ML20038C897

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LER 81-022/01T-0:on 811113,six Variable Spring Hangers on Emergency Feedwater Discharge Found Not Carrying Specified Design Loads.Caused by High Temp Conditions During Loading. Hangers to Be Replaced & Insulated from High Temp Environ
ML20038C897
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 12/04/1981
From: Kutzer J
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20038C890 List:
References
LER-81-022-01T, LER-81-22-1T, NUDOCS 8112140239
Download: ML20038C897 (1)


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l3,2, fon November 13, 1981 it was deternuned that six installed variable spring ,

, ,, , hangers were not carrying specified design loads. These spring hangers are

.3 .. located on the emergency feedwater discharge, upper ring headers surrounding ,

,,,,, ,each steam generator, between the steam generator and the steam generator in-

,, ,, ,!sulation. Piping analysis has indicated that the piping stresses are adequatej

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,,,,,lThe apparent cause of this occ rence is setting of the spring coils under

i,ii iload due to high temperature conditions. The spring hangers will be replaced ,

, , , j on Oconee 1 and 2, and the insulation modified to exclude the hangers from the i..-1i high temperature environment. A survey to identify and correct this problem I t,! len other snrine hancers will be conducted. Oconee 3 is not affected. ,

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