ML060380615

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Technical Specification Annual Report
ML060380615
Person / Time
Site: Millstone  Dominion icon.png
Issue date: 01/31/2006
From: Price J
Dominion Nuclear Connecticut
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
06-060
Download: ML060380615 (31)


Text

, VOOft"r.47 "**Dominion-Dominion Nuclear Connecticut, Inc.Millstone Power Station Rope Ferry Road Waterford, CT 06385 U.S. Nuclear Regulatory Commission Attention:

Document Control Desk Washington, DC 20555 JAN 3 1 Serial No.MPS Lic/MAE Docket Nos.06-060 RO 50-336 50-423 DPR-65 NPF-49 License Nos.DOMINION NUCLEAR CONNECTICUT.

INC.MILLSTONE POWER STATION UNITS 2 AND 3 TECHNICAL SPECIFICATIONS ANNUAL REPORT Pursuant to the provisions of Millstone Unit 2 and Millstone Unit 3 Technical Specifications (TS), Dominion Nuclear Connecticut, -Inc (DNC) is submitting the annual reports described below. These annual reports cover unit activities for the period January 1, 2005, to December 31, 2005.Millstone Unit 2: The Millstone Unit 2 activities provided in this report are covered by Section 6.9.1.4,"Annual Reports" as supplemented by Sections 6.9.1.5b and 5c. Details of these activities are as follows:* The results of the steam generator tube inservice inspections performed at Millstone Unit 2 in 2005 are included as Enclosure 1 in accordance with Millstone Unit 2 TS 6.9.1.5b.* There were no exceedances of Technical Specification 3.4.8 at Millstone Unit 2 in 2005; therefore, there is no report to be made on reactor coolant specific activity analysis in accordance with Millstone Unit 2 TS 6.9.1.5c.Millstone Unit 3: The Millstone Unit 3 activities provided in this report are covered by Section 6.9.1.2,"Annual Reports." Details of these activities are as follows:* There were no exceedances of Technical Specification 3.4.8 at Millstone Unit 3 in 2005; therefore, there is no report to be made on reactor coolant specific activity analysis in accordance with Millstone Unit 3 TS 6.9.1.2.b.

Serial No.06-060 Technical Specifications Annual report Page 2 of 3 There are no regulatory commitments contained within this letter.If you have any questions or require additional information, please contact Mr. David W.Dodson at (860) 447-1791, extension 2346.Very truly yours, A n Price t/Vice President

-Millstone Serial No.06-060 Technical Specifications Annual report Page 3 of 3

Enclosures:

(0)Commitments made in this letter: None.cc: U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406-1415 Mr. V. Nerses Senior Project Manager U.S. Nuclear Regulatory Commission One White Flint North 11555 Rockville Pike Mail Stop 8C2 Rockville, MD 20852-2738 Mr. S. M. Schneider NRC Senior Resident Inspector Millstone Power Station Mr. R. Prince NRC Inspector U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406-1415 Enclosure I Millstone Unit 2 2005 Steam Generator Tube Inservice Inspection Millstone Power Station Unit 2 Dominion Nuclear Connecticut, Inc. (DNC)

Serial No.06-060 Page 1 Steam Generator Tube Inspection Millstone Unit 2 (MP2) is a two loop ABB-CE PWR with Babcock and Wilcox (B&W)replacement Steam Generators (SG). Each SG was designed to contain 8523 U-bend thermally treated Inconel 690 tubes. One hot leg tube sheet hole in SG 1 was plugged during construction and the opposing cold leg hole was not drilled, thus SG 1 has 8522 tubes. The tubing is nominally 0.750 inch outside diameter with a 0.0445 inch nominal wall thickness.

During replacement SG fabrication, the tubes were installed using a two-step hydraulic expansion process over the full depth of the 21.06 inch thick tubesheet.

The tubesheet was drilled on a triangular pitch with 1.0 inch spacing. There are 141 rows and 167 columns in each SG. To minimize small radius U-bends, tubes in rows 1 through 3 were installed using a staggered arrangement.

This resulted in the termination of tubes at different locations between the hot and cold legs. For these rows, the tube identification follows the hot leg row/column naming convention.

