ML13305B037

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LER 13-006-00 for Waterford, Unit 3, Regarding Failure of Credited Operator for Air Operated Valve Causes Train Past Inoperability
ML13305B037
Person / Time
Site: Waterford Entergy icon.png
Issue date: 10/31/2013
From: Pellegrin B J
Entergy Operations
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
W3F1-2013-0060 LER 13-006-00
Download: ML13305B037 (9)


Text

10 CFR 50.73 W3F1-2013-0060 October 31, 2013 U.S. Nuclear Regulatory Commission Attn: Document Control Desk 11555 Rockville Pike Rockville, MD 20852

Subject:

Licensee Event Report (LER) 2013-006-00 Waterford Steam Electric Station, Unit 3 (Waterford 3)

Docket No. 50-382 License No. NPF-38

Dear Sir or Madam:

Entergy is hereby submitting Licensee Event Report (LER) 2013-006-00 for Waterford Steam Electric Station, Unit 3 (Waterford 3). This report provides details associated withpast inoperability of one train of a safety related system due to failure of a credited manualoperator for an air operated valve.Based on plant evaluation, it was determined that this condition is reportable pursuant to 10 CFR 50.73(a)(2)(i)(B) and 10 CFR 50.73(a)(2)(ii)(B).

This report contains no new commitments. Please contact Bryan J. Pellegrin, Licensing Manager - Acting, at (504) 739-6203 if you have questions regarding this information.

Sincerely, BJP/WH

Attachment:

Licensee Event Report 2013-006-00Entergy Operations, Inc.

17265 River RoadKillona, LA 70057-3093 Tel 504-739-6203Fax 504-739-6698bpelleg@entergy.comBryan J. PellegrinLicensing Manager - Acting Waterford 3 W3F1-2013-0060 Page 2cc:Mr. Marc L. Dapas, Regional Administrator U.S. NRC, Region IV RidsRgn4MailCenter@nrc.gov U.S. NRC Project Manager for Waterford 3 Kaly.Kalyanam@nrc.gov U.S. NRC Senior Resident Inspector for Waterford 3 Marlone.Davis@nrc.gov Attachment to W3F1-2013-0060 Licensee Event Report 2013-006-00 NRC FORM 366 (10-2010)obo-3 NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION(10-2010)

LICENSEE EVENT REPORT (LER)(See reverse for required number ofDigi /characters for each block)APPROVED BY OMB NO. 3150-0104 EXPIRES 10/31/2013 Estimated burden per response to comply with this mandatory information collectionrequest: 80 hours9.259259e-4 days <br />0.0222 hours <br />1.322751e-4 weeks <br />3.044e-5 months <br />. Reported lessons learned are incorporated into the licensing processand fed back to industry. Send comments regarding burden estimate to the FOIA/PrivacySection (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, orby internet e-mail to infocollects.resource@nrc.gov, and to the Desk Officer, Office ofInformation and Regulatory Affairs, NEOB-10202 (3150-0104), Office of Management andBudget, Washington, DC 20503. If a means used to impose an information collectiondoes not display a currently valid OMB control number, the NRC may not conduct orsponsor, and a person is not required to respond to, the information collection.1. FACILITY NAME2. DOCKET NUMBER

3. PAGEWaterford 3 Steam Electric Station 050003821OF64. TITLEFailure of Credited Manual Operator for Air Operated Valve Causes Train Past Inoperability5. EVENT DATE6. LER NUMBER7. REPORT DATE8. OTHER FACILITIES INVOLVED MONTHDAYYEAR YEARSEQUENTIAL NUMBERREVNOMONTH DAY YEARFACILITY NAME DOCKET NUMBER 090420132013-006-0010312013FACILITY NAME DOCKET NUMBER9. OPERATING MODE11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply)

Mode 120.2201(b)20.2203(a)(3)(i)50.73(a)(2)(i)(C)50.73(a)(2)(vii) 20.2201(d)20.2203(a)(3)(ii)50.73(a)(2)(ii)(A)50.73(a)(2)(viii)(A)20.2203(a)(1)20.2203(a)(4)50.73(a)(2)(ii)(B)50.73(a)(2)(viii)(B)20.2203(a)(2)(i)50.36(c)(1)(i)(A)50.73(a)(2)(iii)50.73(a)(2)(ix)(A)

