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Category:DEFICIENCY REPORTS (PER 10CFR50.55E & PART 21)
MONTHYEARML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML17264A9381997-07-10010 July 1997 Deficiency Rept Re Potential Safety Hazard Associated w/FM-Alco 251 Engin,High Pressure Fuel tube-catalog: 4401031-2 in Which Dual Failure Mode Exists.Caused by Incorrect Forming Process ML18102A3701996-09-0606 September 1996 Part 21 Rept Re Installation of NUS Model OCA 801 Signal Isolator Modules & Model Mth 801 Signal Summator Modules. Replacement Modules Including Spares for Plant,Unit 2 Have Been Inspected by Vendor & Repaired ML18102A3381996-08-21021 August 1996 Part 21 Rept Re Chipping of Latching Mechanism Props Installed in GE 4 Kv magne-blast Circuit Breakers,Type AM-4.16-350-2H.Two Affected Breakers Have Been Returned to Vendor ML18102A5591996-08-0808 August 1996 Part 21 Rept Re Defect in NUS Model OCA801 Signal Isolator Modules.Replacement Modules Installed in Reactor Control & Protection Sys ML18101A8771995-08-0404 August 1995 Interim Part 21 Rept Re Potentially Reportable Deficiency in Edward Valve Model 838YT Check Valves Due to Disk Exhibiting Excessive Leakage.Disk from Original Valve Cleaned, Inspected & Installed in Replacement Valve ML18101A8611995-08-0101 August 1995 Interim Part 21 Rept Re Velan Valve Corp Check Valve Failure to Close.Insp of Internals Showed Moderate Wear in Gap Between Valve Disc & Hanger Arm.New Disc Installed & Valve Tested Satisfactorily ML18038A8971994-09-0707 September 1994 Part 21 Rept Re Defect in Latching Mechanism of Potter & Brumfield Relay on C&D High Voltage Shut Down Alarm Assembly Printed Circuit Boards.Pull Test on Relay Reset Button Incorporated Into Receiving Insp Procedures ML18100B2391994-07-27027 July 1994 Part 21 Rept Re Signal Summators PM-505B & 506B Found to Saturate High When Summators Lose Power & Reenergized. Summators Powered from Independent Vital Instrument Buses & Inverters.Design Changes Implemented ML18100B2271994-07-25025 July 1994 Part 21 Rept Re Cracking in Valve Stem & Plug Connection Pinning Collar Area on PORVs 1PR1 & 1PR2.Caused Attributed to Either IGSCC or Hydrogen Assisted Cracking.Porv Internals Replaced W/Internals Mfg from SS 316 Matl W/Plug Stellited ML18100B2101994-07-14014 July 1994 Deficiency Rept Re PORV Plug & Stem Material Defects. Initially Reported 940714.PORV Internals Were Replaced W/Plug Stellited ML18100B1911994-06-30030 June 1994 Initial Part 21 Rept Re Deficiency in Signal Summators PM-505B & PM-506B Supplied by Westinghouse.Design Changes Implemented & Operators Made Aware of Affects of Power Supply Transient on Summator Operability ML18100A7681993-12-13013 December 1993 Interim Part 21 Rept Re Discovery That Ge/Alco EDGs High Pressure Injection Tube Studs Did Not Meet Correct Matl non- Std & Not Correct Geometry.All Nonconforming Studs Identified & Replaced ML18096B2421993-02-0101 February 1993 Part 21 Rept Re Possible Matl Defect in Stainless Steel Swagelock Tube Fittings.Initially Reported on 921218.List of Part Numbers,Heat Codes & Addl Affected Customers Encl ML20126J5961992-12-31031 December 1992 Part 21 Rept Re Potential Loss of RHR Cooling During Nozzle Dam Removal.Nozzle Dams May Create Trapped Air Column Behind Cold Leg Nozzle Dam.Mod to Nozzle Dams Currently