ML20042A516

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LER 82-003/01T-0:on 820209,steam Generator Tube Leak of Approx 0.11 Gpm Was Indicated by Condensate Steam Air Ejector Offgas Radiation Monitor.Caused by Crack on Tube 74-2.Tube Stabilized & Plugged
ML20042A516
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 03/09/1982
From: Kutzer J
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20042A509 List:
References
LER-82-003-01T-01, LER-82-3-1T-1, NUDOCS 8203230515
Download: ML20042A516 (1)


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g gon February 9, 1982, a steam generator tube leak of approximately 0.11 GPM was ;

indicated by the Condensate Steam Air Ejector Of fgas Radiation Monitor. This

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