10. POWER LEVEL20.2203(a)(2)(ii)50.36(c)(1)(ii)(A)50.73(a)(2)(iv)(A)50.73(a)(2)(x) 100%20.2203(a)(2)(iii) 50.36(c)(2)50.73(a)(2)(v)(A)73.71(a)(4)20.2203(a)(2)(iv)50.46(a)(3)(ii)50.73(a)(2)(v)(B)73.71(a)(5)20.2203(a)(2)(v)50.73(a)(2)(i)(A)50.73(a)(2)(v)(C)OTHERSpecify in Abstract below or in NRC Form 366A20.2203(a)(2)(vi)50.73(a)(2)(i)(B)50.73(a)(2)(v)(D)12. LICENSEE CONTACT FOR THIS LER FACILITY NAME TELEPHONE NUMBER (

Include Area Code

)Waterford 3 Steam Electric Station Bryan Pellegrin (504) 739

-620313. COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT CAUSESYSTEMCOMPONENT MANU-FACTURERREPORTABLE TO EPIXCAUSESYSTEMCOMPONENT MANU-FACTURERREPORTABLE TO EPIXDCCTCVM120Y14. SUPPLEMENTAL REPORT EXPECTED

15. EXPECTED SUBMISSIONDATEMONTHDAYYEARYES (If yes, complete 15. EXPECTED SUBMISSION DATE)

NOABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines

)On September 4, 2013, personnel at Waterford 3 determined that the manual operator for a safetyrelated air operated temperature control valve (ACC-126A) could not perform a full manual closure ofthe valve. Automatic operation was not affected. Manual closure is credited in safety analysis topreserve wet cooling tower inventory as part of the ultimate heat sink. The causal review determinedthat the cause, misalignment of the valve disc to the shaft, had occurred during planned maintenance inJuly of 2012. During this term of past inoperability, required systems and components in the redundantsafety train were also inoperable for short periods of time for surveillance and planned maintenancereasons. The valve was repaired, retested successfully, and declared operable on September 5, 2013.

There was no impact to nuclear safety due to this condition.

This condition is reportable under 10 CFR 50.73(a)(2)(i)(B) and 10 CFR 50.73(a)(2)(ii)(B).

NRC FORM 366A(10-2010)

LICENSEE EVENT REPORT (LER)

CONTINUATION SHEETU.S. NUCLEAR REGULATORY COMMISSION1. FACILITY NAME

2. DOCKET6. LER NUMBER
3. PAGEWaterford 3 Steam Electric Station 05000382YEARSEQUENTIAL NUMBERREVNO.2OF 62013 -006 -00NARRATIVENRC FORM 366A (10-2010)

INITIAL CONDITIONS Waterford Steam Electric Station, Unit 3 (Waterford 3), was operating steady-state in Mode 1, at or near 100% power at the time of discovering the condition.EVENT DESCRIPTION On September 3, 2013, Condition Report CR-WF3-2013-04274 was initiated due to a degrading trend in Auxiliary Component Cooling Water system (ACCW) [BS] Train A High Point Header pressure.

Engineering recommended testing the closure of valve ACC-126A (ACCW Header A Component Cooling Water (CCW) Heat Exchanger Outlet Temperature Control Valve) [TCV] using the manualoperator to verify functionality of the credited manual operator in the event a compensatory measure was required.On September 4, 2013, ACC-126A was closed using remote operation in preparation to manuallyoperate the valve. A high point pressure of 16.8 psig was noted prior to transferring to manual control.Per design calculation, a minimum of 16.4 psig header pressure is required to ensure meeting theallowable leakage requirements. During transfer to manual control, high point pressure decreased to 0 psig and could not be increased by using the manual operator. Automatic control was restored to ACC-126A and high point header pressure recovered to 20.1 psig. While design header pressure could bemaintained while aligned for automatic operation, the manual operator was unable to close the valve sufficiently to attain the required pressure.A troubleshooting team was formed to determine the cause of the manual operator's inability to fullyclose ACC-126A. The manual operator was inspected with the following findings: no evidence ofdamaged or missing gear teeth, worm sector gear and worm were properly and adequately greased, and the close travel stop screw had approximately 1/4 inch of adjustment remaining. The conclusion ofthe inspection was that the manual operator was misaligned to the shaft and required additional travel adjustment to ensure ACC-126A achieved full closure. Two adjustments were required to be made to obtain an acceptable high point header pressure: 1) the close stop screw was adjusted 1/4 inch out,and 2) the manual override mounting bolts were loosened to allow maintenance personnel to furtherrotate the manual operator relative to the valve shaft (approximately 1/8 inch). Once the adjustmentswere made, ACC-126A achieved a high point header pressure of 18.8 psig using the manual valve operator.A review of past maintenance on ACC-126A determined that this condition had existed since a plannedvalve rebuild that occurred in July of 2012. During the rebuild, which replaced the valve shaft, the newvalve shaft required drilling of the valve disc tapper pin holes to attach the manual valve operator. Asthe technical manuals did not address this, the hole locations were drilled using the old shaft as aguide. This resulted in a slight misalignment of the valve disc on the valve shaft that precluded tightmanual closure of the valve seat. Automatic valve closure was not affected. This went unrecognizedfollowing maintenance because operation of the manual valve operator was not adequately retested.On September 5, 2013, following maintenance and retest, ACC-126A was restored to operation and ACCW Train A was declared operable.