Underway. Ltrs to Affected Utils Encl ML20118B4391992-09-11011 September 1992 Part 21 Rept Re Degradation in Abb Type 27N Undervoltage Relays Used in Electrical Switchgear.Recommends That Users Review Applications Requiring Exposures Greater than 1E03 Rads TID W/Time Delay Function Option ML18095A4031990-08-0202 August 1990 Part 21 Rept Re MSIV Design Deficiency at Plant.Design Spec Provided by Westinghouse Did Not Specify Requirement to Provide Seal in Capability & Util Design Process Failed to Recognize Deficiency ML18095A2321990-05-24024 May 1990 Part 21 Rept Re Discrepancies Identified in ECCS Flow Orifice K Factors Supplied by Westinghouse.Initially Reported on 900518.Util Fabricated New Orifice Plates to Original Specs ML18095A2251990-05-22022 May 1990 Part 21 Rept Re Insufficient Welds on Pedestal Support Alignment Lug & Slide Shoe for 11,12,21 & 22 Charging/Safety Injection Pumps.Initially Reported on 900516.Windows Cut in Support Pedestals to Gain Access to Affected Areas ML18094B4461990-04-27027 April 1990 Part 21 Rept Re shaft-to-pinion Key Failures in Limitorque Actuators.Initially Reported on 900424.Caused by Reduction of cross-sectional Area & Ultimate Propagation of Cracks. Util Intends to Replace Keys in Actuators W/Keys of Steel ML18094A4421989-05-16016 May 1989 Part 21 Rept Re Defect in Solid State Protection Sys. During Mods in Solid State Protection Sys Cabinets,Noted That Two Wires Became Dislodged from Circuit Board.Visual Insp & Complete Pull Test Performed ML18093A8281988-05-0606 May 1988 Part 21 & Deficiency Rept Re Asea Brown Boveri,Power Distribution,Inc Low Voltage K-Line Circuit Breakers. Efforts Underway to Define Quantity & Type of Component Parts That May Need to Be Replaced ML20153G0111988-05-0606 May 1988 Part 21 Rept Re Potential Defect in Bussman Buss KTK-R Fuse Blocks W/Part Numbers 2078,2079 & 2080.Purchasing Records Reviewed to Identify If Any Parts Were Actually Used or Shipped to Customers.Results Listed ML18093A4721987-10-23023 October 1987 Part 21 Rept Re Calibr Gas Leakage Problem in Exo-Sensors, Inc Containment Hydrogen Analyzer Sys.Caused by Design Deficiency Associated W/Calibr Gas Subassembly.Monitoring Program to Be Maintained for Period After Sys Mods ML20215G2441987-06-16016 June 1987 Part 21 Rept Re Failure of Load Sequencing Equipment Supplied in Aug 1977 During Scheduled Testing.Caused by Open Electrical Connection on One Crimp Lug.Since 1978,insulated Lugs Used on All Equipment FVY-86-105, Part 21 Rept Re Design Defect Relating to Limitorque Motor Operators Mfg Prior to 1975.Mfg Contacted & Retrofit Kits Installed on safety-related & nonsafety-related Operators. Addl Info Encl1986-11-10010 November 1986 Part 21 Rept Re Design Defect Relating to Limitorque Motor Operators Mfg Prior to 1975.Mfg Contacted & Retrofit Kits Installed on safety-related & nonsafety-related Operators. Addl Info Encl ML20215G5351986-10-10010 October 1986 Part 21 Rept Re Vendor Tests of air-operated Diaphragm Valves Revealing Natural Frequencies Less than Required Values of 33 Hz.Initially Reported on 841227.No Adverse Effects Noted During Testing ML20215G6801986-10-10010 October 1986 Part 21 Rept Re Vendor Tests of air-operated Diaphragm Valves Revealing Natural Frequencies Less than Required Values of 33 Hz.Initially Reported on 841227.No Adverse