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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029E3351994-05-10010 May 1994 LER 94-006-00:on 940415,both Trains of CREVS Declared Inoperable.Caused by Tornado Warning & Sighting of Tornado Moving Toward Plant.Tornado Warnings downgraded.W/940510 Ltr ML20029E2021994-05-0909 May 1994 LER 94-004-00:on 940408,determined That TS Pressurizer Cooldown Limit Exceeded on 930618 & Not Restored within Required Timeframe.Caused by Unanticipated Sys Interaction. SI for Check Valve Opening Tests revised.W/940509 Ltr ML20029D8151994-05-0303 May 1994 LER 94-005-00:on 940403,inadvertent Fwis Occurred.Caused by Personnel Failure to Follow Work Document Instructions. Corrective Action:Individuals Were Counseled on Requirements to Follow Work Document Instruction steps.W/940503 Ltr ML20046B8351993-07-30030 July 1993 LER 93-017-00:on 930621,discovered 24-hour Telephone Notification Had Not Been Carried Out as Required by TS LCO 3.7.11.1 Action Statement (b)(2)(a) Due to Personnel Error. NRC Informed of Missed notification.W/930730 Ltr ML20046B8501993-07-30030 July 1993 LER 93-018-00:on 930704,DG Started Due to Improper WO Planning.Restored Power to 1BB Shutdown Board & Stopped Running DGs.W/930730 Ltr ML20046A4691993-07-19019 July 1993 LER 93-016-00:on 930619,Phase A,Auxiliary Bldg & Containment Isolations Manually Initiated as Result of Fuel Assembly Failing to Remain in Upright Position After Being Released. All Fuel Movement stopped.W/930719 Ltr ML20045J0111993-07-14014 July 1993 LER 93-015-00:on 930614,1A Start Bus Alternate Feeder Breaker Tripped Upon Start of Unit 1 RCP Which Resulted in Start of DG Due to Current Transformer Wired Incorrectly. Restored Offsite Power & Secured Final DG.W/930714 Ltr ML20045H0171993-07-12012 July 1993 LER 93-014-00:on 930611,determined That Inadequate Ventilation Design Resulted in Potential Inoperability of Vital Power Equipment.Design Being modified.W/930712 Ltr ML20045B9951993-06-15015 June 1993 LER 93-004-01:on 930222,determined That Blind Flange on Elevation 734 Personnel Airlock Outer Housing Leaking.Due to Improper Installation of Blind Flange.Evaluation Performed of Other 14 Double O-ring Blind flanges.W/930615 Ltr ML20045B9311993-06-10010 June 1993 LER 93-013-00:on 930514,fire Watch Was Not Performed within Time Frame Required by Tech Specs Due to Inadequate Supervision by Fire Protection Foreman.Fire Watch Patrol reestablished.W/930610 Ltr ML20045A7261993-06-0707 June 1993 LER 93-011-00:on 930507,discovered That Fire Barrier Breached W/O Proper Compensatory Measures Established.On 930505,door Leading to Room Housing Containment Spray HX 1A Breached.Roving Fire Watch Established & LCO 3.7.12 Entered ML20044H4501993-06-0303 June 1993 LER 93-012-00:on 930504,apparent Failure to Properly Identify & Plug SG Tube Determined to Exceed TS Plugging Limit.Caused by eddy-current Coordinator Not Ensuring Task requirements.Eddy-current Procedure revised.W/930603 Ltr ML20044H1561993-05-28028 May 1993 LER 93-010-00:on 930430,Westinghouse Identified Error in Development of Calculations for Cold Overpressure Mitigation Sys Setpoints.Caused by Vendor Failure to Consider Elevation Difference.Engineering Evaluation Performed ML20044E6341993-05-17017 May 1993 LER 93-009-00:on 930417,TS Surveillance Not Performed for Three Pipe Support Snubbers Because of Omission of Snubbers from Surveillance Instruction for Visual Insp.Snubbers Visually Inspected & Functionally tested.W/930517 Ltr ML20044B6751993-02-23023 February 1993 LER 93-001-00:on 930124,Unit 1 Ice Bed Temperature Recorder in MCR Declared Inoperable.Caused by Ineffective Communication.Appropriate Personnel Involved W/Event Have Been counseled.W/930223 Ltr ML20044B6141993-01-21021 January 1993 LER 92-026-00:on 921222,determined That Several ASME Section XI Pressure Tests Not Performed Due to Section XI Program Implementation Not Being well-defined,controlled or Documented.Test Expeditiously performed.W/930121 Ltr ML20024H2441991-05-22022 May 1991 LER 91-007-00:on 910422,LCO 3.0.3 Entered When Shaft of Train a Main Control Room Air Handling Unit Failed from Fatigue & Train B Out of Svc for Maint.Caused by Shaft Misalignment.New Shaft installed.W/910522 Ltr ML20029C1761991-03-21021 March 1991 LER 91-002-00:on 910211,unit Operated in Condition Prohibited by Tech Spec 3.3.3.8 Limiting Condition for Operation.Cause Under Investigation.Night Order Issued to Personnel Re Removal of Equipment from svc.W/910321 Ltr ML20029C1231991-03-18018 March 1991 LER 90-016-01:on 901117,determined That Calibr of Nuclear Instrumentation Sys intermediate-range Channels Set Nonconservatively.Caused by Lack of Operability Control for Rod Motion.Action Plan developed.W/910318 Ltr ML20029A6711991-02-25025 February 1991 LER 91-002-00:on 910124,LCOs 3.0.5 & 3.8.1.1 Entered When Both Trains of Emergency Gas Treatment Sys Declared Inoperable.Caused by Blown Fuse & Excessive Cycling of Air Start Sys.Fuse replaced.W/910225 Ltr ML20028H0331990-09-27027 September 1990 LER 90-019-00:on 900828,failure to Update P-250 Plant Computer Constants Resulted in Axial Flux Difference.Caused by Inadequate Procedures & Inappropriate Personnel Actions. Procedure 0-PI-NXX-092-001.0 revised.W/900927 Ltr ML20028G9201990-09-26026 September 1990 LER 90-020-00:on 900829,ventilation Sys Inoperable Due to Train B Diesel Generator Out of Svc.Caused by Stuck Microswitch Contacts on Pressure Switch 0-PS-311-172. Pressure Switch Adjusted & Returned to svc.W/900926 Ltr ML20044A9361990-07-0909 July 1990 LER 90-011-00:on 900608,determined That Actual Nuclear Instrumentation Sys Power Range Detector Currents Were 20% to 31% Lower than Predicted.Caused by Calibr Values Being Incorrectly Calculated.Channels corrected.W/900709 Ltr ML20044A3241990-06-25025 June 1990 LER 90-010-00:on 900526,limiting Condition for Operation Entered Because MSIV Failed to Close When Another MSIV Inoperable for Maint.Cause Attributed to Valve Stem & Valve Guide Binding.Operations Training Ltr issued.W/900625 Ltr ML20043H5091990-06-21021 June 1990 LER 90-009-00:on 900527,automatic Start of Auxiliary Feedwater Pumps Occurred When Both Main Feedwater Pumps Placed in Tripped Condition.Caused by Personnel Error.Trip Circuitry Reset & Operators counseled.W/900621 Ltr