NRC FORM 366A(10-2010)

LICENSEE EVENT REPORT (LER)

CONTINUATION SHEETU.S. NUCLEAR REGULATORY COMMISSION1. FACILITY NAME

2. DOCKET6. LER NUMBER
3. PAGEWaterford 3 Steam Electric Station 05000382YEARSEQUENTIAL NUMBERREVNO.3OF 62013 -006 -00NARRATIVENRC FORM 366A (10-2010)

A brief timeline of events follows:

7/8/2012to7/27/2012ACC-126A was rebuilt under WO-00320439. The valve shaft, bushings, packing, and t-ring were replaced. The replacement shaft was sent to vendor for machining as the valve shafts are procured without the valve disc tapper pin holes drilled.ACCW A high point header pressure reached approximately 25.8 psig when tested in automatic mode. Retest in manual mode not required or performed.9/3/2013 CR-WF3-2013-04274 was initiated due to a degraded trend in ACCW A High PointHeader pressure. Engineering recommended testing the closure of ACC-126A viathe manual override to verify functionality in the event a compensatory measure was required.9/4/2013 ACC-126A was closed in preparation to manually operate the valve in accordance with OP-002-001 (Auxiliary Component Cooling Water). A high point pressure of16.8 psig was achieved prior to transferring to manual control. During transfer to manual control, high point pressure decreased to 0 psig and could not be increased by using the manual override. (CR-WF3-2013-04290)9/4/2013 Engineering and maintenance formed a troubleshooting team to identify and correct the issue with ACC-126A.9/4/2013 Manual override was inspected with no signs of damage. The travel stop on the manual override was adjusted and header pressure increased to 8 psig.9/4/2013 Valve disc assembly was rotated approximately 1/4 inch to obtain more travel from the manual override. Header pressure increased to 18.5 psig.9/5/2013 ACC-126A was declared Operable after satisfactory retest under automatic and manual operations.9/5/2013 CR-WF3-2013-04324 was initiated identifying that ACC-126A(B) had a safety function to close via the manual override while simultaneously maintaining a high point pressure of 16.4 psig.9/5/2013 The manual override for ACC-126B (Train B) was tested. High point header pressure reached 18.8 psig.REPORTABLE OCCURRENCE Technical Specification (TS) 3.7.3 requires two independent trains of CCW [BS] and ACCW [BS] to beoperable in Modes 1, 2, 3 and 4. TS 3.7.4 requires two independent trains of Ultimate Heat Sink (UHS)

[BS] to be operable in Modes 1, 2, 3 and 4 with each train consisting of a Dry Cooling Tower (DCT)

[BS] and a Wet Cooling Tower (WCT) [BS] and its associated water basin. Both specify an allowed outage time (AOT) of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.As valve ACC-126A was unable to meet a specified safety function regarding its manual valve operator from July 2012 to September 2013 (past inoperable), the AOT was exceeded. This condition isreportable under the following criteria: 10 CFR 50.73(a)(2)(i)(B), Any operation or condition which wasprohibited by the plant's Technical Specifications.