Effects Noted During Testing ML20206S0841986-06-30030 June 1986 Part 21 Rept Re Possible Cut Wires in Wire Harness of Bbc Brown Boveri K600/K800 Circuit Breakers.Initially Reported on 860509.Safety Implications Listed.Gear Guard Designed to Prevent Cut Wires ML20140J4261986-03-31031 March 1986 Part 21 Rept Re Nuclear Valves Shipped to Pse&G.Internal Parts Lapped Which Could Reduce or Eliminate Nickel Plating Resulting in Seat Leakage & Shifting Problems ML20210G9921985-08-13013 August 1985 Part 21 Rept Re Failure of Isolated Worm Shaft Gear When Certain Critical Speeds Combined W/Repetitive Transfer of Actuator Clutch Mechanism from Manual (Handwheel) to Motor Drive Mode.Two Possible Solutions Noted ML20116E8481985-04-23023 April 1985 Part 21 Rept Forwarding Rev 1 to Insp Procedure for Investigating Emergency Diesel Generators for Fractured Welds on Air Deflectors.Rev Will Be Forwarded to Each Facility ML20092D9711984-06-15015 June 1984 Part 21 Rept Re Thermal Nonrepeatability & Other Calibr Errors in Barton Lot 1 Transmitters.Initially Reported on 840615.Transmitter Defects Identified & Expected Error Deviations Calculated.Utils Notified ML20082F3621983-11-17017 November 1983 Part 21 Rept Responding to IE Bulletin 83-06, Nonconforming Matls Supplied by Tube-Line Corp. List of Matls & Sys in Which Installed Encl ML18082A1421980-02-15015 February 1980 Final Deficiency Rept:Check Valve 2DR-7 Failed to Meet Applicable Seismic Class I Loading.Caused by Design Defect. Addl Support Will Be Completed by 800228 ML18081B0481979-12-21021 December 1979 Final Deficiency Rept Re Undetectable Failure in Engineered Safety Features Actuation Sys.Testing Procedures Revised to Include Testing of Permissive Circuitry P4 on Periodic Basis.Unit Will Be Tested Prior to Operation ML18081B0601979-12-0303 December 1979 Initial Deficiency Rept Re Potential Dropped Rod Events Leading to Calculated DNB Ratios Lower than Reported to NRC for Certain Westinghouse Plants.Util Is Investigating Condition for Applicability to Facility ML18081A3751979-10-0505 October 1979 Significant Deficiency Rept Re Containment Purge & pressure- Vacuum Relief Valves.Actuator Torque Values Were Insufficient to Move Valves from Open to Closed Positions W/ Design Differential Pressure of 60 Psi.Design Reviewed ML18081A3781979-10-0505 October 1979 Significant Deficiency Rept 79-06 Re Steam Generator Water Level Instrumentation.Pipe Breaks in Containment Could Lead to Elevated Temp Readings Which Could Result in Delayed Protection Sys Actuation.Setpoints to Be Changed ML18081A7551979-10-0404 October 1979 Interim Deficiency Rept Re Max Flow of RHR Pump During post- LOCA Mode.Caused by Low Sys Resistance to Pump Runout Conditions.Sys Resistance Increased by Placement of Resized Orifices ML18079A9521978-10-28028 October 1978 Deficiency Rept:On 780928,during Routine Design Review, Undersizing of Refueling Water Storage Tank Was Discovered. Tank Storage Capacity Has Been Increased.Design Drawings for Tank Piping & Foundation Will Be Modified ML20086C0041976-07-0101 July 1976 Interim Deficiency Rept Re Fan Coil Unit Motor 15 Failure to Meet Test Requirements.Initially Reported on 760611.Fan Coil Unit Motor from Unit 1 Installed in Place of Motor 15.Faulty Motor Returned to Westinghouse for Repair ML20086C0201976-06-17017 June 1976 Interim