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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029E3351994-05-10010 May 1994 LER 94-006-00:on 940415,both Trains of CREVS Declared Inoperable.Caused by Tornado Warning & Sighting of Tornado Moving Toward Plant.Tornado Warnings downgraded.W/940510 Ltr ML20029E2021994-05-0909 May 1994 LER 94-004-00:on 940408,determined That TS Pressurizer Cooldown Limit Exceeded on 930618 & Not Restored within Required Timeframe.Caused by Unanticipated Sys Interaction. SI for Check Valve Opening Tests revised.W/940509 Ltr ML20029D8151994-05-0303 May 1994 LER 94-005-00:on 940403,inadvertent Fwis Occurred.Caused by Personnel Failure to Follow Work Document Instructions. Corrective Action:Individuals Were Counseled on Requirements to Follow Work Document Instruction steps.W/940503 Ltr ML20046B8351993-07-30030 July 1993 LER 93-017-00:on 930621,discovered 24-hour Telephone Notification Had Not Been Carried Out as Required by TS LCO 3.7.11.1 Action Statement (b)(2)(a) Due to Personnel Error. NRC Informed of Missed notification.W/930730 Ltr ML20046B8501993-07-30030 July 1993 LER 93-018-00:on 930704,DG Started Due to Improper WO Planning.Restored Power to 1BB Shutdown Board & Stopped Running DGs.W/930730 Ltr ML20046A4691993-07-19019 July 1993 LER 93-016-00:on 930619,Phase A,Auxiliary Bldg & Containment Isolations Manually Initiated as Result of Fuel Assembly Failing to Remain in Upright Position After Being Released. All Fuel Movement stopped.W/930719 Ltr ML20045J0111993-07-14014 July 1993 LER 93-015-00:on 930614,1A Start Bus Alternate Feeder Breaker Tripped Upon Start of Unit 1 RCP Which Resulted in Start of DG Due to Current Transformer Wired Incorrectly. Restored Offsite Power & Secured Final DG.W/930714 Ltr ML20045H0171993-07-12012 July 1993 LER 93-014-00:on 930611,determined That Inadequate Ventilation Design Resulted in Potential Inoperability of Vital Power Equipment.Design Being modified.W/930712 Ltr ML20045B9951993-06-15015 June 1993 LER 93-004-01:on 930222,determined That Blind Flange on Elevation 734 Personnel Airlock Outer Housing Leaking.Due to Improper Installation of Blind Flange.Evaluation Performed of Other 14 Double O-ring Blind flanges.W/930615 Ltr ML20045B9311993-06-10010 June 1993 LER 93-013-00:on 930514,fire Watch Was Not Performed within Time Frame Required by Tech Specs Due to Inadequate Supervision by Fire Protection Foreman.Fire Watch Patrol reestablished.W/930610 Ltr ML20045A7261993-06-0707 June 1993 LER 93-011-00:on 930507,discovered That Fire Barrier Breached W/O Proper Compensatory Measures Established.On 930505,door Leading to Room Housing Containment Spray HX 1A Breached.Roving Fire Watch Established & LCO 3.7.12 Entered ML20044H4501993-06-0303 June 1993 LER 93-012-00:on 930504,apparent Failure to Properly Identify & Plug SG Tube Determined to Exceed TS Plugging Limit.Caused by eddy-current Coordinator Not Ensuring Task requirements.Eddy-current Procedure revised.W/930603 Ltr ML20044H1561993-05-28028 May 1993 LER 93-010-00:on 930430,Westinghouse Identified Error in Development of Calculations for Cold Overpressure Mitigation Sys Setpoints.Caused by Vendor Failure to Consider Elevation Difference.Engineering Evaluation Performed ML20044E6341993-05-17017 May 1993 LER 93-009-00:on 930417,TS Surveillance Not Performed for Three Pipe Support Snubbers Because of Omission of Snubbers from Surveillance Instruction for Visual Insp.Snubbers Visually Inspected & Functionally tested.W/930517 Ltr ML20044B6751993-02-23023 February 1993 LER 93-001-00:on 930124,Unit 1 Ice Bed Temperature Recorder in MCR Declared Inoperable.Caused by Ineffective Communication.Appropriate Personnel Involved W/Event Have Been counseled.W/930223 Ltr ML20044B6141993-01-21021 January 1993 LER 92-026-00:on 921222,determined That Several ASME Section XI Pressure Tests Not Performed Due to Section XI Program Implementation Not Being well-defined,controlled or Documented.Test Expeditiously performed.W/930121 Ltr ML20024H2441991-05-22022 May 1991 LER 91-007-00:on 910422,LCO 3.0.3 Entered When Shaft of Train a Main Control Room Air Handling Unit Failed from Fatigue & Train B Out of Svc for Maint.Caused by Shaft Misalignment.New Shaft installed.W/910522 Ltr ML20029C1761991-03-21021 March 1991 LER 91-002-00:on 910211,unit Operated in Condition Prohibited by Tech Spec 3.3.3.8 Limiting Condition for Operation.Cause Under Investigation.Night Order Issued to Personnel Re Removal of Equipment from svc.W/910321 Ltr ML20029C1231991-03-18018 March 1991 LER 90-016-01:on 901117,determined That Calibr of Nuclear Instrumentation Sys intermediate-range Channels Set Nonconservatively.Caused by Lack of Operability Control for Rod Motion.Action Plan developed.W/910318 Ltr ML20029A6711991-02-25025 February 1991 LER 91-002-00:on 910124,LCOs 3.0.5 & 3.8.1.1 Entered When Both Trains of Emergency Gas Treatment Sys Declared Inoperable.Caused by Blown Fuse & Excessive Cycling of Air Start Sys.Fuse replaced.W/910225 Ltr ML20028H0331990-09-27027 September 1990 LER 90-019-00:on 900828,failure to Update P-250 Plant Computer Constants Resulted in Axial Flux Difference.Caused by Inadequate Procedures & Inappropriate Personnel Actions. Procedure 0-PI-NXX-092-001.0 revised.W/900927 Ltr ML20028G9201990-09-26026 September 1990 LER 90-020-00:on 900829,ventilation Sys Inoperable Due to Train B Diesel Generator Out of Svc.Caused by Stuck Microswitch Contacts on Pressure Switch 0-PS-311-172. Pressure Switch Adjusted & Returned to svc.W/900926 Ltr ML20044A9361990-07-0909 July 1990 LER 90-011-00:on 900608,determined That Actual Nuclear Instrumentation Sys Power Range