During the period from July 2012 to September 2013 when ACC-126A (Safety Train A) was pastinoperable, there were several instances where Safety Train B required systems and components werealso inoperable short periods of time for surveillance and maintenance reasons. This condition isreportable under the following criteria: 10 CFR 50.73(a)(2)(ii)(B), Any event or condition that resulted in NRC FORM 366A(10-2010)

LICENSEE EVENT REPORT (LER)

CONTINUATION SHEETU.S. NUCLEAR REGULATORY COMMISSION1. FACILITY NAME

2. DOCKET6. LER NUMBER
3. PAGEWaterford 3 Steam Electric Station 05000382YEARSEQUENTIAL NUMBERREVNO.4OF 62013 -006 -00NARRATIVENRC FORM 366A (10-2010) the nuclear power plant being in an unanalyzed condition that significantly degraded plant safety.BACKGROUND - SYSTEM DESIGN Waterford 3 is a Combustion Engineering design pressurized water reactor [AC] with two recirculatingtype steam generators [SG]. Safety related components and systems are comprised of redundant trains, A and B, each train capable of design accident mitigation.The ACCW System is a redundant train system which supplements the heat removal of the Dry CoolingTowers (DCT) in cooling the Component Cooling Water (CCW) System by providing cooling water to the shell side of the CCW Heat Exchangers. The ACCW system removes heat load from the CCWsystem (at the CCW heat exchangers) and rejects the heat load to the atmosphere via Wet CoolingTower (WCT). The ACCW system is designed to operate during normal operation and following adesign basis event or accident. Upon receipt of a Safety Injection Actuation Signal (SIAS), the ACCW removes sufficient heat from the CCW to ensure that the CCW supply temperature does not exceed its design basis maximum temperature of 115 degrees F by providing sufficient flow through the CCW heat exchanger while minimizing the water consumption of the Wet Cooling Towers. ACCW FlowControl is facilitated by the throttling of valve ACC-126A via temperature control loop CC ITAC7070A.ACC-126A is a 12 inch, Type 9211, Fisher butterfly valve that is capable of bubble tight closure. Thevalve is equipped with a Fisher double acting piston actuator. ACC-126A is a fail-as-is air-operatedvalve (AOV) and is provided with a backup nitrogen accumulator, if needed, to perform its safety related functions. The actuator accessories include two Fisher filter regulators, a Masoneilan I/P transducer and a Fisher positioner. The air supply for ACC-126A is supplied either by the Instrument Air system

[LD] or Nitrogen Accumulator 1 [LK]. In the event ACC-126A is required to close to preserve WCTinventory margin post-accident, manual operation via the hand-wheel manual operator would berequired and is credited in plant design basis documents and site procedures.The control signal from temperature controller CC-ITIC7070A [TC] on CP-33 opens or closes ACC-126A to a desired flow control position utilizing CCW Heat Exchanger Outlet Temperature as thefeedback. ACC-126A has a reverse acting fail-as-is piston actuator. When the positioner is provided a3 psig signal, ACC-126A will fully open (approximately 90 degrees) and when provided a 15 psig signal,ACC-126A will fully close (approximately 0 degrees).

During normal operation ACC-126A is in the AUTOMATIC mode of operation. Typically the temperature setpoint on CP-33 is between 84 - 87 degrees F during the summer. The ACCW systemis normally in standby during the winter months as the DCT handles the cooling during the wintermonths. ACC-126A is required to regulate flow through the shell side of the CCW Heat Exchangersuch that constant outlet temperature is maintained. ACC-126A is controlled by temperature controller CC ITIC7070A on CP-33. The tube side outlet temperature (CC ITE7075A) [TC] of the CCW heatexchanger controls the valve. If the temperature exceeds the setpoint during normal operation the valve begins to control flow. Under accident conditions, ACC-126A is required to modulate this flow to the WCT until post-accident heat can be removed by the DCT's alone. (NOTE: The modulation position ofACC-126A is credited for reducing evaporative losses to maintain WCT water inventory for the entireaccident.) ACC-126A is provided with a nitrogen accumulator to perform this function during a loss of instrument air.On SIAS, the setpoint is automatically raised to 115 degrees F provided WCT Basin temperature is NRC FORM 366A(10-2010)

LICENSEE EVENT REPORT (LER)