Deficiency Rept Re Polar Gantry Crane Gear Misalignment.Initially Reported on 760611.Caused by Misalignment of Hoist Drum Gear & Pinion.Drum Assembly Realigned & Secured & Dressing Gears Initiated ML20086C0301976-06-10010 June 1976 Final Deficiency Rept Re Pressurizer Snubber Malfunction. Initially Reported on 760402.Caused by Heavy Corrosion Buildup.Nine Units Replaced W/Pacific Scientific Units & 54 Units Replaced W/Combination of Redesigned Units ML20086C0421976-06-0202 June 1976 Interim Deficiency Rept Re Automatic Transfer of 4-kV Outside Feed.Initially Reported on 760512.Caused by Design Error.Circuitry for Automatic Bus Transfer Redesigned to Eliminate Possibility of Transfer ML20086C0741976-05-28028 May 1976 Suppl to Deficiency Rept Re Steam Generator Head Cladding Indications.Initially Reported on 760408.Cause Still Under Investigation.Ultrasonic Exam Conducted 1999-06-01
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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IPOWER REACTOR II EVENT NUMBER: 2 7 53 2 II FACILITY: SALEM REGION: 1 NOTIFICATION DATE: 07/14/94 UNIT: [l] [ ] [ ] STATE: NJ NOTIFICATION TIME: 15:56 [ET]
RX TYPE: [1] W-4-LP I [2] W-4-LP EVENT DATE: 07/14/94 EVENT TIME: OO:OO[EDT]
NRC NOTIFIED BY: F. x. THOMSON LAST UPDATE DATE: 07/14/94 HQ OPS OFFICER: THOMAS ANDREWS NOTIFICATIONS EMERGENCY CLASS: NOT APPLICABLE 10 CFR SECTION:
cccc 21. 21 UNSPECIFIED PARAGRAPH UNIT SCRAM CODE I Rx CRITIINIT PWRI INIT RX MODE CURR PWRI CURR RX MODE 1 N y 100 POWER OPERATION 100 POWER OPERATION EVENT TEXT
- - - PORV PLUG AND STEM MATERIAL DEFECTS AT SALEM UNIT 1 - - -
THE FOLLOWING IS A
SUMMARY
OF THE RESULTS OF PSE&G'S EVALUATION IN ACCORDANCE WITH 10CFR21 CONCERNING A DEFICIENCY DUE TO THE CRACKING IDENTIFIED IN THE VALVE STEM AND PLUG CONNECTION PINNING COLLAR AREA ON UNIT 1 PORVS lPRl & 1PR2. THE CAUSE OF THIS CRACKING HAS BEEN ATTRIBUTED TO EITHER INTERGRANULAR STRESS CORROSION CRACKING (IGSCC) OR HYDROGEN ASSISTED CRACKING. THE CRACKING IN THE PINNING COLLAR AREA COULD CONTINUE TO PROPAGATE EVENTUALLY RESULTING IN THE PLUG SEPARATING FROM THE STEM RENDERING THE PORVS INOPERABLE. THE UNIT 2 PORVS CURRENTLY ARE PROVIDED WITH INTERNALS MANUFACTURED FROM 17-4 PH MATERIAL, AND THEREFORE UNIT 2 IS NOT WITHIN THE SCOPE OF THIS 10CFR21 EVALUATION.
THE REACTOR TRIP AND INADVERTENT SI INITIATION THAT OCCURRED ON APRIL 7, 1994 AT SALEM UNIT 1 RESULTED IN THE TWO (2) PRESSURIZER POWER OPERATED RELIEF VALVES (PORV) TO CYCLE MULTIPLE TIMES DURING THE EVENT. SUBSEQUENT INSPECTION OF THE VALVE INTERNALS (PLUG, STEM, AND CAGE) REVEALED CRACKS IN THE PINNING COLLARS OF EACH OF THE TWO PLUGS, AND SIGNIFICANT UNEXPECTED WEAR AND GALLING ON THE 1PR2 STEM AND PLUG. FOLLOWING IDENTIFICATION OF THE CRACKING, THE 10CFR21 EVALUATION PROCESS WAS INITIATED ON MAY 9, 1994.
INSPECTION OF SPARE VALVE INTERNALS LOCATED IN THE WAREHOUSE ALSO REVEALED CRACKS IN THE PINNING COLLAR. THE THREE SETS OF VALVE INTERNALS WERE EXAMINED BY WESTINGHOUSE TO DETERMINE THE CAUSE OF THE CRACKING. THE SUBSEQUENT INVESTIGATION AND EXAMINATIONS REVEALED THAT THE CRACKS ORIGINATED AND GREW PRIMARILY AS A RESULT OF EITHER INTERGRANULAR STRESS CORROSION CRACKING OR HYDROGEN ASSISTED CRACKING. IT IS NOTED THAT A FOURTH SET OF INTERNALS THAT HAD BEEN INSTALLED IN THE PLANT FOR 1 WEEK ALSO REVEALED CRACKING.