ML20043E5401990-06-0707 June 1990 LER 90-008-00:on 900514,two Control Room Isolations Occurred as Result of Spurious Spikes.Caused by Loose Terminations on Relay Socket.Loose Connections Properly terminated.W/900607 Ltr ML20043A4211990-05-16016 May 1990 LER 90-010-00:on 900416,containment Ventilation Isolation Occurred.Caused by Allowing Gaseous Radiation Level to Increase Too Close to Alarm Setpoint.Recovery from Isolation initiated.W/900516 Ltr ML20043A2261990-05-14014 May 1990 LER 90-009-00:on 900404,lower Containment Radiation Monitor Found Inoperable & Lower Containment Atmosphere Aligned to Upper Containment Radiation Monitor During Sampling.Caused by Personnel Error.Chemistry Training revised.W/900514 Ltr ML20043A2271990-05-14014 May 1990 LER 90-006-00:on 900414,auxiliary Bldg Isolation Occurred from Spent Fuel Pit Area Radiation Monitors 0-RM-90-102 & 103.Caused by Personnel Error.Training Ltr Issued to Instrument Mechanics & Operations personnel.W/900514 Ltr ML20043A2201990-05-14014 May 1990 LER 90-007-00:on 900413,discovered That Tech Spec Surveillance Requirement Not Performed within Required Interval.Caused by Personnel Error.Surveillance Successfully Performed Since missed.W/900514 Ltr ML20042G7861990-05-0909 May 1990 LER 90-005-00:on 900409,emergency Start of Four Emergency Diesel Generators Occurred While Attempting Transfer of Power.Caused by Personnel Error.Individuals Reprimanded, Training Initiated & Procedures revised.W/900509 Ltr ML20042G7931990-05-0909 May 1990 LER 90-008-00:on 900410,reactor Trip Occurred Resulting from General Warning Alarm on Both Trains of Solid State Protection Sys.Caused by Personnel Error.Individuals Disciplined & Site Wide Message distributed.W/900509 Ltr ML20042F3741990-05-0202 May 1990 LER 90-003-00:on 900404,control Room Ventilation Sys (CRVS) Transferred to Pressurization Mode.Caused by Electrical Transient in Vital Instrument Ac Bus PY-21A.CRVS Reset & Returned to Normal Operating modes.W/900502 Ltr ML20042E4191990-04-13013 April 1990 LER 90-007-00:on 900317 & 26,containment Ventilation Isolations Occurred During Purge Activities.Caused by Inadequate Procedural Guidance for Setpoint Determination. Alarm & Trip Setpoints increased.W/900413 Ltr ML20042E2021990-04-13013 April 1990 LER 90-005-00:on 900315,inadvertent Containment Vent Isolation Occurred While Preparing to Purge Containment. Caused by Lack of Attention to Detail by Operator.Operator Counseled & Received Administrative reprimand.W/900413 Ltr ML20012F5221990-04-0505 April 1990 LER 90-006-00:on 900307,containment Ventilation Isolation Occurred.Caused by Containment Particulate Level Too Close to Setpoint.Module Replaced.Radiation Alarm Setpoint Increased from 10% to 40% of Tech Spec limit.W/900406 Ltr ML20012D8611990-03-23023 March 1990 LER 90-004-00:on 900221,handswitches Controlling Operation of Isolation Valves on Steam Supply Line to Auxiliary Feedwater Pump Found in Manual Position.Cause Undetermined. Handswitches Placed in P-auto position.W/900323 Ltr ML20012C4271990-03-12012 March 1990 LER 90-003-00:on 900211,inadvertent Containment Vent Isolation Occurred.Caused by Lack of Attention to Detail in That Operator Did Not Look Closely Enough at Switch Designations.Personnel Involved counseled.W/900312 Ltr ML20011F7191990-03-0101 March 1990 LER 89-031-01:on 891205,RHR Pumps Determined to Have Deadheading Problem Identified by NRC Bulletin 88-004.Caused by Inadequate Technical Response to Bulletin.Training Ltr Issued to 10CFR50.59 reviewers.W/900301 Ltr ML20011F7421990-02-26026 February 1990 LER 90-002-00:on 900127,control Room Isolation Occurred When Circuit Breaker Opened Supplying Power to Radiation Monitor. Caused by Failure by Personnel to Exercise Sufficient Caution.Responsible Engineers reinstructed.W/900226 Ltr ML20011F7391990-02-26026 February 1990 LER 90-002-00:on 891122,value for Distance from Floor to Ctr Line of Level Switch 2-LS-87-21 Transposed in Variable Leg Calculation.Caused by Inattention to Detail.Procedure Revised to Replace Incorrect setpoint.W/900226 Ltr ML20006E3311990-02-0909 February 1990 LER 90-001-00:on 900112,Limiting Condition for Operation 3.0.3 Entered When Three of Four Lower Compartment Cooler Fan Motors Exceeded Lubrication Frequency.Caused by Personnel Error.Personnel counseled.W/900209 Ltr ML20006D5341990-02-0707 February 1990 LER 90-001-00:on 900108,discovered That Several ERCW Valves Not Being Periodically Verified to Be Correct.Caused by Personnel Error During Procedure Revs & Workplan Reviews. Info Notice Issued to Workplan reviewers.W/900207 Ltr ML19354E1631990-01-22022 January 1990 LER 89-036-00:on 891221,discovered That Surveillance Test Results Used for Declaring Diesel Generator 1B-B Operable Deficient.Caused by Instruction Not Including 60 Minute Run Time.Event Will Be Reviewed w/supervisors.W/900122 Ltr ML19354D8941990-01-16016 January 1990 LER 89-034-00:on 891215,leak Identified from Fitting on Vol Control Tank Level Transmitter & Auxiliary Bldg Evacuated, Preventing Fire Watch Patrol from Entering Bldg for Hourly Rounds.Fitting tightened.W/900116 Ltr ML19354D9061990-01-16016 January 1990 LER 89-033-00:on 891216,refueling Water Storage Tank Level Transmitters Failed High Due to Freezing from Extremely Cold Weather & Inappropriate Use of Calculations.Engineering Procedures Revised & Heating Installed in encl.W/900116 Ltr ML20005F8851990-01-0909 January 1990 LER 89-035-00:on 891210,turbine/reactor Trip Occurred from hi-hi Feedwater Level of 75% in Steam Generator 3.Caused by Failure of Loop 3 Main Feedwater Regulating Valve to Close. Equipment Adjusted & repaired.W/900109 Ltr ML20005E0801989-12-22022 December 1989 LER 89-032-00:on 891205,RHR Pumps Determined to Have Deadheading Problem,Per NRC Bulletin 88-004,resulting in Plant Operation Outside Design Basis.On 891128,RHR Pump Exceeded Head Criteria.Pumps started.W/891222 Ltr ML20005E0831989-12-22022 December 1989 LER 89-032-00:on 891201,discovered That Tech Spec Surveillance Requirement to Verify That Valves 1-67-748 & 2-67-748 in Open Position Not Met.Caused by Personnel Error.Correct Valve Position verified.W/891222 Ltr ML20005E1161989-12-22022 December 1989 LER 89-030-00:on 891204,fire Suppression Sys Deluge Valve Isolated More than 1 H W/O Required Continuous Fire Watch Establishment.Caused by Personal Communication Breakdown. Valve Opened & Foreman in Charge counseled.W/891222 Ltr 1994-05-09