Secondary side tube support structures include seven lattice grid supports on the vertical section of the tubes and twelve "fan bar assemblies on the U-bend section of the tubes. All lattice grid supports are full supports.SG replacement was completed during 2R1 1 (Fall 1992). The new SGs have accrued 7.037 Effective Full Power Years (EFPY) of operation as of the end of Cycle 16 (April 2005). The 910 MW Unit operates with a hot leg temperature of 601 degrees Fahrenheit.

The Millstone Unit 2 SG eddy current testing (ECT), conducted at the end of Cycle 16, was completed on April 25, 2005. The examinations, personnel, and equipment conformed to the requirements of NEI 97-06, rev. 1, Steam Generator Program Guidelines; EPRI Pressurized Water Reactor Steam Generator Examination Guidelines:

Revision 6; and Millstone Unit 2 Technical Specifications.

Performed in SG 1 only, the inspection included a 100% bobbin coil exam and 298 special interest and diagnostic exams utilizing Motorized Rotating Pancake Coil (MRPC) technology.

The only indications of degradation recorded were attributed to mechanically induced wear. ECT identified two tubes with nine (9) percent throughwall fan bar wear, unchanged from the 2R14 results. No tubes were removed from service or otherwise repaired.One hundred percent (100%) of all in-service tubes (8522 tubes) in SG 1 were examined full length with the standard bobbin coil technique.

The tubes were examined tube end to tube end (TEC-TEH) from the hot leg channel head.Two hundred ninety-eight (298) tubes were examined with the MRPC plus-point probe;one hundred forty-two (142) hot-leg roll transition exams and one hundred fifty-six (156)special interest and diagnostic examinations.

MRPC examination locations are summarized below and in Table 2.The extent for the roll transition area examination was top of tube sheet hot (TSH) +3/-3 inches. This area was selected based on the historical hot leg sludge pile region as compiled from previous SG 1 and SG 2 (2R13, 2R14, and 2R15) results. The 142 tube Serial No.06-060 Page 2 locations selected for examination make up fifty percent (50%) of this total sludge region (284 tubes) identified from both SGs. Approximately seventy-four (74%) of the tubes in the sample had previously identified Sludge (SLG) indications in SG 1. SLG indications reported during the current inspection are mapped in Attachment

5. One tube with a historical Partial Tubesheet Expansion (PTE) indication was also examined TSH-TEH.One hundred and fifty-six (156) tubes were examined at a specific area of interest.

The sixty-three (63) preplanned examinations were conducted at locations of previously identified dents, dings, bulges, possible loose parts, over expansions, and fan bar wear.Ninety-three (93) diagnostic examinations were conducted at locations associated with indications reported during the current inspection.

These included dents, dings, bobbin I-codes, possible loose parts, and tubes surrounding possible or known loose parts.This ECT examination was conducted following five cycles (7.037 EFPY) of operation with the replacement SGs. There were no indications of any corrosion related tube cracking.ECT reported two (2) tubes with nine (9) percent throughwall

(%TW) fan bar wear. The ECT results from 2R14 also reported 9%TW wear on these tubes, thus the wear has not progressed over the past two operating cycles. Additional details on fan bar wear in both SGs are provided in Table 3 and Attachment 6.One Volumetric Indication (VOL) was reported.

This VOL indication has been reported since the June 1997 examination with MARPC. It is believed to be associated with a Manufacturing Buff Mark (MBM) and exhibits no change since first reported.

Additional details are provided in Attachment 7.Twenty-five (25) PLP indications were also reported.

These ECT reported indications were grouped in eleven (11) locations as shown in Attachment

4. Seventeen (17) of the indications were initially reported with the bobbin coil examination and eight (8) with the MRPC examination.

Loose parts were observed in an additional three (3) locations during SSI. There were no indications of wear associated with any of the PLP indications or any of the loose parts that were reported.

Additional information is included in Table 4.Although no primary side ECT was performed, SSI reported thirteen (13) loose parts in SG 2. Nine (9) were removed. Three (3) pieces of Flexitallic gasket and one (1) sludge rock remain wedged between tubes. No wear associated with any of the loose parts in SG 2 was reported during the performance of the visual examination.