Detector Currents Were 20% to 31% Lower than Predicted.Caused by Calibr Values Being Incorrectly Calculated.Channels corrected.W/900709 Ltr ML20044A3241990-06-25025 June 1990 LER 90-010-00:on 900526,limiting Condition for Operation Entered Because MSIV Failed to Close When Another MSIV Inoperable for Maint.Cause Attributed to Valve Stem & Valve Guide Binding.Operations Training Ltr issued.W/900625 Ltr ML20043H5091990-06-21021 June 1990 LER 90-009-00:on 900527,automatic Start of Auxiliary Feedwater Pumps Occurred When Both Main Feedwater Pumps Placed in Tripped Condition.Caused by Personnel Error.Trip Circuitry Reset & Operators counseled.W/900621 Ltr ML20043E5401990-06-0707 June 1990 LER 90-008-00:on 900514,two Control Room Isolations Occurred as Result of Spurious Spikes.Caused by Loose Terminations on Relay Socket.Loose Connections Properly terminated.W/900607 Ltr ML20043A4211990-05-16016 May 1990 LER 90-010-00:on 900416,containment Ventilation Isolation Occurred.Caused by Allowing Gaseous Radiation Level to Increase Too Close to Alarm Setpoint.Recovery from Isolation initiated.W/900516 Ltr ML20043A2261990-05-14014 May 1990 LER 90-009-00:on 900404,lower Containment Radiation Monitor Found Inoperable & Lower Containment Atmosphere Aligned to Upper Containment Radiation Monitor During Sampling.Caused by Personnel Error.Chemistry Training revised.W/900514 Ltr ML20043A2271990-05-14014 May 1990 LER 90-006-00:on 900414,auxiliary Bldg Isolation Occurred from Spent Fuel Pit Area Radiation Monitors 0-RM-90-102 & 103.Caused by Personnel Error.Training Ltr Issued to Instrument Mechanics & Operations personnel.W/900514 Ltr ML20043A2201990-05-14014 May 1990 LER 90-007-00:on 900413,discovered That Tech Spec Surveillance Requirement Not Performed within Required Interval.Caused by Personnel Error.Surveillance Successfully Performed Since missed.W/900514 Ltr ML20042G7861990-05-0909 May 1990 LER 90-005-00:on 900409,emergency Start of Four Emergency Diesel Generators Occurred While Attempting Transfer of Power.Caused by Personnel Error.Individuals Reprimanded, Training Initiated & Procedures revised.W/900509 Ltr ML20042G7931990-05-0909 May 1990 LER 90-008-00:on 900410,reactor Trip Occurred Resulting from General Warning Alarm on Both Trains of Solid State Protection Sys.Caused by Personnel Error.Individuals Disciplined & Site Wide Message distributed.W/900509 Ltr ML20042F3741990-05-0202 May 1990 LER 90-003-00:on 900404,control Room Ventilation Sys (CRVS) Transferred to Pressurization Mode.Caused by Electrical Transient in Vital Instrument Ac Bus PY-21A.CRVS Reset & Returned to Normal Operating modes.W/900502 Ltr ML20042E4191990-04-13013 April 1990 LER 90-007-00:on 900317 & 26,containment Ventilation Isolations Occurred During Purge Activities.Caused by Inadequate Procedural Guidance for Setpoint Determination. Alarm & Trip Setpoints increased.W/900413 Ltr ML20042E2021990-04-13013 April 1990 LER 90-005-00:on 900315,inadvertent Containment Vent Isolation Occurred While Preparing to Purge Containment. Caused by Lack of Attention to Detail by Operator.Operator Counseled & Received Administrative reprimand.W/900413 Ltr ML20012F5221990-04-0505 April 1990 LER 90-006-00:on 900307,containment Ventilation Isolation Occurred.Caused by Containment Particulate Level Too Close to Setpoint.Module Replaced.Radiation Alarm Setpoint Increased from 10% to 40% of Tech Spec limit.W/900406 Ltr ML20012D8611990-03-23023 March 1990 LER 90-004-00:on 900221,handswitches Controlling Operation of Isolation Valves on Steam Supply Line to Auxiliary Feedwater Pump Found in Manual Position.Cause Undetermined. Handswitches Placed in P-auto position.W/900323 Ltr ML20012C4271990-03-12012 March 1990 LER 90-003-00:on 900211,inadvertent Containment Vent Isolation Occurred.Caused by Lack of Attention to Detail in That Operator Did Not Look Closely Enough at Switch Designations.Personnel Involved counseled.W/900312 Ltr ML20011F7191990-03-0101 March 1990 LER 89-031-01:on 891205,RHR Pumps Determined to Have Deadheading Problem Identified by NRC Bulletin 88-004.Caused by Inadequate Technical Response to Bulletin.Training Ltr Issued to 10CFR50.59 reviewers.W/900301 Ltr ML20011F7421990-02-26026 February 1990 LER 90-002-00:on 900127,control Room Isolation Occurred When Circuit Breaker Opened Supplying Power to Radiation Monitor. Caused by Failure by Personnel to Exercise Sufficient Caution.Responsible Engineers reinstructed.W/900226 Ltr ML20011F7391990-02-26026 February 1990 LER 90-002-00:on 891122,value for Distance from Floor to Ctr Line of Level Switch 2-LS-87-21 Transposed in Variable Leg Calculation.Caused by Inattention to Detail.Procedure Revised to Replace Incorrect setpoint.W/900226 Ltr ML20006E3311990-02-0909 February 1990 LER 90-001-00:on 900112,Limiting Condition for Operation 3.0.3 Entered When Three of Four Lower Compartment Cooler Fan Motors Exceeded Lubrication Frequency.Caused by Personnel Error.Personnel counseled.W/900209 Ltr ML20006D5341990-02-0707 February 1990 LER 90-001-00:on 900108,discovered That Several ERCW Valves Not Being Periodically Verified to Be Correct.Caused by Personnel Error During Procedure Revs & Workplan Reviews. Info Notice Issued to Workplan reviewers.W/900207 Ltr ML19354E1631990-01-22022 January 1990 LER 89-036-00:on 891221,discovered That Surveillance Test Results Used for Declaring Diesel Generator 1B-B Operable Deficient.Caused by Instruction Not Including 60 Minute Run Time.Event Will Be Reviewed w/supervisors.W/900122 Ltr ML19354D8941990-01-16016 January 1990 LER 89-034-00:on 891215,leak Identified from Fitting on Vol Control Tank Level Transmitter & Auxiliary