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9407210139 940714 PDR ADOCK 05000272 1I S PDR
FACILITY: SALEM PAGE # 2 OF EVENT NUMBER: 27532 THE CAUSE OF THE STRESS CORROSION CRACKING WAS ATTRIBUTED TO THE FOLLOWING FACTORS. THE PLUG WAS MANUFACTURED FROM TYPE 420 STAINLESS STEEL AND SUBJECTED TO A 975 [DEGREE] F TEMPERING HEAT TREATMENT. THIS CAUSED THE MATERIAL TO BECOME SENSITIZED REDUCING ITS CORROSION RESISTANCE, AND CAUSED THE MATERIAL TO BECOME LESS DUCTILE REDUCING ITS FRACTURE TOUGHNESS. A TAPERED FIT BETWEEN THE STEM AND THE PLUG CAUSED HOOP STRESSES TO BE EXERTED ON THE PLUG AT THE PINNING COLLAR. THE COMBINATION OF THE MATERIAL CONDITION AND THE HOOP STRESSES WERE SUCH THAT STRESS CORROSION CRACKING OCCURRED IN A RELATIVELY SHORT PERIOD OF TIME, ESPECIALLY FOR THE SPARE VALVE INTERNALS WHICH HAD NOT SEEN ACTUAL SERVICE BUT ONLY LEAK TESTING AND ENVIRONMENTAL HUMIDITY WHILE IN STORAGE. THE INVESTIGATION WAS UNABLE TO DETERMINE IF THE CRACKING WOULD HAVE ARRESTED ITSELF AFTER SOME PERIOD OF OPERATION OR CONTINUED TO PROPAGATE.
THE PORVS AT SALEM ARE 2" AIR OPERATED-SPRING RETURN VALVES SUPPLIED BY THE COPES VULCAN, INC. THE VALVES HAVE A WORKING PRESSURE RATING OF 2485 PSIG AT 680 [DEGREES] F PER ANSI B16.5 FOR 1500 LB. RATING. THE NORMAL OPERATING PRESSURE FOR THE PORVS IS 2235 PSIG AT 650 [DEGREES] F. THE PORVS ARE SET TO OPEN AT A PRESSURE OF 2335 PSIG AND CLOSE AT 2315 PSIG ..
THE VALVE INTERNALS ARE COMPRISED OF THE PLUG, STEM AND CAGE. THE CAGE IS A HOLLOW CYLINDER SURROUNDING THE. PLUG, AND IS PROVIDED WITH A NUMBER OF FLOW PORTS WHICH EVENLY DISTRIBUTE FLOW THROUGH THE VALVE. THE PLUG/STEM ASSEMBLY MOVES WITHIN THE CAGE CYLINDER IN RESPONSE TO OPEN OR CLOSE CONTROL SIGNALS TO THE ACTUATOR EITHER OPENING OR THE CAGE FLOW PORTS. THE PLUG IS JOINED AND SECURED TO THE STEM THROUGH A CONICAL THREADED CONJUNCTION. AT THE TOP OF THE PLUG IS AN INTEGRAL PINNING COLLAR.
FOLLOWING ASSEMBLY OF THE PLUG/ STEM A PINNING HOLE IS DRILLED THROUGH THE PLUG COLLAR AND STEM AND A ROLL PIN IS INSERTED. IN MOST CASES, THE PINNING HOLE IS DRILLED PRIOR TO HEAT TREATMENT. IT IS AT THE PINNING COLLAR LOCATION WHERE STRESS 'CORROSION CRACKING OCCURRED. SINCE BOTH OF THE PORV PLUGS INSTALLED AT UNIT 1 (AS WELL AS THE THIRD AND FOURTH PLUG ASSEMBLIES UTILIZED AS SPARES) WERE CONSTRUCTED USING THE SS 420 MATERIAL, A COMMON MODE TYPE FAILURE DUE TO THE PLUG CRACKS IDENTIFIED MAY HAVE AFFECTED BOTH PORVS. IT IS BELIEVED THAT SHOULD THE CRACKS HAVE CONTINUED TO PROPAGATE THROUGH THE PLUG, BOTH PORVS COULD HAVE BEEN RENDERED INOPERABLE IN EITHER THE OPEN OR CLOSED POSITION.