[Table view] Category:RO)
MONTHYEARML20029E3351994-05-10010 May 1994 LER 94-006-00:on 940415,both Trains of CREVS Declared Inoperable.Caused by Tornado Warning & Sighting of Tornado Moving Toward Plant.Tornado Warnings downgraded.W/940510 Ltr ML20029E2021994-05-0909 May 1994 LER 94-004-00:on 940408,determined That TS Pressurizer Cooldown Limit Exceeded on 930618 & Not Restored within Required Timeframe.Caused by Unanticipated Sys Interaction. SI for Check Valve Opening Tests revised.W/940509 Ltr ML20029D8151994-05-0303 May 1994 LER 94-005-00:on 940403,inadvertent Fwis Occurred.Caused by Personnel Failure to Follow Work Document Instructions. Corrective Action:Individuals Were Counseled on Requirements to Follow Work Document Instruction steps.W/940503 Ltr ML20046B8351993-07-30030 July 1993 LER 93-017-00:on 930621,discovered 24-hour Telephone Notification Had Not Been Carried Out as Required by TS LCO 3.7.11.1 Action Statement (b)(2)(a) Due to Personnel Error. NRC Informed of Missed notification.W/930730 Ltr ML20046B8501993-07-30030 July 1993 LER 93-018-00:on 930704,DG Started Due to Improper WO Planning.Restored Power to 1BB Shutdown Board & Stopped Running DGs.W/930730 Ltr ML20046A4691993-07-19019 July 1993 LER 93-016-00:on 930619,Phase A,Auxiliary Bldg & Containment Isolations Manually Initiated as Result of Fuel Assembly Failing to Remain in Upright Position After Being Released. All Fuel Movement stopped.W/930719 Ltr ML20045J0111993-07-14014 July 1993 LER 93-015-00:on 930614,1A Start Bus Alternate Feeder Breaker Tripped Upon Start of Unit 1 RCP Which Resulted in Start of DG Due to Current Transformer Wired Incorrectly. Restored Offsite Power & Secured Final DG.W/930714 Ltr ML20045H0171993-07-12012 July 1993 LER 93-014-00:on 930611,determined That Inadequate Ventilation Design Resulted in Potential Inoperability of Vital Power Equipment.Design Being modified.W/930712 Ltr ML20045B9951993-06-15015 June 1993 LER 93-004-01:on 930222,determined That Blind Flange on Elevation 734 Personnel Airlock Outer Housing Leaking.Due to Improper Installation of Blind Flange.Evaluation Performed of Other 14 Double O-ring Blind flanges.W/930615 Ltr ML20045B9311993-06-10010 June 1993 LER 93-013-00:on 930514,fire Watch Was Not Performed within Time Frame Required by Tech Specs Due to Inadequate Supervision by Fire Protection Foreman.Fire Watch Patrol reestablished.W/930610 Ltr ML20045A7261993-06-0707 June 1993 LER 93-011-00:on 930507,discovered That Fire Barrier Breached W/O Proper Compensatory Measures Established.On 930505,door Leading to Room Housing Containment Spray HX 1A Breached.Roving Fire Watch Established & LCO 3.7.12 Entered ML20044H4501993-06-0303 June 1993 LER 93-012-00:on 930504,apparent Failure to Properly Identify & Plug SG Tube Determined to Exceed TS Plugging Limit.Caused by eddy-current Coordinator Not Ensuring Task requirements.Eddy-current Procedure revised.W/930603 Ltr ML20044H1561993-05-28028 May 1993 LER 93-010-00:on 930430,Westinghouse Identified Error in Development of Calculations for Cold Overpressure Mitigation Sys Setpoints.Caused by Vendor Failure to Consider Elevation Difference.Engineering Evaluation Performed ML20044E6341993-05-17017 May 1993 LER 93-009-00:on 930417,TS Surveillance Not Performed for Three Pipe Support Snubbers Because of Omission of Snubbers from Surveillance Instruction for Visual Insp.Snubbers Visually Inspected & Functionally tested.W/930517 Ltr ML20044B6751993-02-23023 February 1993 LER 93-001-00:on 930124,Unit 1 Ice Bed Temperature Recorder in MCR Declared Inoperable.Caused by Ineffective Communication.Appropriate Personnel Involved W/Event Have Been counseled.W/930223 Ltr ML20044B6141993-01-21021 January 1993 LER 92-026-00:on 921222,determined That Several ASME Section XI Pressure Tests Not Performed Due to Section XI Program Implementation Not Being well-defined,controlled or Documented.Test Expeditiously performed.W/930121 Ltr ML20024H2441991-05-22022 May 1991 LER 91-007-00:on 910422,LCO 3.0.3 Entered When Shaft of Train a Main Control Room Air Handling Unit Failed from Fatigue & Train B Out of Svc for Maint.Caused by Shaft Misalignment.New Shaft installed.W/910522 Ltr ML20029C1761991-03-21021 March 1991 LER 91-002-00:on 910211,unit Operated in Condition Prohibited by Tech Spec 3.3.3.8 Limiting Condition for Operation.Cause Under Investigation.Night Order Issued to Personnel Re Removal of Equipment from svc.W/910321 Ltr ML20029C1231991-03-18018 March 1991 LER 90-016-01:on 901117,determined That Calibr of Nuclear Instrumentation Sys intermediate-range Channels Set Nonconservatively.Caused by Lack of Operability Control for Rod Motion.Action Plan developed.W/910318 Ltr ML20029A6711991-02-25025 February 1991 LER 91-002-00:on 910124,LCOs 3.0.5 & 3.8.1.1 Entered When Both Trains of Emergency Gas Treatment Sys Declared Inoperable.Caused by Blown Fuse & Excessive Cycling of Air Start Sys.Fuse replaced.W/910225 Ltr ML20028H0331990-09-27027 September 1990 LER 90-019-00:on 900828,failure to Update P-250 Plant Computer Constants Resulted in Axial Flux Difference.Caused by Inadequate Procedures & Inappropriate Personnel Actions. Procedure 0-PI-NXX-092-001.0 revised.W/900927 Ltr ML20028G9201990-09-26026 September 1990 LER 90-020-00:on 900829,ventilation Sys Inoperable Due to Train B Diesel Generator Out of Svc.Caused by Stuck Microswitch Contacts on Pressure Switch 0-PS-311-172. Pressure Switch Adjusted & Returned to svc.W/900926 Ltr ML20044A9361990-07-0909 July 1990 LER 90-011-00:on 900608,determined That Actual Nuclear Instrumentation Sys Power Range Detector Currents Were 20% to 31% Lower than Predicted.Caused by Calibr Values Being Incorrectly Calculated.Channels corrected.W/900709 Ltr ML20044A3241990-06-25025 June 1990 LER 90-010-00:on 900526,limiting Condition for Operation Entered Because MSIV Failed to Close When Another MSIV Inoperable for Maint.Cause Attributed to Valve Stem & Valve Guide Binding.Operations Training Ltr issued.W/900625 Ltr ML20043H5091990-06-21021 June 1990 LER 90-009-00:on 900527,automatic Start of Auxiliary Feedwater Pumps Occurred When Both Main Feedwater Pumps Placed in Tripped Condition.Caused by Personnel Error.Trip Circuitry