on all spare parts that contained roll pins. These parts were
to be returned to the vendor or modified prior to use. The inspector reviewed the
design and procurement procedures and material codes and noted that they were
revised to assure that spare parts and equipment are addressed in design
modifications and changes made in the plant The vendor manuals and drawings
were revised to reflect the changes made in the valves.
The licensee plans to perform assessments of four safety and four nonsafety-related
systems to determine whether design changes offectively addressed spare parts and
procurement and were correctly reflected in vendor manuals and drawings. Those
systems include: auxiliary feedwater, main feedwater, essential service water,
service water, component cooling water, main generator, residual heat removal, and
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main turbine systems. The auxiliary feedwater system functional assessment was
reviewed in NRC Report 50-482/97-05. l
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IV. Plant Support
R1 Radiological Protection and Chemistry Controls
R 1.1 Personnel Entrance into Hiah Radiation Area Without Reauired Dosimetry
a. Insoection Scone (71750)
On March 20,1997, an engineer and a quality control inspector entered the
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pipechase in the 1988 foot level of the auxiliary building, a high radiation area, I
without wearing the required thermoluminescent dosimeter. The inspector reviewed
the performance improvement request, radiation protection procedures, and the
corrective actions taken in response to the personnel failure.
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b. Observations and Findinas
Procedure AP 25A-001, " Radiation Protection Manual," Revision 2, Step 6.8.1, !
requires that individuals wear their issued radiation dosimetry devices in the l
radiation controlled area at all times. The individuals did not sign on to the radiation
work permit for the task they were to perform using the automated method because
they had not been added to the computer database yet. The individuals had been
authorized for the radiation work permit. The health physics technician assigned to ,
monitor the task identified that the individuals were not wearing their i
thermoluminescent dosimeters after they had been the area approximately I
10 minutes. The individuals were wearing alarming dosimeters, as required by the '
radiation work permit. These dosimeters indicated that the two individuals had
received 1 and 2 mrem of exposure.
The inspector reviewed the corrective actions taken or identified by the licensee. ,
The licensee initiated significant Performance Improvement Request 97-0844. The l
licensee indicated that the root cause of this event was personal error. The licensee
canceled the individuals' access to the radiation controlled area until the radiation
protection manager counseled the individuals. This licensee-identified and corrected
violation is being treated as a noncited violation, consistent with Section Vll.B.1 of
the NRC Enforcement Policy (482/9708-06).
c. Conclusions 1
A noncited violation resulted when two engineers failed to follow procedures by
entering the radiation controlled area without thermo!uminescent dosimetry. j
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R 1.2 Personnel Contamination Due To Check Source Leakaae
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a. Inspection Scone (71750)
- The inspector reviewed the licensee's response to check source leakage and a
i subsequent personnel contamination event.
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b. Observations and Findinas
On February 27,1997, a radiation protection technician discovered that the check
source in Area Radiation Monitor SD-RE-047, postaccident sampling system area
radiation monitor, separated Trom the swing arm due to adhesive degradation. Two
instrumentation and control technicians removed the detector electronics package
from the area radiation monitor for the postaccident sampling system in order to
take it to the instrumentation and control shop for calibration. During the survey to
permit a conditional release of the detector electronics package, the check source
fell to the floor, spilling Strontium-90. This led to the three technicians becoming
contaminated. Radiation protection technicians contained the spill, decontaminated
the in?trumentation and control technicians, and cleaned up the contamination.
Radiation protection personnel initiated Performance improvement Request 97-0640
to address the contamination.
The check source in this particular area radiation monitor had been held in place
only by an adhesive. Degradation of this adhesive resulted in the source separation
from the swing arm. Area Radiation Monitor SD-RE-047 is the only area radiation
monitor of this type installed at Wolf Creek. All other area radiation monitors use a
later model detector which utilizes a set screvv to affix the source to the swing arm.
While this issue has no generic applicability at Wolf Creek, the radiation protection
manager is evaluating whether generic industry notification would be appropriate.
The initial skin dose assessment calculation estimated the skin dose based on
Strontium activity alone and failed to consider dose from Yttrium. This calculation
was performed using the Varskin Mod 1 computer program by a technician who had
little experience performing skin dose assessments. The more experienced
technician who normally performed skin dose calculations was not available during
the initial assessment, but returned in time to identify the error upon review. After
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correcting the assessment, radiation protection personnel assigned a maximum skin
dose equivalent exposure for this event of 1.96 Rem to the finger of one technician,
well!ess than the 50 Rem limit of 10 CFR Part 20.
