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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029E3351994-05-10010 May 1994 LER 94-006-00:on 940415,both Trains of CREVS Declared Inoperable.Caused by Tornado Warning & Sighting of Tornado Moving Toward Plant.Tornado Warnings downgraded.W/940510 Ltr ML20029E2021994-05-0909 May 1994 LER 94-004-00:on 940408,determined That TS Pressurizer Cooldown Limit Exceeded on 930618 & Not Restored within Required Timeframe.Caused by Unanticipated Sys Interaction. SI for Check Valve Opening Tests revised.W/940509 Ltr ML20029D8151994-05-0303 May 1994 LER 94-005-00:on 940403,inadvertent Fwis Occurred.Caused by Personnel Failure to Follow Work Document Instructions. Corrective Action:Individuals Were Counseled on Requirements to Follow Work Document Instruction steps.W/940503 Ltr ML20046B8351993-07-30030 July 1993 LER 93-017-00:on 930621,discovered 24-hour Telephone Notification Had Not Been Carried Out as Required by TS LCO 3.7.11.1 Action Statement (b)(2)(a) Due to Personnel Error. NRC Informed of Missed notification.W/930730 Ltr ML20046B8501993-07-30030 July 1993 LER 93-018-00:on 930704,DG Started Due to Improper WO Planning.Restored Power to 1BB Shutdown Board & Stopped Running DGs.W/930730 Ltr ML20046A4691993-07-19019 July 1993 LER 93-016-00:on 930619,Phase A,Auxiliary Bldg & Containment Isolations Manually Initiated as Result of Fuel Assembly Failing to Remain in Upright Position After Being Released. All Fuel Movement stopped.W/930719 Ltr ML20045J0111993-07-14014 July 1993 LER 93-015-00:on 930614,1A Start Bus Alternate Feeder Breaker Tripped Upon Start of Unit 1 RCP Which Resulted in Start of DG Due to Current Transformer Wired Incorrectly. Restored Offsite Power & Secured Final DG.W/930714 Ltr ML20045H0171993-07-12012 July 1993 LER 93-014-00:on 930611,determined That Inadequate Ventilation Design Resulted in Potential Inoperability of Vital Power Equipment.Design Being modified.W/930712 Ltr ML20045B9951993-06-15015 June 1993 LER 93-004-01:on 930222,determined That Blind Flange on Elevation 734 Personnel Airlock Outer Housing Leaking.Due to Improper Installation of Blind Flange.Evaluation Performed of Other 14 Double O-ring Blind flanges.W/930615 Ltr ML20045B9311993-06-10010 June 1993 LER 93-013-00:on 930514,fire Watch Was Not Performed within Time Frame Required by Tech Specs Due to Inadequate Supervision by Fire Protection Foreman.Fire Watch Patrol reestablished.W/930610 Ltr ML20045A7261993-06-0707 June 1993 LER 93-011-00:on 930507,discovered That Fire Barrier Breached W/O Proper Compensatory Measures Established.On 930505,door Leading to Room Housing Containment Spray HX 1A Breached.Roving Fire Watch Established & LCO 3.7.12 Entered ML20044H4501993-06-0303 June 1993 LER 93-012-00:on 930504,apparent Failure to Properly Identify & Plug SG Tube Determined to Exceed TS Plugging Limit.Caused by eddy-current Coordinator Not Ensuring Task requirements.Eddy-current Procedure revised.W/930603 Ltr ML20044H1561993-05-28028 May 1993 LER 93-010-00:on 930430,Westinghouse Identified Error in Development of Calculations for Cold Overpressure Mitigation Sys Setpoints.Caused by Vendor Failure to Consider Elevation Difference.Engineering Evaluation Performed ML20044E6341993-05-17017 May 1993 LER 93-009-00:on 930417,TS Surveillance Not Performed for Three Pipe Support Snubbers Because of Omission of Snubbers from Surveillance Instruction for Visual Insp.Snubbers Visually Inspected & Functionally tested.W/930517 Ltr ML20044B6751993-02-23023 February 1993 LER 93-001-00:on 930124,Unit 1 Ice Bed Temperature Recorder in MCR Declared Inoperable.Caused by Ineffective Communication.Appropriate Personnel Involved W/Event Have Been counseled.W/930223 Ltr ML20044B6141993-01-21021 January 1993 LER 92-026-00:on 921222,determined That Several ASME Section XI Pressure Tests Not Performed Due to Section XI Program Implementation Not Being well-defined,controlled or Documented.Test Expeditiously performed.W/930121 Ltr ML20024H2441991-05-22022 May 1991 LER 91-007-00:on 910422,LCO 3.0.3 Entered When Shaft of Train a Main Control Room Air Handling Unit Failed from Fatigue & Train B Out of Svc for Maint.Caused by Shaft Misalignment.New Shaft installed.W/910522 Ltr ML20029C1761991-03-21021 March 1991 LER 91-002-00:on 910211,unit Operated in Condition Prohibited by Tech Spec 3.3.3.8 Limiting Condition for Operation.Cause Under Investigation.Night Order Issued to Personnel Re Removal of Equipment from svc.W/910321 Ltr ML20029C1231991-03-18018 March 1991 LER 90-016-01:on 901117,determined That Calibr of Nuclear Instrumentation Sys intermediate-range Channels Set Nonconservatively.Caused by Lack of Operability Control for Rod Motion.Action Plan developed.W/910318 Ltr ML20029A6711991-02-25025 February 1991 LER 91-002-00:on 910124,LCOs 3.0.5 & 3.8.1.1 Entered When Both Trains of Emergency Gas Treatment Sys Declared Inoperable.Caused by Blown Fuse & Excessive Cycling of Air Start Sys.Fuse replaced.W/910225 Ltr ML20028H0331990-09-27027 September 1990 LER 90-019-00:on 900828,failure to Update P-250 Plant Computer Constants Resulted in Axial Flux Difference.Caused by Inadequate Procedures & Inappropriate Personnel Actions. Procedure 0-PI-NXX-092-001.0 revised.W/900927 Ltr ML20028G9201990-09-26026 September 1990 LER 90-020-00:on 900829,ventilation Sys Inoperable Due to Train B Diesel Generator Out of Svc.Caused by Stuck Microswitch Contacts on Pressure Switch 