Reset & Operators counseled.W/900621 Ltr ML20043E5401990-06-0707 June 1990 LER 90-008-00:on 900514,two Control Room Isolations Occurred as Result of Spurious Spikes.Caused by Loose Terminations on Relay Socket.Loose Connections Properly terminated.W/900607 Ltr ML20043A4211990-05-16016 May 1990 LER 90-010-00:on 900416,containment Ventilation Isolation Occurred.Caused by Allowing Gaseous Radiation Level to Increase Too Close to Alarm Setpoint.Recovery from Isolation initiated.W/900516 Ltr ML20043A2261990-05-14014 May 1990 LER 90-009-00:on 900404,lower Containment Radiation Monitor Found Inoperable & Lower Containment Atmosphere Aligned to Upper Containment Radiation Monitor During Sampling.Caused by Personnel Error.Chemistry Training revised.W/900514 Ltr ML20043A2271990-05-14014 May 1990 LER 90-006-00:on 900414,auxiliary Bldg Isolation Occurred from Spent Fuel Pit Area Radiation Monitors 0-RM-90-102 & 103.Caused by Personnel Error.Training Ltr Issued to Instrument Mechanics & Operations personnel.W/900514 Ltr ML20043A2201990-05-14014 May 1990 LER 90-007-00:on 900413,discovered That Tech Spec Surveillance Requirement Not Performed within Required Interval.Caused by Personnel Error.Surveillance Successfully Performed Since missed.W/900514 Ltr ML20042G7861990-05-0909 May 1990 LER 90-005-00:on 900409,emergency Start of Four Emergency Diesel Generators Occurred While Attempting Transfer of Power.Caused by Personnel Error.Individuals Reprimanded, Training Initiated & Procedures revised.W/900509 Ltr ML20042G7931990-05-0909 May 1990 LER 90-008-00:on 900410,reactor Trip Occurred Resulting from General Warning Alarm on Both Trains of Solid State Protection Sys.Caused by Personnel Error.Individuals Disciplined & Site Wide Message distributed.W/900509 Ltr ML20042F3741990-05-0202 May 1990 LER 90-003-00:on 900404,control Room Ventilation Sys (CRVS) Transferred to Pressurization Mode.Caused by Electrical Transient in Vital Instrument Ac Bus PY-21A.CRVS Reset & Returned to Normal Operating modes.W/900502 Ltr ML20042E4191990-04-13013 April 1990 LER 90-007-00:on 900317 & 26,containment Ventilation Isolations Occurred During Purge Activities.Caused by Inadequate Procedural Guidance for Setpoint Determination. Alarm & Trip Setpoints increased.W/900413 Ltr ML20042E2021990-04-13013 April 1990 LER 90-005-00:on 900315,inadvertent Containment Vent Isolation Occurred While Preparing to Purge Containment. Caused by Lack of Attention to Detail by Operator.Operator Counseled & Received Administrative reprimand.W/900413 Ltr ML20012F5221990-04-0505 April 1990 LER 90-006-00:on 900307,containment Ventilation Isolation Occurred.Caused by Containment Particulate Level Too Close to Setpoint.Module Replaced.Radiation Alarm Setpoint Increased from 10% to 40% of Tech Spec limit.W/900406 Ltr ML20012D8611990-03-23023 March 1990 LER 90-004-00:on 900221,handswitches Controlling Operation of Isolation Valves on Steam Supply Line to Auxiliary Feedwater Pump Found in Manual Position.Cause Undetermined. Handswitches Placed in P-auto position.W/900323 Ltr ML20012C4271990-03-12012 March 1990 LER 90-003-00:on 900211,inadvertent Containment Vent Isolation Occurred.Caused by Lack of Attention to Detail in That Operator Did Not Look Closely Enough at Switch Designations.Personnel Involved counseled.W/900312 Ltr ML20011F7191990-03-0101 March 1990 LER 89-031-01:on 891205,RHR Pumps Determined to Have Deadheading Problem Identified by NRC Bulletin 88-004.Caused by Inadequate Technical Response to Bulletin.Training Ltr Issued to 10CFR50.59 reviewers.W/900301 Ltr ML20011F7421990-02-26026 February 1990 LER 90-002-00:on 900127,control Room Isolation Occurred When Circuit Breaker Opened Supplying Power to Radiation Monitor. Caused by Failure by Personnel to Exercise Sufficient Caution.Responsible Engineers reinstructed.W/900226 Ltr ML20011F7391990-02-26026 February 1990 LER 90-002-00:on 891122,value for Distance from Floor to Ctr Line of Level Switch 2-LS-87-21 Transposed in Variable Leg Calculation.Caused by Inattention to Detail.Procedure Revised to Replace Incorrect setpoint.W/900226 Ltr ML20006E3311990-02-0909 February 1990 LER 90-001-00:on 900112,Limiting Condition for Operation 3.0.3 Entered When Three of Four Lower Compartment Cooler Fan Motors Exceeded Lubrication Frequency.Caused by Personnel Error.Personnel counseled.W/900209 Ltr ML20006D5341990-02-0707 February 1990 LER 90-001-00:on 900108,discovered That Several ERCW Valves Not Being Periodically Verified to Be Correct.Caused by Personnel Error During Procedure Revs & Workplan Reviews. Info Notice Issued to Workplan reviewers.W/900207 Ltr ML19354E1631990-01-22022 January 1990 LER 89-036-00:on 891221,discovered That Surveillance Test Results Used for Declaring Diesel Generator 1B-B Operable Deficient.Caused by Instruction Not Including 60 Minute Run Time.Event Will Be Reviewed w/supervisors.W/900122 Ltr ML19354D8941990-01-16016 January 1990 LER 89-034-00:on 891215,leak Identified from Fitting on Vol Control Tank Level Transmitter & Auxiliary Bldg Evacuated, Preventing Fire Watch Patrol from Entering Bldg for Hourly Rounds.Fitting tightened.W/900116 Ltr ML19354D9061990-01-16016 January 1990 LER 89-033-00:on 891216,refueling Water Storage Tank Level Transmitters Failed High Due to Freezing from Extremely Cold Weather & Inappropriate Use of Calculations.Engineering Procedures Revised & Heating Installed in encl.W/900116 Ltr ML20005F8851990-01-0909 January 1990 LER 89-035-00:on 891210,turbine/reactor Trip Occurred from hi-hi Feedwater Level of 75% in Steam Generator 3.Caused by Failure of Loop 3 Main Feedwater Regulating Valve to Close. Equipment Adjusted & repaired.W/900109 Ltr ML20005E0801989-12-22022 December 1989 LER 89-032-00:on 891205,RHR Pumps Determined to Have Deadheading Problem,Per NRC Bulletin 88-004,resulting in Plant Operation Outside Design Basis.On 891128,RHR Pump Exceeded Head Criteria.Pumps started.W/891222 Ltr ML20005E0831989-12-22022 December 1989 LER 89-032-00:on 891201,discovered That Tech Spec Surveillance Requirement to Verify That Valves 1-67-748 & 2-67-748 in Open Position Not Met.Caused by Personnel Error.Correct Valve Position verified.W/891222 Ltr ML20005E1161989-12-22022 December 1989 LER 89-030-00:on 891204,fire Suppression Sys Deluge Valve Isolated More than 1 H W/O Required Continuous Fire Watch Establishment.Caused by Personal Communication Breakdown. Valve Opened & Foreman in Charge counseled.W/891222 Ltr 1994-05-09