Bldg Evacuated, Preventing Fire Watch Patrol from Entering Bldg for Hourly Rounds.Fitting tightened.W/900116 Ltr ML19354D9061990-01-16016 January 1990 LER 89-033-00:on 891216,refueling Water Storage Tank Level Transmitters Failed High Due to Freezing from Extremely Cold Weather & Inappropriate Use of Calculations.Engineering Procedures Revised & Heating Installed in encl.W/900116 Ltr ML20005F8851990-01-0909 January 1990 LER 89-035-00:on 891210,turbine/reactor Trip Occurred from hi-hi Feedwater Level of 75% in Steam Generator 3.Caused by Failure of Loop 3 Main Feedwater Regulating Valve to Close. Equipment Adjusted & repaired.W/900109 Ltr ML20005E0801989-12-22022 December 1989 LER 89-032-00:on 891205,RHR Pumps Determined to Have Deadheading Problem,Per NRC Bulletin 88-004,resulting in Plant Operation Outside Design Basis.On 891128,RHR Pump Exceeded Head Criteria.Pumps started.W/891222 Ltr ML20005E0831989-12-22022 December 1989 LER 89-032-00:on 891201,discovered That Tech Spec Surveillance Requirement to Verify That Valves 1-67-748 & 2-67-748 in Open Position Not Met.Caused by Personnel Error.Correct Valve Position verified.W/891222 Ltr ML20005E1161989-12-22022 December 1989 LER 89-030-00:on 891204,fire Suppression Sys Deluge Valve Isolated More than 1 H W/O Required Continuous Fire Watch Establishment.Caused by Personal Communication Breakdown. Valve Opened & Foreman in Charge counseled.W/891222 Ltr 1994-05-09
[Table view] Category:RO)
MONTHYEARML20029E3351994-05-10010 May 1994 LER 94-006-00:on 940415,both Trains of CREVS Declared Inoperable.Caused by Tornado Warning & Sighting of Tornado Moving Toward Plant.Tornado Warnings downgraded.W/940510 Ltr ML20029E2021994-05-0909 May 1994 LER 94-004-00:on 940408,determined That TS Pressurizer Cooldown Limit Exceeded on 930618 & Not Restored within Required Timeframe.Caused by Unanticipated Sys Interaction. SI for Check Valve Opening Tests revised.W/940509 Ltr ML20029D8151994-05-0303 May 1994 LER 94-005-00:on 940403,inadvertent Fwis Occurred.Caused by Personnel Failure to Follow Work Document Instructions. Corrective Action:Individuals Were Counseled on Requirements to Follow Work Document Instruction steps.W/940503 Ltr ML20046B8351993-07-30030 July 1993 LER 93-017-00:on 930621,discovered 24-hour Telephone Notification Had Not Been Carried Out as Required by TS LCO 3.7.11.1 Action Statement (b)(2)(a) Due to Personnel Error. NRC Informed of Missed notification.W/930730 Ltr ML20046B8501993-07-30030 July 1993 LER 93-018-00:on 930704,DG Started Due to Improper WO Planning.Restored Power to 1BB Shutdown Board & Stopped Running DGs.W/930730 Ltr ML20046A4691993-07-19019 July 1993 LER 93-016-00:on 930619,Phase A,Auxiliary Bldg & Containment Isolations Manually Initiated as Result of Fuel Assembly Failing to Remain in Upright Position After Being Released. All Fuel Movement stopped.W/930719 Ltr ML20045J0111993-07-14014 July 1993 LER 93-015-00:on 930614,1A Start Bus Alternate Feeder Breaker Tripped Upon Start of Unit 1 RCP Which Resulted in Start of DG Due to Current Transformer Wired Incorrectly. Restored Offsite Power & Secured Final DG.W/930714 Ltr ML20045H0171993-07-12012 July 1993 LER 93-014-00:on 930611,determined That Inadequate Ventilation Design Resulted in Potential Inoperability of Vital Power Equipment.Design Being modified.W/930712 Ltr ML20045B9951993-06-15015 June 1993 LER 93-004-01:on 930222,determined That Blind Flange on Elevation 734 Personnel Airlock Outer Housing Leaking.Due to Improper Installation of Blind Flange.Evaluation Performed of Other 14 Double O-ring Blind flanges.W/930615 Ltr ML20045B9311993-06-10010 June 1993 LER 93-013-00:on 930514,fire Watch Was Not Performed within Time Frame Required by Tech Specs Due to Inadequate Supervision by Fire Protection Foreman.Fire Watch Patrol reestablished.W/930610 Ltr ML20045A7261993-06-0707 June 1993 LER 93-011-00:on 930507,discovered That Fire Barrier Breached W/O Proper Compensatory Measures Established.On 930505,door Leading to Room Housing Containment Spray HX 1A Breached.Roving Fire Watch Established & LCO 3.7.12 Entered ML20044H4501993-06-0303 June 1993 LER 93-012-00:on 930504,apparent Failure to Properly Identify & Plug SG Tube Determined to Exceed TS Plugging Limit.Caused by eddy-current Coordinator Not Ensuring Task requirements.Eddy-current Procedure revised.W/930603 Ltr ML20044H1561993-05-28028 May 1993 LER 93-010-00:on 930430,Westinghouse Identified Error in Development of Calculations for Cold Overpressure Mitigation Sys Setpoints.Caused by Vendor Failure to Consider Elevation Difference.Engineering Evaluation Performed ML20044E6341993-05-17017 May 1993 LER 93-009-00:on 930417,TS Surveillance Not Performed for Three Pipe Support Snubbers Because of Omission of Snubbers from Surveillance Instruction for Visual Insp.Snubbers Visually Inspected & Functionally tested.W/930517 Ltr ML20044B6751993-02-23023 February 1993 LER 93-001-00:on 930124,Unit 1 Ice Bed Temperature Recorder in MCR Declared Inoperable.Caused by Ineffective Communication.Appropriate Personnel Involved W/Event Have Been counseled.W/930223 Ltr ML20044B6141993-01-21021 January 1993 LER 92-026-00:on 921222,determined That Several ASME Section XI Pressure Tests Not Performed Due to Section XI Program Implementation Not Being well-defined,controlled or Documented.Test Expeditiously performed.W/930121 Ltr ML20024H2441991-05-22022 May 1991 LER 91-007-00:on 910422,LCO 3.0.3 Entered When Shaft of Train a Main Control Room Air Handling Unit Failed from Fatigue & Train B Out of Svc for Maint.Caused by Shaft Misalignment.New Shaft installed.W/910522 Ltr ML20029C1761991-03-21021 March 