0-PS-311-172. Pressure Switch Adjusted & Returned to svc.W/900926 Ltr ML20044A9361990-07-0909 July 1990 LER 90-011-00:on 900608,determined That Actual Nuclear Instrumentation Sys Power Range Detector Currents Were 20% to 31% Lower than Predicted.Caused by Calibr Values Being Incorrectly Calculated.Channels corrected.W/900709 Ltr ML20044A3241990-06-25025 June 1990 LER 90-010-00:on 900526,limiting Condition for Operation Entered Because MSIV Failed to Close When Another MSIV Inoperable for Maint.Cause Attributed to Valve Stem & Valve Guide Binding.Operations Training Ltr issued.W/900625 Ltr ML20043H5091990-06-21021 June 1990 LER 90-009-00:on 900527,automatic Start of Auxiliary Feedwater Pumps Occurred When Both Main Feedwater Pumps Placed in Tripped Condition.Caused by Personnel Error.Trip Circuitry Reset & Operators counseled.W/900621 Ltr ML20043E5401990-06-0707 June 1990 LER 90-008-00:on 900514,two Control Room Isolations Occurred as Result of Spurious Spikes.Caused by Loose Terminations on Relay Socket.Loose Connections Properly terminated.W/900607 Ltr ML20043A4211990-05-16016 May 1990 LER 90-010-00:on 900416,containment Ventilation Isolation Occurred.Caused by Allowing Gaseous Radiation Level to Increase Too Close to Alarm Setpoint.Recovery from Isolation initiated.W/900516 Ltr ML20043A2261990-05-14014 May 1990 LER 90-009-00:on 900404,lower Containment Radiation Monitor Found Inoperable & Lower Containment Atmosphere Aligned to Upper Containment Radiation Monitor During Sampling.Caused by Personnel Error.Chemistry Training revised.W/900514 Ltr ML20043A2271990-05-14014 May 1990 LER 90-006-00:on 900414,auxiliary Bldg Isolation Occurred from Spent Fuel Pit Area Radiation Monitors 0-RM-90-102 & 103.Caused by Personnel Error.Training Ltr Issued to Instrument Mechanics & Operations personnel.W/900514 Ltr ML20043A2201990-05-14014 May 1990 LER 90-007-00:on 900413,discovered That Tech Spec Surveillance Requirement Not Performed within Required Interval.Caused by Personnel Error.Surveillance Successfully Performed Since missed.W/900514 Ltr ML20042G7861990-05-0909 May 1990 LER 90-005-00:on 900409,emergency Start of Four Emergency Diesel Generators Occurred While Attempting Transfer of Power.Caused by Personnel Error.Individuals Reprimanded, Training Initiated & Procedures revised.W/900509 Ltr ML20042G7931990-05-0909 May 1990 LER 90-008-00:on 900410,reactor Trip Occurred Resulting from General Warning Alarm on Both Trains of Solid State Protection Sys.Caused by Personnel Error.Individuals Disciplined & Site Wide Message distributed.W/900509 Ltr ML20042F3741990-05-0202 May 1990 LER 90-003-00:on 900404,control Room Ventilation Sys (CRVS) Transferred to Pressurization Mode.Caused by Electrical Transient in Vital Instrument Ac Bus PY-21A.CRVS Reset & Returned to Normal Operating modes.W/900502 Ltr ML20042E4191990-04-13013 April 1990 LER 90-007-00:on 900317 & 26,containment Ventilation Isolations Occurred During Purge Activities.Caused by Inadequate Procedural Guidance for Setpoint Determination. Alarm & Trip Setpoints increased.W/900413 Ltr ML20042E2021990-04-13013 April 1990 LER 90-005-00:on 900315,inadvertent Containment Vent Isolation Occurred While Preparing to Purge Containment. Caused by Lack of Attention to Detail by Operator.Operator Counseled & Received Administrative reprimand.W/900413 Ltr ML20012F5221990-04-0505 April 1990 LER 90-006-00:on 900307,containment Ventilation Isolation Occurred.Caused by Containment Particulate Level Too Close to Setpoint.Module Replaced.Radiation Alarm Setpoint Increased from 10% to 40% of Tech Spec limit.W/900406 Ltr ML20012D8611990-03-23023 March 1990 LER 90-004-00:on 900221,handswitches Controlling Operation of Isolation Valves on Steam Supply Line to Auxiliary Feedwater Pump Found in Manual Position.Cause Undetermined. Handswitches Placed in P-auto position.W/900323 Ltr ML20012C4271990-03-12012 March 1990 LER 90-003-00:on 900211,inadvertent Containment Vent Isolation Occurred.Caused by Lack of Attention to Detail in That Operator Did Not Look Closely Enough at Switch Designations.Personnel Involved counseled.W/900312 Ltr ML20011F7191990-03-0101 March 1990 LER 89-031-01:on 891205,RHR Pumps Determined to Have Deadheading Problem Identified by NRC Bulletin 88-004.Caused by Inadequate Technical Response to Bulletin.Training Ltr Issued to 10CFR50.59 reviewers.W/900301 Ltr ML20011F7421990-02-26026 February 1990 LER 90-002-00:on 900127,control Room Isolation Occurred When Circuit Breaker Opened Supplying Power to Radiation Monitor. Caused by Failure by Personnel to Exercise Sufficient Caution.Responsible Engineers reinstructed.W/900226 Ltr ML20011F7391990-02-26026 February 1990 LER 90-002-00:on 891122,value for Distance from Floor to Ctr Line of Level Switch 2-LS-87-21 Transposed in Variable Leg Calculation.Caused by Inattention to Detail.Procedure Revised to Replace Incorrect setpoint.W/900226 Ltr ML20006E3311990-02-0909 February 1990 LER 90-001-00:on 900112,Limiting Condition for Operation 3.0.3 Entered When Three of Four Lower Compartment Cooler Fan Motors Exceeded Lubrication Frequency.Caused by Personnel Error.Personnel counseled.W/900209 Ltr ML20006D5341990-02-0707 February 1990 LER 90-001-00:on 900108,discovered That Several ERCW Valves Not Being Periodically Verified to Be Correct.Caused by Personnel Error During Procedure Revs & Workplan Reviews. Info Notice Issued to Workplan reviewers.W/900207 Ltr ML19354E1631990-01-22022 