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20212J6311999-10-0101 October 1999 SER Accepting Request for Relief from ASME Boiler & Pressure Vessel Code,Section Xi,Requirements for Certain Inservice Insp at Plant,Unit 1 ML20217G3721999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Sequoyah Nuclear Plant.With ML20212F0831999-09-23023 September 1999 Safety Evaluation Granting Relief from Certain Weld Insp at Sequoyah Nuclear Plant,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(ii) for Second 10-year ISI Interval ML20212F4761999-09-23023 September 1999 Safety Evaluation Supporting Amends 246 & 237 to Licenses DPR-77 & DPR-79,respectively ML20212C4761999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Sequoyah Nuclear Plant.With ML20210L4361999-08-0202 August 1999 Cycle 9 12-Month SG Insp Rept ML20216E3781999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20210L4451999-07-31031 July 1999 Unit-2 Cycle 10 Voltage-Based Repair Criteria 90-Day Rept ML20210G6631999-07-28028 July 1999 Cycle 9 90-Day ISI Summary Rept ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20209H3831999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Sequoyah Nuclear Plant.With ML20211F9031999-06-30030 June 1999 Cycle 9 Refueling Outage ML20196J8521999-06-28028 June 1999 Safety Evaluation Authorizing Proposed Alternative to Use Iqis for Radiography Examinations as Provided for in ASME Section III,1992 Edition with 1993 Addenda,Pursuant to 10CFR50.55a(a)(3)(i) ML20195K2951999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20206Q8951999-05-0505 May 1999 Rev 0 to L36 990415 802, COLR for Sequoyah Unit 2 Cycle 10 ML20206R5031999-04-30030 April 1999 Monthly Operating Repts for April 1999 for Sequoyah Units 1 & 2.With ML20205P9811999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20204C3111999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20205B6631999-02-28028 February 1999 Underground Storage Tank (Ust) Permanent Closure Rept, Sequoyah Nuclear Plant Security Backup DG Ust Sys ML20203H7381999-02-18018 February 1999 Safety Evaluation of Topical Rept BAW-2328, Blended U Lead Test Assembly Design Rept. Rept Acceptable Subj to Listed Conditions ML20211A2021999-01-31031 January 1999 Non-proprietary TR WCAP-15129, Depth-Based SG Tube Repair Criteria for Axial PWSCC Dented TSP Intersections ML20198S7301998-12-31031 December 1998 Cycle 10 Voltage-Based Repair Criteria 90-Day Rept ML20199G3641998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20197J5621998-12-0303 December 1998 Unit 1 Cycle 9 90-Day ISI Summary Rept ML20197K1161998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20195F8061998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Sequoyah Nuclear Plant.With ML20154H6091998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20154H6251998-09-17017 September 1998 Rev 0 to Sequoyah Nuclear Plant Unit 1 Cycle 10 Colr ML20153B0881998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Sequoyah Nuclear Plant.With ML20239A0631998-08-27027 August 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Sequoyah Nuclear Plant,Units 1 & 2 ML20236Y2091998-08-0707 August 1998 Safety Evaluation Accepting Relief Requests RP-03,RP-05, RP-07,RV-05 & RV-06 & Denying RV-07 & RV-08 ML20237B5221998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Snp ML20237A4411998-07-31031 July 1998 Blended Uranium Lead Test Assembly Design Rept ML20236P6441998-07-10010 July 1998 LER 98-S01-00:on 980610,failure of Safeguard Sys Occurred for Which Compensatory Measures Were Not Satisfied within Required Time Period.Caused by Inadequate Security Procedure.Licensee Revised Procedure MI-134 ML20236R0051998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Sequoyah Nuclear Plant ML20249A8981998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Sequoyah Nuclear Plant,Units 1 & 2 ML20247L5141998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Sequoyah Nuclear Plant ML20217K4471998-04-27027 April 1998 Safety Evaluation Supporting Requests for Relief 1-ISI-2 (Part 1),2-ISI-2 (Part 2),1-ISI-5,2-ISI-5,1-ISI-6,1-ISI-7, 2-ISI-7,ISPT-02,ISPT-04,ISPT-06,ISPT-07,ISPT-8,ISPT-01 & ISPT-05 ML20217E2221998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Sequoyah Nuclear Plant ML20248L2611998-02-28028 February 1998 Monthly Operating Repts for Sequoyah Nuclear Plant,Units 1 & 2 ML20199J2571998-01-31031 January 1998 Cycle 9 Voltage-Based Repair Criteria 90-Day Rept ML20202J7911998-01-31031 January 1998 Monthly Operating Repts for Jan 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20199J2441998-01-29029 January 1998 Snp Unit 2 Cycle Refueling Outage Oct 1997 ML20199F8531998-01-13013 January 1998 ASME Section XI Inservice Insp Summary Rept for Snp Unit 2 Refueling Outage Cycle 8 ML20199A2931997-12-31031 December 1997 Revised Monthly Operating Rept for Dec 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20198M1481997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20197J1011997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20199C2951997-11-13013 November 1997 LER 97-S01-00:on 971017,vandalism of Electrical Cables Was Observed.Caused by Vandalism.Repaired Damaged Cables, Interviewed Personnel Having Potential for Being in Area at Time Damage Occurred & Walkdowns ML20199C7201997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Sequoyah Nuclear Plant L-97-215, SG Secondary Side Loose Object Safety Evaluation1997-10-23023 October 1997 SG Secondary Side Loose Object Safety Evaluation 1999-09-30
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Tennessee vanev Autnanty, Post once 90,2000, sovity-omy. Tennessee 37379-2000 Ken Powers Vco Prescent. Sm.oyt Nxkrar Plant May 3, 1994 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555 Gentlemen:
TENNESSEE VALLEY AUTHORITY - SEQUOYAH NUCLEAR PLANT UNIT 1 - DOCKET NO. 50-327 - FACILITY OPERATING LICENSE DPR LICENSEE EVENT REPORT (LER) 50-327/94005 The enclosed LER provides details concerning inadvertent feedwater isolations that occurred during the preparation for unit start-up. These events are being reported in accordance with 10 CFR 50.73(a)(2)(iv) as automatic engineered safety feature actuations.