In response to the error in performing the skin dose assessment, the radiation
protection manager initiated Performance Improvement Request 97-1000 to address
programmatic enhancements to reduce the probability of future similar errors. The
radiation protection manager decided to shift to Varskin Mod 2, and initiated the
necessary programmatic changes. Completion of the transition is expected by
September 1,1997.
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c. Conclusions
The inspector concluded that the initial radiation protection technician response to
the spill was appropriate and effective in limiting the spread of contamination and
cleaning up the spill. While the initial dose assessment error initially underestimated
the skin dose, the licensee identified and corrected the error and initiated corrective
actions to address this error.
R5.1 Chemistry Trainina Error
a. Inspection Scope (71750)
The inspector reviewed the circumstances that resulted from improper analysis
results for reactor coolant system activity samples,
b. Observations and Findinas
On February 17,1997, and February 21,1997, a chemistry technician reported
reactor coolant system specific activity at 1.099 and 0.8018 micro-curies per cubic
centimeter. These analyses results were subsequently determined to be inaccurate
because the technician who performed the analyses placed the sample directly on
the detector rather than on the proper shelf corresponding with a calibrated
geometry within the detection chamber,
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The technician who performed these analyses recently transferred from radiation
protection to chemistry. During the training for this technician, chemistry personnel i
assumed that since radiation protection technicians also utilized this counter,
detailed training on sample placement would not be needed.
The chemistry supervisor initiated Performance improvement Request 97-0554 and
Reportability Evaluation Report 97-020. Reportability Evaluation Report 97-020 ;
concluded that this event was not reportable because the samples were actually j
taken and counted, and subsequent chemistry analysis was able to bound the
sample results for the incorrect geometry to demonstrated that the analysis results
were actually within Technical Specification requirements and consistent with
previous and subsequent activity analysis results.
The chemistry manager described planned corrective actions for Performance ;
improvement Request 97-0554, including specific on-the-job training requirements I
which will require technicians to demonstrate familiarity with the detector shelves
and the use of calibrated geometries in the analysis.
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c. Conclusions
, The inspector concluded that chemistry management responded appropriately by
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identifying and correcting this training deficiency.
, V. Manaaement Meetinas
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X1 Exit Meeting Summary
The inspectors presented the inspection results to members of licensee management at the
conclusion of the inspection on April 4,1997. The licensee acknowledged the findings
presented. .
The inspectors asked the licensee whether any materials examined during the inspection
should be considered proprietary. No proprietary information was identified.
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ATTACHMENT
SUPPLEMENTAL INFORM ATION
PARTIAL LIST OF PERSONS CONTACTED
Licensee
C. W. Fowler, Manager, integrated Planning and Scheduling
O. L. Maynard, President and Chief Executive Officer
B. T. McKinney, Plant Manager
R. Muench, Vice President Engineering
W. B. Norton, Manager, Performance Improvement and Assessment
R. L. Sims, Manager, System Engineering
C. C. Warren, Chief Operating Officer
INSPECTION PROCEDURES USED
IP 71707 Plant Operations
IP 37551 Onsite Engineering
IP 61726 Surveillance Observations
IP 62707 Maintenance Observations
IP 71750 Plant Support Activities
IP 92901 Followup - Plant Operations
IP 92902 Followup - Maintenance
IP 92903 Followup - Engineering
ITEMS OPENED, CLOSED, AND DISCUSSED
Onened
9708-01 VIO Failure to follow procedure-liquid transfers to waste monitor
(Section 08.1)
9708-02 VIO Failure to update operational risk assessment
(Section M1.6)
9708-03 VIO Failure to perform Technical Specification surveillance
when emergency diesel generator was inoperable
(Section M8.1)
9708-04 URI Response time discrepancy with control room ventilation
radioactivity monitors (Section E1.1)
9708-05 VIO USAR discrepancy (Section E8.1)
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Closed
50-482/96-006 LER Actuation of engineered safety features due to failure of
Steam Generator C Feedwater Regulating Valve
(Section E8.2)
50-482/96-008 LER Inoperability of essential service water room ventilation
(Section M8.1)
50-482/9614-04 URI USAR Discrepancies (Section E8.1)
50-482/9617-02 URI Failure to follow procedures (Section 06.1)
Opened and
Closed
9708-06 NCV Personnel Entrance into high radiation area without
' required dosimetry (Section R1.1)
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