January 1990 LER 89-036-00:on 891221,discovered That Surveillance Test Results Used for Declaring Diesel Generator 1B-B Operable Deficient.Caused by Instruction Not Including 60 Minute Run Time.Event Will Be Reviewed w/supervisors.W/900122 Ltr ML19354D8941990-01-16016 January 1990 LER 89-034-00:on 891215,leak Identified from Fitting on Vol Control Tank Level Transmitter & Auxiliary Bldg Evacuated, Preventing Fire Watch Patrol from Entering Bldg for Hourly Rounds.Fitting tightened.W/900116 Ltr ML19354D9061990-01-16016 January 1990 LER 89-033-00:on 891216,refueling Water Storage Tank Level Transmitters Failed High Due to Freezing from Extremely Cold Weather & Inappropriate Use of Calculations.Engineering Procedures Revised & Heating Installed in encl.W/900116 Ltr ML20005F8851990-01-0909 January 1990 LER 89-035-00:on 891210,turbine/reactor Trip Occurred from hi-hi Feedwater Level of 75% in Steam Generator 3.Caused by Failure of Loop 3 Main Feedwater Regulating Valve to Close. Equipment Adjusted & repaired.W/900109 Ltr ML20005E0801989-12-22022 December 1989 LER 89-032-00:on 891205,RHR Pumps Determined to Have Deadheading Problem,Per NRC Bulletin 88-004,resulting in Plant Operation Outside Design Basis.On 891128,RHR Pump Exceeded Head Criteria.Pumps started.W/891222 Ltr ML20005E0831989-12-22022 December 1989 LER 89-032-00:on 891201,discovered That Tech Spec Surveillance Requirement to Verify That Valves 1-67-748 & 2-67-748 in Open Position Not Met.Caused by Personnel Error.Correct Valve Position verified.W/891222 Ltr ML20005E1161989-12-22022 December 1989 LER 89-030-00:on 891204,fire Suppression Sys Deluge Valve Isolated More than 1 H W/O Required Continuous Fire Watch Establishment.Caused by Personal Communication Breakdown. Valve Opened & Foreman in Charge counseled.W/891222 Ltr 1994-05-09
[Table view] Category:RO)
MONTHYEARML20029E3351994-05-10010 May 1994 LER 94-006-00:on 940415,both Trains of CREVS Declared Inoperable.Caused by Tornado Warning & Sighting of Tornado Moving Toward Plant.Tornado Warnings downgraded.W/940510 Ltr ML20029E2021994-05-0909 May 1994 LER 94-004-00:on 940408,determined That TS Pressurizer Cooldown Limit Exceeded on 930618 & Not Restored within Required Timeframe.Caused by Unanticipated Sys Interaction. SI for Check Valve Opening Tests revised.W/940509 Ltr ML20029D8151994-05-0303 May 1994 LER 94-005-00:on 940403,inadvertent Fwis Occurred.Caused by Personnel Failure to Follow Work Document Instructions. Corrective Action:Individuals Were Counseled on Requirements to Follow Work Document Instruction steps.W/940503 Ltr ML20046B8351993-07-30030 July 1993 LER 93-017-00:on 930621,discovered 24-hour Telephone Notification Had Not Been Carried Out as Required by TS LCO 3.7.11.1 Action Statement (b)(2)(a) Due to Personnel Error. NRC Informed of Missed notification.W/930730 Ltr ML20046B8501993-07-30030 July 1993 LER 93-018-00:on 930704,DG Started Due to Improper WO Planning.Restored Power to 1BB Shutdown Board & Stopped Running DGs.W/930730 Ltr ML20046A4691993-07-19019 July 1993 LER 93-016-00:on 930619,Phase A,Auxiliary Bldg & Containment Isolations Manually Initiated as Result of Fuel Assembly Failing to Remain in Upright Position After Being Released. All Fuel Movement stopped.W/930719 Ltr ML20045J0111993-07-14014 July 1993 LER 93-015-00:on 930614,1A Start Bus Alternate Feeder Breaker Tripped Upon Start of Unit 1 RCP Which Resulted in Start of DG Due to Current Transformer Wired Incorrectly. Restored Offsite Power & Secured Final DG.W/930714 Ltr ML20045H0171993-07-12012 July 1993 LER 93-014-00:on 930611,determined That Inadequate Ventilation Design Resulted in Potential Inoperability of Vital Power Equipment.Design Being modified.W/930712 Ltr ML20045B9951993-06-15015 June 1993 LER 93-004-01:on 930222,determined That Blind Flange on Elevation 734 Personnel Airlock Outer Housing Leaking.Due to Improper Installation of Blind Flange.Evaluation Performed of Other 14 Double O-ring Blind flanges.W/930615 Ltr ML20045B9311993-06-10010 June 1993 LER 93-013-00:on 930514,fire Watch Was Not Performed within Time Frame Required by Tech Specs Due to Inadequate Supervision by Fire Protection Foreman.Fire Watch Patrol reestablished.W/930610 Ltr ML20045A7261993-06-0707 June 1993 LER 93-011-00:on 930507,discovered That Fire Barrier Breached W/O Proper Compensatory Measures Established.On 930505,door Leading to Room Housing Containment Spray HX 1A Breached.Roving Fire Watch Established & LCO 3.7.12 Entered ML20044H4501993-06-0303 June 1993 LER 93-012-00:on 930504,apparent Failure to Properly Identify & Plug SG Tube Determined to Exceed TS Plugging Limit.Caused by eddy-current Coordinator Not Ensuring Task requirements.Eddy-current Procedure revised.W/930603 Ltr ML20044H1561993-05-28028 May 1993 LER 93-010-00:on 930430,Westinghouse Identified Error in Development of Calculations for Cold Overpressure Mitigation Sys Setpoints.Caused by Vendor Failure to Consider Elevation Difference.Engineering Evaluation Performed ML20044E6341993-05-17017 May 1993 LER 93-009-00:on 930417,TS Surveillance Not Performed for Three Pipe Support Snubbers Because of Omission of Snubbers from Surveillance Instruction for Visual Insp.Snubbers Visually Inspected & Functionally tested.W/930517 Ltr ML20044B6751993-02-23023 February 1993 LER 93-001-00:on 930124,Unit 1 Ice Bed Temperature Recorder in MCR Declared Inoperable.Caused by Ineffective Communication.Appropriate Personnel Involved W/Event