Sincerel ,
]
Ken Powers Enclosure i cc: See page 2 l
l i
i IC00'? 4 i S
9405100139 940503 g PDR ADOCK 05000327 PDR u S 4
U.S. Nuclear Regulatory Commission Page 2 May 3, 1994 cc (Enclosure):
INFO Records Center Institute of Nuclear Power Operations 700 Galleria Parkway Atlanta, Georgia 30339-5957 Mr. D. E. LaBarge, Project Manager U.S. Nuclear Regulatory Commission One White Flint, North 11555 Rockville Pike Rockville, Maryland 20852-2739 NRC Resident Inspector Sequoyah Nuclear Plant l 2600 Igou Ferry Road Soddy-Daisy, Tennessee 37379-3624 Regional Administrator i U.S. Nuclear Regulatory Commission l Region II 101 Marietta Street, NW, Suite 2900 Atlanta, Georgia 30323-2711
NRC form 366 U.S. NUCLEAR REGULATORY COMMISSION Approved OMB No. 3150-0104 (5-92) Expires 5/31/95 LICENSEE EVENT REPORT (LER)
FACILI1Y NAME (1) lDOCKETNUMBER(2) l f.AGL13L
_Segqgy3h_Naglgar PlanilSQt{L_Unli 1 IQl5j0lalRj3JLlLlll0LLOL1 TITLE (4)
_1nadvertent fer.dwa.ter Isolations (FWIs) DRrlDS Er.tPAIAllon for Unit Start-ug
_EvfftT_ DAY (5) 1 LER HU!iBER (6) LR_f PQRT DATE (7) l OTHER FACILITIES INVQ1XLQ_13) l l l l l$EQUENTIALl l REVISION l l l l FACILITY NAMES lDOCKETNUMBER(S)
MQNlti[ DAY l YEA 8_jyJA.R_kj__NytiQER l [JVfLDELitmwLOALirIA8_I 10151010L1 II I l 1 LI l_I I l l I 1 014101319141914l l0l015l l 0 1 0 1 01 51 01 31 91 41 __10]1LQ10lallI OPERATING l lTHISREPORTISSUBMITTEDPURSUANTTOTHEREQUIREMENTSOf10CFR%:
MODE l l_[Chesk_Que_Qr_ mart _Qf thel 0llRwin9Mlli (9) l 31 l20.402(b) l_l20.405(c) lMl50.73(a)(2)(iv) l_l73.71(b)
POWER l L_l20.405(a)(1)(1) l_l50.36(c)(1) Ll50.73(a)(2)(v) l_l73.71(c)
LEVEL l l_l20.405(a)(1)(ii) l_l50.36(c)(2) l_]S0.73(a)(2)(vil) l_l0THER(Specifyin
__[10) 10 10 10_L_ l20.405( a)(1 )( l i i ) l_l50.73(a)(2)(i) l_l50.73(a)(2)(viii)(A) l Abstract below and in l_l20.405(a)(1)(iv) l_l50.73(a)(2)(li) l_l50.73(a)(2)(viii)(B) l Text, NRC form 366A)
L_lzoaasta)(1)(v) I istL22Laitziliii) I 15L231anzux) I LICENSEE CONTACT FOR THIS LER (12)
NAME l TELEPHONE _NVliHER lAREACODEl Alairanewski . Compliante_Lirensing LLLLLLLa_LLLLI - LLl_LL4J1 COMPLETE ON.LLlL4E FOR EACH COMPQNEtiLf.A11URLDESfRLSED_LN THIS REPORT (13) l l l l REPORTABLE l l l l l l REPORTABLE l C AUS E} $ Y S T E M I COMPQNENL} MANUF AC T URER L10_1EPRQS_L [CAustl31sIEt1LCOMPONENT lMANVfAClyRE8j_IQ_NERpll I I I I I I I I I I I X LAl A l BilLRLkWLlllLLI Y I I I 1 i i I L_L_1 I I I I I I l 1 l 1 l l 1 I l 11 I I I I l_j i I I I _1 11 I I 1_11 1 J l I l
_ SUP_P1E!1LNI ALREEDR13XELCIED _114 ) l LXPECTED lLiQN_TE LRALLY{AL
__ L__ l SUBMISSION l l l l YES (If ves. (pmplete EXPECTEDJURM1331(LN_DAIE) l X l N0 j DATE (15) L_L_LL_1 I ABSTRACT (Limit to 1400 spaces, i.e.. approximately fifteen single-space typewritten lines) (16)
On April 3, 1994, at 1024 and 1840 Eastern daylight time (EDT) and on April 9, 1994, at 0239 EDT with Unit 1 in hot standby (Mode 3), inadvertent FWIs occurred. The first event occurred during troubleshooting activities with the reactor trip breaker (RTB) auxiliary contacts as a result of personnel's failure to follow the work instruction.
The involved individuals were counseled on the requirements to follow work document instruction steps. The second event occurred upon closure of the RTBs in the preparation for rod-drop testing. The subsequent testing and inspection of the breaker did not confirm the root cause of the spurious WI. Test instrumentation data indicated that the signal may have been created by voltage spikes during movement of the auxiliary switch rotary contacts as the breaker traveled to the closed position. The third event occurred during observation of the RTB after one of the two RTBs failed to close. While explaining an observed difference between two breaker-locking levers, an individual inadvertently moved the locking lever on the closed breaker. This resulted in the breaker traveling to the open position and the initiation of an FWI. The cause of the event was personnel error. The appropriate disciplinary action was taken with the involved individual. Both RTBs were replaced. The replacement breakers were inspected, tested, and placed in service.
