ML18081B060

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Initial Deficiency Rept Re Potential Dropped Rod Events Leading to Calculated DNB Ratios Lower than Reported to NRC for Certain Westinghouse Plants.Util Is Investigating Condition for Applicability to Facility
ML18081B060
Person / Time
Site: Salem PSEG icon.png
Issue date: 12/03/1979
From: Martin T
Public Service Enterprise Group
To:
Shared Package
ML18081B057 List:
References
NUDOCS 8002190166
Download: ML18081B060 (1)


Text

. , ......

Thomas J. Martin Public Service Electric arid Gas Company 80 Park Place Newark, N.J. 07101 201 /430-8316 Vice President Engineering and Constru~ian*

  • December 3, 1979
  • Mr *. Boyce H. Gr.ier, Director U.S *. Nuclear Regulatory Commission Office of Inspection and Enforcement Region I
  • 631 Park Avenue . .

King of .Prussia, Pennsylvania 19406

Dear* Mr. Grier:

10CFR50.55(e) "SIGNIFICANT DEFICIENCY" DROPPED ROD EVENT ANALYSES NO. 2 UNIT SALEM GENERATING STATION PSE&G has been notified by Westinghouse. (letter of November 15,.

1979) *that they have identified the potential for certain

  • single dropped rod events leading to calculated DNB ratios lower*than reported to the NRC for certain classes of Westinghouse Plants. Therefore, the SAR analysis m~y not represent the most limiting assumption for credible single
  • failure.

It is our understanding that this condition was reported to your office by Westinghouse on November 15, 1979 under 10CFR50.59 for Salem No. 1 Unit and 10CFR50.55(e) for Salem

.*No.* 2* Unit.*

Please be advised that PSE&G is currently investigating this condition for applicability to the Salem facilities.

very tr.uly yours ,

CC M:t. L*. J. Norrholm NRC, Hancocks Bridge