DURING DESIGN BASIS TRANSIENTS, THE PORVS ARE UTILIZED TO PREVENT CHALLENGES TO THE PRESSURIZER SAFETY VALVES AND PROVIDE RCS OVERPRESSURE PROTECTION. THE PORV(S) ARE ASSUMED TO BE AVAILABLE OR MADE AVAILABLE IN THE EVENT OF (A) THE INADVERTENT SAFETY INJECTION (SI) AT POWER TRANSIENT AND (B) THE LOW TEMPERATURE OVERPRESSURE PROTECTION (LTOP) TRANSIENT DURING SHUTDOWN. WITH THE EXCEPTION OF THESE TWO TRANSIENTS, THE PRESSURIZER SAFETY VALVES WOULD BE AVAILABLE TO PROVIDE RCS OVERPRESSURE PROTECTION SHOULD THE PORVS FAIL. SHOULD THE PORVS OPEN AND FAIL TO CLOSE, THE FAILED PORVS WOULD BE MANUALLY ISOLATED BY THE PORV BLOCK VALVES TO PREVENT A LOSS OF REACTOR COOLANT.
THE INADVERTENT SI AT POWER TRANSIENT [(A) ABOVE] CREDITS THE AVAILABILITY OF THE PORVS SHOULD THE PRESSURIZER BECOME WATER SOLID TO PROVIDE RCS OVERPRESSURE PROTECTION. SINCE THE PRESSURIZER SAFETY VALVES ARE NOT DESIGNED TO RELIEVE WATER UNDER SATURATED CONDITIONS, AND COULD POTENTIALLY FAIL IN THE OPEN POSITION IF THE PORVS ARE UNAVAILABLE DURING THIS (Continued on next page)
- I FACILITY: SALEM PAGE # 3 OF EVENT NUMBER: 27532 TRANSIENT, THE TRANSIENT COULD DEGRADE FROM A CONDITION 2 EVENT TO A CONDITION 3 EVENT. HOWEVER, EVEN IN THE EVENT OF A PRESSURIZER SAFETY FAILING IN THE OPEN POSITION, THE CONSEQUENCES OF THIS ACCIDENT WOULD STILL BE BOUNDED BY THE SMALL BREAK LOCAL ANALYSIS RESULTS. SHOULD THE PORVS FAIL IN THE OPEN POSITION, PORV BLOCK VALVES CAN BE CLOSED TO ISOLATE THE RCS AND PREVENT COOLANT LOSS.
DURING (B) ABOVE, THE PORVS LIFT SETTING IS ADJUSTED TO A SETPOINT EQUAL TO OR LESS THAN 375 PSIG WHEN THE RCS COLD LEG TEMPERATURES ARE LESS THAN 312
[DEGREES] F DURING MODE 4 AND MODE 5 TO PROVIDE LOW TEMPERATURE OVERPRESSURE PROTECTION. THE SETPOINT FOR THE PORVS HAS BEEN DEVELOPED SUCH THAT IN THE EVENT OF A MASS INPUT TRANSIENT (I.E., THE START OF A SI PUMP) OR A HEAT INPUT TRANSIENT (I.E., THE START OF AN IDLE RCP) WITH THE RCS WATER SOLID, THE PRESSURE-TEMPERATURE (P-T) LIMITS CALCULATED IN ACCORDANCE WITH 10CFR50, APPENDIX G AND CONTAINED IN TECHNICAL SPECIFICATION 3.4.9.1 WOULD NOT BE EXCEEDED. A MINIMUM OF ON PORV SHOULD BE AVAILABLE TO MITIGATE THESE TYPES OF OVERPRESSURE TRANSIENTS AND MAINTAIN RCS PRESSURE WITHIN P-T LIMITS. THEREFORE, THE FAILURE OF THE PORVS TO OPEN DUE TO THE STRESS .CORROSION CRACKING IDENTIFIED COULD RESULT IN EXCEEDING THE P-T LIMITS. IT IS BASED ON THIS FUNCTION OF THE PORVS THAT PSE&G HAS CONCLUDED THAT THIS DEFICIENCY COULD RESULT IN A SUBSTANTIAL SAFETY HAZARD, AND IS THEREFORE REPORTABLE IN ACCORDANCE WITH 10CFR21.