NRC Form 366(6-89)
I NRC Form 366A U.S. NUCLEsR REGULATORY COMMISSION Approved OMB No. 3150-0104 (5-92) Expires 5/31/95 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) lDOCKETNUMBER(2) l LER N1LMQER (6) l l PA$E (3) l l l l SEQUENTIAL l l REVISION l l l l l Sequoyah Nuclear Plant (SQN), Unit 1 l [YH Bj _j_j M ER l _lJiMEL1 l l l l
[QJ3]Q.l0LQ13 12 17 19_LLl--I O l 0 1 5 l-!_D I Ol_0]_Zj0Fl017 TEXT (If more space is required, use additional NRC Form 366A's) (17)
I. PLANT CONDITIONS Unit I was in hot standby, Mode 3, for the three events.
II. DESCRIPTION OF L.ENT A. Etents Event No. 1 On April 3, 1994, at 1024 Eastern daylight time (EDT), an inadvertent feedwater isolation (WI) occurred. The event occurred during the performance of troubleshooting activities associated with the reactor trip breaker (RTB) (EIIS Code AA) auxiliary contacts. During testing of the contacts for voltage and resistance, the mechanics connected the test equipment to the wrong set of contacts, resulting in the initiation of an FWI signal. The engineered safety feature actuation was discussed between the control room operators and the mechanics, and the control room operators determined that the actuation was addressed by work document precautionary notes. Because the potential for an WI actuation was identified in the work document, it was determined that the event was not required to be called in to NRC (event notification under 10 CFR 50.72). After the troubleshooting of the RTB subsequent to Event No. 2, reportability was reevaluated and it was determined that the FWI inadvertently actuated by the mechanics was reportable. The confusion associated with event reportability stemmed from the belief that the precautionary note contained in the procedure implied that the WI actuation was part of a preplanned sequence of events.
Event No. 2 i On April 3, 1994, at 1840 EDT, an inadvertent WI occurred. The event occurred upon closure of the RTBs (EIIS Code AA) in preparation for rod (EIIS Code i AA)-drop testing. As the RTBs traveled closed, a spurious FWI signal was generated by one of the two RTBs.
Event No. 3 On April 9, 1994, at 0239 EDT, an inadvertent FWI occurred. The event occurred during observation of the RTBs (EIIS Code AA) after one of the two RTBs failed to close. Before the event, the control room operator attempted to close the RTBs in the preparation for rod-drop testing. When the operato'r initiated RTB closure, one of the two RTBs failed to close. Operations personnel proceeded to the breaker compartment area to examine the breakers. While explaining an observed difference between the two breaker-locking levers, an individual inadvertently moved the locking lever on the closed breaker. This resulted in the breaker traveling to the open position and the initiation of an FWI.
NRC form 366(6-89)
NRC form 366A U.S. NUCLEAR REGULATORY COMMISSION Approved OMB No. 3150-0104 (5-92) Expires 5/31/95 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) lDOCKETNUMDER(2) l_ (E!LHUMQER_{bL j._ l PAGE_(3) l l l l SEQUENTIAL l l REVISION l l l l l Sequoyah Nuclear Plant (SQN), Unit 1 l (YEAR _Ll_UWDEL_LLnuMetti l l l l
[E1510.lEl0}3_lLll._[9_ld j-l_Q_[_Q_l 5 l l Q_LO_[ 01 31QEl 01 7 TEXT (If more space is required, use additional NRC Form 366A's) (17)
B. InQpe rable_ lit ruc turCS_,_CompQnen t a ,_DI_SyS tema_rnat_ cont ribu t e d_t o_the_even t Event No. 1 During routine testing of RTB "A" contacts, it was identified that a high resistance existed on the breaker's auxiliary contact that is an input to the P-4 logic of the solid-state protection system. The breaker was removed from its compartment for troubleshooting to determine the cause of the high resistance. The breaker contacts were cleaned, tested, and found to be acceptable.
Event No. 2 By the use of alarm data, it was determined that a spurious FWI signal was initiated by RTB "A" as it traveled to the closed position. Subsequent to the l event, troubleshooting was performed to determine the cause for the spurious j FWI. The breaker was repeatedly cycled with test instrumentation connected to i critical locations of the breaker and the control circuit. No anomalies were identiffed. The "A" breaker was replaced.
Event No. 3 After troubleshooting and replacement of the "A" RTB for Event No. 2 and testing of the replacement breaker, the main control room operator initiated breaker closure with the main control room handswitch. RTB "B" did not close.
It could not be determined why RTB "B" failed to close. The inspection of the "B" breaker did not identify any failed components. The "B" breaker was replaced.
C. Datea_and_Approxima.te Times oL11ajor Occurrencea April 2, 1994 RTB "A" failed breaker-contact testing on an auxiliary at 0120 EDT contact. The breaker was removed from the compartment for troubleshooting.
April 3, 1994 During troubleshooting, mechanics were in the process of at 1024 EDT taking breaker contact voltage and resistance readings.
An FWI was inadvertently initiated by the mechanics.
April 3, 1994 RTB "A" was reinstalled in its compartment and was at 1750 EDT returned to service.
April 3, 1994 The RTBs were closed. Breaker closure initiated a at 1840 EDT spurious FWI.
NRC Form 366(6-89)
NRC Form 366A U.S. NUCLEAR REGULATORY COMMISSION Approved OMB No. 3150-0104 (5-92) Enpires 5/31/95 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) lDOCKETNUMBER(2)j LER NUMBLR (6) l l PAGE_13) l l l l SEQUENTIAL l l REVISION l l l l l Sequoyah Nuclear Plant (SQN), Unit 1 l jlfARju l NUl1QER l l NILMEIR_1 l l l l 101510121213121719_I4I--I010IsI--I01 0 LaL410tL2LL TEXT (If more space is required, use additional NRC Form 366A's) (17)
April 9, 1994 The control room operator attempted to close the RTBs.
at 0227 EDT RTB "B" did not close. An assistant shift operations supervisor (AS0c' M an assistant unit operator were sent to the RTB a m to look for obvious reasons for the failure of Breaker ~a" to close.
April 9, 1994 The ASOS inadvertently moved the locking lever at 0239 EDT on RTB "A" while explaining an observed difference between RTB "A" and "B" locking levers. RTB "A" tripped open. The opening of the breaker initiated an FWI as designed.
l D. Other Systems or Secondary Functians Affectnd l
None. ;
E. tielhoLoLDisfov_ery l l
In each event, various annunciators alarmed on the main control room panels. l The control room operators determined that an FWI occurred. l l
F. Opfrat.oI_Acliona l In each event, no operator actions were required in response to the INIs.
Operations personnel reestablished long-cycle feedwater operation after the FWI signal was cleared.
