ML19350E682

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LER 80-209/03L-0:on 800922,no post-maint Testing Performed After Maint on RHR Heat Exchanger Discharge Isolation Valve. Caused by Personnel Error.List Issued Listing All Valves Which Require pre- or post-maint Testing
ML19350E682
Person / Time
Site: Sequoyah Tennessee Valley Authority icon.png
Issue date: 06/18/1981
From:
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19350E679 List:
References
LER-80-209-03L, LER-80-209-3L, NUDOCS 8106230434
Download: ML19350E682 (2)


Text

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CONTROL BLOCK: l -I l l l l (PLEASE PRINT'dR'TTPE ALL RENULRED I.N'FO'RMATION)

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64 IS 0!0l -l0l0!Oi0 l0 LICEP45E NUP.18ER l- l0 IO' 2Sh -5l 26 D LICERSE 1I fl:ll TYPE JO@l 57 Ca t by

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69 0 lEVENT 9 JDATE 2 l2 l 8 74l0, @l 76 0lREPORT6l ll DAT 8 El 8 l1soj@ , 26, S 60 61 00CICET rJUMOEM

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    ".            ' EVENT OESCRIPTION ANO PROB ABLE CONSECUENCES h                                                                          .

i 1012 l l A continuine review of maintenance'recuests MR's) on 5/22/81 discovered that with

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10#2i 1 Unit 1 in Mode 5 on 9/22/80, maintenance was performed on 1-FCV-70-156. residual he~at I iTTTl I remo+al heat exchariner discharge isolation valve. to adiust the limit ' switch and no I I o I 5 I I post-maintenance testine was cerformed as recuired by Surveillance Recuiree ent -4.0.5 I

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ITTTI 1 which invokes ASME Section XI. ihere was no effect'upon public health or safelv. I 10171 'l Previous occurrences - six (reference SORO-50-327 /80190. '80200, 81048, and 80208) . I I lo la l l

                                                                                                                                                                                                              
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CAUaE OESCRIPTION AND CORRECTIVE ACTIONS h

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I i l i l I cif the valve and did not perfdirm the re6uired t'est as allowed by nrocedures. A I

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Iii?I I technical instruction is beine issue 1 which orovides a list of n11 valves which require I*I3I I pre- and'nost-maintenance testine and examples.of tvoes of maintenance which require  ! . I1 i*I I__cesting_ o u 9 80

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ITTil8 I9Oi 0 l 01@l12 I  :: NA 80 LOS$ OF OR DauAGE TO FACILITY TvrE IhIfI &

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LER SUPPLEMENTAL INFORMATION SQRO-50-327/80209 Technical Specification Involved: 4.0.5 Reported 'Jnder Technical Specification: 6.9.1.13.c Date of Occurrence: 9/22/80 Time of Occurrence: 0400 CDT Identification and Description of Occurrence: A continuing review of maintenance requests (KR's) on 5/22/81 discovered that on 9/22/80, maintenance was performed on 1-FCV-70-156. Conditions Prior to Occurrence: Unit 1 in Mode 5 with RCS temperature and pressure at 180 F and 310 psig Apparent Cause of Occurrence: Personnel involved did not consider the maintenance per ormed to affect the

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performance of the valve and did not perform the required test. Analysis of Occurrence:' The corrective actions being taken will prevent future occurrences of failure to perform post-maintenance testing. The continuing review of MR's will continue

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                  ,to discover events of this type which have occurred in the past. These events will be reported as applicable, but this corrective action should prevent
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future occurrences. Corrective Action: Employees have been reinstructed on pre- and post-maintenance testing. A technical instruction is being issued which provides a list of all valves which require pre- and post-maintenance testing along with types of maintenance which require testing. Failure Data: None l l .

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