1991 LER 91-002-00:on 910211,unit Operated in Condition Prohibited by Tech Spec 3.3.3.8 Limiting Condition for Operation.Cause Under Investigation.Night Order Issued to Personnel Re Removal of Equipment from svc.W/910321 Ltr ML20029C1231991-03-18018 March 1991 LER 90-016-01:on 901117,determined That Calibr of Nuclear Instrumentation Sys intermediate-range Channels Set Nonconservatively.Caused by Lack of Operability Control for Rod Motion.Action Plan developed.W/910318 Ltr ML20029A6711991-02-25025 February 1991 LER 91-002-00:on 910124,LCOs 3.0.5 & 3.8.1.1 Entered When Both Trains of Emergency Gas Treatment Sys Declared Inoperable.Caused by Blown Fuse & Excessive Cycling of Air Start Sys.Fuse replaced.W/910225 Ltr ML20028H0331990-09-27027 September 1990 LER 90-019-00:on 900828,failure to Update P-250 Plant Computer Constants Resulted in Axial Flux Difference.Caused by Inadequate Procedures & Inappropriate Personnel Actions. Procedure 0-PI-NXX-092-001.0 revised.W/900927 Ltr ML20028G9201990-09-26026 September 1990 LER 90-020-00:on 900829,ventilation Sys Inoperable Due to Train B Diesel Generator Out of Svc.Caused by Stuck Microswitch Contacts on Pressure Switch 0-PS-311-172. Pressure Switch Adjusted & Returned to svc.W/900926 Ltr ML20044A9361990-07-0909 July 1990 LER 90-011-00:on 900608,determined That Actual Nuclear Instrumentation Sys Power Range Detector Currents Were 20% to 31% Lower than Predicted.Caused by Calibr Values Being Incorrectly Calculated.Channels corrected.W/900709 Ltr ML20044A3241990-06-25025 June 1990 LER 90-010-00:on 900526,limiting Condition for Operation Entered Because MSIV Failed to Close When Another MSIV Inoperable for Maint.Cause Attributed to Valve Stem & Valve Guide Binding.Operations Training Ltr issued.W/900625 Ltr ML20043H5091990-06-21021 June 1990 LER 90-009-00:on 900527,automatic Start of Auxiliary Feedwater Pumps Occurred When Both Main Feedwater Pumps Placed in Tripped Condition.Caused by Personnel Error.Trip Circuitry Reset & Operators counseled.W/900621 Ltr ML20043E5401990-06-0707 June 1990 LER 90-008-00:on 900514,two Control Room Isolations Occurred as Result of Spurious Spikes.Caused by Loose Terminations on Relay Socket.Loose Connections Properly terminated.W/900607 Ltr ML20043A4211990-05-16016 May 1990 LER 90-010-00:on 900416,containment Ventilation Isolation Occurred.Caused by Allowing Gaseous Radiation Level to Increase Too Close to Alarm Setpoint.Recovery from Isolation initiated.W/900516 Ltr ML20043A2261990-05-14014 May 1990 LER 90-009-00:on 900404,lower Containment Radiation Monitor Found Inoperable & Lower Containment Atmosphere Aligned to Upper Containment Radiation Monitor During Sampling.Caused by Personnel Error.Chemistry Training revised.W/900514 Ltr ML20043A2271990-05-14014 May 1990 LER 90-006-00:on 900414,auxiliary Bldg Isolation Occurred from Spent Fuel Pit Area Radiation Monitors 0-RM-90-102 & 103.Caused by Personnel Error.Training Ltr Issued to Instrument Mechanics & Operations personnel.W/900514 Ltr ML20043A2201990-05-14014 May 1990 LER 90-007-00:on 900413,discovered That Tech Spec Surveillance Requirement Not Performed within Required Interval.Caused by Personnel Error.Surveillance Successfully Performed Since missed.W/900514 Ltr ML20042G7861990-05-0909 May 1990 LER 90-005-00:on 900409,emergency Start of Four Emergency Diesel Generators Occurred While Attempting Transfer of Power.Caused by Personnel Error.Individuals Reprimanded, Training Initiated & Procedures revised.W/900509 Ltr ML20042G7931990-05-0909 May 1990 LER 90-008-00:on 900410,reactor Trip Occurred Resulting from General Warning Alarm on Both Trains of Solid State Protection Sys.Caused by Personnel Error.Individuals Disciplined & Site Wide Message distributed.W/900509 Ltr ML20042F3741990-05-0202 May 1990 LER 90-003-00:on 900404,control Room Ventilation Sys (CRVS) Transferred to Pressurization Mode.Caused by Electrical Transient in Vital Instrument Ac Bus PY-21A.CRVS Reset & Returned to Normal Operating modes.W/900502 Ltr ML20042E4191990-04-13013 April 1990 LER 90-007-00:on 900317 & 26,containment Ventilation Isolations Occurred During Purge Activities.Caused by Inadequate Procedural Guidance for Setpoint Determination. Alarm & Trip Setpoints increased.W/900413 Ltr ML20042E2021990-04-13013 April 1990 LER 90-005-00:on 900315,inadvertent Containment Vent Isolation Occurred While Preparing to Purge Containment. Caused by Lack of Attention to Detail by Operator.Operator Counseled & Received Administrative reprimand.W/900413 Ltr ML20012F5221990-04-0505 April 1990 LER 90-006-00:on 900307,containment Ventilation Isolation Occurred.Caused by Containment Particulate Level Too Close to Setpoint.Module Replaced.Radiation Alarm Setpoint Increased from 10% to 40% of Tech Spec limit.W/900406 Ltr ML20012D8611990-03-23023 March 1990 LER 90-004-00:on 900221,handswitches Controlling Operation of Isolation Valves on Steam Supply Line to Auxiliary Feedwater Pump Found in Manual Position.Cause Undetermined. Handswitches Placed in P-auto position.W/900323 Ltr ML20012C4271990-03-12012 March 1990 LER 90-003-00:on 900211,inadvertent Containment Vent Isolation Occurred.Caused by Lack of Attention to Detail in That Operator Did Not Look Closely Enough at Switch Designations.Personnel Involved counseled.W/900312 Ltr ML20011F7191990-03-0101 March 1990 LER 89-031-01:on 891205,RHR Pumps Determined to Have Deadheading Problem Identified by NRC Bulletin 88-004.Caused by Inadequate Technical Response to Bulletin.Training Ltr Issued to 10CFR50.59 reviewers.W/900301 Ltr ML20011F7421990-02-26026 February 1990 LER 90-002-00:on 900127,control Room Isolation Occurred When