Have Been counseled.W/930223 Ltr ML20044B6141993-01-21021 January 1993 LER 92-026-00:on 921222,determined That Several ASME Section XI Pressure Tests Not Performed Due to Section XI Program Implementation Not Being well-defined,controlled or Documented.Test Expeditiously performed.W/930121 Ltr ML20024H2441991-05-22022 May 1991 LER 91-007-00:on 910422,LCO 3.0.3 Entered When Shaft of Train a Main Control Room Air Handling Unit Failed from Fatigue & Train B Out of Svc for Maint.Caused by Shaft Misalignment.New Shaft installed.W/910522 Ltr ML20029C1761991-03-21021 March 1991 LER 91-002-00:on 910211,unit Operated in Condition Prohibited by Tech Spec 3.3.3.8 Limiting Condition for Operation.Cause Under Investigation.Night Order Issued to Personnel Re Removal of Equipment from svc.W/910321 Ltr ML20029C1231991-03-18018 March 1991 LER 90-016-01:on 901117,determined That Calibr of Nuclear Instrumentation Sys intermediate-range Channels Set Nonconservatively.Caused by Lack of Operability Control for Rod Motion.Action Plan developed.W/910318 Ltr ML20029A6711991-02-25025 February 1991 LER 91-002-00:on 910124,LCOs 3.0.5 & 3.8.1.1 Entered When Both Trains of Emergency Gas Treatment Sys Declared Inoperable.Caused by Blown Fuse & Excessive Cycling of Air Start Sys.Fuse replaced.W/910225 Ltr ML20028H0331990-09-27027 September 1990 LER 90-019-00:on 900828,failure to Update P-250 Plant Computer Constants Resulted in Axial Flux Difference.Caused by Inadequate Procedures & Inappropriate Personnel Actions. Procedure 0-PI-NXX-092-001.0 revised.W/900927 Ltr ML20028G9201990-09-26026 September 1990 LER 90-020-00:on 900829,ventilation Sys Inoperable Due to Train B Diesel Generator Out of Svc.Caused by Stuck Microswitch Contacts on Pressure Switch 0-PS-311-172. Pressure Switch Adjusted & Returned to svc.W/900926 Ltr ML20044A9361990-07-0909 July 1990 LER 90-011-00:on 900608,determined That Actual Nuclear Instrumentation Sys Power Range Detector Currents Were 20% to 31% Lower than Predicted.Caused by Calibr Values Being Incorrectly Calculated.Channels corrected.W/900709 Ltr ML20044A3241990-06-25025 June 1990 LER 90-010-00:on 900526,limiting Condition for Operation Entered Because MSIV Failed to Close When Another MSIV Inoperable for Maint.Cause Attributed to Valve Stem & Valve Guide Binding.Operations Training Ltr issued.W/900625 Ltr ML20043H5091990-06-21021 June 1990 LER 90-009-00:on 900527,automatic Start of Auxiliary Feedwater Pumps Occurred When Both Main Feedwater Pumps Placed in Tripped Condition.Caused by Personnel Error.Trip Circuitry Reset & Operators counseled.W/900621 Ltr ML20043E5401990-06-0707 June 1990 LER 90-008-00:on 900514,two Control Room Isolations Occurred as Result of Spurious Spikes.Caused by Loose Terminations on Relay Socket.Loose Connections Properly terminated.W/900607 Ltr ML20043A4211990-05-16016 May 1990 LER 90-010-00:on 900416,containment Ventilation Isolation Occurred.Caused by Allowing Gaseous Radiation Level to Increase Too Close to Alarm Setpoint.Recovery from Isolation initiated.W/900516 Ltr ML20043A2261990-05-14014 May 1990 LER 90-009-00:on 900404,lower Containment Radiation Monitor Found Inoperable & Lower Containment Atmosphere Aligned to Upper Containment Radiation Monitor During Sampling.Caused by Personnel Error.Chemistry Training revised.W/900514 Ltr ML20043A2271990-05-14014 May 1990 LER 90-006-00:on 900414,auxiliary Bldg Isolation Occurred from Spent Fuel Pit Area Radiation Monitors 0-RM-90-102 & 103.Caused by Personnel Error.Training Ltr Issued to Instrument Mechanics & Operations personnel.W/900514 Ltr ML20043A2201990-05-14014 May 1990 LER 90-007-00:on 900413,discovered That Tech Spec Surveillance Requirement Not Performed within Required Interval.Caused by Personnel Error.Surveillance Successfully Performed Since missed.W/900514 Ltr ML20042G7861990-05-0909 May 1990 LER 90-005-00:on 900409,emergency Start of Four Emergency Diesel Generators Occurred While Attempting Transfer of Power.Caused by Personnel Error.Individuals Reprimanded, Training Initiated & Procedures revised.W/900509 Ltr ML20042G7931990-05-0909 May 1990 LER 90-008-00:on 900410,reactor Trip Occurred Resulting from General Warning Alarm on Both Trains of Solid State Protection Sys.Caused by Personnel Error.Individuals Disciplined & Site Wide Message distributed.W/900509 Ltr ML20042F3741990-05-0202 May 1990 LER 90-003-00:on 900404,control Room Ventilation Sys (CRVS) Transferred to Pressurization Mode.Caused by Electrical Transient in Vital Instrument Ac Bus PY-21A.CRVS Reset & Returned to Normal Operating modes.W/900502 Ltr ML20042E4191990-04-13013 April 1990 LER 90-007-00:on 900317 & 26,containment Ventilation Isolations Occurred During Purge Activities.Caused by Inadequate Procedural Guidance for Setpoint Determination. Alarm & Trip Setpoints increased.W/900413 Ltr ML20042E2021990-04-13013 April 1990 LER 90-005-00:on 900315,inadvertent Containment Vent Isolation Occurred While Preparing to Purge Containment. Caused by Lack of Attention to Detail by Operator.Operator Counseled & Received Administrative reprimand.W/900413 Ltr ML20012F5221990-04-0505 April 1990 LER 90-006-00:on 900307,containment Ventilation Isolation Occurred.Caused by Containment Particulate Level Too Close to Setpoint.Module Replaced.Radiation Alarm Setpoint Increased from 10% to 40% of Tech Spec limit.W/900406 Ltr ML20012D8611990-03-23023 March 1990 LER 90-004-00:on 900221,handswitches Controlling Operation of