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Category:DEFICIENCY REPORTS (PER 10CFR50.55E & PART 21)
MONTHYEARML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML17264A9381997-07-10010 July 1997 Deficiency Rept Re Potential Safety Hazard Associated w/FM-Alco 251 Engin,High Pressure Fuel tube-catalog: 4401031-2 in Which Dual Failure Mode Exists.Caused by Incorrect Forming Process ML18102A3701996-09-0606 September 1996 Part 21 Rept Re Installation of NUS Model OCA 801 Signal Isolator Modules & Model Mth 801 Signal Summator Modules. Replacement Modules Including Spares for Plant,Unit 2 Have Been Inspected by Vendor & Repaired ML18102A3381996-08-21021 August 1996 Part 21 Rept Re Chipping of Latching Mechanism Props Installed in GE 4 Kv magne-blast Circuit Breakers,Type AM-4.16-350-2H.Two Affected Breakers Have Been Returned to Vendor ML18102A5591996-08-0808 August 1996 Part 21 Rept Re Defect in NUS Model OCA801 Signal Isolator Modules.Replacement Modules Installed in Reactor Control & Protection Sys ML18101A8771995-08-0404 August 1995 Interim Part 21 Rept Re Potentially Reportable Deficiency in Edward Valve Model 838YT Check Valves Due to Disk Exhibiting Excessive Leakage.Disk from Original Valve Cleaned, Inspected & Installed in Replacement Valve ML18101A8611995-08-0101 August 1995 Interim Part 21 Rept Re Velan Valve Corp Check Valve Failure to Close.Insp of Internals Showed Moderate Wear in Gap Between Valve Disc & Hanger Arm.New Disc Installed & Valve Tested Satisfactorily ML18038A8971994-09-0707 September 1994 Part 21 Rept Re Defect in Latching Mechanism of Potter & Brumfield Relay on C&D High Voltage Shut Down Alarm Assembly Printed Circuit Boards.Pull Test on Relay Reset Button Incorporated Into Receiving Insp Procedures ML18100B2391994-07-27027 July 1994 Part 21 Rept Re Signal Summators PM-505B & 506B Found to Saturate High When Summators Lose Power & Reenergized. Summators Powered from Independent Vital Instrument Buses & Inverters.Design Changes Implemented ML18100B2271994-07-25025 July 1994 Part 21 Rept Re Cracking in Valve Stem & Plug Connection Pinning Collar Area on PORVs 1PR1 & 1PR2.Caused Attributed to Either IGSCC or Hydrogen Assisted Cracking.Porv Internals Replaced W/Internals Mfg from SS 316 Matl W/Plug Stellited ML18100B2101994-07-14014 July 1994 Deficiency Rept Re PORV Plug & Stem Material Defects. Initially Reported 940714.PORV Internals Were Replaced W/Plug Stellited ML18100B1911994-06-30030 June 1994 Initial Part 21 Rept Re Deficiency in Signal Summators PM-505B & PM-506B Supplied by Westinghouse.Design Changes Implemented & Operators Made Aware of Affects of Power Supply Transient on Summator Operability ML18100A7681993-12-13013 December 1993 Interim Part 21 Rept Re Discovery That Ge/Alco EDGs High Pressure Injection Tube Studs Did Not Meet Correct Matl non- Std & Not Correct Geometry.All Nonconforming Studs Identified & Replaced ML18096B2421993-02-0101 February 1993 Part 21 Rept Re Possible Matl Defect in Stainless Steel Swagelock Tube Fittings.Initially Reported on 921218.List of Part Numbers,Heat Codes & Addl Affected Customers Encl ML20126J5961992-12-31031 December 1992 Part 21 Rept Re Potential Loss of RHR Cooling During Nozzle Dam Removal.Nozzle Dams May Create Trapped Air Column Behind Cold Leg Nozzle Dam.Mod to Nozzle Dams Currently Underway. Ltrs to Affected Utils Encl ML20118B4391992-09-11011 September 1992 Part 21 Rept Re Degradation in Abb Type 27N Undervoltage Relays Used in Electrical Switchgear.Recommends That Users Review Applications Requiring Exposures Greater than 1E03 Rads TID W/Time Delay Function Option ML18095A4031990-08-0202 August 1990 Part 21 Rept Re MSIV Design Deficiency at Plant.Design Spec Provided by Westinghouse Did Not Specify Requirement to Provide Seal in Capability & Util Design Process Failed to Recognize Deficiency ML18095A2321990-05-24024 