Circuit Breaker Opened Supplying Power to Radiation Monitor. Caused by Failure by Personnel to Exercise Sufficient Caution.Responsible Engineers reinstructed.W/900226 Ltr ML20011F7391990-02-26026 February 1990 LER 90-002-00:on 891122,value for Distance from Floor to Ctr Line of Level Switch 2-LS-87-21 Transposed in Variable Leg Calculation.Caused by Inattention to Detail.Procedure Revised to Replace Incorrect setpoint.W/900226 Ltr ML20006E3311990-02-0909 February 1990 LER 90-001-00:on 900112,Limiting Condition for Operation 3.0.3 Entered When Three of Four Lower Compartment Cooler Fan Motors Exceeded Lubrication Frequency.Caused by Personnel Error.Personnel counseled.W/900209 Ltr ML20006D5341990-02-0707 February 1990 LER 90-001-00:on 900108,discovered That Several ERCW Valves Not Being Periodically Verified to Be Correct.Caused by Personnel Error During Procedure Revs & Workplan Reviews. Info Notice Issued to Workplan reviewers.W/900207 Ltr ML19354E1631990-01-22022 January 1990 LER 89-036-00:on 891221,discovered That Surveillance Test Results Used for Declaring Diesel Generator 1B-B Operable Deficient.Caused by Instruction Not Including 60 Minute Run Time.Event Will Be Reviewed w/supervisors.W/900122 Ltr ML19354D8941990-01-16016 January 1990 LER 89-034-00:on 891215,leak Identified from Fitting on Vol Control Tank Level Transmitter & Auxiliary Bldg Evacuated, Preventing Fire Watch Patrol from Entering Bldg for Hourly Rounds.Fitting tightened.W/900116 Ltr ML19354D9061990-01-16016 January 1990 LER 89-033-00:on 891216,refueling Water Storage Tank Level Transmitters Failed High Due to Freezing from Extremely Cold Weather & Inappropriate Use of Calculations.Engineering Procedures Revised & Heating Installed in encl.W/900116 Ltr ML20005F8851990-01-0909 January 1990 LER 89-035-00:on 891210,turbine/reactor Trip Occurred from hi-hi Feedwater Level of 75% in Steam Generator 3.Caused by Failure of Loop 3 Main Feedwater Regulating Valve to Close. Equipment Adjusted & repaired.W/900109 Ltr ML20005E0801989-12-22022 December 1989 LER 89-032-00:on 891205,RHR Pumps Determined to Have Deadheading Problem,Per NRC Bulletin 88-004,resulting in Plant Operation Outside Design Basis.On 891128,RHR Pump Exceeded Head Criteria.Pumps started.W/891222 Ltr ML20005E0831989-12-22022 December 1989 LER 89-032-00:on 891201,discovered That Tech Spec Surveillance Requirement to Verify That Valves 1-67-748 & 2-67-748 in Open Position Not Met.Caused by Personnel Error.Correct Valve Position verified.W/891222 Ltr ML20005E1161989-12-22022 December 1989 LER 89-030-00:on 891204,fire Suppression Sys Deluge Valve Isolated More than 1 H W/O Required Continuous Fire Watch Establishment.Caused by Personal Communication Breakdown. Valve Opened & Foreman in Charge counseled.W/891222 Ltr 1994-05-09
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20212J6311999-10-0101 October 1999 SER Accepting Request for Relief from ASME Boiler & Pressure Vessel Code,Section Xi,Requirements for Certain Inservice Insp at Plant,Unit 1 ML20217G3721999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Sequoyah Nuclear Plant.With ML20212F0831999-09-23023 September 1999 Safety Evaluation Granting Relief from Certain Weld Insp at Sequoyah Nuclear Plant,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(ii) for Second 10-year ISI Interval ML20212F4761999-09-23023 September 1999 Safety Evaluation Supporting Amends 246 & 237 to Licenses DPR-77 & DPR-79,respectively ML20212C4761999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Sequoyah Nuclear Plant.With ML20210L4361999-08-0202 August 1999 Cycle 9 12-Month SG Insp Rept ML20216E3781999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20210L4451999-07-31031 July 1999 Unit-2 Cycle 10 Voltage-Based Repair Criteria 90-Day Rept ML20210G6631999-07-28028 July 1999 Cycle 9 90-Day ISI Summary Rept ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20209H3831999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Sequoyah Nuclear Plant.With ML20211F9031999-06-30030 June 1999 Cycle 9 Refueling Outage ML20196J8521999-06-28028 June 1999 Safety Evaluation Authorizing Proposed Alternative to Use Iqis for Radiography Examinations as Provided for in ASME Section III,1992 Edition with 1993 Addenda,Pursuant to 10CFR50.55a(a)(3)(i) ML20195K2951999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20206Q8951999-05-0505 May 1999 Rev 0 to L36 990415 802, COLR for Sequoyah Unit 2 Cycle 10 ML20206R5031999-04-30030 April 1999 Monthly Operating Repts for April 1999 for Sequoyah Units 1 & 2.With ML20205P9811999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20204C3111999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20205B6631999-02-28028 February 1999 Underground Storage Tank (Ust) Permanent Closure Rept, Sequoyah Nuclear Plant Security Backup DG Ust Sys ML20203H7381999-02-18018 February 1999 Safety Evaluation of Topical Rept BAW-2328, Blended U Lead Test Assembly Design Rept. Rept Acceptable Subj to Listed Conditions ML20211A2021999-01-31031 January 1999 Non-proprietary TR WCAP-15129, Depth-Based SG Tube Repair Criteria for Axial PWSCC Dented TSP Intersections ML20198S7301998-12-31031 December 1998 Cycle 10 Voltage-Based Repair Criteria 90-Day Rept ML20199G3641998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20197J5621998-12-0303 December 1998 Unit 1 Cycle 9 90-Day ISI Summary Rept ML20197K1161998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20195F8061998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Sequoyah Nuclear Plant.With ML20154H6091998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20154H6251998-09-17017 September 1998 Rev 0 to