PRIOR TO RESTART FOLLOWING THE APRIL 7 EVENT, THE UNIT 1 PORV INTERNALS (PLUG AND STEM) WERE REPLACED WITH INTERNALS MANUFACTURED FROM SS 316 MATERIAL WITH THE PLUG STELLITED. THE REPLACEMENT CAGES WERE MANUFACTURED FROM 17-4 PH STAINLESS STEEL.
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..B);:
~ i 1
INITIAL 10CFR21 Nq IFICATION PORV PLUG AND STEM MATERIAL P.UBLIC SERVICE ELECTR.C AND GAS CO.
SALEM GENERATING STATi ON UNIT 1 I
- I The following is a summary of the re'ults of PSE&G 1 S evaluation in accordance with 10CFR21 concernin' a deficiency due to the cracking identified in the valve ste'. and plug connection pinning collar area on Unit 1 PORVs lPRl & i* *R2. The cause of this cracking has been attributed to eith*r Intergranular Stress Corrosion Cracking (IGSCC) or hydrog.n assisted cracking. The cracking in the pinning collar area ::ould continue to propagate eventually resulting in the plug sep'rating from the stem rendering the PORVs inoperable. The~ \unit 2 PORVs currently are provided with internals manufactured: :from 17-4 PH material, and therefore Unit 2 is not within the s: 'ope of this 10CFR21 evaluation. ::
- i The reactor trip and inadvertent SI ~
- nitiation that occurred on April 7, 199,4 at Salem Unit 1 result: :a in the two (2) pressurizer Power Operated Relief Valves (PORV) : :*o cycle multiple times during the event. Subsequent inspec.. ion of the valve internals (plug, stem and cage) revealed crack: in the pinning collars of each of the two plugs, and significa. ,t unexpected wear and galling on the 1PR2 seem and plug. '.allowing identification of the cracking, the 10CFR.21 evaluation\ \process was initiated on May 9, 1994. Inspection of spare valve nternals located in the 1
warehouse also revealed cracks in th: : pinning collar. The three sets of valve internals were examine . by Westinghouse to determine the cause of t.he cracking.!; The subsequent investigation and examinations revea *ed that the cracks originated and grew primarily as a r *sult of either intergranular stress corrosion cracking or hydroge '. assisted cracking. It is noted that a fourth set of internals! '.that had been installed in the plant for 1 week also revealed c *acking.
I!
I' The cause of the stress corrosion er :eking was attributed to the following factors. The plug was man :factured from type 420 stai11less t;teel and subjected to a 9 ;s°F tempering heat treatment. This caused the material I *to become sensitized reducing its corrosion resistance, a~'.~ caused the material to become less ductile reducing its fra;ture toughness. A tapered fit between the stem and the plug ca :sed hoop stresses to be exerted on the plug at the pinning c~'.llar. The combination of the material condition and the hoop 'tresses were such that stress corrosion cracking occurred i,; a relatively short period of time, especially for the spare va.ve internals which had not seen actual se:r.-vice but only leak te, !ting and environmental humidity while in storage. The inve tigation was unable to determine if the cracking would havei~rrest.ed itself after some period of operation or continued to ~opagate.