Isolation Valves on Steam Supply Line to Auxiliary Feedwater Pump Found in Manual Position.Cause Undetermined. Handswitches Placed in P-auto position.W/900323 Ltr ML20012C4271990-03-12012 March 1990 LER 90-003-00:on 900211,inadvertent Containment Vent Isolation Occurred.Caused by Lack of Attention to Detail in That Operator Did Not Look Closely Enough at Switch Designations.Personnel Involved counseled.W/900312 Ltr ML20011F7191990-03-0101 March 1990 LER 89-031-01:on 891205,RHR Pumps Determined to Have Deadheading Problem Identified by NRC Bulletin 88-004.Caused by Inadequate Technical Response to Bulletin.Training Ltr Issued to 10CFR50.59 reviewers.W/900301 Ltr ML20011F7421990-02-26026 February 1990 LER 90-002-00:on 900127,control Room Isolation Occurred When Circuit Breaker Opened Supplying Power to Radiation Monitor. Caused by Failure by Personnel to Exercise Sufficient Caution.Responsible Engineers reinstructed.W/900226 Ltr ML20011F7391990-02-26026 February 1990 LER 90-002-00:on 891122,value for Distance from Floor to Ctr Line of Level Switch 2-LS-87-21 Transposed in Variable Leg Calculation.Caused by Inattention to Detail.Procedure Revised to Replace Incorrect setpoint.W/900226 Ltr ML20006E3311990-02-0909 February 1990 LER 90-001-00:on 900112,Limiting Condition for Operation 3.0.3 Entered When Three of Four Lower Compartment Cooler Fan Motors Exceeded Lubrication Frequency.Caused by Personnel Error.Personnel counseled.W/900209 Ltr ML20006D5341990-02-0707 February 1990 LER 90-001-00:on 900108,discovered That Several ERCW Valves Not Being Periodically Verified to Be Correct.Caused by Personnel Error During Procedure Revs & Workplan Reviews. Info Notice Issued to Workplan reviewers.W/900207 Ltr ML19354E1631990-01-22022 January 1990 LER 89-036-00:on 891221,discovered That Surveillance Test Results Used for Declaring Diesel Generator 1B-B Operable Deficient.Caused by Instruction Not Including 60 Minute Run Time.Event Will Be Reviewed w/supervisors.W/900122 Ltr ML19354D8941990-01-16016 January 1990 LER 89-034-00:on 891215,leak Identified from Fitting on Vol Control Tank Level Transmitter & Auxiliary Bldg Evacuated, Preventing Fire Watch Patrol from Entering Bldg for Hourly Rounds.Fitting tightened.W/900116 Ltr ML19354D9061990-01-16016 January 1990 LER 89-033-00:on 891216,refueling Water Storage Tank Level Transmitters Failed High Due to Freezing from Extremely Cold Weather & Inappropriate Use of Calculations.Engineering Procedures Revised & Heating Installed in encl.W/900116 Ltr ML20005F8851990-01-0909 January 1990 LER 89-035-00:on 891210,turbine/reactor Trip Occurred from hi-hi Feedwater Level of 75% in Steam Generator 3.Caused by Failure of Loop 3 Main Feedwater Regulating Valve to Close. Equipment Adjusted & repaired.W/900109 Ltr ML20005E0801989-12-22022 December 1989 LER 89-032-00:on 891205,RHR Pumps Determined to Have Deadheading Problem,Per NRC Bulletin 88-004,resulting in Plant Operation Outside Design Basis.On 891128,RHR Pump Exceeded Head Criteria.Pumps started.W/891222 Ltr ML20005E0831989-12-22022 December 1989 LER 89-032-00:on 891201,discovered That Tech Spec Surveillance Requirement to Verify That Valves 1-67-748 & 2-67-748 in Open Position Not Met.Caused by Personnel Error.Correct Valve Position verified.W/891222 Ltr ML20005E1161989-12-22022 December 1989 LER 89-030-00:on 891204,fire Suppression Sys Deluge Valve Isolated More than 1 H W/O Required Continuous Fire Watch Establishment.Caused by Personal Communication Breakdown. Valve Opened & Foreman in Charge counseled.W/891222 Ltr 1994-05-09
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20212J6311999-10-0101 October 1999 SER Accepting Request for Relief from ASME Boiler & Pressure Vessel Code,Section Xi,Requirements for Certain Inservice Insp at Plant,Unit 1 ML20217G3721999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Sequoyah Nuclear Plant.With ML20212F0831999-09-23023 September 1999 Safety Evaluation Granting Relief from Certain Weld Insp at Sequoyah Nuclear Plant,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(ii) for Second 10-year ISI Interval ML20212F4761999-09-23023 September 1999 Safety Evaluation Supporting Amends 246 & 237 to Licenses DPR-77 & DPR-79,respectively ML20212C4761999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Sequoyah Nuclear Plant.With ML20210L4361999-08-0202 August 1999 Cycle 9 12-Month SG Insp Rept ML20216E3781999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20210L4451999-07-31031 July 1999 Unit-2 Cycle 10 Voltage-Based Repair Criteria 90-Day Rept ML20210G6631999-07-28028 July 1999 Cycle 9 90-Day ISI Summary Rept ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20209H3831999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Sequoyah Nuclear Plant.With ML20211F9031999-06-30030 June 1999 Cycle 9 Refueling Outage ML20196J8521999-06-28028 June 1999 Safety Evaluation Authorizing Proposed Alternative to Use Iqis for Radiography Examinations as Provided for in ASME Section III,1992 Edition with 1993 Addenda,Pursuant to 10CFR50.55a(a)(3)(i) ML20195K2951999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20206Q8951999-05-0505 May 1999 Rev 0 to L36 990415 802, COLR for Sequoyah Unit 2 Cycle 10 ML20206R5031999-04-30030 April 1999 Monthly Operating Repts for April 1999 for Sequoyah Units 1 & 2.With ML20205P9811999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20204C3111999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20205B6631999-02-28028 