Sequoyah Nuclear Plant Unit 1 Cycle 10 Colr ML20153B0881998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Sequoyah Nuclear Plant.With ML20239A0631998-08-27027 August 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Sequoyah Nuclear Plant,Units 1 & 2 ML20236Y2091998-08-0707 August 1998 Safety Evaluation Accepting Relief Requests RP-03,RP-05, RP-07,RV-05 & RV-06 & Denying RV-07 & RV-08 ML20237B5221998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Snp ML20237A4411998-07-31031 July 1998 Blended Uranium Lead Test Assembly Design Rept ML20236P6441998-07-10010 July 1998 LER 98-S01-00:on 980610,failure of Safeguard Sys Occurred for Which Compensatory Measures Were Not Satisfied within Required Time Period.Caused by Inadequate Security Procedure.Licensee Revised Procedure MI-134 ML20236R0051998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Sequoyah Nuclear Plant ML20249A8981998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Sequoyah Nuclear Plant,Units 1 & 2 ML20247L5141998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Sequoyah Nuclear Plant ML20217K4471998-04-27027 April 1998 Safety Evaluation Supporting Requests for Relief 1-ISI-2 (Part 1),2-ISI-2 (Part 2),1-ISI-5,2-ISI-5,1-ISI-6,1-ISI-7, 2-ISI-7,ISPT-02,ISPT-04,ISPT-06,ISPT-07,ISPT-8,ISPT-01 & ISPT-05 ML20217E2221998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Sequoyah Nuclear Plant ML20248L2611998-02-28028 February 1998 Monthly Operating Repts for Sequoyah Nuclear Plant,Units 1 & 2 ML20199J2571998-01-31031 January 1998 Cycle 9 Voltage-Based Repair Criteria 90-Day Rept ML20202J7911998-01-31031 January 1998 Monthly Operating Repts for Jan 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20199J2441998-01-29029 January 1998 Snp Unit 2 Cycle Refueling Outage Oct 1997 ML20199F8531998-01-13013 January 1998 ASME Section XI Inservice Insp Summary Rept for Snp Unit 2 Refueling Outage Cycle 8 ML20199A2931997-12-31031 December 1997 Revised Monthly Operating Rept for Dec 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20198M1481997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20197J1011997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20199C2951997-11-13013 November 1997 LER 97-S01-00:on 971017,vandalism of Electrical Cables Was Observed.Caused by Vandalism.Repaired Damaged Cables, Interviewed Personnel Having Potential for Being in Area at Time Damage Occurred & Walkdowns ML20199C7201997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Sequoyah Nuclear Plant L-97-215, SG Secondary Side Loose Object Safety Evaluation1997-10-23023 October 1997 SG Secondary Side Loose Object Safety Evaluation 1999-09-30
[Table view] |
Text
--. . _ _ _ - - - - _ _ _ _ _ _ _ _ _ _ _ _ _ - - - _ . - - - _ - ._ _ .- .
1 i -* . l a-e i
1 Tennessee Valley Authority. Post Othce Bcx 2000, Soddy-Daisy. Tennessee 37379-2000 Robert A. Fenech Wce President, Sequoyah Nuclear Plant July 12, 1993 1
l U.S. Nuclear Regulatory Commission j ATTN: Document Control Desk {
Washington, D.C. 20555 j Gentlemen: 1 l
1
.l '
1 TENNESSEE VALLEY AUTHORITY - SEQUOYAII NUCLEAR PLANT UNITS 1 AND 2 -
DOCKET NOS. 50-327 AND 50-328 - FACILITY OPERATING LICENSES DPR-77 AND DPR LICENSEE EVENT REPORT (LER) 50-327/93014 The enclosed LER provides details of a condition where a ventilation j L single failure will affect both trains of both unit's vital 125-volt, direct-current power equipment.
l This event is being reported in accordance with 10 CFR 50.73(a)(2)(ii)(B) as a condition that was outside the design basis of the plant.
Sincerely, ff M' Robert A. Fenech Enclosure cc: See page 2 l 'i 4
1500E7 9307160246 930712 Q /
PDR ADOCK 05000327- pt /p .,
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Y U.S. Nuclear Regulatory Commission j Page 2 July 12, 1993 cc-(Enclosure).:
INFO Records Center.
Institute of Nuclear Power Operations 700 Galleria Parkway i Atlanta, Georgia 30339-5957 ,
t Mr. D. E. LaBarge, Project Manager U.S. Nuclear Regulatory Commission i One White Flint, North 11555 Rockville Pike Rockville, Maryland 20852-2739 NRC Resident Inspector Sequoyah Nuclear Plant 2600-Igou Ferry Road Soddy-Daisy, Tennessee 37379-3624 Regional Administrator U.S. Nuclear Regulatory. Commission Region II 101 Marietta Street, NW, Suite 2900 Atlanta, Georgia 30323-2711 p
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NRC fdrm 366 U.S. NUCLEAR REGULATORY COMMISSION Approved OMB No. 3150-0104
- ( 6-89 ) ' Expires 4/30/92 LICDISEE EVENT REPORT (LER)
FAClllTY NAME (1) l DOCKET NUMBER (2) l_LAGf A
_Seguoyal L Nullear Plant (1Qtil..JLn11 1 101510l010131217l1j0Fl016 TITLE (4)
_An_Jnadeguate Ventilation Drsion Results (D_Entential Inopitability of Vital Power Equipment JVFUJ@L(S) l LER NjlMBER (6) l REEORT DATE (7) l OTHER FACILillES INVOLVED (8) l l l l l SEQUENTIAL l l REVISION l l l l FACILITY NAMES lDOCKETNUMBER(S)
LION!tjl_ DAY l1EARlYEARI l NUMBER I lHUMBERIMONit[jDAYlYEARl Sequoy1L_ilnft 2 lajMaj.qlRQj2}&_
l 1 l Ll l_I I I I I I 91_fil_..ll_J L21_2]_91 31 1 O_1 1 I 4 I I o 1 0 1 01 71 112j_91 31 Igjggjggili OPERATING l lTHISREPORTISSUBMITTEDPURSUANTTOTHEREQUIREMENTSOF10CFR5:
MODE l l _ (Check one_DI_mpre of the following)(ll)
_(9) _] Nl l20.402(b) l_]20.405(c) l_l50.73(a)(2)(iv) l_l73.71(b)
POWER l l._l20.405(a)(1)(1) Ll50.36(c)(1) l_l50.73(a)(2)(v) Ll73.71(c)
LEVEL l l_l20.405(a)(1)(ii) l_l50.36(c)(2) l__l50.73(a)(2)(vii) l_l0THER(Specifyin
_J19). Ll SJ_L]20.405(a)(1)(iii) Ll50.73(a)(2)(i) l_l50.73(a)(2)(viii)(A) l Abstract below and in l_l20.405(a)(1)(lv) lM]50.73(a)(2)(ii) l .__.j 50.73( a) ( 2 ) (vi i i ) ( B) l Text, NRC form 366A)
_._ __._ _ _ l _llfL_4D31A)(1)(v) l_.150.73(a)(2)(iii) l_ J59 73(a)(2)(x) !