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"SENT B~: 15: 15 PSE&G LI C &10 301 8165151;# 3/ 4 The PORVs at Salem are 2* air operat1d-spring return valves supplied by Copes Vulcan, Inc .. Tlle!valves have a working pressure rating of 2485 psig at 680° '. per ANSI B16.5 for 1500 lb.
rating. The normal operating pressu'.e for the PORVs is 2235 psig at 650°F. The PORVs are set to open* :at a pressure of 2335 psig and close at 23lS psig. The valve '.nternals are comprised of the plug, stem and cage. The cage i
- a hollow cylinder surrounding the plug, and is provide with a number of flow ports which evenly distribute flow throughithe valve. The plug/stem assembly moves within the cage cylin.er in response to open or close control signals to the actuate: either opening or closing the cage flow ports. The plug is jo$ned and secured to the stem through a conical threaded connectio~. At the top of the plug is an integral pinning collar. Followi g assembly of the plug/stem, a pinning hole is drilled through th ' plug collar and stem and a roll pin is inserted. In most cases !' the pinning hole is drilled prior to heat treatment. It is at t :e pinning collar location where stress corrosion cracking occu red. Since both of the PORV plugs installed at Unit 1 (as well a
- the third and fourth plug assemblies utilized as spares) were .onstructed using the SS 420 material, a common mode type failurel\due to the plug cracks identified may have affected both PO~Vs. It is believed that should the cracks have continued to ~ropagate through the plugl both PORVs could have been rendered ~'.noperable in either the open or closed position. i During design basis transients, the .ORVs are utilized to prevent challenges to the pressurizer safety !valves and provide RCS overpressure protection. The PORV (s}I are assumed to be available or made available in the event of (a)lj the Inadvertent Safe~y Injection (SI) at Power transient and; (b} the Low Temperature Overpressure Protection (LTOP) traris~ent during shutdown. With the exception of these two transient :, the pressurizer safety valves would be available to provide ~CS overpressure protection should the PORVs fail. Should the P ~Vs open and fail to close, the failed PORVs would be manually i '.olated by the PORV Block Valves to prevent a loss of reactor '.oolant.
I The Inadvertent SI at Power t:ransien 1 [(a) above] credits the availability of the PORVs should the pressurizer become water solid to provide RCS overpressure pr :tection. Since the pressurizer safety valves are not de !igned to relieve water under saturated conditions, and could pate !tially fail in the open position if the PORVs are unavailabl : during this transient, the transient could degrade from a Condi lion 2 event to a Condi ti on 3 event. However, even in the event o ! a pressurizer safety failing in the open position, the co.~equences of this accident would still be bounded by the Small ~eak LOCA analysis results.
Should the PORVs fail in the open po !ition, PORV Block Valves can be closed to isolate the RCS and pre ~nt coolant loss.
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During (b) above, the PORVs lift set~ing is adjusted to a setpoint equal to or less than 375 p~ig when the RCS cold leg ternp7ratures are less than 312°F during Mode.4 and Mode 5 t~
provide Low Temperature Overpressure~*Protection. The setpoint
- for the PORVs has been developed sue : that in the event of a mass input transient (i.e., the inadverte ,"t start of a SI pump} or a heat input transient (i.e., the star~ of an idle RCP) with the RCS water solid, the Pressure-Temperature {P-T) limits calculated in accordance with 10CFRSD, Appendix ;*G and contained in Technical Specification 3.4.9.1 would not be ~ceeded. A minimum of one PORV should be available to mitigate!these types of overpressure transients and maintain RCS pressure ;.within P-T limits.
Therefore, the failure of the PORVs ~o open due to the stress corrosion cracking identified could result in exceeding the P-T limits. It is based on this function of the PORVs that PSE&G has concluded that this deficiency could :.result in a substantial safety hazard, and is therefore repo:ri."table in accordance with 10CFR2l.
Prior to restart following the April'7 event, the Unit l PORV internals {plug and stem) were replaeed with internals manufactured from SS 316 material with the plug stellited. The replacement cages were manufactured from 17-4 PH stainless steel.
Should you have any questions regarding this notification, please contact Mr. David Smith at (609) 339.1'1202.
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