ML20071F488

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LER#78-026/03L-1 on 780830:Bchannel RPS Variable Overpwr Trip Reset Demand Alarm Actuated & Would Not Reset.Then,Hi Pwr & Thermal Margin/Low Pressure Trip Units Failed,Both Due to Failure of Devar19-601A,18volt Pwr Supply
ML20071F488
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 09/15/1978
From: Connolley J, Gordon Peterson
OMAHA PUBLIC POWER DISTRICT
To:
Shared Package
ML20071F480 List:
References
LER-78-026-03L, LER-78-26-3L, NUDOCS 7810110117
Download: ML20071F488 (3)


Text

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LICENSEE EVENT REPORT CONTROL BLOCX: l 1

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Io64l l after this alarm came in, the Hi pcver and the: nal =arrin/ lev cressu e trie u .its fer I

,oi5i i"3" cha'nel PSS failed to the tripped condition. The three remaining ??S channels 1 J 66 l l remain *d Operable throughout this event. See LER 78-026 Revisien 0. I 1017 l 1 I

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12 13 18 19 20 SEQUENTI AL CCOUR R ENCE REPORT REVISION EVENT YE AR REPORT NO. COCE TvPL NO.

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t i 101 lSe tevar Model 19-601A.18 velt tovar sur:1v w s the c0 renert irich " m =4.

,ii1 ; l believed to have been an intermittent failure =f this pever surelv vhich resu1*ad 1- 1

{ g gthe failure of two a=plitude selector =edules (see LIR 73-026 Revisic: 0) as the ;cverI i, ,3l l supply cutput was noted to be as high as 27 volts while troubleshooting this failure. !

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  • . POWER OTMER STATVS OtSCOV E R Y D'SCOVERY OESCRIPT:CN STATLS lAl@l46 overator Cbse vation 1 isist121@ l01of91@l 7 g 9 to 1: 11 NA 44 l

45 83 ACT1vtTY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY LCCATION CF RELEASE -

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  • ERSONNEL EXPOSU R E S Nuv8ER TYPE OESCRtPTtON l1 hI **

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  • ERSONNE L INJL AIES NLVSER OESCRIPTION I

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l LIR 78-026 Revision 1 Onaha Public Power District Fort Calhcun Station Unit no. 1 Docket No. 05000285 Attachment No. 1 Safety Analysis

'"he reactor protective system (PSS) is so designed that no single failure can prevent the safe shutdown of the plant if required.

During the time the "3" channel RPS for High power and thermal margin / low pressure were considered inoperable, the PSS vas in a 2 cut of 3 logic providing adequate protection of the reactor.

The apparent cause of this failure was a faulty 18 volt power supply. The output of this power supply was noted, at times during this event, to be as high as 27 volts (or approximately 10 volts over rating) which is ample overload to have caused the previous failure of two amplitude selector modules (rated at 18 volts). See LER 78-026 Revision O. Rovever, the higher than rated output voltage of this power supply was not seen during the a=plitude selector module failures of August 21, 1978.

The PSS vill continue to be checked by visual inspection and by surveill-ance testing in an effert to discover and correct future events of this type.

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1ER 78-026 Revision 1 Omaha Public Power District -

Fort Oalhoun Station Unit No.1 Docket No. 05000285 Attachment No. 2 Failfre Data See LIR 78-026 Revision O. This is the first reportable event for an 18 volt Devar power supply.

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