May 1990 Part 21 Rept Re Discrepancies Identified in ECCS Flow Orifice K Factors Supplied by Westinghouse.Initially Reported on 900518.Util Fabricated New Orifice Plates to Original Specs ML18095A2251990-05-22022 May 1990 Part 21 Rept Re Insufficient Welds on Pedestal Support Alignment Lug & Slide Shoe for 11,12,21 & 22 Charging/Safety Injection Pumps.Initially Reported on 900516.Windows Cut in Support Pedestals to Gain Access to Affected Areas ML18094B4461990-04-27027 April 1990 Part 21 Rept Re shaft-to-pinion Key Failures in Limitorque Actuators.Initially Reported on 900424.Caused by Reduction of cross-sectional Area & Ultimate Propagation of Cracks. Util Intends to Replace Keys in Actuators W/Keys of Steel ML18094A4421989-05-16016 May 1989 Part 21 Rept Re Defect in Solid State Protection Sys. During Mods in Solid State Protection Sys Cabinets,Noted That Two Wires Became Dislodged from Circuit Board.Visual Insp & Complete Pull Test Performed ML18093A8281988-05-0606 May 1988 Part 21 & Deficiency Rept Re Asea Brown Boveri,Power Distribution,Inc Low Voltage K-Line Circuit Breakers. Efforts Underway to Define Quantity & Type of Component Parts That May Need to Be Replaced ML20153G0111988-05-0606 May 1988 Part 21 Rept Re Potential Defect in Bussman Buss KTK-R Fuse Blocks W/Part Numbers 2078,2079 & 2080.Purchasing Records Reviewed to Identify If Any Parts Were Actually Used or Shipped to Customers.Results Listed ML18093A4721987-10-23023 October 1987 Part 21 Rept Re Calibr Gas Leakage Problem in Exo-Sensors, Inc Containment Hydrogen Analyzer Sys.Caused by Design Deficiency Associated W/Calibr Gas Subassembly.Monitoring Program to Be Maintained for Period After Sys Mods ML20215G2441987-06-16016 June 1987 Part 21 Rept Re Failure of Load Sequencing Equipment Supplied in Aug 1977 During Scheduled Testing.Caused by Open Electrical Connection on One Crimp Lug.Since 1978,insulated Lugs Used on All Equipment FVY-86-105, Part 21 Rept Re Design Defect Relating to Limitorque Motor Operators Mfg Prior to 1975.Mfg Contacted & Retrofit Kits Installed on safety-related & nonsafety-related Operators. Addl Info Encl1986-11-10010 November 1986 Part 21 Rept Re Design Defect Relating to Limitorque Motor Operators Mfg Prior to 1975.Mfg Contacted & Retrofit Kits Installed on safety-related & nonsafety-related Operators. Addl Info Encl ML20215G5351986-10-10010 October 1986 Part 21 Rept Re Vendor Tests of air-operated Diaphragm Valves Revealing Natural Frequencies Less than Required Values of 33 Hz.Initially Reported on 841227.No Adverse Effects Noted During Testing ML20215G6801986-10-10010 October 1986 Part 21 Rept Re Vendor Tests of air-operated Diaphragm Valves Revealing Natural Frequencies Less than Required Values of 33 Hz.Initially Reported on 841227.No Adverse Effects Noted During Testing ML20206S0841986-06-30030 June 1986 Part 21 Rept Re Possible Cut Wires in Wire Harness of Bbc Brown Boveri K600/K800 Circuit Breakers.Initially Reported on 860509.Safety Implications Listed.Gear Guard Designed to Prevent Cut Wires ML20140J4261986-03-31031 March 1986 Part 21 Rept Re Nuclear Valves Shipped to Pse&G.Internal Parts Lapped Which Could Reduce or Eliminate Nickel Plating Resulting in Seat Leakage & Shifting Problems ML20210G9921985-08-13013 August 1985 Part 21 Rept Re Failure of Isolated Worm Shaft Gear When Certain Critical Speeds Combined W/Repetitive Transfer of Actuator Clutch Mechanism from Manual (Handwheel) to Motor Drive Mode.Two Possible Solutions Noted ML20116E8481985-04-23023 April 1985 Part 21 Rept Forwarding Rev 1 to Insp Procedure for Investigating Emergency Diesel Generators for Fractured Welds on Air Deflectors.Rev Will Be Forwarded to Each Facility ML20092D9711984-06-15015 June 1984 Part 21 Rept Re Thermal Nonrepeatability & Other Calibr Errors in Barton Lot 1 Transmitters.Initially Reported on 840615.Transmitter