CONTINUATION SHEETU.S. NUCLEAR REGULATORY COMMISSION1. FACILITY NAME

2. DOCKET6. LER NUMBER
3. PAGEWaterford 3 Steam Electric Station 05000382YEARSEQUENTIAL NUMBERREVNO.5OF 62013 -006 -00NARRATIVENRC FORM 366A (10-2010)above 74 degrees F. This change can be observed on the controller setpoint meter. Raising thesetpoint preserves WCT Basin inventory during an accident to meet the 30 day post-LOCA (loss ofcoolant accident) requirements.CAUSAL FACTORS An apparent cause evaluation determined the following causal factors:

Direct Cause: Angular misalignment of the valve disc on the shaft was the direct cause of ACC-126A failing to fully close when using the manual operator. During the July 2012 rebuild, which replaced thevalve shaft, the new valve shaft required drilling of the valve disc tapper pin holes to attach the manualvalve operator. As the technical manuals did not address this, the valve disc tapper pin hole locations were drilled using the old shaft as a guide. This resulted in a misalignment of the manual operator onthe valve shaft that precluded tight closure of the valve seat in manual mode. The cause did not affect closure operation of the valve in automatic mode.Contributing Cause: Four different technical manuals are required when rebuilding ACC-126A. Thesetechnical manuals do not contain necessary links to one another to ensure proper valve setup (i.e.valve disc alignment onto valve shaft.) In addition, the work order instructions did not provide enough guidance to bridge the gaps within these technical documents.

Contributing Cause: Post maintenance testing less than adequate. In June 2012, interim measureswere established to ensure that ACC-126A and ACC-126B would close sufficiently to maintain WCTinventory margin. High point header pressure surveillances, with each valve in automatic, wereinitiated. These surveillances are performed on a 2-month frequency per OP-903-068. However, based on CR-WF3-2013-4324, the safety function for ACC-126A and ACC-126B is to close post-accident to preserve WCT inventory margin using the manual override since all safety related airsources will be depleted. Therefore, the interim surveillances and thus post-maintenance testing were not adequate.EXTENT OF CONDITIONAn Extent of Condition was performed by reviewing all valves that require manual stroking within the InService Testing (IST) Program. The population of IST valves reviewed included air operated, motoroperated, hydraulically operated, and manually operated valves. The manual override for each valvetype was reviewed against the apparent cause for vulnerability. The review concluded that the scotchyoke and rotary type manual overrides were susceptible to the direct cause. Surveillances have beenverified established to test the manual override safety function on the susceptible valves.CORRECTIVE ACTIONS Adjusted ACC-126A manual override to positively seat the valve. As-left high point header pressure was above 16.4 psig. (completed) Tested ACC-126B manual override as part of the operability input for CR-WF3-2013-04324.

High point header pressure was above 16.4 psig. (completed) OP-903-118 (Primary Auxiliaries Quarterly IST Valve Tests) was updated to ensure adequatepost-maintenance testing of the manual override is performed on ACC-126A and ACC-126B.

(completed) Revise the maintenance notes for ACC-126A and ACC-126B to include a caution that theexisting valve shaft tapered pin holes are not to be copied when replacing the shaft. (completed)

NRC FORM 366A(10-2010)

LICENSEE EVENT REPORT (LER)

CONTINUATION SHEETU.S. NUCLEAR REGULATORY COMMISSION1. FACILITY NAME

2. DOCKET6. LER NUMBER
3. PAGEWaterford 3 Steam Electric Station 05000382YEARSEQUENTIAL NUMBERREVNO.6OF 62013 -006 -00NARRATIVENRC FORM 366A (10-2010) Update applicable technical documents to provide adequate cautions, limitations, and guidanceto ensure appropriate disc orientation when changing the valve shaft or disc. (planned CR-WF3-2013-4290)SAFETY SIGNIFICANCEIndustrial Safety: There was no industrial safety significance associated with this issue.Radiological Safety: There was no radiological safety significance associated with this issue.Nuclear Safety: A nuclear safety evaluation was performed using actual meteorological data over the time period and concluded that the Ultimate Heat Sink was fully functional considering the identifiedcondition and that significant water inventory margin was available for all analyzed events and accidents. There was no impact to nuclear safety.

SIMILAR EVENTSA search was performed using the NRC's ADAMS search engine for other similar reported events atWaterford 3 and in the industry. No similar events were identified.ADDITIONAL INFORMATIONEnergy industry identification system (EIIS) codes and component function identifiers are identified in the text with brackets [ ].