February 1999 Underground Storage Tank (Ust) Permanent Closure Rept, Sequoyah Nuclear Plant Security Backup DG Ust Sys ML20203H7381999-02-18018 February 1999 Safety Evaluation of Topical Rept BAW-2328, Blended U Lead Test Assembly Design Rept. Rept Acceptable Subj to Listed Conditions ML20211A2021999-01-31031 January 1999 Non-proprietary TR WCAP-15129, Depth-Based SG Tube Repair Criteria for Axial PWSCC Dented TSP Intersections ML20198S7301998-12-31031 December 1998 Cycle 10 Voltage-Based Repair Criteria 90-Day Rept ML20199G3641998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20197J5621998-12-0303 December 1998 Unit 1 Cycle 9 90-Day ISI Summary Rept ML20197K1161998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20195F8061998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Sequoyah Nuclear Plant.With ML20154H6091998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20154H6251998-09-17017 September 1998 Rev 0 to Sequoyah Nuclear Plant Unit 1 Cycle 10 Colr ML20153B0881998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Sequoyah Nuclear Plant.With ML20239A0631998-08-27027 August 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Sequoyah Nuclear Plant,Units 1 & 2 ML20236Y2091998-08-0707 August 1998 Safety Evaluation Accepting Relief Requests RP-03,RP-05, RP-07,RV-05 & RV-06 & Denying RV-07 & RV-08 ML20237B5221998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Snp ML20237A4411998-07-31031 July 1998 Blended Uranium Lead Test Assembly Design Rept ML20236P6441998-07-10010 July 1998 LER 98-S01-00:on 980610,failure of Safeguard Sys Occurred for Which Compensatory Measures Were Not Satisfied within Required Time Period.Caused by Inadequate Security Procedure.Licensee Revised Procedure MI-134 ML20236R0051998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Sequoyah Nuclear Plant ML20249A8981998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Sequoyah Nuclear Plant,Units 1 & 2 ML20247L5141998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Sequoyah Nuclear Plant ML20217K4471998-04-27027 April 1998 Safety Evaluation Supporting Requests for Relief 1-ISI-2 (Part 1),2-ISI-2 (Part 2),1-ISI-5,2-ISI-5,1-ISI-6,1-ISI-7, 2-ISI-7,ISPT-02,ISPT-04,ISPT-06,ISPT-07,ISPT-8,ISPT-01 & ISPT-05 ML20217E2221998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Sequoyah Nuclear Plant ML20248L2611998-02-28028 February 1998 Monthly Operating Repts for Sequoyah Nuclear Plant,Units 1 & 2 ML20199J2571998-01-31031 January 1998 Cycle 9 Voltage-Based Repair Criteria 90-Day Rept ML20202J7911998-01-31031 January 1998 Monthly Operating Repts for Jan 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20199J2441998-01-29029 January 1998 Snp Unit 2 Cycle Refueling Outage Oct 1997 ML20199F8531998-01-13013 January 1998 ASME Section XI Inservice Insp Summary Rept for Snp Unit 2 Refueling Outage Cycle 8 ML20199A2931997-12-31031 December 1997 Revised Monthly Operating Rept for Dec 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20198M1481997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20197J1011997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20199C2951997-11-13013 November 1997 LER 97-S01-00:on 971017,vandalism of Electrical Cables Was Observed.Caused by Vandalism.Repaired Damaged Cables, Interviewed Personnel Having Potential for Being in Area at Time Damage Occurred & Walkdowns ML20199C7201997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Sequoyah Nuclear Plant L-97-215, SG Secondary Side Loose Object Safety Evaluation1997-10-23023 October 1997 SG Secondary Side Loose Object Safety Evaluation 1999-09-30
[Table view] |
Text
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. TENNESSEE VALLEY AUTHORITY 6N 38A Lookout Place J January 22, 1990 i
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U.S. Nuclear Regulatory Commission ATTN Document Control Desk l Washington, D.C. 20555 Gentlemen:
TENNESSEE VALLEY AUTHORITY - SEQUOYAH NUCLEAR PLANT UNIT 1 - DOCKET NO.
50-327 - FACILITY OPERATINO LICENSE DPR LICENSEE EVENT REPORT (LER) 50-327/89036 The enclosed LER provides details of an event wherein the 1B-B diesel generator was inoperable because of a surveillance run time of less than >
60 minutes at 4400-kilcwatt load. This event is being reported in accordance with 10 CFR 50.73, paragraph a.2.i.
Very truly yours, TENNESSEE VALLEY AUTHORITY
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ce President Nuclear Power Production Enclosure cc (Enclosure):
l Regional Administration j' U.S. Nuclear Regulatory Commission Office of Inspection and Enforcement Region II l 101 Marietta Street, Suite 2900 Atlanta, Georgia 30323 lL 1
INP0 Records Center
[: Institute of Nuclear Power Operations 1100 circle 75 Parkway, Suite 1500 Atlanta, Georgia 30339 NRC Resident Inspector Sequoyah Nuclear Plant 2600 Igou Ferry Road Soddy Daisy, Tennessee 37379 9001290 AD gQ,[dh$27 PDR PDC S
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THE PAPERWORK REDUCTION PROJEC1 (31b00104), OF F ICE j OF MANAGEME NT AND SUDGET.WA$HINGTON, DC 20603 l l
DOCEET NUMOE R (2) PAGE43i l 9 ACILITY NAME Hi Sequoyah Nuclear Plant, Unit 1 0l5l0l0l0l3l2l7 1 lOFl0 l5 )
'" Diesel Generator Ineperable Because of a Surveillance Run Time Less Than the Required I 60 Minutes. 4 EVENT DATE (Si LER NUMeER tll REPORT DATE 171 OTHER f ACILfTIES INVOLVED tel ag;;' A, ' ==,y;; DAv vtAR ' Aciut v M Au;s DUC=ET NUMetaisi MONTH oav vEAR vtAR , MONTH Sequoyah, Unit 2 0151010l0 13 l 2l 8 .