Defects Identified & Expected Error Deviations Calculated.Utils Notified ML20082F3621983-11-17017 November 1983 Part 21 Rept Responding to IE Bulletin 83-06, Nonconforming Matls Supplied by Tube-Line Corp. List of Matls & Sys in Which Installed Encl ML18082A1421980-02-15015 February 1980 Final Deficiency Rept:Check Valve 2DR-7 Failed to Meet Applicable Seismic Class I Loading.Caused by Design Defect. Addl Support Will Be Completed by 800228 ML18081B0481979-12-21021 December 1979 Final Deficiency Rept Re Undetectable Failure in Engineered Safety Features Actuation Sys.Testing Procedures Revised to Include Testing of Permissive Circuitry P4 on Periodic Basis.Unit Will Be Tested Prior to Operation ML18081B0601979-12-0303 December 1979 Initial Deficiency Rept Re Potential Dropped Rod Events Leading to Calculated DNB Ratios Lower than Reported to NRC for Certain Westinghouse Plants.Util Is Investigating Condition for Applicability to Facility ML18081A3751979-10-0505 October 1979 Significant Deficiency Rept Re Containment Purge & pressure- Vacuum Relief Valves.Actuator Torque Values Were Insufficient to Move Valves from Open to Closed Positions W/ Design Differential Pressure of 60 Psi.Design Reviewed ML18081A3781979-10-0505 October 1979 Significant Deficiency Rept 79-06 Re Steam Generator Water Level Instrumentation.Pipe Breaks in Containment Could Lead to Elevated Temp Readings Which Could Result in Delayed Protection Sys Actuation.Setpoints to Be Changed ML18081A7551979-10-0404 October 1979 Interim Deficiency Rept Re Max Flow of RHR Pump During post- LOCA Mode.Caused by Low Sys Resistance to Pump Runout Conditions.Sys Resistance Increased by Placement of Resized Orifices ML18079A9521978-10-28028 October 1978 Deficiency Rept:On 780928,during Routine Design Review, Undersizing of Refueling Water Storage Tank Was Discovered. Tank Storage Capacity Has Been Increased.Design Drawings for Tank Piping & Foundation Will Be Modified ML20086C0041976-07-0101 July 1976 Interim Deficiency Rept Re Fan Coil Unit Motor 15 Failure to Meet Test Requirements.Initially Reported on 760611.Fan Coil Unit Motor from Unit 1 Installed in Place of Motor 15.Faulty Motor Returned to Westinghouse for Repair ML20086C0201976-06-17017 June 1976 Interim Deficiency Rept Re Polar Gantry Crane Gear Misalignment.Initially Reported on 760611.Caused by Misalignment of Hoist Drum Gear & Pinion.Drum Assembly Realigned & Secured & Dressing Gears Initiated ML20086C0301976-06-10010 June 1976 Final Deficiency Rept Re Pressurizer Snubber Malfunction. Initially Reported on 760402.Caused by Heavy Corrosion Buildup.Nine Units Replaced W/Pacific Scientific Units & 54 Units Replaced W/Combination of Redesigned Units ML20086C0421976-06-0202 June 1976 Interim Deficiency Rept Re Automatic Transfer of 4-kV Outside Feed.Initially Reported on 760512.Caused by Design Error.Circuitry for Automatic Bus Transfer Redesigned to Eliminate Possibility of Transfer ML20086C0741976-05-28028 May 1976 Suppl to Deficiency Rept Re Steam Generator Head Cladding Indications.Initially Reported on 760408.Cause Still Under Investigation.Ultrasonic Exam Conducted 1999-06-01
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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J% G g. (- IE FILE COPY Public Servico E'cctric avd Gas Company 80 Park Place Newayk, N.107101 Phone 201/G22-7000 -
June lo, 1976 .
Mr. James P. O'Reilly, Director U. S. Nuclear Regulatory Commission
- Office of Inspection and Enforcement Region 1 631 Park Avenuo King of Prussia, Pennsylvania 19406
Dear Mr. O'Reilly:
PRESSURIZER SNUBBER MALFUNCTION PRESSURIZER SAFETY AND RELIEF VALVE PIPING NO. 1 UNIT SALEM NUCLEAR GENERATING STATION DOCKET NO. 50-272 Supplementary to our letter of April 2, 1976, submitted herewith is our concluding report on the subject equipment malfunction in accordance with 10CFR50.55(e).