In summary, 100% of the tubes in SG 1 (8522 tubes) were inspected, TEC-TEH. There were no tubes that required repair as a result of this examination.

No tubes were plugged or otherwise repaired on a discretionary basis. As a result of the inspection, SG 1 was classified as C-1. A listing and map of tubes reported with wall-thickness loss is included in Attachment

6. The maximum wall-thickness loss was 9% TW.

Serial No.06-060 Page 3 Table 1 -Eddy Current ResultsSG 1 Number of Tubes 8522 Number of Tubes Inspected full length w1Bobbin Probe 8522 Number of Tube Inspections w/MRPC (Total) 298* Hot Leg Transitions

-Original Scope 142* Hot Leg Misc. Special Interest -Diagnostic Exams 60* Cold Leg Misc. Special Interest -Diagnostic Exams 82* U-bend Misc. Special Interest -Diagnostic Exams (tubes) 14 Tubes with Max Fan Bar Wear >= 40% 0 Tubes with Max Fan Bar Wear >= 20% but < 40% 0 Tubes with Max Fan Bar Wear <20% 2 Tubes Plugged 0 Tubes Sleeved 0 I ___________________________

Serial No.06-060 Page 4 Table 2- MRPC Examinations Hot Leg Cold Leg U-bend Previous PTE 1 0 0 Indications

_PLP 2 4 0 DNT/DNG 3 9 8 BLG 2 0 0 OXP 19 14 0 Fan BarWear 0 0 1 2R16 Bobbin I-Codes 3 0 2 Indications

_Bobbin PLPs 3 8 0 PLP Bounding & 27 46 0 Resulting PLPs DNT/DNG 0 1 3 Total 60 82 14 Table 3-. Fan Bar Wear Ro Col SG % TW Support Inch from Support Identifie w Identifier Center d 40 155 1 9 F06 -1.74 2R14 I 9 F06 -1.66 2R16 140 93 1 9 F08 -0.55 2R14 9 F08 -0.53 2R16 37 120 2 6 F07 -0.81 2R15 99 80 2 11 F06 1.26 2R15 Serial No.06-060 Page 5 Table 4 -Loose Parts Summary SG Location Description Method of Removed Discovery 1 R89 C26 Small metal turning wedged between tubes. ECT No R91 C26 PLP indications evident in this area in 02, 97, R88 C27 and 94. No wear was reported.R87 C28 TSC+0.4" 1 R26 C165 Sludge rock located between tubes. PLP ECT No R28 C165 indications evident in 02, 97, and 94. No TSC+5.5" wear was reported.1 R41 C160 Short piece of wire or F:lexitallic gasket. PLP ECT No R42 C159 indications evident in 02. No wear was R40 C159 reported.R43 C158 R41 C158 TSH+0.8" 1 R45 C162 Sludge rock located between tubes. PLP ECT No R47 C162 evident in 02, 97, and 94. No wear was TSC+9.6" reported.1 R127 C50 Sludge formation between tubes. No wear ECT Yes R128 C51 was reported.

No PLP reported via ECT for TSC+9.8" R128 C51.1 R140 C77 Weld slag lying on tube sheet between Visual Yes R139 C78 tubes. No wear was reported.

No PLP R140 C79 reported via ECT for R140 C77 or R140 C79.TSC 1 R28 C99 Demineralizer outlet strainer screen fragment Visual No R29 C98 lodged between tubes and on the tube sheet.TSC No wear was reported.

No PLP was reported via ECT.1 R127 C120 3" long metal clip lying in the periphery on Visual Yes RI 26 C123 the tubesheet adjacent to the listed tubes.R125 C122 No wear was reported.

No PLP was TSH reported via ECT.1 R139 C70 Approximately 20 wire brush bristles lying on Visual Yes TSH the tube sheet and adjacent to the tube. No wear was reported.

No PLP was reported via ECT.1 R130 C57 Sludge formation wedged between tubes. ECT No RI 31 C56 No wear was reported.R132 C57 TSC+5.3"

--Serial No.06-060 Page 6 SG Location Description Method of Removed Discovery 1 R16 C1 Sludge formation lodged between tubes. No ECT Yes R14 C1 wear was reported.TSH+10.8" 1 R96 C33 PLP previously reported in 02. No wear was ECT No TSH+2.0" reported.