.___ LL({NSEE CONTACT _f_QR THlil[B._{12)
NAME l T QEPHONE NUMB.lR lAREACODEl JuDaj tn t ewpfdompl i a n c e L i c entin_g I6l1l5I814131-l7171419 '
__ _ _ COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) l l l l REPORTABLE l l l l J l REPORTABLE l (AU$tlSYS11ttj _(DtiPQN[NT lMANUFA(JiLRIHj TO NPRDS I ICAU$fjSYSTEtjj_10MPONENT IMANV{ACTURERl TO NPRDS I I I I I I l l l l l l
_ _ Ll _l__l_ l I l l I I I I I i l i l i l i l l l l l l 1 1 I I I I I i l I
_ I __ I_LJ l i I L_I I I I I I l i I I I ! I I I _1 1
_ . _ _ _ . _ SUPPLEMENT _AL REERRT EXPECILD (14) l EXPECTED ll10NTHl DAY l YEAR
_- l ___ l SUBMISSION l l l 1YIl_ LlLJRL_r2mplete EXPECTED SUntillSION DATIl I X l NO l DATE (15) l l l l l l ]
ADSTRACT (Limit to 1400 spaces, i.e., approximately fif teen single-space typewritten lines) (16)
On June 11, 1993, at 1315 Eastern daylight time, with Unit I defueled and Unit 2 in Mode 5, it was determined that an inadequate ventilation design affected vital 125-volt (V) direct current (de) equipment operability. The ventilation configuration could result in vital 125-V de power becoming inoperable for both trains of both units from a single failure of the ventilation. The design configuration provides Train B ventilation te the Units 1 and 2 Train B 480-V board rooms. This results in one train of ventilation supplying four vital inverter and battery charger channels. Also, two of the vital battery rooms are supplied by the incorrect ventilation train. In 1991, an !
cvaluation was performed indicating that the equipment was operable, and compensatory l measures were established in the event that Train B cooling was lost. Subsequent reviews determined that the supporting logic of the_ evaluation may not have properly considered the use of temporary ventilation and non-1E power supplies. As a result, the design configuration of the ventilation could have impacted equipment operability. The l most probable cause for the inadequate design is inadequate interdiscipline review of )
the initial' design. The design is being modified and the new design configuration will be implemented to provide correct train ventilation to the affected equipment.
NRC Form 366(6-89)
1 l
NRC form 366A U.S. NUCLEAR REGULATORY COMMISSION Approved OMB No. 3150-0104
.(6-89) Enpires 4/30/92 LICENSEE EVENT REPORT (LER)
. TEXT CONTINUATION FACILITY NAME (1) lDOCKETNUMBER(2)J LE!LfMgER (6) l l PAGE (3)
Sequoyah Nuclear Plant (SQN), Unit 1 l
l l l l SEQUENTIAL l l REVISION] l l l l jYEARI l NUMBER I I NU1gf1_1 l l 'l l
' l
_ 101510lalqlL[Lj 7 l9 13 1-1 0 1 1 1 4 l l 0 l_Dl012l0FlOl6 l 1 EXT (If more space is required, use additional NRC form 366A's) (17)
- 1. PLANT CONDITIONS Unit 1 was defueled; Unit 2 was in Mode 5, cold shutdown, for a forced outage.
II. DESCRIPTION OF EVENTS A. Event on June 11, 1993, at 1315 Eactern daylight time (EDT), it was determined that an inadequate ventilation design affected vital 125-volt (V) direct current .
(de) power (EIIS Code EF) equipment operability. The ventilation configuration could result in vital 125-V de power becoming inoperable for both trains of both units from a single failure of the ventilation. The design configuration provides Train B ventilation to the Units 1 and 2 Train B 480-V board rooms. Contained in this area is the vital control power system equipment (Channels I through IV). This results in Train B ventilation supplying the inverters (EIIS Code INVT) and battery chargers (EIIS Code BYC)
(see attached sketch for equipment layout). This configuration was determined to exist from the original design. The design problem was identified and documented in 1991 on a condition adverse to quality report (CAQR). The evaluation of the CAQR indicated that continued operation was acceptable based on compensatory measures that were required in the event that Train B cooling was lost. This was based, in part, on a philosophy that the ventilation 6 systems were not required for electrical equipment operability. A root cause analysis (RCA) performed for the original CAQR identified that ventilation trains were reversed for two battery rooms in addition to the single train ventilation to the inverters and chargers. During the issuance of the design ;
change to resolve this problem, it was determined that the supporting logic of
the evaluation may not have properly considered the use of temporary ventilation and non-1E power supplies. This was questioned as a result of recent philosophy changes following the reevaluation of the impacts of ventilation systems on the operability of electrical equipment in support of restart. As a result, the design configuration of the ventilation could impact equipment operability.
B. Inoperable _Struc.tures4_Compsnentsa_or_Syatema_Ihat_ Contributed to the_ Event !
None.
C. Date a_antLApprDXimatLIlmes__of_Eaj oLDrrurrencea '
June 12, 1991- A design problem of the ventilation in the 480-V board at 1400 EDT room was identified. A CAQR was issued with an evaluation- l supporting continued operation.
NRC form 366(6-89)
NRC Form 366A U.$._ NUCLEAR REGULATORY COMMISSION Approved OMB No. 3150-0104 (6-893 Expires 4/30/92 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION
[kCILITYNAME(1) lDOCKETNUMBER(2) l LER NUMBER (6) I _j PAGE (3) l l l l SEQUENTIAL l l REVISION l l l l l Sequoyah Nuclear Plant (SQN), Unit 1 l lYEAR l l NUliDER l l NUMBER l l l l l InisinJnin1Lill71913 I I o i 1 141-1oI o I 013!arjalJ_
TEXT (If more space is required, use additional NRC Form 366A's) (17)
July 16, 1991 An RCA was performed for the CAQR. The RCA indicated that the condition existed from initial design and that the train ventilation supply for two vital battery rooms was reversed.
June 10, 1993 During the final review for the design change to resolve at 1806 EDT this problem, it was determined that the evaluation logic may not have properly considered the use of temporary ventilation and non-1E power supplies. The evaluation logic was questioned because of recent philosophy changes following the reevaluation of the impacts of ventilation systems on electrical equipment operability (Restart item 178). The CAQR was revised.