ANALYSIS The original deficiency discovered during Hot Functiona'l Test, SUP 50.0 involved removal of twelve (12) snubber units, ten (10) of which were restricting thermal pipe movements and two (2) which were removed for evaluation purposes. Subject units were returned to the manufacturer, International Nuclearsafeguards (INC) for operational load testing and disassembly inspection which was witnessed by PSE&G QA Engineer. The results of the retest and disassembly indicated the following:
- 1. F'ive units functioned within required operational load limits and disassembly was no,t performed. These units were identified as: Size No. 1, S/N 271 and S/N 273; Size No. 2, S/N 75 and S/N 118; and Size No. 3, S/N 002281.
- 2. Seven units were disassembled on the basis of the unit being either completely jammed or showing operational load values that exceeded manufacturer's specifications during retest.
The completely jammed units that were disassembled on the basis of excessive operations loading during retest are:
Size No. 2, S/N 73, 74*, 78 and Size No. 3, S/N 002276**.
- Typographical error on report of 4/1/76, which listed this as S/N 47 on Page 1, Par. 4.
- Erroneously reported as S/N 00'2281 on report of 4/1/76 (second reference only) on Page 2, Par. 1.
8311220538 760628 PDR ADOCK 05000272 S PDR ,
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Mr. James P. O'Reilly 6/10/76- ;
4 Results of the investigation of disassembled units revealed the !
following: four (h) units malfunctioned due to heavy corrosion '
buildup on the units' internal components. These were all Size No. 2, S/N 92, 110 and 111 (all three were completely jammed) and S/N 78 vhich displayed heavy corrosion primarily on the i needle thrust bearing surfaces. The remaining three (3) units of the seven (7) units disassembled were Size No. 2, S/N 73 and 7h; and Size No. 3, S/N 002276, none of which' visually displayed any obvious reason for malfunction.
Five of the twelve units were installed with the shipping preset screv left in place. These screws sheared during Hot Functional i Test were on Size No. 1, S/N 271; Size No. 2, S/N 74, 78 and 1181 and Size No. 3, S/N 002281. The fact that these units were installed with the preset screw in place has lead PSE&G Engineering to conclude that this factor was not a major contributing cause of the malfunctions. This conclusion was reached on the basis that three units remained operable after removal from the Salem Site, (Size No. 1, S/N 271; Size No. 2, S/N 118; and Size No. 3, S/N 002281) and the other two units malfunctioned due to other obvious reasons; Size No. 2, S/N 78 for heavy corrosion on the
. thrust bearing and Size No. 2, S/N Th for heavy hammer marks on Housing OD inflicted during the removal operation which affected alignment and operational retest values.
SUMMARY
AND CORRECTIVE MEASURES PSE&G Energy Laboratory conducted a chemical analysis and evaluation of the heavy corrosion compounds removed from the' internal parts of Unit S/N 111. The Energy Laboratory's. report identifies the source of corrosion of the carbon steel internals as possible from rainwater containing carbon dioxide that entered the unit between the travel screw and the housing bushing.
Access of. vater to the snubber internals was attributed to the vertical position of the snubber as installed.
Replacement units consisted of: A. Redesigned INC units that have corrosive resistant hardened stainless steel wear surfaces
.and other features which will prohibit water entry and, B. Pacific Scientific Corporation (PSA) units Sizes 1, 3, lo and 35 The Pacific Scientific units have been subjected to extensive physical and environmental tests by the manufacturer and have been evaluated acceptable by PSE&G Co. for the intended service.
The corrective action taken for'the original sixty-three (63)
(INC) snubbers with carbon steel internals is as follows:
9 Units have been replaced with Pacific Scientific Units 5h Units are being replaced with a combinat.on of redesigned (INC) units and Pacific Scientific Units. ,
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Mr. James P. O'Reilly 6/10/76 Any additional snubbers which may be required for No. 1 Unit will be of the redesigned (INC) units or Pacific Scientific Units.
The replacement installations vill be completed by July 15, 1976.
Snubbers to be used for No. 2 Unit will be based on the per-formance of No. 1 Unit snubbers.
SAFETY IMPLICATIONS We are continuing our investigation of the restraining effects on the pressurizer piping system due to malfunctioning snubbers during hot functional test heat up period. From our analysis it appears that no damage to the piping system occurred during this event. We are however continuing our investigation through the use of Ultrasonic Testing of areas of interest in the subject piping and vill compare these results with the data from the previously completed preservice Ultrasonic Test history. Positive results from this test will further verify that the piping is acceptable and consequently the system vill be approved for service and no further reports vill be made.
This investigation vill be completed by July 5, 1976 and the results will be available at the plant site.
If additional information is desired,,we vill be pleased to discuss it with you.
Very truly yours,
)1 E. N. Schwa e Manager of Quality Assurance Engineering and Construction-Department
- CC Dr. Ernest Volgenan Bethesda, Md.
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