Loose part was not observed visually.1 R94 C33 PLP previously reported in 02. No wear was ECT No TSH+2.0" reported.

Loose part was not observed visually.1 R23 C102 Weld slag previously identified in 03 and 02. Visual No R24 C103 No wear was detected.R24 C101 TSC+1.0" 2 R30 C97 Cold staywell.

Sludge rock wedged between Visual No R31 C96 tubes. No wear was observed.R32 C97 2 R137 C102 Hot periphery.

Flexitallic gasket metallic Visual Yes R136 C103 piece. No wear was observed.RI 34 C1 03 2 R138 C80 Hot periphery.

Flexitallic gasket metallic Visual Yes R138 C81 piece. No wear was observed.R140 C81 R139 C82 R141 C82 R141 C84 R137 C80__ _ R140 083 _ _ _ _2 R139 C70 Hot periphery.

Demineralizer outlet strainer Visual Yes screen fragment.

No wear was observed.2 R127 C50 Hot periphery.

Flexitallic gasket metallic Visual No R126 C49 piece. No wear was observed.R127 C48 R125 C50 2 R139 C72 Hot periphery.

Flexitallic gasket metallic Visual No R138 C73 piece. No wear was observed.2 R141 C88 Weld wire. Cold Periphery.

No wear was Visual Yes RI 41 C86 observed R141 C84 2 R37 C80 Cold staywell.

.Flexitallic gasket metallic Visual No R39 C80 piece. No wear was observed.R37 C82 R38 C81 R39 C82 Serial No.06-060 Page 7 SG Location Description Method of Removed Discovery 2 Cold annulus near R1 00 C25. Piece of wire. Visual Yes No contact with any tubes. No wear observed.2 No-tube lane near R4 1. Flat head screw. Visual Yes No contact with any tubes. No wear observed.2 No-tube lane near R4 01. Metal turning. No Visual Yes contact with any tubes. No wear observed.2 Cold annulus near R140 C85. Demineralizer Visual Yes outlet strainer screen fragment.

No contact with any tubes. No wear observed.

Serial No.06-060 Page 8 Attachments Attachment 1 2 3 4 5 6 7 Title Acronyms Tube Sheet Map and Listing -DNG Indications Tube Sheet Map and Listing -DNT Indications Tube Sheet Map and Listing -PLP Indications Tube Sheet Map and Listing -SLG Indications Tube Sheet Map and Listing -% TW FB Indications Tube Sheet Map and Listing -VOL Indications Serial No.06-060 Page 9 Attachment I Acronyms B&W Babcock & Wilcox BLG Bulge C Column DNG Ding DNT Dent ECT Eddy Current Testing EFPY Effective Full Power Years FB Fan Bar MP 2 Millstone Unit 2 MRPC Motorized Rotalting Pancake Coil OXP Over Expansion PLP Possible Loose Part PTE Partial Tubesheet Expansion% TW Percent Throughwall R Row SG 1 Steam Generator Number 1 SG 2 Steam Generator Number 2 SLG Sludge SSI Secondary Side! Inspection TEC Tube End Cold-leg TEH Tube End Hot-leg TSC Top of Tube Sheet Cold-leg TSH Top of Tube Sheet Hot-leg VOL Volumetric Indication Serial No.06-060 Page 10 Attachment 2 DNG Indications Millstone Unit 2 GROUP B DNG I nd cations 7 .TUBES 12 Millstone Unit 2 04/05 -2R16 DNG Indications

-'uWI IMID O 5 Vn L S/G 1 HOT PRIMARY FACE TOTAL TUBES: 8523 SELECTED TUBES: 12 OUT OF SERVICE (#): I SCALE: 0.066571 X Fri May 27 08:42:51 2005 w NOZZLE lAnl -A.PA.Q.8* n^ ..e-01 130 130 120 120 110 110 100 100 90 90 80 80 70 60 50S 0 0 40 -<30-2 0 4000 00'10 -oee 70 MANWAY 9 -60 it40 40 80 90-30 ff 20 100_ _-10 W o I U w U 110 I2I I 1 120 130 140 1SO I 160 10 20 30 40 50 60 Framatome ANP Inc.Customer Name: Millstone Unit 2 5/26/2005 4:30:43 PM Component:

S/G 1 Page 1 of 1 DNG Indications QUERY: DNG Indications ROW 20 20 21 25 29 57 59 69 103 114 132 136 COL VOLTS DEG CHN IND 61 4.26 184 1 DNG 63 4.36 184 1 DNG 104 5.47 185 1 DNG 64 6.59 183 1 DNG 34 2.71 188 1 DNG 158 5.05 186 1 DNG 42 2.81 184 1 DNG 72 4.02 187 1 DNG 32 3.19 186 1 DNG 99 4.26 186 1 DNG 55 4.89 185 1 DNG 63 4.18 184 1 DNG%TW LOCATION e= =========

==F01 +12.29 F07 +5.18 F01 +7.10 F06 +2.22 01H +20.24 F06 +5.69 TSC +14.91 04C +28.11 06C +19.94 02H +33.86 TSC +0.61 F02 +3.80 EXT EXT TC TEN TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER UTIL 1 UTIL 2 CAL ILEG HR====sH=O===T_==

HR 32 HOT HR 31 HOT HR 25 HOT HR 32 HOT HR 8 HOT HR 68 HOT HR 5 HOT HR 32 HOT HR 4 HOT HR 22 HOT HR 13 HOT HR 14 HOT PROBE 610UL 610UL 610UL 610UL 610UL 610UL 61OUL 610UL 610UL 61OUL 61OUL Total Tubes : 12 Total Records: 12 Serial No.06-060 Page 1 1 Attachment 3 DNT Indications I I Millstone Unit 2 GROUP B DNT indications a- TUBES 13 Millstone Unit 2 04/05 -2R16 DNT Indications S/G 1 HOT PRIMARY FACE TOTAL TUBES: 8523 SELECTED TUBES: 13 OUT OF SERVICE (#): 1 SCALE: 0.066571 X Fri May 27 08:44:22 2005._.tcm 2 Ul* : SMj HOT FEW NOZZLE IAO --IAO 0.130 130 120 t 120 110 110 100 r 100 90 90 80 so 70 60 -C C 70 MANWAY W- 60 50 40-30 40-I 30 6.1 e ----g0- -------20-70 ---10 20 10 --_ -_ _ _10 W U W U ---W U U F Uw ., 110 140 150 10 20 30 40 50 60 120 130 160 Framatome ANP Inc.Customer Name: Millstone Unit 2 5/26/2005 4:31:17 PM Component:

S/G 1 Page 1 of 1 DNT Indications QUERY: DNT Indications ROW COL VOLTS DEG CHN IND %TW'- _ _=l nf=_ == = -e ===16 167 3.11 177 P 1 DNT 20 61 4.26 178 P 1DNT 20 63 3.77 179 P 1DNT 37 108 3.98 180 P 1 DNT 48 129 2.98 184 P 1 DNT 49 106 3.33 181 P 1 DNT 60 113 3.86 182 P 1 DNT 85 42 2.36 180 P 1DNT 87 52 3.69 183 P 1DNT 92 53 3.16 179 P 1DNT 92 91 4.01 175 P 1DNT 108 S1 3.64 181 P 1 DNT 113 70 3.24 178 P 1 DNT LOCATION 07H +0.68 F07 -0.40 F06 +1.97 F06 +0.56 F05 +0.33 07C +1.74 07C +1.61 07C +1.68 07C +1.67 07C +1.49 07H +1.40 07C +1.55 07C +1.20 EXT EXT UTIL 1 TEC TEH HR TEC TEH HR TEC TE HRR TEC TEH HR TEC TER HR TEC TEH HR TEC TER HR TEC TER HR TEC TER HR TEC TEH HR TEC TEH HR TEC TER HR TEC TEH HR UTIL 2 CAL # LEG 66 HOT 32 HOT LAR 31 HOT 28 HOT 63 HOT 28 HOT 28 HOT 2 HOT 13 HOT 14 HOT 20 HOT 13 HOT 16 HOT PROBE 610UL 610UL 610UL 610UL 610UL 610UL 610UL 610UL 610UL 610UL 610UL 610UL Total Tubes : 13 Total Records: 13 Serial No.06-060 Page 12 Attachment 4 PLP Indications Millstone Unit 2 Millstone Unit 2 04/05 -2R1 6 PLP Indications GROUP B PLP indications TUBES 25-PURM ffW mogus. VauMg 3 IS/G 1 IHOT IPRIMARY FACE TOTAL TUBES: 8523 SELECTED TUBES: 25 OUTOFSERVICE(#):