June 11, 1993 An operability review was performed for the revised CAQR.
at 1315 EDT The condition was determined to affect operability. NRC notification was made in accordance with 10 CFR 50.72(b)(2) as a condition that was outside the design basis of the plant.
D. Other Svslema_or Secondary Functions _Afinnted None.
E. Heihad of D.isnavery During the final review for the design change to resolve this problem, it was determined that_a single failure in the ventilation system could affect four vital power channels. The evaluation logic of the CAQR was questioned because of recent philosophy changes following the reevaluation of the impacts of ventilation systems on electrical equipment operability (Restart Item 178).
F. Operator Actions No operator actions were required.
G. Saf ety Sysientlesponses !
No safety-system responses were required. !
III. CAUSE OF THE EVENT A+ Immediale_ caner The immediate cause of the condition was that one ventilation train was supplying both trains of vital 125-V de power equipment. Under the current !
design configuration, a loss of Train B ventilation would result in a loss of cooling capability to both trains of the vital inverters, the vital battery chargers, and two vital battery rooms.
NRC form 366(6-89)
NRC lorm 366A U.S. NUCLEAR REGULATORY COMMISSION Approved OMB No. 3150-0104 (6-89I Expires 4/30/92 LICENSEE EVD(T REPORT (LER)
TEXT CONTINUATION FACILITY HAME (1) lDOCKETNUMBER(2) l LER NVHDIR (6) l l PA$f,_(2) l l l l SEQUENTIAL l l REVISION] l l l l Sequoyah Nuclear Plant (SQN), Unit 1 l lyfARd l NV!iQIR L_1_NVUDIR_1 l l l l 1Qj5MDjDILl2 17 19 13 l- l 0 l 1 1 4 l .-1_0_L_0_L 01 410LLol_ft TEXT (If more space is required, use additional NRC form 366A's) (17)
B. Raat _Lause The most probable root cause of the design is inadequate interdiscipline review of the initial design. The current design configuration existed for over 20 years. As a result, most of the personnel that worked on that design are no longer available to discuss the condition, and those that are available do not remember the developmental details associated with the design. Had the various engineering disciplines performed proper reviews of the equipment layout and ventilation design, this condition could have been avoided. Major changes to the design control process were made in 1987 that significantly improved the interface reviews.
C. Con 111huling_fattuta A possible contributing cause to the event was that the vital 125-V de power equipment is identified by channel designation (Channels I through IV). This method of identification may have confused the ventilation designers. The designer did provide Trains A and B ventilation to the four battery rooms, indicating that the designers were aware of train applications. However, Battery Room III (Train A) received Train B ventilation and Battery Room IV (Train B) received Train A ventilation.
IV. ANALYSIS OF THE EVENT The operability of the vital 125-V de power system ensures that sufficient power will be available for accident conditions. In the event that Train B ventilation is lost, temporary fans could be used in Modes 5 and 6 to circulate excess cool air from the adjacent rooms. This would be required if vital control power equipment operating temperatures increased to the threshold level as a result of heat loads from the operation of additional equipment in the area. The shared cooling concept is feasible because the air-conditioning equipment was originally sized for a much higher load. Heat-load testing and recent temperature monitoring support the use of the excess capacity. During past plant operation, cooling has been maintained to the equipment. Therefore, there were no adverse consequences to plant personnel or to the public as a result of this event.
V. CORRECTIVE ACTIONS A. hmuedial.e_Carrettive Actions Design change documents have been initiated to provide proper train ventilation to the vital inverters, battery chargers, and Battery Rooms III and IV. These design changes will be implemented to resolve potential ventilation problems.
I i
?
NRC form 366(6-89) l
NRC f$rm 366A U.S. NUCLEAR REGULATORY COMMISSION Approved OMB No. 3150-0104 (6-897 Expires 4/30/92 LICENSEE EVENT REPORT (LER)
, TEXT CONTINUATION FACILITY NAME (1) lDOCKETNUMBER(2) l LM_!! UMBER (6) l l PAGE (3) l l l l$EQUENTIALl l REVISION l l l l l Sequoyah Nuclear Plant (SQN), Unit 1 l jyEARI i N1)MBER l l NUMB G _1 l l l l
___ 10J511dD10J3 12 17 19 13 l-l 0 1 1 14l-l01 0101510fl0l6_
TEXT (If more space is required, use additional NRC form 366A's) (17)
As the system engineers are the focal points for outstanding work on their respective systems, the current philosophy regarding impacts of ventilation systems on electrical equipment operability is being consistently applied in-their evaluation of backlog and emergent work items.
B. Action _to_Prrtv.enLBecurrence An' evaluation of the auxiliary and control building ventilation systems will be performed to determine if similar design flaws exist.
Because the current design change control process is not the same as the initial design process and because of personnel changes, no action la being taken specific to the probable root cause of inadequate interdiscipline review.
V1. ADDITIONAL INFORMATION A. Eniled Componenta None.
B. Erevious SimilarAents A review of previous events identified two LERs (LERs 50-327/84011 and 87039) that are associated with an inadequate ventilation design. Both reports addressed single failures that could affect both trains of the main control room emergency ventilation system. The actions from those events would not have prevented or identified the condition described in this LER where a single ventilation train failure affected both trains of another system.
VII. COMMITMENTS
- 1. Design changes will be implemented before Unit 2 Mode 4 entry from the current outage to provide correct train cooling to the vital inverters, chargers, and Battery Rooms III and IV.
- 2. An evaluation of the auxiliary and control building ventilation systems will_ )
be performed before Unit 2 Mode 4 entry from the current outage to determine !
If similar design flaws exist.
I NRC form 366(6-89)
.l i
- HRC fnrm 366A U.S. NUCLEAR REGULATORY COMMISSIOM Approved OMB No. 3150-0104 -)
(6-899. Expiros 4/30/92 )
LICENSEE EVENT REPORT (LER) j
, TEXT CONTINUATION MCI [lTYNAME(1) lDOCKETNUMDER(2) l LIR NUMBER.(6) ] l PAG U 31 l l l l SEQUENTIAL l l REVISION l l l l l Sequoyah Nuclear Plant (SQN), Unit I l lYEARI I tJ11 TIBER l l NUMBER _(. l l l l l lE(1}jlQlphjLl7. l913 l--! O l 1 14 l-! O j 0 l 0l 6lQ{.La[_fL !
TEXT (If more space is required, use additional NRC form 366A's) (17)
ATTACHMENT 480-V Board Room Equipment Layout (Not to Scale)
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