G. Saf3_tv System RespanSS No safety system responses were required for the events. The equipment receiving the FWI signal responded as designed.
III. CAUSE OF EVENT A. Immadialf_CAuan Event No. 1 >
l l The immediate cause of the FWI signal was that test equipment was connected to i the wrong set of contacts.
l Event No. 2 The immediate cause of the INI was a spurious signal during the closure of the RTBs.
NRC Form 366(6-89) l
NRC Form 366A U.S. NUCLEAR REGULATORY COMMISSION Approved OMB No. 3150-0104 (5-92) Expires 5/31/95 '
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) lDOCKETNUMBER(2) I LER NUMMR_(ftl_1 l PAGE (3) l l l l SEQUENTIAL l l REVISION l l l l l Sequoyah Nuclear Plant (SQN), Unit 1 l lYEARl l NUMBER l . L.t1 UMBER l l l.l l 101510101013 12 l 7 19 14 l-l 0 1 0 l 5 l-l 0 1 0 1 01 510r1 01 7-TEXT (If more space is required, use additional NRC form 366A's) (17) ,
Event No. 3 The immediate cause of the FWI signal was the inadvertent opening of the "A" RTB.
B. Raol_Cause Event No. 1 The cause for the inadvertent FWI was personnel's failure to follow work document instructions for equipment troubleshooting. The mechanics developed the troubleshooting work. instruction and incorrectly believed that steps could be changed during implementation of the troubleshooting instruction. While performing multiple checks of the auxiliary contacts for voltage and .
resistance, an individual incorrectly connected the-test equipment to take )
l measurements from the secondary contacts in the back of the breaker cubicle instead of using the terminal strip as required by the work document. The wrong contacts were connected, resulting in the FWI actuation.
Event No. 2 The cause of the spurious signal was not confirmed. Subsequent to the event, troubleshooting was performed to determine the event's root cause. The spurious signal could not be re-created. The review of test data indicated that the FWI signal may have been initiated by voltage spikes during the movement of the breaker's auxiliary switch rotary contacts as the breaker traveled to the closed position. Discussions with the equipment supplier determined that voltage spikes are not unexpected and are.a result of minute surface irregularities of the contacts. The voltage spikes observed during equipment troubleshooting exceeded the voltage and time thresholds of the solid state protection system for logic change. By engineering judgement, it was determined that the movement of the rotary switch could have initiated the event.
Event No. 3 The cause of the equipment failure resulting in RTB "B" failing to close could not be determined. Equipment examination subsequent to the failure did not identify any hardware damage or failed components. The possible causes for the failure of the breaker to close are the failure of the inertia latch to return to its rest position or the sticking of the 52x relay contact linkage in the drop-out position.
The root cause of the tripping of the "A" RTB was personnel error. The involved individual did not perform self-checking while explaining an observed difference between the RTBs. The individual inadvertently moved a sensitive component (breaker-locking lever) within the breaker compartment.
NRC form 366(6-89)
NRC iorm 366A U.S. NUCLEAR REGULATORY COMMISSION Approved OMB No. 3150-0104 (5-92) Expires 5/31/95 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) lDOCKETNUMBER(2) I L.IR_M)MBER (61 I {__P_AJE ( 3 )
l l l l SEQUENTIAL l l REVISION l l l l l Sequoyah Nuclear Plant (SQN), Unit 1 l lYEAR l l NUMBER l l NUMBER l l l l l 1915101010!3 12 17 19 14 l - 1 0 1 0 I s 1 - 1 0 1 0 1 01 610f1J1LL TEXT (If more space is required, use additional NRC Form 366A's) (17)
C. ContIlhnting_Fac tore None.
IV. ANALYSIS OF EVENT When the unit is in power operation, an WI signal limits the amount of mass in the steam generator in the event of a main steam line break. This limits the energy of a blowdown and prevents the overcooling of the primary system. In the events described in this LER, the WI had no ef fect because the main feedwater isolation valves were closed before the WI signals were initiated. Additionally, the safety functions of the RTBs and WI logic were verified to perform as designed. At no time was there a threat to the health and safety of plant personnel or the general public.
V. CORRECTIVE ACTION A. Immediate Corrective Action No immediate corrective actions were required for the events. Operators promptly diagnosed the plant condition and took actions to restore the affected plant equipment.
B. CoIIsctive Action to Prevent Rfic.urInnce Event No. 1 The involved individuals were counseled on the requirements to follow work l document instruction steps, i Event No. 2 l
The "A" RTB was replaced. The replacement breaker was inspected, tested, i verified to operate properly, and placed in service.
The procedures that close the RTBs will be revised to require the WI reset button to be held in during the closure of the breakers.
1 Event No. 3 l The "B" RTB was replaced. The replacement breaker was inspected, tested, ,
verified to operate properly, and placed in service. The breaker that failed to close was returned to the manufacturer for inspection / evaluation. The inspection results will be reviewed for the need to develop corrective actions.
The appropriate disciplinary action was taken with the involved individual.
NRC form 366(6-89)
+ .
NRC Form 366A U.S. NUCLEAR REGULATORY COMMISSION Approved OMB No. 3150-0104 (5-92) Expires 5/31/95 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) l00CKETNUMBER(2) l LERNUtgm_(jL_l } PAGL(3) l l l l SEQUENTIAL l l REVISION l l l l l Sequoyah Nuclear Plant (SQN), Unit 1 l .llLAR_j__l_fiVMER 1 l NVWfjL1 l l l l Inisjalol0lL1L1LitlL1--LLLLI 5 l-l Ll_0_Lol_11ariaLL TEXT (If more space is required, use additional NRC form 366A's) (17)
VI. ADDITIONAL INFORMATION A. FallasLComponenis Reactor trip breaker, Westinghouse Electric Corporation Breaker Model No. DB-50.
B. PIRYious_Elmilar_ Events Event Nos. 1 and 2 A review of 17 previous FWI event LERs did not identify any similar events where the FWI was initiated as a result of the closure of the RTBs. One event (LER 327/89035) occurred during RTB testing as a result of an inadequate i procedure. The corrective action from that event would not have prevented the event described in this LER.
Event No. 3 A review of previous events identified 11 events (LERs 327/84055, 85023, 86025, 86041, 87060, 89013, 90002, 91011, 93003, 328/92011 and 94003) where the risk I I
associated with the activity being performed was not properly evaluated. Each of the events involved activities associated with sensitive equipment. The corrective actions taken for 10 of the events were specific to the individual event and would not have prevented the event described in this LER. The corrective actions taken for LER 327/93003 were of a generic nature to address the activities associated with sensitive equipment. The procedures that were ,
established and the training that was provided as a result of that event should I have prevented the event described in this LER. l VII. COMMITMENT The procedures that close the reactor trip breakers will be revised by August 22, 1994, to require the FWI reset button to be held in during the closure of the breakers.
NRC form 366(6-89)