NA SCALE: 0.066571 X FYZri May 27 08:51:04 2005 B.'NOZZLE lAn.n4A A of 130 130 120 120 110 110 100 100 90 90 80 SO 70 70 MANWAY S- 60 60 -E 50 r so 40 r 40 30 20 80 90 A_30 20 100 10 -, _ _10 I 110 I I, e7-10 20 30 40 so 60 120 130 140 ISO 160

--Framatome ANP Inc.Customer Name: Millstone Unit 2 5/26/2005 4:34:46 PM Component:

S/G 1 Page 1 of 1 PLP Indications (including any LPI LPM LPR LPS Indications)

QUERY: PLP Indications ROW COL 14 1 16 1 23 102 24 101 24 103 25 102 26 165 28 165 40 159 41 158 41 160 42 159 43 158 45 162 47 162 87 28 68 27 89 26 91 26 94 33 96 33 127 50 130 57 131 56 139 78 VOLTS DEG 0.29 183 0.29 212 1.05 45 0.60 78 0.47 78 2.78 189 0.77 35 0.60 77 1.15 42 0.63 77 0.30 78 0.35 34 0.26 82 0.31 218 0.37 67 0.28 a8 0.31 89 0.26 72 0.16 91 0.32 83 0.45 78 0.81 219 0.34 80 0,70 227 0.20 90 0.19 66 0.14 70 0.21 80 0.29 215 0.11 14 0.24 208 0.22 78 0.43 213 0.28 75 0.36 209 0.11 73 0.10 213 0.23 113 CHN IND 8 PLP 8 PLP 8 PLP 11 PLP 11 pLP 8 PLP 8 PLP 11 PLP 8 PLP 11 PLP 11 PLP 8 PLP 11 PLP 8 PLP 11 PLP 11 PLP 11 PLP 7 PLP 11 PLP 11 PLP 11 PLP 8 PLP 11 PLP 8 PLP 11 PLP 11 PLP 11 PLP 11 PI1P 8 PLP 11 LPS 8 PLP 11 LPS 8 PLP 11 PLP 8 PLP 11 PLP 8 PLP 8 PLP%TW LOCATION EXT EXT UTIL 1 TSH +11.17 TEC TER LAR TSH +10.81 TgC TER LAR TSC +1.21 TEC TER LAR TSC +0.84 TSC TSC LAR TSC +0.19 TSC TSC LAR TSC +0.22 TgC TEN LAR TSC +1.26 TEC TER LAR TSC +0.92 TSC TSC LAR TSC +0.94 TEC TEH LAR TSC +0.61 TSC TSC LAR TSC +5.63 TSC 01C LAR TSC +5.71 TEC TER LAR TSC +5.23 TSC 01C LAR TSC +5.27 TEC TEN LAR TSN +0.36 TSH TSH LAR3.7 TSH +0.08 TSH TSH LAR5.2 TSH +0.72 TSH TSH LAR4.5 TSH +0.80 TEC TER LAR TSH +0.23 TSH TSH LAR3.6 TSH +0.09 TSH TSH LAR5.4 TSC +9.66 TSC 01C LAR TSC +9.31 TEC TER LAR TSC +9.19 TSC 01C LAR TSC +9.64 TEC TER LAR TSC +0.39 TSC TSC LAR7.8 TSC +0.09 TSC TSC LAR9.2 TSC +0.38 TSC TSC LAR TSC +0.26 TSC TSC LAR7.9 TSH +2.08 TEC TEH LAR TSH +1.88 TSH TSH LAR TSH +2.03 TEC TEN LAR TSH +1.96 TSH TSH LAR TSC +9.82 TEC TER LAR TSC +5.54 TSC 01C LAR TSC +5.29 TEC TEN LAR TSC +5.47 TSC 01C LAR TSC +5.27 TEC TER LAP TSC +0.56 TEC TEH LAR UTIL 2 CAL # LEG PROBE_ =_ = 5 5 5= = _ = _e 2 C cS 5 5 5 5 sr VLP VLP VLP VLP VLP VLP VLP VLP VLP 5.60 5.63 37 12 26 4 4 32 26 4 26 4 4 66 4 68 72 72 70 66 72 72 4 66 4 66 5 S 4 5 4 70 3 70 13 4 13 4 13 18 HOT HOT NOT COLD COLD HOT HOT COLD HOT COLD COLD HOT COLD HOT HOT HOT HOT HOT HOT HOT, COLD HOT COLD HOT COLD COLD COLD COLD HOT HOT HOT HOT HOT COLD HOT COLD HOT HOT 610UL 61OUL 610U0L 610PP 610PP 610UL 610UL 610P?610UL 610PP 610PP 6100U 610PP 6100L 610PP 610PP 610PP 610UL 610PP 610PP 610PP 6100L 610PP 6100L 610PP 610PP 610PP 610PP 610UL 610PP 61OUL 610PP 6100L 610PP 610UL 610PP 610UL 610UL Total Tubes : 25 Total Records: 38 Serial No.06-060 Page 13 Attachment 5 SLG Indications Millstone Unit 2 r .--Millstone Unit 2 04/05 -2R16 SLG Indications GROUP SLG Indications (TS SLG Indications (TSC).TUBES 18 9 FANP- FOMS nun modus Vamti 3.'S/G 1 HOT PRIMARY FACE TOTAL TUBES: 8523 SELECTED TUBES: 27 OUT OF SERVICE (#): I SCALE: 0.066571 X Fri May 27 10:59:10 2005**:L NOZZLE 0-0-000 LC__ _ 1 SIX 130 130 120 120 110 110 100 -100 A0 90 90 80 so 70 60 -, 0 50 -11e10 70 MANWAY 8- 60 0 00 40 -.30 j, 20 10 -A 80 26°1 z90 Wc_ _ 70 ---30 20-----10 l I 110 Il 120 130 140 10 20 30 40 50 60 ISO 160 Framatome ANP Inc.Customer Name: Millstone Unit 2 SLG Indications IQUERY: SLG Indications 5/27/2005 11:00:43 AM Component:

SIG I Page I of 1 Component:

S/G 1 Page 1 of 1 ROW 27 28 30 31 31 32 33 33 33 34 34 35 35 36 37 38 39 47 55 113 117 118 121 121 123 128 133 COL VOLTS 46 0.82 47 1.03 47 1.60 46 1.05 48 1.45 47 1.87 46 1.33 48 2.23 50 2.10 47 1.64 49 2.06 48 1.58 50 2.35 47 0.80 50 2.33 49 2.02 50 2.25 54 0.71 70 2.25 60 2.31 60 2.27 75 2.77 60 2.08 62 2.00 68 0.70 61 2.05 64 2.29 DEG CHN 8 8 8 8 8 8 8 8 8 8 8 8 8 8 8 8 8 8 8 8 8 8 8 8 32 8 38 8 8 8 IND %TW SLG SLG SLG SLG SLG SLG SLG SLG SLG SLG SLG SLG SLG SLG SLG SLG SLG SLG SLG SLG SLG SLG SLG SLG SLG SLG SLG LOCATION TSH +0.58 TSH +0.70 TSH +1.05 TSH +1.17 TSH +1.22 TSH +1.08 TSH +0.72 TSH +1.25 TSH +0.94 TSH +0.99 TSH +0.91 TSH +1.24 TSH +1.89 TSH +0.86 TSH +1.54 TSH +0.93 TSH +1.70 TSH +1.10 TSC +0.46 TSC +0.45 TSC +0.45 TSC +0.45 TSC +0.45 TSC +0.48 TSC +1.51 TSC +0.45 TSC +0.45 EXT EXT TEC TER TEC TER TEC TER TEC TEH TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TER TEC TEH TEC TER TEC TER TEC TER TEC TER UTIL 1 UTIL 2 CAL 4 LEG 5 HOT 4 HOT 3 HOT 5 HOT 3 HOT 4 HOT 4 HOT 4 HOT 30 HOT 3 HOT 3 HOT 3 HOT 29 HOT 4 HOT 30 HOT 3 HOT 29 HOT 29 HOT 54 HOT 13 HOT 13 HOT 15 HOT 13 HOT 13 HOT 16 HOT 13 HOT 13 HOT PROBE 61OUL 610UL 610UL 610UL 610UL 610UL 61OUL 610UL 610UL 61OUL 610UL 610UL 610UL 610UL 610UL 610UL 610UL 610UL 610UL 610UL 610UL 610UL 610UL 610UL 610UL 61OUL 61OUL 610UL Total Tubes : 27 Total Records: 27 Serial No.06-060 Page 14 Attachment 6% TW FIB Indications IViillstone Unit 2-r GROUP B TWD Indications Mi stone Unit 2 04/05 -2R16%TW (Bobbin Wear) Indications I TUBES 2 FANP. FDMS nu module Verslon 3" i-S/G1 IHOT PRIMARY FACE TOTAL TUBES: 8523 SELECTED TUBES: 2 OUT OF SERVICE (#): 1 SCALE: 0.066571 X Fri May 27 08:53:07 2005---_111 1U^MEW lb NOZZLE--IAA 1AiA --Ae4 130-r 130 120 -120 110 110 100 100 90_X 90 8O 70 60 -#I V 80 70 MANWAY 40 50 40 30 20 10 -C 80----- 0----- >30 20-10'II ll,'a.e) 0) C) C 31-1 I0I I 4 10 20 30 40 50 60 110 120 130 140 150 160 Framatome ANP Inc.Customer Name: Millstone Unit 2%TW (TWD) Indications 5/26/2005 4:43:23 PM Component:

SIG 1 Page 1 of 1 QUERY: TWD Indications ROW COL VOLTS DEG CHN IND %TW LOCATION EXT EXT UTIL 1 UTIL 2 CAL # LEG , ====== t=5 = A _== to_== S==.---==5=-====s==C-=

tC t=== === ====tt= ==== flCCC-40 155 0.21 113 P 2 TWD 9 F06 -1.66 TEC TEH LAR 69 HOT 140 93 0.29 127 P 2 TWD 9 F08 -0.53 TEC TEH LAR 33 HOT PROBE 610UL 610UL Total Tubes : 2 Total Records: 2 Serial No.06-060 Page 15 Attachment 7 VOL Indications I MiltneUiI Millstone Unit 2 04/05 -2R16 VOL Indications GROUP B VOL Indications U- BES 1 rj.er.*. lIES mc.m. Yams S/G 1 HOT PRIMARY FACE TOTAL TUBES: 8523 SELECTED TUBES: I OUT OF SERVICE (#): NA SCALE: 0.066571 X Fri May 27 08:53:52 2005 I "Wto* M2OSN 1HT SV NOZZLE 6 t11=110-96-f 0190909MOMR 130_c I 130 120 120 110 110 100 100 90 90 80 80 70.2 60 -E 70 MANWAY 8.- 8o 50 -, 40 r 30 -iJ0 1-V------

IV-'0_ _ _ _ _ _ _ _ _ _ _0 0'Xc 6Mc 5o I 40-30-20 20 100 -0c lXO1 10 -xci 1xc svaegevueae, Is o 0g~~~Do 0 ooO 10 10 20 30 40 ia6u6°c lip 50 60 110 120 130 140 150 160 Framatome ANP Inc.Customer Name: Millstone Unit 2 VOL Indications 5/26/2005 4:44:21 PM Component:

S/G 1 Page 1 of 1 X QUERY: VOL Indications ROW COL VOLTS DEG CHN IND %TW LOCATION EXT EXT UTIL 1 UTIL 2 CAL

  • LEG PROBE 2 7 0.77 77 3 VOL TSH +0.15 TSH TSH 70 HOT 61OPP Total Tubes : 1 Total Records: 1