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NAME TELEPHONE NUM9ER ARE A CODE Ceoffrey A. Hipp. Compitiance Licensinn Ennineer 61115 81 41 31 4 7171616 COMPLETE ONE LINE FOR E ACM COMPONENT F AILURE DESCRi3ED IN THIS REPORT H31 CAUsE system COMPONENT "QWl^C- "I?",'R!}' CAusE system COMPONENT *QW'^C "jya,TAngt l I I I I l l l t I I I I f I ! I l l l l 1 1 I I I I I SUPPLEMENTAL REPORT EXPECTED H4l MONTH OAV vfAR SuSMi$$10N vES tle os.
v tornosere Ex9tCTEO Sv0401sstON DATil NO l l l Aesm.CT w.~r to ux wae. a e, en . ew r nee nee nue rve-r,run nea no, On December 21, 1989, with Unit 1 at 100 percent power and Unit 2 at 75 percent power, it was discovered that surveillance test results that had been used as the basis for daclaring the 1B-B diesel generator (D/G) operable following a preventative maintenance (PM) outage, were deficient. The surveillance requirement of Limiting Condition for Operation (LCO) 3.8.1.1 called for at least 60 minutes of D/G operation with a load of 4400 kilowatt (kw) or greater. The D/G had been operated for 63 minutes total but, bscause of gradual loading, for only 52 minutes with a load of 4400 kw or greater. The D/G was declared inoperable retroactive to the beginning of the PM outage, and the dsficient surveillance test was reperformed. Because more than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> had elapsed since the beginning of the D/G PM outage and the remaining D/Gs had not been drmonstrated operable in accordance with Surveillance Requirement 4.8.1.1.2.a.4 as raquired by Action Statement (a) of LCO 3.8.1.1, LCO 3.0.3 was entered until the D/Gs ware demonstrated operable. The root cause of this event has been attributed to an
! inadequate surveillance instruction (SI) that did not clearly exclude gradual loading time from the required 60-minute D/G run time. As corrective action, the SI has been clarified, and the event will be reviewed with shift operations supervisors.
l NiC Perm 366 (6491 l.
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FACILif Y hat.it (U DOCllti NUMBE R (21 ggg gygggg ag, pggg g3, Ssquoyah Nuclear Plant, Unit i vt.R gg,^ 6 qg;q 0 l5 l0 jo l0 l 3l 2l 7 8 l9 -
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0l0 0l 2 0F 0l5 TEXT W more space de secured. vae espioner MC perm Jiisrst (171 Dascription of Event i At 1030 Eastern standard time (EST) on December 21, 1989, with Unit 1 in Mode 1 at l 100 percent power, 2,235 pounds per square inch gauge (psig), 578 degrees Fahrenheit (F) and Unit 2 in Mode 1 at 75 percent power, 2,235 psig. 570 degrees F, it was discovered that surveillance test results that had been used as the basis for declaring the 1B-B diesel generator (D/G) (EIIS Code EK) operable, were deficient.
The 1B-B D/G was removed from service at 0630 EST on December 20, 1989, for its monthly f preventative maintenance (PM) outage. Action (a) of Limiting Condition for Operation (LCO) 3.8.1.1 was entered at that time. This action statement, applicable when either one offsite emergency power circuit er one D/G is inoperable, requires the following !
cetions:
- 1. Demonstrate the operability of the remaining offsite circuits and D/Gs by verifying correct breaker alignments and indicated power availability within one hour and at least once every eight hours thereafter (Surveillance Requirement [SR] 4.8.1.1.1.a).
- 2. Demonstrate the operability of the remaining D/Gs within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> by verifying the diesel starts from ambient conditions and accelerates to at least 900 revolutions per minute (rpm) in 10 seconds or less. The generator voltage and frequency shall be 6,900 +/-690 volts and 60 +/- 1.2 hertz (Hz) within 10 seconds after the start signal (SR 4.8.1.1.2.a.4).
- 3. Restore at least two offsite circuits and four D/Gs to operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in hot standby within the next six hours and in cold shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.
Rsquirement No. 1 above is typically satisfied by completion of Data Sheet 7.1.A of Surveillance Instruction (SI) 7.1, " Diesel Generator AC Electrical Power Source Operability Verification (Diesel Generator /Offsite Source)." Similarly, Requirement No. 2 above is typically satisfied by completion of Data Sheet 7.1.B of SI-7.1.
The 1B-B D/G PM outage continued for the rest of December 20, 1989, with periodic parformances of SI-7.1, Data Sheet 7.1.A (as required) and culminated with a performance of SI-7, " Electrical Power System: Diesel Generators," completed at 0605 EST on Dacember 21, 1989. SI-7 was performed as a postmaintenance test (PMT) to demonstrate operability prior to returning the D/G to service. One of the SRs satisfied by SI-7 is SR 4.8.1.1.2.a.5 which requires:
- Verifying the generator is synchronized, loaded to greater than or equal to 4400-kw in less than or equal to 60 seconds, and operates for greater than or equal to 60 minutes. . .
- The diesel generator start (10 sec) and load (60 see) from standby conditions shall be performed at least once per 184 days in these surveillance tests. All other diesel generator engine starts and loading for the purpose of this surveillance testing may be preceded by an engine idle start, followed by gradual acceleration to synchronous speed (900 rpm), synchronization, and gradual loading.
N".C Form 366A (649)
NR PORM 300A U 5. CUCLEO 4 8 #ULAinY COMMitSION IM715t3 4/30/92 1
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LICENSEE EVENT REPORT (LER) 2.' TEf 'e'!
i,5"n't*lo',MMNi"Gi TEXT CONTINUATION AU'.UEcM.'!alfu '"' "EfEA 1 P.PtRWO Hi TION J $0 IO ICE OF MANAGE ME NT AND DVDG tT, W ASHING TON. DC 20bO3 9 ACILITY NAME (1) DOCR41 NUMSE R (21 ggg gggggg ggy pagg g3, 1 S:quoyah Nuclear Plant, Unit i vs.R a g,p,*, ' g,p olsl0jolol3l2l7 8l 9 -
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0l0 0l3 OF 0 l5 j TEXT M mswo apses a roeused, ese e# toast NRC Fonn JnNs/ (171 Discription of Event (Continued)
The SR requires 60 minutes of operation at 4400 kilowatt (kw) or above when the D/G is l loaded within 60 seconds. However, when the D/G is loaded gradually, as permitted by the note, it is open to interpretation whether the 60 minutes of operation the SR rsquires starts after 4400 kw is loaded or if the 60 minutes includes the gradual loading time. The corresponding section of SI-7 Step 24, which directs the performer to verify the D/G has operated for at least 60 t.d tes while loaded (finish time minus loading start time must be at least 60 minutes)
During the December 21, 1989, performance of SI-7, the time of initial loading of the 1B-B D/G was 0422 EST, the time a 4400-kw load was reached was 0433 EST, and the test finish time was 0525 EST. The surveillance performer calculated a D/G run time of 63 minutes (0525-0422), which was deemed acceptable. When the SI was completed, the rssults were reviewed and approved by the shift operations supervisor (SOS). The 1B-B D/G was then declared operable at 0614 EST, and Action (a) of LCO 3.8.1.1 was exited. Because the LCO had not been in effect for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, it had not been necessary to demonstrate the operability of the other three D/Gs as described previously in Actioni Statement Requirement (2).
At approximately 1030 EST, while reviewing the completed SI-7 package, the SI review crew noticed that the time the D/G was run with a 4400-kw load was 52 minutes (0525-0433), which was less than the required 60 minutes. The SI review crew brought the discrepancy to the SOS's attention, who consulted with plant management. A conservative decision was made to consider the 0605 EST SI-7 performance to be deficient bscause the D/G was not run for 60 minutes with a load of at least 4400 kw, even though the testing was probably edequate for the purpose of a PMT. Consequently, the 1B-B D/G was declared inoperable with the time of inoperability defined as 0630 EST on D cember 20, 1989, because that was when the 1B-B D/G outage started. Because more than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> had elapsed by now and the other three D/Gs had not been demonstrated operable in accordance with SR 4.8.1.1.2.a.4 as required by Action (a) of LCO 3.8.1.1, LCO 3.0.3 w:s entered as of the time of discovery (1030 EST on December 21, 1989). The other three D/Gs were verified operable at 1230 EST by completing a Data Sheet 7.1.B of SI-7.1 (SR 4.8.1.1.2.a.4) for each. LCO 3.0.3 was exited at that time, and Action (a) of LCO 3.8.1.1 was entered. A repeat performance of SI-7 on the IB-B D/G was completed at 1642 EST with a run time at 4400-kw load of 73 minutes. The 1B-B D/G was declared operable at 1700 EST, and LCO 3.8.1.1 was exited.
Cause of Event The root cause of this event has been attributed to an inadequate procedure in that SI-7 did not clearly specify the required 60-minute D/G run time to be with a load of 4400 kw or greater when gradually loaded. A brief summary follows of certain related technical specification (TS) changes to put the event in context.
GC C Form 306A (689)
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NRC issued Generic Letter (GL) 84-15 " Proposed Staff Actions to Improve and Maintain Diesel Generator Reliability " on July 2, 1984, to improve D/G reliability by, in part, reducing the number of cold fast start surveillance tests. In response, a TS change was submitted to allow gradual loading for some D/G tests. Previously, the SR allowed only onbient starting and loading to at least 4400 kw within 6C seconds. The TS change was approved in February 1987, and SI-7 was revised to reflect the new requirements. The wording adopted by these changes is essentially the wording that existed at the time of this event. The SQN TS wording is very slightly different from the typical TS provided es an example in the GL 84-15 letter. The example TS redundantly states the requirement as: loading to 4400 kw or greater and operation at 4400 kw or greater for at least 60 minutes. The SQN TS require loading to 4400 kw or greater and operation for at least 60 minutes. This wording, in combination with the related note allowing gradual loading, allows room for interpretation whether the gradual loading time can be included in the 60 minutes. This potential for ambiguity was carried over into the implementing procedure, SI-7, when it was revised in 1987.
Analysis of Event This event is being reported in accordance with 10 CFR 50.73, paragraph a.2.1, as an operation prohibited by TS, in that the three unaffected D/Gs were not demonstrated operable in accordance with SR 4.8.1.1.2.a.4 with 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> as required by Action Statement (a) of LCO 3.8.1.1.
The standby alternating current (ac) power system is described in Section 8.3.1.1 of the SQN Updated Final Safety Analysis Report. This system continuously supplies power for energizing all ac-powered electrical devices essential to safety. The D/Gs are the standby power source for this system.
Operation of the 1B-B D/G for 52 minutes instead of the required 60 minutes at 4400 kw or greater during the 0605 EST SI-7 performance, was a deficiency in the D/G PMT, but I did not result in any loss of D/G functional capability. The 52 minutes versus 60 minutes was probably insignificant for the purpose of PMT, but the 1B-B D/G was technically inoperable. The reperformance of SI-7 completed at 1642 EST demonstrated I
that the D/G was capable of operating under continuous load for greater than 60 minutes. Therefore, if the 1B-B D/G had been called upon to perform any time after 0630 EST on December 21, 1989, its safety function would have been performed as cxpected. Consequently, at no time were plant safety features compromised. nor did this
! event result in any increased risk to the health and safety of plant personnel or the i gsneral public.
l l
CE.C Form assA (6491
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0 ]O 0l5 OF 0l5 TEKT r# mese apace e rammest ese ashonennt NRC *enn JUh4 W (1h Corrective Actions The immediate corrective actions, upon discovery of the event, were to declare the 1B-B D/G inoperable, verify the other three D/Gs operable in accordance with ,
SR 4.8.1.1.2.a.4, and reperform SI-7 on the 1B-B D/G with a run time of more than j 60 minutes at a load of 4400 kw or greater. The D/G was then returned to service. A l procedure change was immediately initiated to clarify SI-7 to require operation with a !
load of 4400 kw or greater for at least 60 minutes to satisfy acceptance criteria. This !
procedure change was put in effect on December 22, 1989. Additionally, the Operations
- Superintendent will discuss this event in his next monthly SOS meeting.
The last performances of SI-7 on 1A-A, 2A-A, and 2B-B D/Gs have been reviewed to verify operability of those units. Run times at 4400 kw or greater were 69 minutes, 64 minutes, and 68 minutes, respectively. A review of previous SI-7 performances conducted since the Unit 2 Cycle 3 outage in May 1989 has revealed two other occurrences (on August 3, 1989, and August 10, 1989) where a D/G was operated for less than the required 60 minutes with 4400-kw load.
l Additional Information
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There have been 17 LERs previously written as a result of sis not ensuring compliance j with TSs--SQN-50-327/86007, 86013, 86028, 86030, 86035, 86039, 86040, 86042, 86044, 86050, 87002, 87007, 87008, 87009, 89025, SQN-50-328/86006, and 86007. The vast majority of these LERs were written as the result of SQN's SI Review Program. None of i the previous LERs were connected with SI-7 or SI-7.1 surveillance of D/Gs. As previously described, the deficiency in SI-7 was a potential for misinterpretation as opposed to an easily identifiable procedural deficiency or omission.
Commitment The Operations Superintendent will discuss this event in his next monthly SOS meeting.
0696h NRC Fenn 3sSA (6491